ML20211Q955

From kanterella
Jump to navigation Jump to search
Corrected Monthly Operating Rept for Oct 1986
ML20211Q955
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 12/15/1986
From: Reavis J
DUKE POWER CO.
To:
Shared Package
ML20211Q940 List:
References
NUDOCS 8612220201
Download: ML20211Q955 (3)


Text

-_ - - _ _ _ _ _

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-369 UNIT NAME yccuire 1 DATE 12/1s/86

  • REVISION 1 REPORT PONTH october 1986 COMPLETED BY J.

A.

Reavis TELEPHONE 704-373_7s67 m

O

't;en]

License y

Cause & Corrective c32 "e

o3E

,B"e, y

Action to Event No.

Date a,

%h o - pg!

g

$ie

%5 EB 5i Prevent Recurrence 1

F o~

=

lit m o Report #

mo uo 41-p 86-10-01 F

A HH HTEXCH "A2/B2" Heater String Isolated 42-p 86-10-07 F

A HH VALVEX High Pressure Heater "Al" Out of

]

Service Due to Extraction Check Valve

]

Closed 43-P 86-10-15 F

G ZZ ZZZZZZ Computer Point Not Returned to Service Following Test 44-p 86-10-20 S

B CH uxxxx Moisture Carry Over Test

{

45-p 86-10-21 F

A ED INSTRU Loss of "lA" Busline During Relay Testing f

12 86-10-29 F

69.38 A

1 XX VALVEX Rotork Valve Actuator Check-Out l

l 861222O201 861215 PDR ADOCK 05000369 R

PDR, 1

1 2

3 4

Reason:

Method:

Exhibit G - Instructions

[

rc A-Equipment Failure (Explain) 1-Manual for Preparation of Data l

yg B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER)

D-Regulatory Restriction 4-Other (Explain)

File (NLREG-0161)

E-Operator Training 6 License Examination i

F-Adninistrative 5

G-Operational Error (Explain)

Exhibit I - Same Source H-Other (Explain)

(9/77)

~-

MONTHLY REFUELING INFORMATION REQUEST 1.

Facility name: McGuire, Unit 1 2.

Scheduled next refueling shutdown: October, 1987 3.

Scheduled restart following refueling: November, 1987 4.

Will refueling or resumption of operation thereafter require a technical specification change or other license amendment? Yes If yes, what will these be?

Technical Specification Revision If no, has reload design and core configuration been reviewed by Safety Review Committee regarding unreviewed safety questions? N/A 5.

Scheduled date(s) for submitting proposed licensing action and supporting information: N/A 6.

Important licensing considerations (new or different design or supplier, unreviewed design or performance analysis methods, significant changes in design or new operating procedures).

7.

Number of fuel assemblies (a) in the core:

193 (b) in the spent fuel pool:

221 8.

Present licensed fuel pool espacity:

1463 Size of requested or planned increase:

9.

Projected date of last refueling which can be accommmodated by present licensed capacity: August, 2010 t

DUKE POWER COMPANY DATE: December 15, 1986 Name of

Contact:

J. A. Reavis Phone 704-373-7567 i

l

I DOCKET NO: 50-369 REVISION 1 UNIT: McGuire 1 DATE: 12/15/86 NARRATIVE

SUMMARY

Month:

October 1986 McGuire Unit i began the month at 100% power. A string of feedwater heaters were out of service which caused a reduction in efficiency. The heaters were placed back in service on 10/05 and the efficiency increased. The unit remained at 1007. until 10/15 when load was reduced to 97%. A computer point was not returned to service following testing. The problem was corrected and the unit returned to 100% within an hour. The unit remained at 100%

until 10/21 when a run back to 55% power occurred. The run back was caused by a burned contact on a relay. -The unit returned to 100% that evening. On 10/29, the unit was forced off line by a safety question concerning Rotork valves. The unit remained off line for the rest of the month.