ML20207T509

From kanterella
Jump to navigation Jump to search
Notice of Violation from Insp on 861215-17
ML20207T509
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 03/12/1987
From: Reyes L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20207T501 List:
References
50-400-86-93, NUDOCS 8703240083
Download: ML20207T509 (2)


Text

-

i FNCLOSURE1 NOTICE OF VI'1L ATION Carolina Power and Lignt Corepany Docket No. 50-400 Shearon Harris Licensu No. NPf 53 During the Nuclear Regulatory Consnission (NRC) inspection conducted on Decenber 15 - 17, 1986, a violation of NRC requirenents was identified.

The violation involved fatlure to follo's approved plant procedures.

In accordance with the " General Statement of Pritcy and Procedure for NRC Enforcement Actions,"10CFRPart2.Appendixf.(19d6),theviolationislistedbelow:

Technical Specification 6.8.1, states that written proceduras shall be estabitshad, implemented, a id maintained coverino activities referenced in Appendix A of Regulatory Gelde 1.33 Revision 2 February 1970.

Appendix A of Regulatory lu'do 1.33. Revision 2, february 1970 recommended that the authorition and responsibilities for safe operation and shutdown be governed by written Admit.tstrative Proceduros. Operations Management Hanual (OMH) 001, Operations Conduct of Operations, states that plant equipment shall be oporated in actordance with written approved procedures.

Centrary to the abote, the licensee failed to properly review Maintenanco Surveillence Test (HST) 10332, Revision 0, Reactor

'/cssel Level Monitoring System Transmitter Calibration, and the clearanco request a6 required by Administrative Proceduro AP 20 Revision 1,

Clearar co Procuduro, fatture to properly conduct this review resultJd in isolation and deprossurtration of RCS pressure transmitter 1 PT-402 and subsequent operator actions Caused sovural cha160ngos to the RCS pretsure rollef valves.

This is a Savority Levo' IV violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201 Carolina Power and Light Company is hereby required to sub-ilt to this Office within 30 days of the date of thu lotter trant,mitting this Not.co a written staten.cnt or explanation in rep)ly including for each violattuni (1) admission or denidi of the violation (L the reason 00 a

m

(___.

4 l

r Carolina Power and Light Company 2

Docket No. 50 400 Shedron Harris License 'lo. NPF-53 for the violation if admitted (3) the corrective steps which have been taken and the results achieved, (4? the corrective steps which will be taken to avoid further violations, and 45) the date when full compliance will be achieved.

Where good cause is shown, consideration will be given to extending the response time.

FOR 1HE NUCLEAR REGULATORY COMMIS$10N (OriginalsignedbyD.Vorro111for)

Luis A. Reyes, Director Division of Reactor Projects Dated at Atlanta, Georgia this 12th day of March 1987 I'

f l

.-