ML20215G594

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Responds to Violations Noted in Insp Repts 50-424/87-24 on 870306-20 & 50-424/87-27 on 870310-0417.Corrective Action: Procedure 14905-1 Revised to Provide Correction Factors for RCS Temp,Pressurizer Level & Chemistry Sampling
ML20215G594
Person / Time
Site: Vogtle Southern Nuclear icon.png
Issue date: 06/18/1987
From: Gucwa L
GEORGIA POWER CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
SL-2607, NUDOCS 8706230311
Download: ML20215G594 (5)


Text

Georgia Fbwer Company 333 P4edmont Avenue Atlanta, Georgia 30308 Telephone 404 526-6526 Ma?ing Address:

Fbst Office Box 4545 Athnta, Georgia 30302 h

Georgia Power L T. Gucwa the southem electnc system Manager Nuclear i afety and Ocensing 0331m X7GJ17-V120 June 18, 1987 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C.

20555 PLANT V0GTLE - UNIT 1 NRC DOCKET 50-424 OPERATING LICENSE NPF-68 RESPONSE TO NRC INSPECTION REPORTS 4

Gentlemen:

Pursuant to the provisions of 10 CFR 2.201, Georgia Power Company (GPC) submits the following information in response to NRC Inspection Reports-50-424/87-24 and 50-424/87-27 for Plant Vogtle Unit 1 concerning -

the inspections conducted by Mr.

P.

Burnett of NRC Region II on March 6-20, 1987 and Messrs.

H.

H.

Livermore, J.

F.

Rogge, and R. J. Schepans, also of NRC Region II on March 10 - April 17, 1987, respectively.

Two apparent violations were cited in the Notices of Violation for Plant Vogtle Unit 1.

A copy of this response has been provided to NRC Region II for review.

I As discussed with Region II staff, one response is being submitted for both identified violations because procedural inadequacies addressed q

in the Notices of Violation are for the same procedure, 14905-1, and the corrective actions were the same for both violations.

He believe that the Notice of Violation for NRC Inspection Report 50-424/87-27 as submitted by NRC Region II letter dated May 19, 1987, incorrectly refers to Plant Vogtle Unit 2 by docket number and as a result implies that it is in violation also.

The Report Details section of the Inspection Report specifically identifies the violation as being applicable to Plant Vogtle Unit 1

by the violation designator "50-424/87-27-02." Accordingly, our response addresses only Plant Vogtle Unit 1.

Unless we hear otherwise, we will assume that our determination on applicability is correct.

j i

A transcription of the NRC Notices of Violation is provided as.

GPC's response is provided as Enclosure 2.

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GeorgiaPower A U. S. Nuclear Regulatory Commission June 18, 1987 Page Two I

Should you have.any questions in this regard, please contact this office at any time.

Sincerely, L. T. Gucwa JAE/1m

Enclosures:

1, NRC Notices of Violation 2.

Georgia Power Company Response c: Georaia Power Comoany Mr. R. E. Conway Mr. J. P. O'Reilly Mr. G. Bockhold, Jr.

Mr. J. F. D'Amico Mr. C. H. Hayes-G0-NORMS Southern Comoany Services Mr. R. A. Thomas Mr. J. A. Bailey Shaw. Pittma,1. Potts & Trowbridae Mr. B. H. Churchill, Attorney-at-Law Troutman. Sanders. Lockerman & Ashmore Mr. A. H. Domby, Attorney-at-Law U. S. Nuclear Reaulatory Commission Dr. J. N. Grace, Regional Administrator Ms. M. A. Miller, Licensing Project Manager, NRR (2 copies)

Mr. J. F. Rogge, Senior Resident Inspector-Operations, Vogtle Georaians Aaainst Nuclear Enerov Hr. D. Feig Ms. C. Stangler 0331m 7WMS.

GeorgiaPower A J

ENCLOSURE 1 PLANT V0GTLE - UNIT 1 NRC DOCKET 50-424 OPERATING LICENSE NPF-68 NRC NOTICES OF VIOLATION I

y10LATION 50-424/87-24-01

" Technical Specification 4.4.6.2.1 - requires that the reactor coolant system unidentified leakage be demonstrated to be less than one gallon per minute in modes 1,

2, 3,.and 4. by the performance of ~a reactor coolant system inventory balance at least once per 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

Contrary to the above, Procedure 14905-1 in use for this Technical Specification surveillance during a period encompassing March -7,

1987, was inadequate to perform the task in that it did not properly account for. changes in average-system temperature or pressurizer level in determining the change in inventory.

This is a Severity Level IV violation-(Supplement I)."

VIOLATION 50-424/87-27-02

" Technical Specification 6.7.la requires that procedures shall be established, covering activities delineated in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978.

Operations Procedure No..14905-1, Rev.

6 "RCS Leakage Calculation (Inventory Balance)" contains the methodology to calculate unidentified leakage.

Contrary to the above, on April 7, 1987, the NRC inspection identified that Operations Procedure No. 14905-1 had not been adequately established in that the procedure was not capable of calculating the unidentified leakage appropriately to determine if the acceptance criteria had been exceeded.

This is a Severity Level IV Violation (Supplement I)."

0331m El-1 06/18/87 SL-2607 mns

Y l

GeorgiaPower A ENCLOSURE 2 PLANT V0GTLE - UNIT 1 NRC DOCKET 50-424 OPERATING LICENSE NPF-68 RESPONSE TO NRC NOTICES OF VIOLATION RESPONSE TO VIOLATIONS 50-424/87-24-01 AND 50-424/87-27-02 Admission or denial of alleaed violations:

The events did occur as stated in the Inspection Reports.-

Reason for the violations:

Procedure 14905-1 was implemented to meet Technical Specification 4.4.6.2.1.d with the required compensation for pressure isolation valves (PIV) leakage performed in accordance with Procedure 14450-1.

PIV leakage was measured at a test pressure less than operating pressure and corrected per the requirements of the 1983 edition of the ASME Section XI Code, Paragraph IWV-3427(b).

The correction produced a potentially high PIV leak rate resulting in a negative unidentified leak rate value.

Additionally, the RCS water volume used in the development of Procedure 14905-1 was determined to be too small.

After additional reviews and discussions, it was determined that a larger RCS water volume was more appropriate and was more consistent with the RCS leak rates calculated in accordance with NUREG-1107, "RCSLK9:

Reactor Coolant System Leak Rate Determination for PWRs."

0331m E2-1 06/18/87 SL-2607 700775

c L

GeorgiaPower d l

ENCLOSURE 2 (Continued)

RESPONSE TO NRC NOTICES OF VIOLATION

_ Corrective steos which have been taken and the results' achieved:

Procedure :14905-1 was revised to provide correction factors for RCS temperature, pressurizer level, chemistry sampling, CVCS filter leakage, and pressure isolation valve leakage.

Subsequent to issuance of revised

' Procedure 14905-1, no negative unidentified leak rates have been

. calculated.

Additionally, the Operations Department has utilized the RCSLK9 program to validate Procedure 14905-1 calculations with results obtained being within the.2 GPM for acceptable procedures.

Corrective steos which will be taken to avoid further violations:

Corrective actions for these violations have been completed.

Date when full como11ance will be achieved:

Full compliance was achieved with. the approval and implementation of Procedure 14905-1, Revision 8, dated May 8, 1987.

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0331m E2-2 06/18/87 SL-2607 700775