ML20212L149

From kanterella
Jump to navigation Jump to search
Monthly Operating Rept for Oct 1986
ML20212L149
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 10/31/1986
From: Morgan H, Siacor E
SOUTHERN CALIFORNIA EDISON CO.
To:
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
NUDOCS 8701290334
Download: ML20212L149 (9)


Text

.,

NRC MONTHLY OPERATING REPORT-DOCKET NO.

50-206-UNIT NAME SONGS - 1 DATE uny,mhor 14. 1986 COMPLETED BY E. R. Siacor TELEPHONE (714) 368-6223 OPERATING STATUS

1. Unit Name: San Onofre Nuclear Generating Station, Unit 1 2.-Reporting Period: October 1986
3. Licensed Thermal Power (MWt):

1347

4. Nameplate Rating (Gross MWe):

456

5. Design Electrical Rating (Net MWe):

436 6.' Maximum Dependable Capacity (Gross MWe):

456

7. Maximum Dependable Capacity (Net PWe):

-436

8. If Changes Occur In Capacity Ratings (Items Number 3 Through 7)

Since Last Report, Give Reasons:

NA

9. Power Level To Which Restricted, If Any (Net MWe):

390

10. Reasons For Restrictions, If Any:

Self-imposed power level limit to control steam generator tube corrosion.

This Month Yr.-to-Date Cumulative

11. Hours In Reporting Period 745.00 7,296.00 169,880.00
12. Number Of Hours Reactor.Was Critical 576.37 1,644.13 97,747.42
13. Reactor Reserve Shutdown Hours 0.00 0.00 0.00
14. Hours Generator On-Line 535.55 1,412.53 93,784.30

-15. Unit Reserve Shutdown Hours 0.00 0.00 0.00

16. Gross Thermal Energy Generated (MWH) 599,252.39 1,395,559.00 118,705,786.05
17. Gross Electrical Energy Generated (MWH) 193,112.70 440,962.38 40,270,596.38
18. Net Electrical Energy Generated (MWH) 176,018.00 384,060.00 38,024,535.00
19. Unit Service Factor 71.89%

19.36%

55.21%

20. Unit Availability Factor 71.89%

19.36%

55.21%

21. Unit Capacity Factor (Using MDC Net) 54.19%

12.07%

51.34%

22. Unit Capacity Factor (Using DER Net) 54.19%

12.07%

51.34%

23. Unit Forced Outage Rate 14.54%

35.68%

21.39%

24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

Mid-Cycle outage-April 10, 1987, 45-day duration 25.-If Shutdown At End Of Report Period, Estimated Date of Startup:

NA

26. Units In Test Status (Prior To Commercial Operation):

Forecast Achieved INITIAL CRITICALITY NA NA INITIAL ELECTRICITY NA NA COMMERCIAL OPERATION NA NA 8701290334 861031 7596u/3 kDR ADOCK 05000206 k

PDR l' l i

i

j-AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-206 UNIT-SONGS - 1 DATE November 14, 1986 COMPLETED BY E. R. Siacor

' TELEPHONE (714) 368-6223 MONTH: October 1986 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 10.13-17 49.29 2-0.00 18 374.29 3

0.00 19 375.79' 4

201.63 20 312.54 5

315.92 21 324.96 6

371.92 22 357.42 7

373.21

' 23 369.04 8

370.67 24-373.71 9

370.67 25 386.96 10 285.42 26 357.04 11 0.00 27 378.38 12 0.00 28 378.63 13 0.00 29 377.83 14 0.00 30 375.75 15 6.88 31 255.46 16 38.88 7596u/4

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET No. 50-206 UNIT NAME SONGS - 1

. REPORT MONTH OCTOBER 1986 DATE-Nnvanhar 14.

14A6 COMPLETED BY E.

L Siacor TELEPHONE f71al 368-6223 Method of Shutting Down System Component Cause & Corrective 1

Du ra t ion 2

3 LER 4

4 Action to No.

Date Type (Hours)

Reason Reactor No.

Code Code Prevent Recurrence 100 860904 F

15.11 A

4 86-011 SJ P-Plant Shutdown was initiated as required by Technical Specification 3.3.1 and 3.0.3 due to inoperability of the West Main Feedwater Pump.

Outage continued from previous month.

101 861002 F

44.52 A

1 NA SJ

'P Plant shutdown was initiated to.

Investigate and repair oil leak in the West Main Feedwater Pump (MFP).

The oil. leak was due to improperly installed motor bea ring sea ls.

The seals were reinstalled properly and the l en k wa s repa i red.

102 861010 S

118.32 B

2 NA KB ISV Plant shutdown was initiated for a planned outage to repair South Turbine Plant Heat Exchanger Sa l twa te r i n l et isolation valve and piping.86-013 SJ P

While shutting down for the scheduled outage, with Unit 1 at 20% power, the East MFP shaf t driven tube oil pump suction piping was found leaking, resulting.in reduced tube oil p ressu re.

The leak was due to a crack at the threaded connection of-the suction piping to the shaft driven lube oil pump.

The crack either pre-existed or was initiated during installation, and propagated over a period of time due to normal-pump vibration. As corrective action, new suction piping connections were fabricated and installed on the East and West MFP shaft driven tube oil pump.. The East MFP was returned to service and monitoring of oil leaks continued.

I 2

3 4

F-Fo rced Reason:

Method:

IEEE Std. 803-1983 S-Scheduled A-Equipment Failure (Explain) 1-Manual B-Ma intenance or Test 2-Manua l Scram.

C-Refueling 3-Automatic Scram.

D-Regulatory Restriction 4-Continuation from E-Operator Training & License Examination -

Previous Month F-Admi n i s t ra t ive 5-Reduction of 20%.

C-Ope ra t iona l Error (Expla in) or Greater in the H-Other (Expla in)

Past 24 Hours 7596u/5 6-Other (Explain)

' UNIT SHUTDOWNS AND POWER REDUCTIONS-DOCKET No.- 50-206 UNIT NAME 3ONGS - 1 REPORT MONTH OCTOBER 1986 DATE November 14. 1986 COMPLETED BY- :.

R.

Siacor TELEPHONE 1714) 368-6223 Method of Shutting Down System Component Cause & Corrective 1

Du ra t ion 2

3 LER 4

4 Action to No.

Date Type (Hours)

Reason Reactor No.

Code Code Prevent Recurrence 103 861016 F

31.50 A

1 NA SJ -

P Plant shutdown was initiated to investigate and repair oil leak in the discharge piping of the East MFP shaft driven lube oil pump.

Tne discharge and suction piping connection to the shaft driven oil pump was replaced with stainless steel flexible hoses.

104 861031 S

0.00 8

5 NA NA NA Power reduction to clean condenser water boxes.

I 1

2 3

4 F-f o rced Reason:

Method:

IEEE Std. 803-1983 S-Scheduled A-Equipment Fa ilure (Expla in) 1-Manual D-Ma intenance or Test C-Refueling '

2-Manual Sc ra m.

3-Automa tic Scram.

D-Regulatory Restriction 4-Continuation from E-Operator Training & License Examination Previous Month F-Adm in i s t ra t ive 5-Reduction of 20%

C-Ope ra t iona l Error ( Expla in) or Creater in the H-Othe r ( Expla in)

Past 24 Hours 6-Other (Expla in) 7596u/6

e

SUMMARY

OF OPERATING EXPERIENCE FOR THE MONTH DOCKET 50-206 UNIT SONGS - 1 DATE November 14, 1986 COMPLETED BY E'. R. Siacor TELEPHONE (714) 368-6223 DATE TIME EVENT October 1 0001 The Unit is in Mode 3.

Preparations for Mode 2 entry in progress.

0325 Entered Mode 2.

0333 Reactor made critical 1500 Entered Mode 1<

1507 Unit synchronized to the grid.

October 2 0055 Initiated a precautionary shutdown to investigate lube oil leak on West Main Feedwater Pump (MFP).

0304 Unit taken off line.

0405 Entered Mode 3.

October 3 1754 Entered Mode 2 following repairs to West MFP oil leak.

1815 Reactor made critical.

2328 Entered Mode 1.

2335 Unit synchronized to the grid.

October 4 0500 Reactor power at 35%.

Turbine load at 150 MWe gross.

October 5 1245 Reactor power at 95%. Turbine load at 395 MWe gross.

October 10 1730 Commenced scheduled shutdown for South Turbine Plant Cooling Water Heat Exchanger outage to repair saltwater inlet isolation valve and piping.

2111 Reactor manually tripped, entered Mode 3.

2116 East MFP declared inoperable due to leak in shaft driven lube oil pump suction piping.

October 14 0605 Declared East MFP operable following repair to the shaft driven lube oil pump suction piping.

7596u/7

SUMMARY

OF OPERATING EXPERIENCE FOR THE MONTH (Continued)

DATE TIME EVENT October 15 1049 Entered Mode 2 following completion of repairs to Turbine Plant Cooling Water Heat Exchanger inlet isolation valve and piping.

1104 Reactor made critical.

1923 Entered Mode 1.

1928 Unit synchronized to the grid.

October 16 0405 Commenced plant shutdown to repair oil leak in East MFP shaft driven lube oil pump discharge piping connection.

0703 Entered Mode 2.

0705 Unit taken off line.

0728 Entered Mode 3.

October 17 0939 Entered Mode 2 following replacement of suction and discharge piping connections to the shaft driven lube oil pump for the East and West MFPs with new stainless steel flexible hoses.

0953 Reactor made critical.

1430 Entered Mode 1.

1435 Unit synchronized to the grid.

October 18 0100 Reactor power at 92%. Turbine load at 395 MWe gross.

October 20 0400 Commenced power reduction to 65% to heat treat the circulating water intake tunnels.

0500 Reactor power at 65%. Turbine load at 270 MWe gross. Tunnels in reverse flow.

0957 Commenced power increase following completion of heat treating operations.

Circulating water tunnels remain in reverse flow.

1452 Reactor power at 83%. Turbine load at 351 MWe gross.

7596u/8

SUMMARY

OF OPERATING EXPERIENCE FOR -THE MONTri (Continued) 0 ATE TIME EVENT October 22 0600 Commenced power reduction to allow return of circulating water tunnels to normal flow configuration.

0610 Reactor power at 67%. Turbine load at 295 MWe gross.

0652 Cormenced power increase following return of circulating water tunnels to normal flow configuration.

0735 Reactor power at 91%. Turbine load at 393 MWe gross.

October 31 0545 Commenced power reduction for condenser water box cleaning.

0638 Reactor power at 60%. Turbine load at 270 MWe gross.

0720 Commenced further load reduction due to decreasing condenser vacuum.

0749 Reactor power at less than 20%.

Turbine load at 60 MWe gross.

0825 Increased reactor power to 30% and turbine load to 120 MWe gross.

1849 Commenced power increase following completion of condenser water box cleaning and condenser vacuum stabilization.

2400 The Unit is in Mode 1 at 85% reactor power. Turbina load at 369 MWe gross.

Power increase continuing.

7596u/9

~

o.

I REFUELING INFORMATION DOCKET NO.

50-206 UNIT SONGS - 1 DATE November 14. 1986 COMPLETED BY E. R. Siacor TELEPHONE (714) 368-6223 MONTH:

October 1986 1.

Scheduled date for next refueling shutdown.

March 1988 2.

Scheduled date for restart following refueling.

June 1988 3.

Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?

Not yet determined What will these be?

Not yet determined 4.

Scheduled date for submitting proposed licensing action and supporting information.

Not applicable 5.

Important Licensing considerations associated with refueling, e.g. new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.

None 6.

The number of fuel assemblies.

a) In the core.

157 b) In the spent fuel storage pool.

146 7.

Licensed spent fuci storage capacity. 216 Intended change in spent fuel storage capacity. Under review 8.

Projected date of last refueling tSat can be discharged to spent fuel storage pool assuming present capacity.

March 1988 7596u/9

T P) e ~:-

m Southem Califomia Edison Company SAN ONOFRE NUCLEAR GENtR ATING ST ATION P O BOK128 SAN CLEMENTE. CALIFORNIA 92672 H.E. MORGAN HONE crariou u.~. cia November 14, 1986 i"***2*'

Director Office of Resource Management U.S. Nuclear Regulatory Commission Washington, D.C.

20555

Dear Sir:

Subject:

Docket No. 50-206 Monthly Operating Report for October 1986 San Onofre Nuclear Generating Station, Unit 1 Enclosed is the Monthly Operating Report as required by Section 6.9.1.10 of Appendix A, Technical Specifications to Provisional Operating License DPR-13 for San Onofre Nuclear Generating Station, Unit 1.

Please contact us if we can be of further assistance.

Sincerely, MbM Enclosures cc:

J. B. Martin (Regional Administrator, USNRC Region V)

F. R. Huey (USNRC Senior Resident Inspector, Units 1, 2 and 3)

R. F. Dudley, Jr. (USNRC Unit 1 Project Manaser, Office of Nuclear Reactor Regulation)

Institute of Nuclear Power Opera'. ions (INPO)

Y Nh n

e