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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 ML20249A7661998-06-11011 June 1998 Safety Evaluation Supporting Amend 222 to License NPF-3 ML20249A7551998-06-11011 June 1998 Safety Evaluation Supporting Amend 223 to License NPF-3 ML20216B9401998-04-15015 April 1998 Safety Evaluation Supporting Amend 221 to License NPF-3 ML20216B8381998-04-14014 April 1998 Safety Evaluation Supporting Amend 220 to License NPF-3 ML20202C6131998-02-0303 February 1998 Safety Evaluation Supporting Amend 219 to License NPF-3 ML20199J9511998-01-30030 January 1998 SER Related to Exemption from Section Iii.O of App R,To 10CFR50,for Davis-Besse Nuclear Power Station,Unit 1 ML20198R4771998-01-13013 January 1998 SER Approving Second 10-year Interval Inservice Inspection Program Plan Requests for Relief for Davis-Besse Nuclear Power Station,Unit 1 ML20203C1401997-12-0202 December 1997 Safety Evaluation Supporting Amend 217 to License NPF-3 ML20203B2141997-12-0202 December 1997 Safety Evaluation Supporting Amend 218 to License NPF-3 ML20203C2701997-12-0202 December 1997 Safety Evaluation Supporting Amend 216 to License NPF-3 ML20138L0491997-02-11011 February 1997 Safety Evaluation Supporting Amend 214 to License NPF-3 ML20128L3001996-10-0202 October 1996 SER Supporting Dbnp IPE Process of Identifying Most Likely Severe Accidents & Severe Accident Vulnerabilities ML20058M9591993-09-28028 September 1993 SE Accepting Licensee Response to GL 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants.' ML20057A3791993-08-20020 August 1993 SE Concluding That Second 10-yr Interval Inservice Insp Program Plan for Plant Has Unacceptable Exam Sample as Discussed in Encl Inel TER ML20056G4301993-08-18018 August 1993 Safety Evaluation Re Inservice Testing Program Requests for Relief.Licensee Made Changes to Subj Program to Include Exercising & fail-safe Testing of Auxiliary Feedwater Valves AF-6451 & AF-6452,in Response to TER Anomaly 8 ML20126A3051992-12-0808 December 1992 Safety Evaluation Supporting Amend 176 to License NPF-3 ML20056B2721990-08-20020 August 1990 Safety Evaluation Granting Relief from ASME Code Repair Requirements for ASME Code 3 Piping ML20248H6371989-10-0303 October 1989 Safety Evaluation Supporting Amend 139 to License NPF-3 ML20248D8271989-09-29029 September 1989 Safety Evaluation Accepting Util 890228 & 0630 Submittals Presenting Proposed Designs to Comply w/10CFR50.62 ATWS Rule Requirements ML20248E2771989-09-20020 September 1989 Safety Evaluation Supporting Amend 138 to License NPF-3 ML20248B3801989-09-20020 September 1989 Safety Evaluation Supporting Amend 137 to License NPF-3 ML20247E6901989-09-0505 September 1989 Safety Evaluation of Audit of Facility Design for Resolution of IE Bulletin 79-27 Re Loss of non-Class IE Instrumentation & Control Power Sys Bus During Operation.Preventive Maint & Testing Program Should Be Developed for Bus Power Sources ML20245K1871989-08-15015 August 1989 Safety Evaluation Supporting Amend 136 to License NPF-3 ML20245F5791989-08-0404 August 1989 Safety Evaluation Supporting Amend 134 to License NPF-3 ML20245H9531989-08-0404 August 1989 Safety Evaluation Supporting Amend 135 to License NPF-3 ML20247J8731989-05-18018 May 1989 Safety Evaluation Supporting Amend 133 to License NPF-3 ML20245G0371989-04-25025 April 1989 Safety Evaluation Supporting Amend 131 to License NPF-3 ML20245F0631989-04-25025 April 1989 Safety Evaluation Supporting Amend 132 to License NPF-3 ML20244D4031989-04-13013 April 1989 Safety Evaluation Supporting Amend 130 to License NPF-3 ML20196D9601988-12-0808 December 1988 Safety Evaluation Re Util Response Concerning Auxiliary Feedwater Sys Reliability Study.Util Should Ensure That Sys Mods Do Not Result in Net Reduction in Sys Reliability ML20207K7911988-10-0404 October 1988 Safety Evaluation Supporting Operation in Cycle 6 W/O Removing Flaws in Cracked HPI Nozzle ML20207K1071988-09-19019 September 1988 Safety Evaluation Supporting Amend 120 to License NPF-3 ML20207H9271988-08-24024 August 1988 Safety Evaluation Supporting Amend 117 to License NPF-3 ML20207H3891988-08-19019 August 1988 Safety Evaluation Supporting Amend 116 to License NPF-3 ML20207E3931988-08-0202 August 1988 Safety Evaluation Supporting Amend 114 to License NPF-3 ML20207D5171988-08-0202 August 1988 Safety Evaluation Supporting Amend 115 to License NPF-3 ML20150C4621988-03-0909 March 1988 Safety Evaluation Supporting Amend 109 to License NPF-3 1999-08-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
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/[* -) Tif. 'n UNITED STATES NUCLEAR REGULATORY COMMISSION g%Q W ASHINGTON, D. C. 20555 SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION SUPPORTING AMENDMENT N0. 95 TO FACILITY OPERATING LICENSE NO. NPF-3 TOLED0 EDIS0N COMPANY AND THE CLEVELAND ELECTRIC ILLUMINATING COMPANY DAVIS-BESSE NUCLEAR POWER STATION, UNIT NO. 1 DOCKET NO. 50-346 INTRODUCTION By letter dated June 6, 1986, Toledo Edison Company (TED or the licensee) requested amendment to the Technical. Specifications (TSs) appended to Facility Operating License No. NPF-3 for the Davis-Besse Nuclear Power Station, Unit No. 1.
The proposed amendment would modify Surveilla ce Requirement 4.4.10.1.b to extend the surveillance period of inspection and operability testing of the Reactor Vessel Internals Vent Valves (RVVVs) to coincide with the next reactor vessel head removal but not later than the refueling outage following Cycle E operation which is expected to occur no later than March 1988.
Following review of the initial application, a telephone conference was held with the NRC staff and representatives of Toledo Edison Company and Babcock and Wilcox Company (B&W) on July 24, 1986 to obtain clarification and to request additional information. The licensee submitted additional information regarding mechanical design, materials of construction, comparison of Three MileIslandNuclearStation,UnitNo.1(TMI-1)andDavis-Bessedesigns,and chemistry of the Reactor Coolant System (RCS) by letter dated July 30,'1986 (No. 1292).
BACKGROUND In 1975, the NRC revised 10 CFR 50.55a to require an " Inservice Inspection" of various safety related components, including pumps and valves, to be performed in accordance with the ASME Boiler and Pressure Vessel Code,Section XI, "to the extent practical within the limitations of design, geometry, and materials of construction." The Davis-Besse TS Section 4.4.10.1.b requires that the RVVVs be demonstrated operable at least once per 18 months with a provision that an extension of 25% (4.5 months) may be granted for the 18-month period.
The RVVVs were last tested in accordance with the surveillance requirement on October 12, 1984 during the refueling outage for Cycle 5.
The refueling outage was completed in December 1984 and the facility was restarted in early January 1985. The core design for Cycle 5 allowed for 390 effective 86oe280233 e60820 PDR ADOCK 05000346 P
PDR
. full power days and, therefore, even with a capacity factor as low as 60%, the surveillance requirement could be met when the reactor vessel head was removed to refuel. However, in early June 1985, a loss of feedwater event occurred and the facility has not operated since then.
In order to meet the TS requirement, valve operability wnuld need to be demonstrated not later than August 27, 1986, unless the requested extension is granted.
The Davis-Besse facility is expected to be restarted about November 1986.
Approximately 12-13 months additional operating life remains in the Cycle 5 core. Therefore, refueling would not be expected to be required until about March 1988. Thus, the interval from the last surveillance test could be as long as about 42 months.
Toledo Edison provided a justification for the requested extension by reference to paragraph IWA-2400(c) of Section XI, ASME Boiler and Pressure Vessel Code, addendum of Summer 1978 which states:
...For power units that are out of service continuously for 6 months or more, the inspection interval during which the outage occurred may be extended for a period equivalent to the outage."
Toledo Edison noted that while the plant has been in the prolonged outage, the internals vent valves have not been exposed to the turbulent flow environment that exists when the plant is operating. The flow through the core while cooling is provided by the Decay Heat Removal System is less than 1% of the flow with four reactor coolant pumps operating. Under these conditions, the internals vent valves do not experience the large differential pressure that exists when the plant is operating. Without this large differential pressure, the vent valves are being held closed only by gravity in a quiescent environment.
At TMI-1, where the RVVVs were held in a similar environment for over three years, no adverse effects were found upon inspection and exercising of the RVVVs. Becaure of the similarities in valve design, construction and water chemistry between TN 1 and Davis-Besse, Toledo Edison Company asserts that the favorable performance of the RVVVs at TMI-1 would. indicate the acceptability of extending the surveillance interval at Davis-Besse for a comparable period.
A review of the results obtained from RVVV surveillance tests performed at eight operating B&W plants was performed by B&W. The data repnrted about 400 inspections and exercises over the past ten years without a failure. These data demonstrate that the RVVVs have exhibited a high degree of reliability with no observable degradation in valve operability with reactor age.
DISCUSSION AND EVALUATION The intervals vent valves are installed in the core support shield to prevent a pressure unbalance which might delay or interfere with emergency core cooling following a postulated inlet pipe rupture. The arrangement consists of four 14-inch inside diameter vent valve assemblies installed in the cylindricci wall of the internal core support shield. The internals vent valves provide a direct path to vent steam in the upper plenum through the break following a postulated cold-leg rupture. The vent valves are required i
because the arrangement of the RCS could delay.the venting of steam generated in the core after the system is depressurized, if significant quantities of coolant remair. in the reactor inlet piping at the end of the blowdown period.
Without venting of the steam, the pressure in and above the core region could be g,reater than the pressure in the reactor vessel inlet annulus where emergency coolant is injected. This pressure differential could retard flow into the core. The vent valves provide a flowpath from the region above the core directly to the pipe rupture location. This flowpath allows the pressures to equalize and permits emergency coolant water to reflood the core rapidly.
In its evaluation of the licensee's request to extend the RVVV surveillance interval, the NRC staff considered the results from the approximately 400 inspections and exercises which have been performed at all operating B&W facilities.
The typical interval t'etween RVVV inspection and exercise was 12 to 18 months with a maximum test interval (with the exception of TMI-1) of about two years.
In the case of TMI-1, the longest interval between tests was 37 months. These inspections indicate a high degree of reliability for the RVVVs sir.ce no degradation in valve operability has been observed.
The NRC staff also evaluated infomation pertaining to the RCS chemistry, material compatability and corrosion resistan.ce, and the reactor coolant environment. The chemistry of the RCS water is controlled to minimize corrosion and material activations and to assure the reliability of reactor and steam generator equipment. The licensee reported that the RCS water has not been out of specification at any time since the last surveillance test of the RVVVs. Comparison of the critical elements of water chemistry such as the concentrations of boron, fluoride, oxygen', and chloride, as well as the pH for the Davis-Besse and TMI-1 plants, indicates that the water environments in both plants are similar. The RVVVs at TMI-1 were not exercised for about 37 months -- slightly less than the maximum interval to be expected in the case of the RVVVs at Davis-Besse. The staff believes that the favorable TMI-1 results are indicative of what would be expected at Davis-Besse.
Corrosion, which could have an effect on the operation of RVVVs, has been considered. The parts vulnerable to corrosion are the shaft, bushing, and the body. These components are constructed of Type 431 martensitic stainless steel, Stellite No. 6, and Type 304 austenitic stainless steel respectively.
Available data for the RCS hot operating conditions indicate that the general corrosion rates of these materials, as reported by the licensee, are in the range of 0.05 mils / year or less. This information has been verified independently by the NRC staff in the scientific literature (Reference 3).
Since the accumulation of the corrosion deposit is about three times the corrosion rate, the expected thickness of the deposited material would be 0.15 mils per year. The minimum cold clearance gap dimensions vary from 3 to 60 mils, therefore the gap would not close and hinder the operation of the valve during the period of time until the next test of the RVVVs.
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1 ENVIRONMENTAL CONSIDERATION This amendment involves changes in the installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20.
We have determined that the amendment involves no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that this amendment involves no significant hazards consideration and there has been no public comment on such finding. Accordingly, this amendment meets the eligibility criteria for categorical exclusion set forthin10CFR51.22(c)(9). Pursuant to 10 CFR 51.22(b), no environmental impact statement or environmental assessment need be prepared in connection with the issuance of this amendment.
CONCLUSION We have concluded, based on the considerations discussed above, that:
(1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, and (2) such activities will be conducted in compliance with the Commission's regulations and the issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public.
Dated: August 20, 1986 Principal Contributors:
R. Lipinski G. Hammer
t
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References:
1.
Letter from Joe Williams, dr., Toledo Edison, to John F. Stolz, NRC, dated June 6, 1986.
2.
Letter from Jae Williams, Jr., Toledo Edison, to John F. Stolz, 1
NRC, dated July 30, 1986.
s 3.
Uhlig, Herbert, H., " Corrosion and Corrosion Control," John Wiley and Sons Inc., 2nd Edition, 1971.
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