ML20209D769

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Partially Withheld Insp Rept 50-285/87-06 on 870301-31 (Ref 10CFR73.21).Violation Noted:Failure to Maintain Log of Entries Into Vital Areas.Major Areas Inspected:Operational Safety Verifications & Security Observations
ML20209D769
Person / Time
Site: Fort Calhoun 
Issue date: 04/14/1987
From: Boardman J, Harrell P, Hunnicutt D, Hunter D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20209D745 List:
References
50-285-87-06, 50-285-87-6, NUDOCS 8704290355
Download: ML20209D769 (13)


See also: IR 05000285/1987006

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APPENDIX B

U. S. NUCLEAR REGULATORY COMMISSION

REGION IV

NRC Inspection Report:

50-285/87-06

License:

DPR-40

,

Docket:

50-285

' Licensee: Omaha Public Power District

1623 Harney Street

s

Omaha, Nebraska 68102

Facility Name:

Fort Calhoun Station

Inspection At:

Fort Calhoun Station, Blair, Nebraska

Inspection Conducted:

March 1-31, 1987

Y! /y/P7

Inspector:

.

P. H. Harrell, Senior Resident Reactor

Date

Inspector

N

./R. Boardman,ReactorInspector,

Date

erations Section, Reactor Safety Branch

Approved:

N/

/ 'W87

D. M. Hunnicutt, Chief, Operations Section,

D8te '

Reactor Safety Branch

8704290353 870422

PDR

ADOCK 05000285

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PDR

Ci M

ds/ar

D. Y Hunter, Chief, Reactor Project

Date

Section B, Reactor Projects Branch

Inspection Summary

Inspection Conducted March 1-31, 1987 (Report 50-285/87-06)

Areas Inspected:

Routine, unannounced inspection including operational safety

verifications, maintenance, surveillance, plant tours, safety related system

walkdown, security observations, in-office review of periodic and special

reports, preparation for refueling activities, refueling activities, review of

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the welding program, containment local leak rate testing, and followup on

Generic Letter 83-28 (Salem ATWS event).

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-Results: Within the 12 areas inspected, 1 violation (failure to maintain a log

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of entries into vital areas, paragraph 8) was identified.

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DETAILS

1.

Persons Contacted

    • R. Andrews, Division Manager-Nuclear Production
    • W. Gates, Plant Manager

C. Brunnert, Supervisor-0perations Quality Assurance

M. Core, Supervisor-Maintenance

T. Dexter, Supervisor-Security

    • J. Fisicaro, Supervisor-Nuclear Regulatory and Industry Affairs

J. Foley, Supervisor-I&C and Electrical Field Maintenance

  1. J. Gasper, Manager-Administrative and Training Services
    • R. Jaworski, Section Manager-Technical Services

M. Kallman, Supervisor-Security

L. Kusek, Supervisor-0perations

    • D. Munderloh, Plant Licensing Engineer

T. McIvor, Supervisor-Technical

  • K. Morris, Division Manager-Quality Assurance and Regulatory Affairs

R. Mueller, Plant Engineer

  • A. Richard, Manager-Quality Assurance

G. Roach, Supervisor-Chemical and Radiation Protection

J. Kecy, Acting Reactor Engineer

  • S. Willrett, Supervisor-Administrative Services and Security
  • Denotes attendance at the monthly exit interview held on April 3, 1987.
  1. Denotes attendance at a meeting held by J. Boardman on March 20, 1987.

(see paragraph 15)

The inspector also contacted other plant personnel, including operators,

technicians, and administrative personnel.

2.

Followup on Previously Identified Items

(Closed) Open Item 285/8bO3-03:

Establishment of an inspection program

for type-86 lockout relays.

The licensee performed a review, in accordance with IE Bulletin 84-02

commitments, to establish a program for inspection of type-86 relays.

The

review performed by the licensee's engineering staff recommended that an

inspection program be established by plant personnel for inspection of

type-86 relays.

The licensee's plant staff disagreed with the engineering

staff's recommendation in that an additional inspection program was not

required.

The licensee's plant staff determined that an acceptable

program existed through the use of the established surveillance test

program.

Based on a review performed by the licensee's plant staff, it

was verified that each relay was tested on a monthly basis by the

performance of system surveillance tests.

The plant staff also noted

during the review that redundant relays existed for each safety-related

signal processed.

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The NRC inspector reviewed a selected sample of relays to verify that a

surveillance test was performed to verify proper relay operation. No

problems were noted during the review.

3.

Operational Safety Verifications

The NRC inspector conducted reviews and observations of selected

activities to verify that facility operations were performed in

confomance with the requirements established under 10 CFR, administrative

procedures, and the Technical Specifications (TS). The NRC inspector made

several control room observations to verify:

Proper shift staffing

.

Operator adherence to approved procedures and TS requirements

.

Operability of reactor protective system and engineered safeguards

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equipment

Logs, records, recorder traces, annunciators, panel indications, and

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switch positions complied with the appropriate requirements

Proper return to service of components

.

Maintenance orders (MO) initiated for equipment in need of

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maintenance

Appropriate conduct of control room and other licensed operators

.

During a control room tour at approximately 11:00 a.m. on March 9,1987,

the NRC inspector noted that the licensee had taken the 480-volt electrical

distribution bus, MCC 3A2, out of service at 7:00 a.m. to perform preventive

maintenance activities. By removing the MCC from service with the reactor

coolant temperature greater than 300 degrees, the licensee had entered a

TS limiting condition for operation (LCO). The LC0 of TS 2.7(2)f requires

that the licensee place MCC 3A2 back in service within 8' hours or enter an

action statement that required the plant to be placed in a cold shutdown

,

condition within the following 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br />. The licensee placed MCC 3A2 back

in service at 2:42 p.m. and exited the TS LC0.

During discussions with operations personnel, the NRC inspector detemined

that licensee personnel were not aware that taking MCC 3A2 out of service

caused the plant to be placed in an LC0. Upon notification by the NRC

inspector, actions were taken by the licensee to ensure the MCC was

returned to service as soon as possible. Management personnel stated that

the failure to recognize the plant was in an LCO was an inadvertent

oversight by operations personnel. This occurrence was discussed by plant

management with operations personnel to increase their awareness level of

the need to verify that plant conditions do not cause an unknown entry

into an LCO.

In addition, the outage planning data base was updated by

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the licensee to ensure that no MCCs were removed from service during future

outages when the reactor coolant temperature was above 300 degrees.

No violations or deviations were identified.

4.

Plant Tours

The NRC inspector conducted plant tours at various times to assess plant

and equipment conditions. The following items were observed during the

tours:

General plant conditions

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Equipment conditions, including fluid leaks and excessive vibration

.

Plant housekeeping and cleanliness practices including fire hazards

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and control of combustible material

Adherence to the requirements of radiation work permits

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Work activities performance in accordance with approved procedures

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During tours of the plant, the NRC resident inspector noted the following

items:

An individual was entering the containment building with a

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respirator; however, the individual's security badge indicated that

he was not qualified to wear a respirator. The licensee places a

,

white dot on the security badge to indicate that an individual is

qualified for respirator use.

In this case, the individual with the

respirator did not have a white dot on his security badge.

The NRC inspector called the apparent problem to the attention of the

security guard stationed at the containment access door. The

security guard stopped the individual from entering containment and

determined that the individual intended to use the respirator. The

individual explained that he was respirator qualified and that when

his badge was issued, the white dot was inadvertently left off. The

security guard checked with the individual responsible for respirator

qualification and detennined that the individual attempting to enter

containment was not respirator qualified.

The security guard instructed

the individual to leave the area immediately.

In discussions with the licensee, management personnel stated that

they felt the general employee training program was adequate to

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ensure that unqualified personnel did not use respirators.

Management personnel stated that they felt that the problem discussed

above was a problem with a particular individual. This conclusion

was based on the fact that no other instances of this type had been

reported during the current refueling outage. The individual

involved was provided individualized instruction in what

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qualifications were required for him to be allowed to wear a

respirator.

Fire Doors 989-11 and 1011-1 were found not to be functioning

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properly in that the doors wouldn't always close.

By not closing,

the fire barriers associated with the doors became nonfunctional.

Upon notification by the NRC inspector, the licensee repaired the

doors.

During a tour of containment on March 27, 1987, the plant manager and

maintenance supervisor found a contract quality control (QC) inspector

sleeping.

The QC inspector was performing tool accountability activities,

but no work was in progress at the time of the discovery.

The contract QC

inspector was terminated shortly thereafter.

The NRC inspector discussed

the incident with the chemistry and radiation protection (CARP) supervisor

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to verify that health physics (HP) technicians were aware of.their

responsibility of ensuring individuals did not sleep in radiation areas.

The CARP supervisor stated that the HP technicians were aware of their

responsibility.

The plant manager discussed the incident with all plant

supervisors and stressed that any individual caught sleeping on duty would

be disciplined.

No violations or deviations were identified.

5.

Safety-Related System Walkdown

The NRC inspector walked down accessible portions of the following

safety-related system to verify system operability.

Operability was

determined by verification of selected valve and switch positions.

The

system was walked down using the drawing and procedure noted:

Shutdown cooling system (Procedure 01-SC-1, Revision 24, and

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Drawing E-23866-210-130, Revision 38)

During the walkdown, the NRC inspector noted minor discrepancies of an

editorial nature between the drawing, procedure, and plant as-built

conditions for the selected areas checked.

None of the conditions noted

affected the operability or safe operation of the system.

Licensee

personnel stated that the noted minor discrepancies would be corrected.

No violations or deviations were identified.

6.

Monthly Maintenance Observations

The NRC inspector reviewed and/or observed selected station maintenance

activities on safety-related systems and components to verify the

maintenance was conducted in accordance with approved procedures,

regulatory requirements, and the TS.

The following items were considered

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during the reviews and/or observations:

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The TS limiting conditions for operation were met while systems or

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components were removed from service

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Approvals were obtained prior to initiating the work

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Activities were accomplished using approved M0s and were inspected,

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as applicable

Functional testing and/or calibrations were performed prior to

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returning components or systems to service

Quality control records were maintained

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Activities were accomplished by qualified personnel

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Parts and materials used were properly certified

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Radiological and fire prevention controls were implemented

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The NRC inspector reviewed and/or observed the following maintenance

activities:

Rebuilding of main steam safety valves (M0 870946)

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Replacement of insulation on 4160-volt buses (M0 863672)

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Change out of sleeve bearings on electrical breakers (M0 845331)

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Repair of a battery charger (M0 817548)

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Replacement of a bonnet gasket on a safety injection valve

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(M0 858023)

No violations or deviations were identified.

7.

Monthly Surveillance Observations

The NRC inspector observed selected portions of the performance of and/or

reviewed completed documentation for the TS required surveillance testing

on safety-related systems and components.

The NRC inspector verified the

following items during the testing:

Testing was performed by qualified personnel using approved

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procedures

Test instrumentation was calibrated

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The TS limiting conditions for operation were met

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Removal and restoration of the affected system and/or component were

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accomplished

Test results conformed with TS and procedure requirements

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Test results were reviewed by personnel other than the individual

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directing the test

Deficiencies identified during the testing were properly reviewed and

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resolved by appropriate management personnel

The NRC inspector observed and/or reviewed the documentation for the

following surveillance test activities.

The procedures used for the test

activities are noted in parenthesis.

Channel B safety injection actuation signal test (ST-ESF-2-F.2)

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Auxiliary feedwater pump monthly cieck (ST-FW-1-F.2)

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Exercising of ventilation air valves (ISI-VA-1-F.1)

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Calibration of containment pressure switch (CP-D/765)

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No violations or deviations were identified.

8.

Security Observations

The NRC inspector verified the physical security plan was being

implemented by selected observation of the following items:

The security organization was properly manned

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Persor.nel within the protected area (PA) displayed their

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identification badges

Vehicles were properly authorized, searched, and escorted or

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controlled within the PA

Persons and packages were properly cleared and checked before entry

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into the PA was permitted

The effectiveness of the security program was maintained when

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security equipment failure or impairment required compensatory

measures to be employed

During this inspection, the NRC inspector noted that the licensee had not

established a program for maintaining a log for persons entering vital

areas not equipped with security badge card readers.

The discussion of

this apparent violation contains safeguards information, as defined in

10 CFR Part 73.21; therefore, the details of this apparent violation are

provided in Appendix A and the Attachment to this inspection report.

9.

In-Office Review of Periodic and Special Reports

In-office review of periodic and special reports was performed by the NRC

resident inspector and/or the Fort Calhoun project inspector to verify the

following, as appropriate:

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Reports included the information required by appropriate NRC

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requirements

Test results and supporting information were consistent with desigr.

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predictions and specifications

Determination that planned corrective actions were adequate for

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resolution of identified problems

Detennination as to whether any information contained in the report

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should be classified as an abnormal occurrence

The following reports were reviewed:

Monthly operations report for February 1987

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Core reload methodology changes for Cycle 11, dated March 18, 1987

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Amendment for a change to the TS related to testing of the emergency

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diesel generators, dated March 13, 1987

Notification of raising the current cold leg temperature, dated

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March 11, 1987

Revised schedule and justification for replacement of Valcor valves,

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dated March 4, 1987

No violations or deviations were identified.

10. Preparation for Refueling

The NRC inspector reviewed selected procedures to verify that the

technical and administrative requirements provided in the procedures

adequately incorporated controls and requirements stated in the TS, codes,

and standards. The procedures reviewed were evaluated to verify that

controls had been established for the following elements:

Receipt, inspection, and storage of new fuel and control element

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assemblies (CEA)

Fuel handling, transfer, and core verification

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Inspection of irradiated fuel

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Preoperational checkout of refueling equipment

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Handling and movement of the reactor core internals

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Establishment of administrative measures for the activities such as

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lines of supervision, shif t manning, radiation monitoring,

comunications, and training

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The NRC inspector reviewed the following procedures for the elements

listed above.

Number

Title

Revision

SP-CEA-3

Procedure for CEA

3

Unloading, Inspection, and

Storage of Individual CEAs

OP-11

Reactor Core Refueling

18

Procedure

SP-FE-1

Visual Inspection of

4

Irradiated Fuel

HP-FH-2

Refueling Equipment

10

Preoperational Maintenance

MP-ilE-1

Polar Crane Annually or

7

at Refueling Inspection

HP-RC-7-2-A

Upper Guide Structure

20

and ICI Plate Removal

SP-flFR-1

Fuel Receipt Procedure

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The i4RC inspector witnessed activities related to the receipt, inspection,

and storage of new fuel and CEAs. The inspector verified that the

inspections were performed in accordance with the requirements established

by Procedures SP-NFR-1 and SP-CEA-3. The selected verifications performed

by the inspector included determination that the personnel performing the

inspections were qualified, documentation was accurately completed, and

the fuel and CEAs were properly handled.

Based on the observations and

reviews perfonred by the NRC inspector, it appeared that the fuel and CEAs

were inspected and handled appropriately.

The NRC inspector also observed and/or reviewed completed documentation of

other selected portions of preparation for refueling activities. The

activities included fuel handling equipment and crane operational

verification, proper operation of radiation monitors, and verification

that the source range monitors operated properly.

Prior to contencement of outage activities, the licensee issued a

refueling cutage manual. This manual provided a single reference source

for the various activities related to the outage. The information

provided in the manual included a description of the outage organization

and responsibilities; time, place, and subject of the various outage

meetings; administrative information; and a discussion of how to properly

perform activities that have been previously identified as problem areas.

No violations or deviations were identified.

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11. Review of Welding Program

During this inspection period, the NRC resident inspector assisted an NRC

welding specialist from Region IV in a detailed review of the licensee's

welding program. During the review, a violation of the failure to

properly control special prccesses was identified. The results of the

program review are provided in NRC Inspection Report 50-285/87-08.

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12. Followup on Generic Letter 83-28

Generic Letter (GL) 83-28 was issued by the NRC to require licensees to

implement corrective actions based on the Salem ATWS event. This portion

of the inspection was performed to verify that the licensee had properly

implerented a program for post-trip reviews. The requirements for

post-trip reviews are provided in GL 83-28 as Items 1.1 and 1.2.

The NRC Office of Nuclear Reactor Regulation (NRR) performed a review of

the documentation submitted by the licensee in response to the

requirements of GL 83-28.

Based on the review, NRR issued a safety

evaluation report (SER) on October 22, 1985, for Item 1.1 and on June 13,

1985, for Item 1.2.

The SERs issued by NRR concluded that the licensee's

post-trip review data and information capabilities were acceptable. The

NRC inspector performed a review to verify that the licensee had

implemented a program for post-trip review as stated in the SERs. The

program implementation was verified by review of the documentation listed

below.

A sequence-of-events computer printout to verify that the types of

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parameters available during post-trip reviews included the items

required by the SER

Procedure OP-1 "liaster Checklist for Startup or Trip Recovery," to

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verify that post-trip review and permission for restart

responsibilities were clearly defined

Post-trip review packages compiled during past reactor trips to

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verify that the appropriate documentation (e.g., completed startup

procedures, sequence-of-events printouts, instrument recorder

tracings and strip charts, etc.) was available

Based on the review performed by the NRC inspector, it appears that the

licensee has implemented an adequate post-trip review program.

Items 1.1

and 1.2 of GL 83-28 are considered closed.

No violations or deviations were identified.

13. Refueling Activities

The NRC inspector reviewed / observed various activities performed during

refueling to verify the activities were performed in accordance with the

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TS and approved licensee procedures. The activities observed / reviewed

included the following:

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Proper shift staffing by qualified individuals was provided

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Containment integrity was established and maintained

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Good housekeeping and loose object control on the refueling bridge

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Fuel handling operations were perfonned in accordance with approved

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The proper refueling cavity water level was maintained

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Chemistry sampling was perfonned at the frequency specified in the TS

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During observation / review of the above activities, no problems were noted

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by the NRC inspector. During this inspection period, the licensee

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offloaded all fuel assemblies into the spent fuel pool to check for fuel

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integrity. The fuel integrity checks were made due to an increase in the

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iodine level in the reactor coolant system during the past fuel cycle.

Any fuel assemblies that were found to be leaking will not be returned to

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the core, but will be replaced with a nonleaking assembly. This

inspection of refueling activities will continue into the next inspection

period.

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No violations or deviations were identified.

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14. Containment Local Leak Rate Testing

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The NRC inspector verified through observation and records review that the

local leak rate test program for testing of mechanical and electrical

penetrations was being performed in accordance with TS requirements. The

NRC inspector observed / reviewed the following items.

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All electrical and mechanical penetrations listed in the TS were

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tested in accordance with the licensee's approved procedure

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Procedure ST-CONT-2, " Containment Local Leak Detection Tests - Type B,"

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provided the appropriate instructions for testing of penetrations

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The test equipment used was in current calibration

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The pressure used for testing conformed to the pressure specified in

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the TS

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Repairs were initiated for any penetrations discovered to be leaking

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Action was taken to verify that the maximum allcwable leakage rate

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was not exceeded upon discovery of a leaking penetration

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Based on the reviews performed during the inspection period, it appeared

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that the licensee was implementing an appropriate leak rate testing

program. At the end of this inspection period, the licensee had not

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completed the testing of all penetration assemblies. This portion of this

inspection will be continued into the next inspection period.

No violations or deviations were identified.

15. Exit Interview

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The NRC inspector met with Mr. R. L. Andrews (Division Manager - Nuclear

Production) and other members of the licensee staff at the end of this

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inspection.~ At this meeting, the NRC inspector sumarized the scope of

the inspection and the findings,

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Mr. J. Boardman met with licensee personnel on March 20, 1987, to provide

information related to a proposed inspection in the area of corrective

action programs. During the meeting, Mr. Boardman outlined the scope and

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nature of the inspection and submitted a request for copies of licensee

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documentation associated with the inspection. Licensee personnel stated

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that the documentation would be provided in the near future. See

paragraph 1 of this inspection report for meeting attendees.

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