ML20215D326
| ML20215D326 | |
| Person / Time | |
|---|---|
| Site: | Dresden |
| Issue date: | 11/30/1986 |
| From: | Eenigenburg E, Maxwell D COMMONWEALTH EDISON CO. |
| To: | NRC OFFICE OF ADMINISTRATION (ADM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
| References | |
| 86-208, NUDOCS 8612160318 | |
| Download: ML20215D326 (34) | |
Text
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OPERATING DATA REPORT d;.
i DOCKET NO. 050-237
'N DATE December 1, 1986
[
COMPLETED BY D. C. Man ell TELEPHONE 815/942-2920 OPERATING STATUS NOTES 1.
Unit Name:
Dresden II s
2.
. Reporting Period:
November, 1986 3
Licensed Thermal Power (MWt):
2.527 4.
Nameplate Rating (Gross MWe):
828 5
Design Electrical Rating (Net NWe): 794 6.
Maximum Dependable capacity (Gross MWe): 812 7
Maximum Dependable Capacity (Net MWe):
772 8.
If Changes Occur in Capacity Ratings (ltems 3 Through 7) Since Last Report, Give Reasons:
N/A i
~
9 Power Level to Which Restricted, if Any (Net MWe): N/A 10.
Reasons For Restrictions, if Any: N/A This Month Yr-to-Date Cumulative II.
Hours in Reporting Period 720 3,016 145,080 k~
13 Reactor Reserve Shutdown Hours 0
0 0
12.
Number of Hours Reactor Was Critical 689.1 7.110.1 110.807.6 14.
Hours Generator On-Line 681.3 6.763.3 105.747.9 15 Unit Reserve Shutdown Hours 0
0 16.
Gross Thermal Energy Generated (MWH) 1.317.260 15.238.443 216.872.082 l
17 Gross Electrical Energy Generated (MWH) 421,909
_ 4.902.902 69.402.665 15.
Net Electrical Energy Generated.(MWH) 397.889 4.655.671 65.591.785 19 Unit Service Factor 44,6 84.4 72.9 20.
Unit Availability Factor 94.6 84.4 72.9 1
21.
Unit Capacity Factor (Using MDC Net) 71.6 75.2 58.6 22.
Unit Capacity Factor (Using DER Net) 69.6 73.1 56.9 23 Unit Forced Outage Rate 0
8.2 12.1 24.
Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
10th Refueling outage started Il-29-86 25 If Shut Down At End Of Report Period, Estimated Date of Startup:
3-14-87 AD KO
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D n
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d OPERATING DATA REPORT DOCKET NO. 050-249 DATE December 1,1986 COMPLETED BY D. C. hb>mell TELEPHONE 815/942-2920 OPERATING STATUS NOTES j
1.
Unit Name: Dresden III 2.
Reporting Period:
November, 1986 3
Licensed Thermal Power (MWt):
2 527 4.
Nameplate Rating (Gross HWe):
ang 5
Design Electrical Rating (Net MWe): 794 6.
Maximum Dependable Capacity (Gross MWe): a19 7
Maximum Dependable Capacity (Net MWe):
773 8.
If Changes Occur in Capacity Ratings (items 3 Through 7) Since Last Report, Give Reasons:
N/A 9
Power Level to Which Restricted, if Anj (Net NWe): N/A 10.
Reasons For Restrictions, if Any: N/A l
This Month Yr-to-Date Cumulative 11.
Hours in Reporting Period 720 8,016 134,665 12.
Number of Hours Reactor Was Critical 657.4 2,099.4 98,696.1 13 Reactor Reserve Shutdown Hours 0
0 0
14.
Hours Generator On-Line 636.2 1,843.3 91,636.6 15 Unit Reserve Shutdown Hours 0
0
~
0 16.
Gross Thermal Energy Generated (MWH) 1,371,059 3,675,477 185,448,113 i
17 Gross Electrical Energy Generated (MWH) 440,496 1,145,011 59,984,244
~
l 18.
Net Electrical Energy Generated.(MWH) 417.488 1.039.163 56.765.457 19 Unit Service Factor 88.4 23.0 68.0 20.
Unit Availability Factor 88.4 23.0 68.0 21.
Unit Capacity Factor (Using MDC Net) 75.0 16.8 54.5 i
22.
Unit Capacity Factor (Using DER Net) 73.0 16.3 53.1 23.
Unit Forced Outage Rate 11.6 15.3 12.4 24.
Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
l 1
25.
If Shut Down At End Of Report Period, Estimated Date of Startup:
l l
l i
COMMONWEALTH EDISON COMPANY 4
DRESDEN STATION MAXIMUM DAILY LOAD MONTH OF NOVEMBER, 1986 HOUR MAXIMUM DAILY LOAD DAY ENDING KW 1
2100 1,452,700 2
2400 1,395,500 3
0600 1,451,700 4
0100 1,433,900 5
1900 1,450,100 6
1000 1,446,800 7
0100 1,439,500 8
1000 1,438,600 9
1500 1,436,300 10 1200 1,446,700 11 2400 850,000 12 2400 1,228,700 13 1100 1,389,300 14 1600 635,700 15 2400 998,100 16 2400 1,249,700 17 1500 1,397,200 18 0100 624,900 19 0100 1,160,700 20 2000 1,055,300 21 2200 1,241,500
(
22 2400 1,384,800 23 0200 1,401,500 24 2400 1,420,000 25 0200 1,419,900 I
26 0800 1,413,700 27 0700 1,412,200 28 0800 1,415,300 l
29 0100 263,600 30 1700 815,600
's AVERAGE DAILY UNIT POWER LEVEL DOCKET NO, 050-237 UNIT II DATE December 1,1986 COMPLETED BY D. C. Maxwell TELEPHONE 815/942-2900 MONTH November, 1986 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 616 17 59g 2
618 18 590 3
616 19 589 4
620 20 584 5
615 21 580 6
607 22 582 7
610 23 578 g
609 24 575 l
604 9
25 562 10 608 26 567 11 584 27 551 12 589 28 550 13 585 29 46 14 592 30 o
15 602 16 597
-)
AVERAGE DAILY UNIT POWER LEVEL DOCKET 110. 050-249 UNIT III DATE December 1, 1986 COMPLETED BY D. C. Maxwell TELEPHONE 815/942-2920 MONTH November, 1986 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DALLY POWER LEVEL (MWe-Net)
(MWe-Net) 1 756 17 599 2
586 18 447 3
761 19 404 4
755 20 410 5
759 21 477 6
757 22 681 i
7 750 23 736 8
751 24 764 9
758 25 773 i
10 432 26 795 769 1I 29 27 12 442 28 785 l
13 288 29 781 14 0
30 764 15 44 16 481 l
l l
DOCKET NO. 050-237 UNIT NAME 11 UNIT SHUTDOWNS AND POWER REDUCTIONS DATE December 1, 1986 COMPLETED BY D. C. Maxwell TELEPHONE (815) 942-2920 REPORT MONTH NOVEMBER, 1986 METHOD OF LICENSEE CAUSE & CORRECTIVE NO, DATE TYPEl DURATION REASON 2 SHUTTING EVENT SYSTEM COEPONENT ACTION TO (HOURS)
DOWN REACTOR 3 REPORT F CODE 4 CODES PREVENT RECURRENCE i
1 j'
(30.9) 10th refueling outage, planned 9
86-11-29 S
30:57 C
2 Turbine off-line manually to 1
Rx scram when mode switch moved l
from "Run" to " Refuel".
t i
l l
l I
i 1
2 3
F:
Forced Reason:
4 Method:
Exhibit G-Instructions for S:
Scheduled A-Equipment Failure (Explain) 1-Manual Preparation of Data l
B-Maintenance or Test i
2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (
) File D-Regulatory Restriction 4-Other (Explain)
E-Operator Training & License Examination j
F-Administrative l
G-Operational Error I
H-Other (Explain)
'T DOCKET NO. 050-249 - -
UNIT NAME III UNIT SHUTDOWNS AND POWER REDUCTIONS DATE December 3,1986 COMPLETED BY D. C. Maxwell TELEPHONE (815) 942-2920 REPORT MONTH NOVEMBER, 1986 METHOD OF LICENSEE CAUSE & CORRECTIVE NO.
DATE' TYPEl DURATION REASON 2 SHUTTING EVENT SYSTEM COMPONENT ACTION TO (HOURS)
DOWN REACTOR 3 REPORT F CODE 4 CODES PREVENT RECURRENCE 6
86-11-10 F
28:16 G
3 86-021-0 I.M. error - power lead to (28.3) drywell MSIV's air supply lifted inadvertently during maintenance.
l 7
86-11-13 F
55:30 G
3 86-019-0 E.M. error - feeder breaker (55.5) on ESS bus inadvertently opened.
l l
1 2
3 4
F:
Forced Reason:
Method:
Exhibit G-Instructions for S:
Scheduled A-Equipment Failure (Explain) 1-Manual Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (
) File D-Regulatory Restriction 4-Other (Explain)
(NUREG-Ol61)
E-Operator Training & License Examination.
F-Administrative i
G-Operational Error
(
H-Other (Explain) 1
.m.
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s OME$DEC1 Wilt 2 SAFET Y RELATFD !441NTI!J A'4CE NATURE OF LFR OR 00TAGL H ALFUP.C T I D'd t 0U I P'? tN T f*AlteTEMANLF NU'1M R CAUSE
'8 E S UL T Cn4Rt.CTIVE 44.T I tL4 REPACMLD vat,VE, LFF T 04 Md2-1391-2 WALVt P Rr W E rd f lVE N/A dR U%3107 If45T ALLElJ H A'40 WHC e t, LEFT OK Mu 2-1501-10A 09R RF C T IVE N/A Wd 054t-01 h
s REPAIRS TO FAILFO A MONITOR TO BE 00'4E 2-2604-A CURRfCTIVe ti/A g
DdYdLLL H2H2 MO'eliOA 4 W4 055 9t20 04 W.R.
C 57t68 h
RJM 04 CukRECTIVE N/A REPLACED QUA0 TRIP CARD, PERFORMED
- WR 05 t>75 %
C ALIBR ATION CHECK FFR PROCE00RE, LEFT OK-CHtCKEO AND REPL AC LD LI-263-57A AND t
RPS AtlO PCIS SYSTLM CORRFCTIVE N/A WR 056n66 CALIBRATED NtW T rat 4SMI TTER PER PROCEDURL g
REPL ACEO Af40 ADJUSTF0 LIMIT LEVFR PFR MOV-2-203-20 PRE W F r4 T IVE N/A
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REPL ACE 0 SN APLOCK AND LFVER AND M d tf 2 01-2 S PROVFNTIVE N/A f*Siv lut LIMII spliCH W4 05F35F ADJUSTED ARM PER PROCFOURE g
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04E50trl UNTT 2/3
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3 AFr.T V REL AT ED :t AIWiENaNCC' fiQ itlar nF LER OR OUTAGt MOLFUNCTIord EQUIP fEPai M AI.4f tN Af4LT PJU*BFR C AUS E
- ESULI CORR EC T I V E AC T 1014 fJ/ A CHECKFD AND FO'JMD FAO P203LEM, CALI3 RATED SPARE 3-1159 CORRECitV6 fl/ A SPA 4E F LPl 4 AL T E Mf' 00fa iR Ol t.F R WR D91% 47 PER PRdCf DURE, L EF T OK FOR S I Al40uY L IQU T O CO:4TROFL S tsG T IFAIN "A*
CURRECTIVE F4/ A CLOSt0 Al40 REW1 RED THF THREE DOORS AS WR D54105 REQUESTED, PL A 4K FLANGE WAS INSTALLE0, LEFT OK
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CLEAR 4ED CAI>LE, CQBLF PANS PR E V014 T I VE N/A WR 054839 DTS-12 (OR4ECTIVE N/A C ALIdR ATED G AUGF AS PER WORK LLRI P9LSS. LAUGT WR 055224 If4STRUCT10TJS USING l'ROCEDURES, LEFT OK LLRT PRCS504E GAlfGr. DIS-31 CORRFLTIVE N/A C AlluR ATED PRE SSUPE GAUGE PER WORK WR 05522%
INSTRUCTIONS, LEFT OK COLlHRATE 015-31 Pit E V Fi4 Y I V E N/A CALIi$ RATED TEST GAUGE PER PROCEDURE WR 05n5d?
OTS-32 PR E Vf ;4 T t V E N/A C AL I BR AT ED TdSI GAUGE PFR PROCEDURE, WR d% e> 5tt 3 LFFT OK I UN C H Aii'9E O POWa SOPPtY C OM E L T I Vc N/A REPLACEO 03 Aft 0 Q4, RE SOLDERED SEVER AL WA 0%7127 JulNTS, LfFT OK OUTPUI JRLA4f4 10 15-1 0/6 PRr gr?a r g yt s/a igg,IEl4E0 LOJSt SC R r.J AND VOLTAGES WR US??17 CitECKfD GOOD, 740 PPOSLE**S I?4 BREAMER UR Cui3 I C AL, LEFT OK
t1F 30/04 Urs! T 2/ 6 SArtTY RELAffd '4 A I N T E H ANC L
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'44TUPE OF LF4 03 00TAGt
!4 A lf Uh(T 10f4 C O UI Pt*t'll M A I.4 T E ti A'!C F NU%5 F R LAUSE PtSULT C'IRU LC T I V F ACTIO*4
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SPARf ax L5/EL T R ANi'51 T IE R PM VfNitti
'J/ A PERFO'tt1EU PJ Of tCUPE L F OUN.) TR APIS
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fdTURF OF LER OR OUI A';E MALF9':LT104 E 7J I P"L'a i M A I N T L*J A'!U.
'89H 6f R LAUSt MESULT CORPECTIVE A C T 10's g
SO 3-201-2 A-3 P7FVEf 4T IVE N/A 4CPLACEO SULEN0lO VALVE MANIFOLD f4 S f t1 59LF'.0ID VAtVri-duiPd4TD HR 0347i9 ASSEltBLY FOR ALL OUT1)DA'tu MS IV' S.
COMPLE TED Pr.0CEDURE, LErT UK Sd3-203-IA-5 PRfVEtaTIVE f1/ A RFPL ACt0 SOLEN 0lO M ANIFOLD ASSEM8L f S Iffl0A4D f*SI V SOLfY11D VALVF W 334724 PER WORK If4S TRUC T [ UNS h
PRI1GRY C J'Jf A lf4dr r4T I5OLATION PREVENTIVE N/A RFPLACED RtLAY ON MAGNETIC C0ll SYSTEM LOGIC HFA RELAYS WK 0 % 661 A S SE N'1LY AND AUJUSTED PER PROCEDURES SLAVES 1-54 h
HPCI SYSTLM LOGIC PRE JEc4 TIVE T4/ A R FisulL T H.F. A.
RELAYS PER PROCEDURES WR 036T23 SLAVES 1-39 LPCI SYSThM L OG ir.
P RE V E I4 T I V E N/A
--8------
REPL ACEO COILS Af40 C Allf1R ATED PER WR U36724 PROCEDURES SLAVI5 1-Th 3-1601-60
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H-PRATT PR IM A4Y r.ONI A INr4FNT 4lP, 0 3 92 89 110LTS PER WORK INSTRUCTIONS AND VALUE TOROUF D AND ST AKED, LEFT OK h
1-2-2302 PRF Vf fit IVE N/A PERFOR MF D A COUPLING AllGt4ME NT CHECK ON HPCI PU'4P WR U41040 HPCI PUMPS, CHANGED GRE ASE, CHANGE 0 00dPLIr4G POLTS, FLOATFU COUPLING, LEFT OK PT-3-1641-60 P R F V E ta i ! V t.
f!/ A RFPL ACL7 AND GRE ASLD O-RING O'4 CO*JOUlf PRES SUPP. PRdS. lit Af 35.
WR 042214 SIDF OF Tit ANSf41 T IER, PERF ORf1ED C ALI:iR A T IO:4 PER PROCLOURE, LEFT OK
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US rLLCIRu"ATICS PRFVENTIVE N/A IN5ptCIFO AND UVERHAULE9 PER PROCEJURE
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Wd 042456
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203-W CURRTLilVt
'f/ A stL 4r8K FL ANGE i WF RF REMOVLD ANO RELIFF E L E C T R O.4 A l l C RSLIEF VAtVE W4 0440.56 Valvt utiH '! C 4 GASKFT INSTALLED, ORAlfa
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Liedr5 I I GH T F NF O UP, REPLACED VAlvF PER prs)CLOURE, LEFT OK
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fu GD d's U'41 T 3 S AFr TV ' HE L ATFD Milfilf 44NCE I4 A t tN E Di LER OD OdfGGE MALFUffCTION L'Jtil e '4L* 41 "AINTE'4 ANLE f uP rg cgu$g
.PESULT COR REC TI VF ACTION ADJUSTED DACKING AND LU51RICATED STEM, 3-220-1 PRFVFieflVE N/A-MAlid 5fLAM Ll:40 9R A l'1 VALVE
'4 R i>4405a LEFT OK 201-1-3 Ctiq4rC gVE et/ A REriOVED PILOT ASSEMPLY AND REBUILT 3 AND MAIN STEAM ISULAT104 V4LVE WR 044051 4 WAY PI L:1T VALVES, RFuulLT AIR CVLINDER REPACKE0 VALVE, TESTED CK 3
REdUILT 3 WAY AND 4 WAY VALVES, RE8UILT 2 0 3 fi COPU LTIVE
':/ A MAir6 STLAM 150LAT10'4 VALVE WR 04'.0%
AIR CYL!r.ERS, RFPACKED VALVES, TESTED UK 4
H EbU ll T 3 WAY AND 4 WAY VALVES, RE3UILT 203-2-0 CURRECTIVE N/A MAIN STLA4 I SLsL A T I ON VALVE WR 044967 AIR CYLINDERS, REPACKED VALVE, TESTFD OK 003-0401-023-015 PREVFf4TIVE t1/ A LEAK TESIFO ORIVES PER PROCFOURE SPARL CRD'S WR 044080 i
1 3-1302 PRE VF'4T IVe f4/ A CL E A t400 AND REPALMED COUPLING USING HPCI TUdalNL P9MOS WR 044097 GREASE, FLUATED COUPLING, LEFT OK INSPECTED OIL IANK HaSE, FOUND 3-2300 PRFVENTIVE P4/ A HPC I OIL IATM WR 044998 EVtRYTHING TO JF OK 34-1503 PRE /ENTIVe N/A REPLACE 0 LOWER HEAD AND HEAD GASKET AND I
LPCI HEAT FACH.
'A' Wi4 044104 TOP HE AD Ar4t) HEAD GASKET, HADE NEW STUDS A'80 REPLACED NOTS, LEFT OK 0/d l uG IPMfi4T l'A T CH C OR KF C T I Vi.
N/A l'IST ALLFU Lowr A SWING 69LT, NEW 0-RINGS, WA 044115 CLOSED 0/W EJUIPMFNT HATCH PER PR UC E DUR E, L LF T OK LPRN 32-O m PFJ v Er. T I V E b/A PERFUQMFD PROCLOURL, WILL REPLACE 3-705-002 WR 344445 DETELTUR ON WR=45749 I
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T4 A TilRF OF trH OR 00TAGt r44Lf 0NC T I O's C OU I /'itMT f* A l f 4 T E *3A Nu E
'su"3f R CAUSE RLSULT CDARECTIVE ACTION g
3-705-00?
PREVf t4T IVE M/A FOUND DETFCTOR SHORTED, dlLL REPLACF LPR?1 c.,C - 4 0- 0 0 HR 04445%
O'4 UR 34 57 <e 9 g
HF4 PELAY 575-131 PHt ti tat IVC N/A COPtPLE Tf D RFL AY REL'UILOING PER WR D45244 PROCEDURE h
3-305-112 COanFCTIVE t4/ A DIS A SSEtiLLLD VAL VF, CHANGED GASKET Aten
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HCU VAlvF, LP-23 E6 WR 046266 WEDGE, Il4SPELTED VALVE Ir4TERf4ALS AND OLD WEDGC, REASSEMBLED VALVE, LCFT OK
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3-305-112 f.OR RE L T I VE N/A DISA SSEMottD VALVE, CHANGE 0 GASKET A f40 HCU VALVE WR 046207 WEUGE, IP4SPECTED V ALVE INTERNALS AND OLD 14-27 DT 4FDGE, RE4SSEMBL EO V ALVE, LFFT OK 3-305-It?
CUR:4FCTIVE N/A DISASSEP3tEO VALVE, CHANGE 0 GASKET At40 HCU VALVF WR 046263 dEDGE, INSPECTED VALVE INTERNALS AND OLO 14-23 06 WFDGE, REASSEMJLED VALVE, LEFT OK
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3-305-112 CORRfCTIVE F4/ A DISASSE'1DLLD VALVE, CHAT 4GED GASKEl AND HCU VALVE WR D ',6 7 69 WEDGE, INSPECTLD VALVE INTERNALS AND OLD 4 EDGE, REASSEMBLED VALVE, LEFT OK
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3-305-112 CORRfCTIVt N/A O!S%5SEMhtED VALVE, CHANGE 0 OUT GASKET HLU VALVI WC D462iG A?40 WE DGE. INSPE CTED VALVE INTERNALS 10-23 (6 ANO OLD WEOGE, RL ASSEMBI ED VALVE, 3-3u5-112 CORMLTIVE N/A DISA SSEM3tEO VALVt, CHA%ED GASKEY ANO HCU VALVE Wd 046276 WEDGE, INSPFCTED VALVE It4TERNALS AND OLD 26-39 Gio WEDGE, REASStM9 LEO VALVE, LEFT OK 3-30%-112 CORHrCTIVE N/A DISASSEW. LED VALVE, CHANGE 0 GASKET AND
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HCU VALVF WR U46771 WEDGL, INSPFCTED OLD WEDGE A;40 VALVE 16 _11 F3 INir ANALS AND RE AS5EMBLEO V4LVE,
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3-305-1!?
C0HdfLTIVE ti/ A Of SA SSL%L EO V ALVF, CH A'4GE0 G ASM ET AND HCU VALVE WR J45213 dFDGE, INSPECTED VALVF INTERNALS AND OLO 10-47 C-1/
wc Dr. E. R E A SSE'13t ED V ALVE,
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'8 A I 4 T t N A NCE NUMdEd CAUSL PESULT COARECTIVE ACT10's REVOVED ULO GASM ET AND WEDGE ANO-3-305-112 Ct#REL T LV:-
N/A i
HCU VALVE WA 046279 RE AS SFHDLED WI T61 NEW, INSPECTED 10-43 C-11 INTERNALS AND OLO WEOGE, LEFT OK DISA SSEMolt0 V AL VE, CHANGED GASKET A N')
3-305-112 Cd9dfCTivt N/A HCU VALVE WK b 4 62 t!9 4FOGE, INSPFCTED INTERNALS AND OLD OS-39 n-10 WFOGL, REASSEM6LLO VALVE, LEFT OK 1-305-112 FORtFLYlVE N/A DISASStMiiLCD VAlvC, CHANGED GASKET AN9 HCU VALVF W4 0462dl WE DG ai, INSPECTED VALVE INTERNALS A!40 OLD 22-34 F-10 WEOGE, REASSEM4 LEO VALVE, LEFT OK REPL ACt'0 L AMPS WITH CORRECT TYPE AND LOC AL I ND I C A T Os> r oq
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P R F V E N T I V t-N/A 2A WA 94 e,718 CHEC KE D FOA NORM AL OPERA T ION, LEFT OK I
REPA IPED LOC AL I:49ICATOR LIGHT SOCKFT.
LOCAL I.4nlC A ld7 r oR tid I S 01 -
P RE V E '4 T I VE N/A 2TA dd 046T20 CL0 SED INIJICATION, LEFT OK LOCAL C u*. I R OL "u 1201-2 P RI V F t4 T I V E N/A REPLACE 0 WRO'4G PULDS WITH CORRECI ONES, WK 046719 CYLLED VALVE, LEFT 0%
1 CALtdRATED A.40 INSTALLED GAUGF PER 04Yb.f LL TJ IOxOS AP T it A;4 SM I T T ER PREVfHTIVE N/A 3-leM2-13 utt 04F300 PROCEDURE, REMOVED GAUGE AND VERIFIED I
PR0"ER OPFAATION OF PROCEDURE, LEFT OK 3-203-33-30 A40 TE-3D PREvrNTIVE f 4/ A INST ALLED A'f 0 RE MOVED btINO FL ANGES ANJ EL EL TRa4 A I IC S WR d4T110 CAPS
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INSTALLEO A*10 RF M9VED ISL ING FL ANGF 3-203-A Pd F V Er4 T IVL N/A TARGFT ROCK hR 041311
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3=5 74 T P4 F V f i4 T IVe
't/ A INiDECTED COOLER, LVERYTHING OK HPCI ROOM CG1L6R WR 3413o?
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04F SO Efd
't il T 1 5%FLTY U. L 4 T FD F* A I N T r,3 AsC E f4GTt)xF UF LER 09 PO T A f,f M 4 Lr g t:C r [ 0,.
L90 t P'4L'4 T f* A I:4 T Ltl Af 47 flW%f R LAUSt PESUlf CO,tRECTIVE ACTION l
(49R* AI.17 E D ALL SRM A.4D IRM CARLES PER SRM A r4D IR9 CAdLO DF4U ffF PP.Fvf'4Tive
- J/ A WR 44T444 PROCEDURE, LEFT OM FnUND 40 PR03 TEM WiiH EliHLR THE LPRM 3-705-007-Ic-31-4 PRFVFMIIVt
't/ A LPRii
N/A REMOVED COPPCR TU31NG AND INSPECTCD CRD E-6 AIR LINL WH 047526 FOR CRACKS, FOUND NO Pd0BLEH,PEINSTALLEO T USi teG AND TIGHTENED FITTIt4GS, LEFT OK HPCI ROOM CuGLrR Pe4 0V F N T I V L-N/A VERIFILD PLUGS INSTALLED, REMOVED SCAFFOLDING, LEFT GK Wd 04T719 3-705-002] 40-41'4 PRT VF.N il VE N/A PFRFORMED PRaCEDURE AND FOUND P40 LPRM WA 0479u0 PROBLEM LPRM 16-25-0 PRFVf7 TIVL N/A
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PERFUR ME D PROCLDURL ON LPRM, FOUNO NO WR 041949 PROBLEMS LPRf4 08-230 PatVFNT[VC N/A PERFORMED PROCEDUR E ON LPRM, FOU;40 NU WR 043024 PRD3LFMS TOROUED ALL DRIVES, REMOVE 0 C INST ALLE D 003-0201-0?0-015 CURRFCTIVE
'f/ A C0c4 TR OL Rt10 9RIVrS WR 046766 f 4F.d OR IVES Pi:R PROCFOURFS, PF4 FORMED PROCEDURE AND FOUND NO 3-705-002 PREVENilVE N/A LPRM 32-25-0 (CH. 51 WR 04d%9 PR01LFMS RFt1HvFO OLO ACCUM AND INSTALLED NEed ONE CR0 ACCUw P-4 154-311 CORRECTIVt N/A KR 046466 PER PROCEOURE
D* T SUt N II'll T $
SAFEff RE L A T Eu.4 41't I F.4 A t4C C
.44TO4r (W LFR OR OUTAGL M A L FUflL T IO'a 6 0 J I e"' L 'a i M A l t4 T t'I A *47.F SU'4F R CAUSC PESULT CURRFC TIVE ACTION R rPL AC E D TwD F A?4 PE ARINGS AND TWD DELTS 3-ST41 CUR 4rLTIVt it/ A HPCI ROF CoutF R Wn U4JE47 305-12T PRf vr*4T IVt N/A TIGHTFNED T*fd FDUR PACKING NUTS, LEFT OK OCCUMULATOR 18-3%
WA 049090 3-3JS-101 CODRECTIVE N/A IN ST ALLED I4E W ST EM AND 0150 ASSEMBLY ACCON 22-19 SL9A" 101 l '4L t T WR D49301 WITH NLW FLEXITALIC, LEFT DK VALUE DI SASSEMuLED V AL VE, IN SP EC T ED INTERNALS, 3-305-101 CURRECTIVE tt/ A ACCUM 02-39 WR 049307 INSTALLFD tif.e STEM AND WEDGE ASSEMBLY SCRAM 101 I..L E T VALVf AND GASKET, LEFT OK DISASSEMBLED VALVF, INSPECTED INTERNALS, 3-305-1u1 CURdECTIVE f4/ A QC C U*
10-*3 WR J49391 INSTALLED teFW STEM Af40 WEDGE ASSEMdLY SCR AM 101 f t.L L T VAldF AND GASKET, LEFT OK DISASSEMBLED VALVE, INSPECTED INTERNALS, 3-305-1J1 COPRECTIVF F4/ A ACCUM 10-4f WR 049104
[NSTALLED I4EW STEM Af40 WEDGE A S SE M P,L Y SCRAM 101 !!4LET V ALVE AND GASKET, LEFT OK 4
DISASSEMBLED VALVF, It4 SP EC T E D INTERNALS, 3-305-101 COPHICTIVE N/A A CC U!1 18-31 WR U4930%
INSTALLED NF4 STEM AND WEDGE A S S Et'3L Y SCRAM 101 IHLET VAL /f At:0 GASKET, LEFT OK DI SP SSEHdLED V At VF, INSPECTED INTERNALS, 3-305-1J1 C09RFCTIVE N/A ACCUM 26-39 WR d4930s
[t4ST ALLED f40.e S T E*1 AN3 WEDGE ASSEMBLY SCRAM 101 INLLT V AL Jr Af40 G ASMLT.
DISASSEMdLED VALVE, If4SPECTFD INTERNALS, 3-305-lut COPRFLTIVt "a/ A I
ACCUS 02-23 WR 04d337 INST ALLE D (4t W WFOGL AND STEM ASSEM3LY SCRAN 101 INLEI VALU A*JD G A SKET I
3-335-101 CukRFLTIvt tt/ A DISA SStM3 LED VALVF, INSPECTED INTERNALS -
ACCUM 10-19 WR 049304 INSTALLED NEW STEM Ai40 WEDGE ASSEMBLY SCROM 101 l at. L T VALVF AND GASKLT
)
)
~, --- -
T4 i '.n.4 U d i T 3 r
).
S AFEVY HI L AirD MAINTrr n'4CE e
'4 A it U OF LFR 00 DUToGL F1ALFONLT101 t00!P'1L'ff
" A I N T L*l A'JL'
'luti;5E d.
CAUSE RESULT CORREC TIVE ACT IO.4
)
3-305-101 COPdELTIVE f:/ A O!SSSSEMitLtD VALVF, INSPECTED INTERNALS, ACCOM 10-31 SC*A" 101 f fet ti Wd 947 V INiTALLFO NE. STEM Ar4D WEDGE ASSEMdLY VAltf Af40 GASKET 3-3o5-101 C ajp grt T IVt
'l/ 4
^--------- ---------
OISASSEMcLLD VALVE, INSPECTED INTERNALS ACCU'i ')6-23 SL9A" INLLT VALVF WR J49110 IM1TALLED f4Cd STEe Ar4D WEDGE ASSEM3LY ANO GASKET 3-305-101 00pdECTIVc N/A RFMovFD OLD STEM AND DISC, INSTALLED
)
ACCU?! 10-23 S C R A'1 I NLti T VALVE W4 U49312 UEW STEM A.iD DISC ASSEMBLY WITH NEd FLEX!TATIC
)
CAD $4-31 Paf Vct4T IV E N/A ADJUSTED PACKING ON SCRAH OUTLET VALVE WK J47335 STEF
)
00 I ts u l - 21 COReFCTIVE N/A.
INST ALLF0 f4Ed VALVE WITH 2 NEW GASKETS, WR D49449 ADJUST ED P ACKING GL Af40, LEFT OK DRYWFLL CAM CAS ROTILE CURRICTIVE N/A REBUILT REGULATDa AND VERIFIED NJ LEAKS, REGULATOR W4 049469 LEFT OK 0
L I M I T OR JU c 2101-47 CORRf C TI'/t N/A HEPLACED CRACKED TOP HOUSING, G A SK E T S i
j WR u49524 A40 w0RN GEAR TEETH, REGREASED, LEFT OK
)
NO-3-3703 CORRFCTIVt N/A INiTALLED NEW PACKING, LEFT OK WR ;)4 96 7'e
)
50 3-2599-lo PRE Vf NT IVf-
F LO'4 CO!4 TROL WR 050396 FOR CLOSE AN0 ODEN LIGHTS
)
D3 ft0-TIOS COPRFCTIVE
'l/ A DISA5SEMBLED LI:41TORQUL AND CLE ANED Wd 010R94 I N T E 4'4 AL S, REASSEMBLLD USING NEW (A SKET S ANO JUAD R INGS, AND GREASF c
i
?Rf 5DE'l 18'41 T 3 SAFETV nE L A l00 H 4 ttitr!4UtCE
<4 A Teter or led OR DJTAGE H ALFUNL T IO'8 Equipnesi M414Tir34NC6 tiO* if d CAOSt RESULT CORPtCTIVE ACT IO44 dEPLACEO MOTOP AND COMPLETED "0 TOR MJV 1001-1A l'Rf vF '4 T I-V E N/A WR 05075?
TFST, LEFT OK f
M-11RFD-579 EOORECTIVE Pf/ A ADJUSTEO SPRING HANGER TO COLD LOAD HPCI IURPIf4; SittM 5tlP P L Y LINE WR 4%1130 SETTING, TIGHTENED ALL JAM P4UTS, LEFT OK SUPPORT MdV 2301-36 PRfVfNTIVE N/A CLEA?dEO A 40 REPL AttD GRE ASE IN GEAREO WR 05145?
LIMIT SWITCH AN9 REPLACF3 WIRING AP4D CONNEC T ORS h
REPA IRED PEPIETR A TION PER PROCEDtlRE X204L, X2045 PRf VF '4 T IVE P!/ A j
ELFCTHICAL Pf f4E T't A T 10:45 WR 051469 CLEARCD Jtt:10 ER LOG Ff4TRIES AND MADE U3 dil S SE S 30 Af4J l'i PW E V ET4 T I Vt N/A WR 051569 SYSTEM 81ACK TO NORMAL. LEFT OK I
INST ALLEO NT W HOTOR PFR edORK MO-3-1001-SA PR E VF ?4 T I V L "4/ A Wa 05)hu I NS T RtlC T I Oi45, LEFT OK I
MJ 2101-9 PRE /F f4 T I VE N/A RFPL ACED WIRE, CHAR 4GED CONOUIT E XI T, Wd 053509 COliPLETED MOTOR tr ADS At10 POWER CABLE I
SPLICES PER PROCEDURE, LEFT UK MJ1-1301-1 PR E vr ?.T I V E N/A REMOVf.O ANd nIS A SSEM3 LED MOTOR,T IE S WR 05 M4 3 HOLDING THE STARTER WERE 3ROKE, REPLACE 0 NOIDH, WORK WILL HE 00t4E ON WRO54906 T I GH T F.4 E0 F.I T T IN GS ON $0LEt4910 VALVES SCRAM SJLLNJIus P'4f VE NT IVi F4/ A I
WR 053761 PFR 6.0RK INSTRUCTIONS TO STOP LEAKS
)
MOV 2301-4 PRFdF4TIVE tJ/ A REPLACEO MOTOR PER PROCEDURE, LEFT 04 W.4 055909
)
)
)
ndF ;% 1 tral T 3 SAF L TY Rt L A f f u P4 A l*lTT'4 A*4C E 14A IUx F Of LEM OR OdTAGt
'1 A L F ll4 C T 10:4 20 V I P %'11 MA I N T i33'K F N U't. t +t CAUSE PhSULT CORRECTIVE ACTIO'4 3-20 3
'9, C.D,L P 4 F Vr.4 T I VC
'J / A WIRF0 VALVE et&?40LE UP 50 IT COULO '40T flE E L ECiv.0:4ATICS WR 053037 MOVED, RE*4JVLD Wi% S S-4 ST4RT UP 4
i 40JtiST(0 Lit *! T ARMS TO GET PROPER 3-1001-60 Pe< Ev F'4T I Vs f./ A TOROT, VEf4T VALVL WR 053'752 LIGHT IN0! CATION, LEFT OK REPAIRED UV M.M. OEPT ON WRC 55408 P/t3 Vt?4T VALVL 1691-22 PRf VF'4T ivE TJ/ A VR 053953 I
T IGH T E NED FII T itJG TO STOP AIR LEAK HCU 46-11 PREVENTIVL N/A WR 054781 TIGtiTr fJU FI TilGS AND STOPPE0 AIR LEAK HLU 5d-31 Pkf VF.4T IVE N/A WR D542ts?
I CLEANED IrTERNALS OF t0TH VALVES At40 3-IS?? 3 3 L3 4f' CU R RF C T I V t.
M/A "d" C054 PU 4P VAULT COULFR WR 054?M RE ASSE Malf u,LE F T OK ISOLATION VALVFS i
3-2 62-4 4-S t. -4 0 - $"
PRfvFNTIVE N/A TIGHTFNED PACKIPJG ON ALL VALVES, NO RECIHL Pil1P SUCTION CJO WR 054*156 LFAFING, A;4P CHECK TAKEN, LEFT OK I
DISCHAPGE V4LVES LT3-1641->A4Sa fORRFCTIVt N/A ORAINFO A'3D dACKFILLEO INSTRUMdNT LINES INSTPUMcNI L i ce0 5 3-1439A-l/2" 18 4 05 % ?/ A
.dI TH CLE AN DE'4[N. ELATER.
VERIFit0 A t40 3-163si'-1/2" PROPER O(4-SC AL E INDICATIO!1 0F LEVEL Ira C0rlTROL ROOM, LFFT OK M 0 3-310 t>
PRE V8.vi l vt-t;/ A PfktdRMFD It4 SP EC T I O?l A!40 REPAIRED #4 kR 055?41 WIRE, LFFT OK I
OPIS 3-15504/.n Pi<f vf;4T IVd f4/ A INSTALLED AND REMOVFD TFS T SET UP TO ISOLA i g 04 r unorosto Sif AP F LO.4 WR a% 2'4 3 ISOL. COND. ST6AH FLOW SENSORS PER MEiLR PituC LOUR E i
I
D R r S 0 6'l tri! T S SAFci( RFLATFO MPIflifNANCE.
4ATUkE OF LFR UR 09 TAC.t MALF9f4CTION E QJ I P ?tE*J T
- A l c4 T L'I A'4 E
'J U% F R CAUSE RESULT CORREtitVE ACTION MOV 1301-4 FRTvr?4TIVE tt/A RAVCHEMED INT ERN AL.*0 TOR LEADS AND We 055334 PERTO1 MFD W0itK PER TRAVELER, L E F T 0%
CH A%f D OUT ACCU.49L ATOR Afl0 USED NEW ACCUMul A T JP 5,- 31 PJ (O%[CT[Vc ti/ A WR 055422 0-RI!4GS A*10 GREASE, LEFT OK CR0 Accura 26-4T Ib-123 C up.R f C T I V t N/A RFMOVED OLO ACCUMULATOR ANJ REPLACED WR 055436 WITH flew Ordf, REPLACED UPPER At40 L0 DER 0-RIf4GS, L EF T OK i
INST ALLFO ANO REMOVED JUMPERS TO ACCU %
A CC U$t. RCO otuCK PH E VF t4 T IVE N/A
r WR US$4$9 FOR REFUEL li4TERLOCK CHECKS, LEFT OK 1
250V dAlfLRV, REACTUR 7L0a PRI VFf4T i vt tJ/ A MEPAIRt0 GROUP 4ED C ABLE WITH R AYCHE M BUS 3A WR 0554T%
RFPA[R SLEEVE PER PROCEDURE
)
50-3-0305-117 PRF VEi4 T IVL N/A TIGHTENED DOWN ON ALL F[TTINGS, LEFT OK WEST-wCST PANK tlT SOLFl40IOS WR 955%63 I
3-2301-4?
PREVENTIVE tt/ A RFwlRED LOCAL VALVE CONTROLS FOR VALVES MOTuP C ON T %L V AL VF P OS I T 1074 un 05560T IN HPCI R 00'1, LFFT OK It401C AT ING LIGHT S I
C*t 3 2,0 <,8 CORRrC TIVE fl/ A COMPLE TE D EQ INSPECTION PER PR OCE D UR E.
H202 M0faIIO3
'B' WR 055 % %
REPL ACE 0 R EGUL AT OR R2 APld TESTED GUGO.
1 Rhi49Vr0 SWITCHES - ARMS OtiLY, Af40 REFUfL GRAPPLL PRE vet 4T IVt ra/A I
WR 05$703 ENTERCU IN JJMPFR LOG b0dK l
PS3-Itot-21 CUPRfCTIVt
'l/ A RIPLACtD THF DAf1 AGLO PRF.SSURE SWITCH AIR Ii4L E T T O U P. Y.J t L L A9 WR 055706 WITH LIKL FOR LIKC, REMJUNTED SWITCH I
BU T TE RF LY VALVE PRESSORL SWITCH ON PICJ MOUf4T ttlG POLE, LEFT OK
)
)
)
W E> Ds N H:4I T 3 j '
SArtTV KELATfD NAINIritV4CE
'4 A I U4 E f4 LFR OR UUTAr.E MALFUNCTIO*4 c Q UI P'1U8 i
" A I t.T L N ANC r NU *t ii R CAUSE it E SulI CORPEC TIVE ACT 10'4 LPRM 24-STA COR R EL T I Vi-fi/ A IN3f ALLEO 'eEW CONNEC TOA, RCSPLICEO WIRE WR 05ST35 INTO CA'LE I.4 C Abt E TU;4NE L, LFFT OK I
3-2 03-I C f.
10 COPdECTIVt N/A A0dED 2 RINGS OF PACK!P4G TO "C" AND M5id WR D53712 1 41r4G TO "D" PSIV, LEFT OK
)
3-00-1601-5o CORRFCTIVe N/A INSTALLE3 NEJ GASKETS AND NEW VALVE, y
TORUS VLt6T VALVE WA 055e34 LEFT OK
)
REM 9VED COVrR, INSPECTED A 40 CLE AN60 HPCI LMHAUST VALHJM BME Ak ER S PREvrNTIVb H/A VR 055917 AND REINSTALLED COVER, LEFT OK
)
O!E5f.L 6f NEd AIOR PR E Vf, N T I V E N/A CLE 4 NF O SFLECTOR Sw!TCH AND REMA00 W4 056020 CONNECTIONS, LEFT OK
)
3-1601-21 VALVE PHEVF NT IVE t4/ A VEd!F IEn WIRING AND T ibHTFNED LOOSE LOCK NR 05*2047 NU T, LfFT 04 3-0297-091 CORRFCTIVt M/A FOUNO SPIP AL WOut40 GASKET TO Eit BAO 150L A T i d'4 VALVE WH 05604%
dEPLACLO WITH Nrw ONE, LEFT OK
)
f 3-0305-114 CURRELTIVE N/A TIGHTFNt0 tWr4 NET 210LTS ANO LEAKAGE CHECK V AL Vf. O.4 CRO ACLUM.
WR 0 5 t> o4 8, STOPPED, L t F T OK
)
3-tent-9A CURRFCTIVs
- !/ A T IGH T EW:D ONN A LL BON:4r f 30LTS, LEFT OK CORE $PMAY CHECK VALVE W4 056049
)
M01-1402-25u PREvFhTIVE t4/ A ADJUSTED PACh[f4G, LEFT OK CORE $ PRAY VALVt WR 05f>052
)
)
)
OF.OEN U s!I 3 SAFLTV HI L A T Lu Pf A It4T U4Q*4E E f4 A itJdF OF LFR OR 00106E M A L F tFIC T 10f 4 L OU I P!4LN T
'1 A I:4TENANCE NU'* 1f 4 CAUSt l'ESULT CORRECTIVE ACT10.4 ADJUSTED PACKING, LIFT OK M33-1402-25A PhE 'tE f 4 T IV L tJ/ A CORE SPdAY WALVE WH 056053 PREVP4 Tivi ti/ A
. TIGHTENED 00.4N ON PACKING 2. FLATS, LEFT 3-03d5-1?T V Altf t 0.4 CH O ACLUM.
WR a*6104 OK D
T IGHTENF D D0a4N ON P ACK ING 2 FL AT S, LEF T 3-030's-127 PRFVFNTIVE N/A g
VALUF 0:4 LRLD ALCu'4 WR 05o105 GK h
'I REPL ACED COMPO'4Et4T 03 0F ISOLATER ANO.
1540-ilA CORRECTIVE tJ/ A FLOW INST LPCI 2 SY Sit *4 WA 056141 PERF 1RMED PROCEDURE FOR C ALibR A TION g
AOJtfSTLD CLOSE Lif*lT AR*1 TO GET PROPER 10ieuS VtNT VALVt A0 3-1601 -6 0 PRfVrt4TIVE N/A POS 1T 10 4 l'iO I L A T 1078 W4 056142 INDILATION, LFFT OK
-l
)
RESET TR IPPED THERMAL UVERLOAD, CYCLED MO-3-3T02 Pf:E V E *4 T I VE N/A WR 056153 VALVE 3 TIMFS, LEFT OK 9
INSTALLED f4EW NOTS AND STUJS FOR COVER, EAST TORUS.i4ICH P R F V E til IVE N/A WR 056173 UPENED AND CLOSED E AST TURUS HATCH FOR b
CLt:A N I Nr., LEFT OK h
CLLANEO GR IT ' I f4 elbow OF PIPE OUT,
'A' LPCI SULT104 SPOOL P4f VE*4T I VE N/A
(
WK 05s116 REINSTALLED' SPOOL PIECE, LEFT OK RElt451 ALLED SPOOL PIECE At3D REPL ACEO 0.4E 030 LPLI iPOOL PIECt odF Vf r4 T IV L N/A WA 0561T7
!4U T THAT WAS LOST, CLFANED OUT GRI T FROM ELond 0F PIPt l
h SPJ"L PIECE INSPECTED JY 0.0.
At40 F 0 0740
'C0 LPCI St k. i l 14 S P O'1 L PM vfl 4 TIVI ta/ A WR O5 e>1 i n 10 P.L CL LI.84, LEFT UK h
l
)
)
3-F ih'd U 41 T 3 SAFcTy REL A TTO 1 A I'lT F'4 ANC c HATURF Tf Lf:R OR OJTAGL H A L F UN(. T I Oi, LQUIPME'!T M A l f 4 T LN 4*1CE NU'O C R CloSE SESULT CortR EC T I VF ACTIO4 ECCS $UCTIO, STR41?llRi Crjr.at CT IVE
'/A REMOVED STRAlf4ERS FOR CLEANINC. AND 14R 0 % 130 It4SPLCTION MY JC, REINST ALLEO USIFIG
)
NEW stuns ANO DOURLF
- JUTS, LEFT OF Sr4 U d' E p.
213al CopdECTIVE
'J/A
' LOOSErlLO F40T S JN CL AMP 30LTS, REPOSITION WA 3 % 227 CL A'?P, RE T I GH T E t4L O PeU T S, LEFT OK k
DRYhfLL PLR SON'Itl 1:4TI'LOCW P!t F VI N T I V E N/A REMOVFD 51RO!4GoACK FOR LLRT p
S T R O'iGU Af5 WH 0562TT
)
N03-3T02 V4LVL XFVFf4T IVE il/ A COMPLEIF0 wnRK PER PROCEDURE 5, LEFT OK WR 0 % 344
)
'n' PLC IRL LOJP SUCilu'l PetFVENTIVd N/A REPL ACED M0TUR At40 ELECTRIC 3 RAKE WIRE S M G-2 C 2-4 t' WR 056424 AND SEALTITF, RFPAIRED DAMAGED INSULATION ON HOTOR LEAD, LEFT OK
)
12SV.DC GROJ'40 PR E VE ta T I V L N/ A TR4CEO GROUND TO CONT ACTS ON MO V ALVE.
)
WR OSo451 blue AND RED-BLACK WIRES OF CAdLL.ARE GROUNDED
)
'A' LPCI SPJOL PRE VEf4T I VE N/A RE99VED AND INSTALLED SP0OL PIECE.4ITH WR 056505 14E W GASKETS, LEF T OK
)
)
'O' LFCI % Punt PRFV0NTIV[
ft/A REM 9VED.AND INST ALLED SPOOL "IECE WITH WA 056506
?4E W G ASMCTS, LLFT OW
)
'C' LPCI SPattL P R E V F :4 T I V; f4/ 4 RF90dFO AND INSTALLEO SPOOL PIECE FOR
)
WR 996507 INSPECTION, INSTALLED WITH NEW GASKET d
'O' LPCI kront P.tf VF NT I VE
'J/ A AFA0VfD SPOOL PIECL Fat INSPECT 104 A 4D WR 0%su e REIN ST ALLEO.41 TH NEW GASKETS
)
)
)
(
~~
I'RE sDE *f II 41 T 5 SAFETY dF L A f ru tis I* sit '44t4C E
==
%ATff(E Of LFR OR OJTAGt H ALFu*aC T I ON C Qu f o'ic*s t ti t ! '4 T t *! C4C F NU" )E R LAUSE PESULT C04RECTIVE ACTION MJ3-1301-4 w A t'/ t; Pitf V 0 r4 T I'/t!
'l/ A CHECKr u LI:tlTS A t40 TORQUE PER WORK i
NR 15a*Td INST RUC T 10'45, FOU*l0 140 PR0dlk 9 ADJU3TED C0f4T AC TS, CYCLLO VALVE, LEFT OK 30-1501-4'.
P*EvF14TIVE N/A INSPtCTED PUMP INPELLER, FOU'40 NO CCSd P U.4 P WM 056630 PRO 3LFMS, MA00 NEW GASKE T S FOR PUP'P, RFPAfELO PdMP, LEFT OK l
i 3-00-41A CORRFCTIVE N/A REPLACEO PdWER SUPPLY At40 ADJUSTED PER 1001 CHAMMLR POWLS SUPPLY FOR WP 0566T4 WORK IN ST R UC T ION S, LCFT 04 LPRM CLEA!aFD GASKET Aten SEAT AREA, QC 3-1402-26C CORRECTIVE N/A H CORL SPRAY SUC T 10.4 VALVE WR 056721 IN SP E C T E D, it4ST ALLLD LOCK TI TE ON G ASKE T, LEFT OK ORYaELL I!4 T c p L OC K DJOR ^TRONG PREdFNit'E tt/ a 1*IS1ALLFD AN) M MOVE 0 STRONGaACK FOR V
HACK WR us6724 TEST, IOROUEU AS REQUESTED, LEFT OK fl ACK FLUSHED TR AN S*4 I T T E RS PER WORK T R A t4S M I T i t P S PREVF:4TIVE f./ A KR 056725 1*4S T RUC T IO.'45, L E F T OK CO'iPLFTED 3ALKFILL OF TRANSMITTERS PER CORE SPdAY I R A %** I T I C d 5 PREVFi4TIVt N/A WR 056726 WORK I N S T R UC T I O*4 5, LEF T UK CG'1PLETED UACKILUSH!r4G OF T R A *4S M I T T E R S CORE SPdAY I Lij 4 T A ANS:11 T TEC 5 PdE vf fv T I VL tt/ A WR 056727 PER w0RK I rwS TRUC T I ONS, LEFT OK FT 1461 ALn pgr v r*4 T IV E N/A CHLC AED C ALI3R AT ION OF T R Ai45til T T ER S W4 055791 PER PROCEDURE, LOOKS GOOD 3 CCSu e tda T x A atili t t*t PRrvrHTIVc st/ A CAllapATeo, COMPLETED TESTING PER 40RK WR 05677?
I N S T n UC T 10r.5, A*30 PERFORMED PROCEDURE
O d 20 L'1 H i! T 1
", Al L' T f RTL A T EJ 4 A I*J T C!{ U4CE.
NnTUgr GF L(R JR OvfACL e* A LFP30 T I C1 t 90 l P"t'l l M A I '4 T t *4 a'tC t~
Nu $ F R LAUSE RESULT CORR nC TIVE ACTIDN
)
ACCUP'OL A f ur 3 tt -21 CGRULTIVE
- t!/ A RE tinVF D SWITCH AN") FUNCTIONAL CHECK OK, W 't u s e, 7.3 %
FOPf D 140 PRO 3LEMS
)
RFMnv00 LEvfL iW I T C H A N') INSPECTED, LS 3-3') 3-12 e r uP REL T Ivi N/A CRD ACCOM S0-)I WR 05*3798 F0d!40 NO PRC sLEMS, REI1ST ALLE0 SWITCH 4'!D VFRIFIED ALARM CLE AR ED '
)
)
A CAD / CAM H202 SO1 plt PUMP CORRECTIVE N/A ret 10VED HEADS AMD CLE AF ED INTERNALS
'd' S Y S T E.1 wk 0%f.797 At40 CHECK 0 RituG S, L EF T OK
.)
CR0 Ob-15 CORRFCTIVE f t/ 4 INSP EC TED SWITCH AND FOUNO tO PROPLEN ACCUMULATUR WR 0 5t,7'#8
)
ftEMOvFD ULD ACCUM AtJO REPLACE 0 WITH ACCUMUL AT.19 11.)7 COR:lFC T I VE N/A WR Os t,79 ')
NEW UNE
)
CHA%EO ACCUPtVL A TOR 10-51 PER PROCEDUR E ACCUMulATOP 10-51 EJkdfCTIVt t!/ A g
wk 056800
)
't CRO I4-51 ALE U'1UL A T OR C.)PRf t. T I VF tJ/ A CHANiEO ACCUMULATOR 14-51 PER PROCEDURE WR M/, pol
)
1402-4J COPRfCTIVt FJ/A CLEANED ALL FIT ARLAS AND GASKET AND VALVL WM D5 6" O'-
RFPACKLD, LEFT OK
-)
3-13N C O R d f.C T I V t.
f t/ A RAie ROD OOWN VALVE A40 LINd THEN
)
I SOL A l l a f u"40L.45tR SA"PLE LI:4F WK US f,a 0 7 6 ACK F L USHEO, LINE IS NOW CLEAR
)
150. Lordo C uNar NS A f t HIGH FLO4 Phrvtr4TIVE N/a PERF URMEO PRdLLOUA L AND b4CKFILLEO WR J%"95 SE NSitlG LIHFS, STARTED
'A' RLCIRC P U *iP Al40 VER IF IED Ido SPURIOUS 1 RIPS
-)
l-i
)
{
A
OklS D d*1 U.41 T ' 3 SAFEi1f RFLATFU H A l*lt F MQPdCL
- 44 TURF pr Lyg up pji a,g fggtr gNty g gt; a
t0JIPMLNT P A t:17 t *! A' Cr flu!!3 E W CAU"E PESULT CURRECTIVC ACT10:4 P S 3-2's 40-20 PREVENilVd is/ A CHtCKru CALI3PATION AND FOUND THE SWI TCH OC AO CO:iPK( SSJ)
WR 0%t."31 TO LE UK I
CR0 Ot,-47 I
.1-1/ )
00PitF L T IVE N/A REPLACEO PRESSURE SWITC'i AND 94 0%%0 CALIBRATED PLR PROCFOURE, LEFT OK I
CRD 38-15 IK-43 CJR4t L TIVE N/A CH ANGE0 ACCUMUL A IOA PEA PRJCEDURE w4 05 f,95 I
?
APRM t CORaf L TIVt N/A A0 JUSTED MET ER MECHANICAL ZERO ADJUST TO WR b%909 2ERO INDICATION WITH ZER0 VOLTS,
)
ADJUSTED FOR PROPER EXPAND lt401 C AT ION I
CRD 02-47 (3-185 PRbSSURF AND PR E VFlil I V E N/A CHA%ED OUT 9ROKEN PIECE OF C0r40UIT AND LEUEL SallCH LOi490! L E i WR U56995 UNE CONNECTOR, LEFT OK
)
- 1 Olt SLL 6tNeit Af uR OREdfNilVL N/A PERF URMF D QU AR TERLY I'ISPECTI0ta AND DIO WR 057000 GEi4F R A T OR SURGE SUPPRESSOR TEST PER PRUCEDURES
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REPLACE 0 CD'liRut VALVES AND 0-RINGS PER 305-12l,122,12.5 PREVENTIVE N/A E-9 END l 6-15 WR 057012 PROC CDURE
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3-305 ACCUP P-9 (54-31)
CUPRFCTIVE
- f/ A INST ALLFO Nr.i ACCU!40LA TOR PFR PR OC E DUR E WR 13570T3
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l 3-305-12 J-6 6 % -213 EURHrCTIVE M/ A REPLActD VALVT SEAT PER PROCEDURE, I
ud 05712".
A0JUSit0 SifM PER AORK I NS TRUC T I ON S
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RF ADJUST t-0 GOHNSCALF TRIP AND CHECKE0 LPRit 40-4'4.
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D8F5054 U eli 3 SOFETY AFLATED 4914'I f it W4C C NLIURF DF LFR Ott OUTAGE
- MALFUD?tilO.4 L CU I P'9E N T H A I N T UI A*lC F t8UNE d.
,L A US t-4ESULT COAPECTIVf ACTION M-t lll LPH" CUP 4FCTIVE f4/ A AFPL ACt O LIGHT RULb A!40 PERFUftMEO Wa 051130 PRUCLDURL TO CHECK UPSCALE AND DOWNSCALE IPIP RE ADJUST ED UPSL ALE TRIP A40 CHECKE0 LPRH 24 -2 5C CORKfLTIVE N/A WR 05T131 00#4SC ALE AL ARM PER PROCCDURE LPR:4 16-OdC CURRFCTIVe f 4/ A RE ADJUSit0 UPSCALF TRIP At3D CHECKED WM 05713?
DO#3SCAlt ALARM PFR PROCEDURE INST ALLFO AND REMOVED JUMPERS AT ROD CRD J-6 PRCVINTIVE
'l/ A W1 05 T 117 SLOCK FDR SHOP REPAIRS ADJu ST ED HIGH GHOSS F A ILURL AL ARP1, TRIP HPCI PRLSSU4f T R UIS'il i it R CORRCLTIVE FJ/ A WR U57199 SETPOINT PER PADLEDURE, GROSS FAILURE TROUaLE AL ARM IS NOW CLFAR
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PUT LIMITS PACK UN, ADJUSTED L IMI T HPCI 2101-6*
Pd E V f'4 T I VE
'4 / A WR D51703 SWITCH AND CYCLED THREL itMFS, WORKS PROPERLY NOJ M SL R OD 't )N ( T UR PRFVENiiVL tJ/ A CD'4PLETfD APPt IC APLF SECTIONS OF WR 057225 PROCEDURE, NO SPURIOUS TRIP OCCURED 2301-10 VALVF P k F VF id 71 Vc N/A ADJtlSTED PACKIf4G TO ELIMINATE LEAKAGE WR 05774')
1402-25A VALVL P,4 F Vi r4 T I VE f t/ A ADJUST c.O P AC AI'4G TO ELIMit1 ATE LEAKAGF Wrt 0%T24I MOV 1402-,l1 PM V5NT IVE N/A RF3190*ITF D AP!J RELONNEC TEU NOIGA, W.
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ItasTALLED L ST ACKS A?e9 SCT LIMITS
0(fi9d*4 UIIT 3
- Ar1 TY Rf L ATE D *t a g NIENA 4C N410df OF LFR OR CUTAGE
- t4LFJNCT101 LOUIPriE*f f "41NTFMANLE NU'1304 C AUiti FE* ULT C04RECTIVE ACTION REINSTALLFO RETAINER AND R E A sSE N 3t LD VALVC 1591-15A COP 4fCTIVE
?!/ A WR OS T ? T'l V 4LV E 1*a UPPER l'E A R I.4G HOU S ING, RE SET LIMITS, LEFT 04 IN$T ALLF0 A'40 CAL!cR ATE 0 A ROSC**0U;4T 8 C05.4 PU4P ILog I R A*1V41 T i f R ParvfNTIvt N/A W4 057779 1151 LEVEL T R Af4SMI T TtiR TO TEST FLOW FROM THE CCSW PU"P FOR TEST, RE:10VFD ROSEMOUNT T R A'!S** I T T ER AFTER TEST,LEFT OK LPCI HE OPT l-1503-A Pd EV fiel I VE
- /4 CHEE KEu PRESSURE, BALKiluSHED BOT 4 WR D5T/o9 TRANS'*!TTER LEGS AND PRESSURE CHECKED 154E SAME, OETERMINEO LPCI
'A' HEAT EXCHANGOt LFAKS 3-1404-6C VALVF EURn0CTIVE tt/ A RFMOVE0 BO 4*4 t i AND PLUG, CLEANED Ai4D WA 057347 INSPECTED INTfRNALS, REASSEMJLED PER
.40RK IF45 TR UC T I J45, LCFT OK RE ADJUST ED HIGd VOLTAGE AND VERIFIED I R a4 CH 1H CORRFC TIVe f1/ A WR 057359 PROPER SETPOINT PFR PROCEDURE, LEFT OK CV3-0305-l'l CORKFCTIVE N/A LOOS ENED C OUP L IN t, t,0LT, ADJUSTLD LUWER CR0 K-? 139-bl W't O'. 7 3 3 0 SitM TO LEt4r.THEN STROKE, TIGHTENED COUP L I NG BOL T, L EF T OK L PR r4 48-4J-a CH.;3 CORRrLTIVE N/A PERFORMFD PROCEDURE, CLFANED CONNECTOR-WR 057606 LnoKS OK t4JW 3-1705-11 f.OR H F C T I V L M/4 df AllGt4F0 Rf CORDER PENS AN0 CAlluRATED.
MAIN STLA3 L i tet, rt40 phC.
yg 957612 PFR PROCEDURE, LEFT OK REM-T Ai40 0 Pard'4TIVL f,/ A CO1PLE TFD PROCtDU7 E FOR PROPER FLOW WA Os FN17 INDILei!ON, LFFT OK DRYalLL W M ini4*ltL I.'4 T E9t D0 K Purvi.TIVL ti/ A IPliT ALLf D Af4') Ar MOVE D STR04BACK FOR SIRONGGACK WR a517f1 TEST, LFFT OK 4
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04 EiDO4 O'4! T 3 SAFLTY RELAIED MAINIFMANCE
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I 3-1402-353 r OR4f LT IVe N/A DI S ASSL** bled V AL VE, Shit 4ED PARTS WITH CORE s"kaY STOP OtrCK VALVf WR 95T7HS CMERY, REASSLM3tED VALVE WITH ORIGINAL 8
G A SK L T, LEFT OK WES i f NGitO'J S t LPd" COPtfCTIVE O/A PFRFdoMED PPUCEDURL OFI LPRM, LEFT OK WR DSF821 3C-1502 PRFVf'at IVE PJ/ A REPL ACED SE AL TITE ON FIT TI'4GS ON MOTOR LPCI PUMP 'id T UR WR 051893 SPACL HFATER, LFFT OK
. CHECKED AIR L I ftr Af40 Flfilf4GS, SNOGGED 3-107-12T CaRRf.CTIVE N/A CRD 16-31 WR 057aio 00#! 4 LE AKIt4G BUL TS T IL L LFAKS STOPPE0, FOUPID i40 MdRE LE AK S.
DW AIRLOCK S T R ONr H A (.F PRF V fi4T I V E N/A
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1501-2 % VALVt.
PRE /C.4 f l Vt il/ A REPL ACED TORyOE SMITCH PER PROCEDURE, WR 95d03?
CHECKED LIMITS AND LaOKED GOOD 250V MITEG if S Pet r /F:4 T I V t:
N/A CLEAlfD BATTERIES AND PERFORMED i
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PR OC EDURE i
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D/W AIRLtik S I R u'!G3 AC A PRE VE '4 T I Vt N/A R O M")VL D Sik O:4Gd A CK AFTER LLRT TFST E 0 %5"-89 COMPLETED i.
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UNIQUE REPORTING REQUIREMENTS
. MAIN STEAM RELIEF-VALVE OPERATIONS Relief valve operations during the reporting period of November, 1986 are summarized in the following table. The table includes information as to which relief valve was actuated.how it was actuated, and the circumstances resulting'in its actuation.
Valves Description Unit Reporting Period Actuated Actuations Conditions of Events 2
11-01-86 to 11-30-86 None 3
11-01-86 to 11-30-86 None
1
SUMMARY
OF OPERATING EXPERIENCE UNIT TWO NOVEMBER, 1986 11-01-86 to 11-30-86 Unit 2 entered the month operating at a power level of 650 MWe and operated continuously at maximum core flow (coastdown) until November 29, 1986 at 0916 hours0.0106 days <br />0.254 hours <br />0.00151 weeks <br />3.48538e-4 months <br />, when the turbine was manually tripped off-line to the unit's tenth refueling outage..The reactor was manually scrammed at 1703 of the same day when the mode switch was purposely moved from "run" to
" shutdown" mode.
Capacity factor for the month was 70.26% and avail-ability was 94.62%.
I
A
SUMMARY
OF OPERATING EXPERIENCE UNIT THREE NOVEMBER, 1986 01-86 to 11-11-86 Unit 3 entered the month operating at a power level of 795'MWe and operated at maximum core flow until 1347 hours0.0156 days <br />0.374 hours <br />0.00223 weeks <br />5.125335e-4 months <br /> of November 10, 1986, when an automatic reactor scram and turbine trip occurred as a power lead to the drywell air supply of the inboard MSIV's was inadvertently lifted by an I.M. during changeout of a control room recorder. The reactor was made critical at 1118 hours0.0129 days <br />0.311 hours <br />0.00185 weeks <br />4.25399e-4 months <br /> of November 11, 1986 and the turbine was brought on-line 1803 hours0.0209 days <br />0.501 hours <br />0.00298 weeks <br />6.860415e-4 months <br /> of the same day.
11-12-86 to 11-15-66 The unit operated, steadily increasing power until 1058 hours0.0122 days <br />0.294 hours <br />0.00175 weeks <br />4.02569e-4 months <br /> of November 13, 1986, when an automatic reactor scram and turbine trip occurred ~as the feed-breaker to the ESS was inadvertently opened by an E.M.
during maintenance activities. The reactor was made critical at 0404 hours0.00468 days <br />0.112 hours <br />6.679894e-4 weeks <br />1.53722e-4 months <br /> of November 15, 1986, and the turbine was brought on-line at 1828 hours0.0212 days <br />0.508 hours <br />0.00302 weeks <br />6.95554e-4 months <br /> of the same day.
11-16-86.to 11-30-86 The unit operated the remainder of the month steadily increasing load (except for normal weekend surveil-lances) reaching a power level of 815 MWe with an availability of 88.37% and a capacity factor of 73.53%.
O Commonwealth Edison Dresden Nuclear Power 9tation R.R. #1 Morris, lilinois 60450 Telephone 815/942-2920 December 1, 1986 EDE LTR: 86-208 Director, Office of Inspection and Enforcement United States Nuclear Regulatory Commission Washington, DC 20555 Attention: Document Control Desk
Dear Sir:
Enclosed, please find Dresden Station's operating data for the month of November, 1986. This information is supplied to your office per the instructions set forth in Regulatory Guide 1.16.
Sincerely, C
E. D. Eenige urg s
Station Manager Dresden Nuclear Power Station EDE:DCM:hjb Enclosure cc: Region III, Regulatory Operations, U.S. NRC Chief, Division Nuclear Safety, State of IL U.S. NRC, Document Management Branch Nuclear Licensing Administrator Nuclear Fuel Services Manager Nuc. Sta. Div. Vice Pres.
Manager, Tech. Serv. Nuc. Sta.
Tech Staff A.E.
(2)
On-Site NRC Inspector Sta. Nuc. Ung. Dept.
Sta. Q.A. Dept.
Comptroller's Office PIP Coordinator INPO Records Center File /NRC Op. Data File / Numerical
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