Letter Sequence Other |
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Results
Other: ML20151L878, ML20215B790, ML20215B804, ML20215G101, ML20215G650, ML20215G653, ML20234D077, ML20236D570, ML20236F145, ML20236F153, ML20236F168, ML20236M855, ML20236M871, ML20237J052
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MONTHYEARML20215G6531987-06-11011 June 1987 Trojan Nuclear Plant Evaluation of Main Feed Line Seismic Restraint Failure Project stage: Other ML20215B7901987-06-11011 June 1987 Forwards Evaluation Rept of Main Steam Pipe Wall Thickness, Describing Fatigue & Finite Element Analyses Performed on Affected Piping,Per ASME Boiler & Pressure Vessel Code.Affected Piping Will Be Reexamined in 1988 Project stage: Other ML20215G1011987-06-12012 June 1987 Forwards Evaluation of Displacement at Main Feedwater Restraint SR4 in Trojan Nuclear Plant & Trojan Nuclear Plant Evaluation of Main Feed Line Seismic Restraint Failure, as Result of Failure During 1987 Refueling Outage Project stage: Other ML20215G6501987-06-30030 June 1987 Evaluation of Displacement at Main Feedwater Restraint SR4 in Trojan Nuclear Plant Project stage: Other ML20234D0771987-06-30030 June 1987 Advises That Util Agrees to Complete One of Three Listed Actions Re Resolution of Main Steam Line Wall Thickness Issue Before Startup from 1989 Refueling Outage Project stage: Other ML20215B8041987-06-30030 June 1987 Evaluation Rept of Trojan Nuclear Plant Main Steam Pipe Wall Thickness Project stage: Other ML20236F1531987-07-17017 July 1987 Final Rept Trojan Nuclear Plant SR8 Failure Root Cause Evaluation Steam Condensation-Induced Water Hammer Project stage: Other ML20236F1451987-07-27027 July 1987 Forwards Bechtel Western Power Corp Final Rept, Trojan Nuclear Plant SR8 Failure Root Cause Evaluation Steam Condensation-Induced Water Hammer & Impell Corp Summary Rept, Independent Review of Action Plan Items.. Project stage: Other IR 05000344/19870261987-07-27027 July 1987 Insp Rept 50-344/87-26 on 870706-10.No Violations or Deviations Noted.Major Areas Inspected:Licensee Action on Previous Insp Findings,External & Internal Exposure Control, Control of Radioactive Matls & Contamination & ALARA Project stage: Request ML20236D5701987-07-27027 July 1987 Advises That Util Plans to Resolve Issue Re Code Acceptability Applications Prior to 871201.Util Will Perform Necessary Design & Order Matls to Repair or Replace Unacceptable Main Steam Line Wall Thickness Areas Project stage: Other ML20236L3451987-07-30030 July 1987 Summary of 870617 Meeting W/Util,Bechtel & Impell Re Results of Analyses Concerning Accumulator Fill Line Failure,Main Feedwater Failure & Main Steam Line Thin Wall at Plant.List of Attendees & Viewgraphs Encl Project stage: Meeting ML20236F1681987-07-31031 July 1987 Rev 1 to Summary Rept, Independent Review of Action Plan Items to Resolve Trojan Main Feedwater Piping Restraint Failure Issue Project stage: Other ML20237J0521987-08-21021 August 1987 Responds to Util Proposing to Resolve Issue Re Main Steam Line Wall Thicknesses Which Did Not Meet Min Requirements.Util Adequately Demonstrated That Safe Operation of Plant Until May 1989 Will Not Be Compromised Project stage: Other ML20237J2151987-08-21021 August 1987 Advises That Technical Issues Re Accumulator Fill Line Failure & Main Feedwater Pipe Restraint Failure Adequately Addressed by Licensee.Summary of 870617 Meeting Encl.W/O Encl Project stage: Meeting ML20236M8711987-11-11011 November 1987 SER Supporting Util Repairs Proposal Re Accumulator Fill Line Failures Project stage: Other ML20236M8551987-11-11011 November 1987 SER Supporting Util Repairs Proposal Re Main Feedwater Line Restraint Failure Project stage: Other ML20236M8371987-11-11011 November 1987 Forwards SERs Re Main Feedwater Line Restraint Failure & Accumulator Fill Line Failures at Plant.Repairs Proposed by Util Acceptable to Ensure Integrity of Damaged Sys for Continuing Plant Operation Project stage: Approval ML20151L8781988-04-15015 April 1988 Forwards Addl Info Re Six Open Items/Recommendations Noted in NRC 871111 Safety Evaluation of Failure of Main Feedwater Sys Restraint SR-8,per Commitment During Audit of long-term Pipe Support Design Verification Program in Jan 1988 Project stage: Other 1987-07-17
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ammum Portland General ElectricCorpEnTy
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David W. Cockfield Vice President, Nuclear June 11, 1987
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Trojan Nuclear Plant
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Docket 50-344 i
License NPF-1 i
U.S. Nuclear Regulatory Commission
. ATTN:
Document Control Desk j
Washington DC 20555 l
j
Dear Sir:
-l Main Steam Line Wall Thickness I
During'the 1987 refueling outage, inspections were performed for the purpose of identifying areas of erosion / corrosion in secondary system piping. Por-tions of the main steam lines were included in these inspections. While j
performing ultrasonic wall. thickness measurements on the "B" main steam j
line, an area at the outlet of the steam flow venturi was identified as being below the specified minimum wall thickness.
Further examination revealed the same condition exists at the venturi outlet for the "A",
"C",
and "D" lines.
l The cause of the wall thickness discrepancy was machining of the pipe spool in preparation for installation of the venturi.
In order to demonstrate the acceptability of continued use of the affected piping, fatigue and finite element analyses were performed in accordance
.with Section III of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code. These analyses are described in Attachment A.
As further verification that wall thinning is not occurring in the area, the affected piping will be reexamined in 1988.
Sincerely, I
Attachment c:
Mr. John B. Martin Regional Administrator, Region V
. U.S. Nuclear Regulatory Connission Mr. R, C. Barr 1RC Resident Inspector Trojan Nuclear Plant l
Mr. David Kish, Director State of Oregon q
Department of Energy 8706170451 870611 PDR ADOCK 05000344
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121 S.W Salrron SUeet Pomand. Oregon 97204