ML20207D746
| ML20207D746 | |
| Person / Time | |
|---|---|
| Site: | Callaway |
| Issue date: | 08/31/1986 |
| From: | Evans S, Randolph G UNION ELECTRIC CO. |
| To: | NRC OFFICE OF RESOURCE MANAGEMENT (ORM) |
| References | |
| ULNRC-1370, NUDOCS 8612310185 | |
| Download: ML20207D746 (6) | |
Text
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l DOCKET NO.
50-483 UNIT NAME CALLAWAY UNIT 1 DATE 9/9/86 CMPLaamu BZ S.
R.
EVANS TELEPBWE 314/676-8742 PART A OPERATIONS
SUMMARY
8/1/86
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- Power reduction to 45% for EHC leak and intake repairs.
Began 10%/hr. power reduction at 2300. Repairs completed and loading
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commenced for full nower operation at 1525. 8/2/86, Attained 1007. power at 1200, 8/3/86.
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8/25/86 - Manual reactor / turbine trip after a turbine runback and subsequent rod control nroblemn durinc a controlled shutdown to renair an RCS RTD loop bypass valve leak.
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8/31/86 - Power reduction to 75% due to turbine runback on loss of "B"
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r i e r,,1,,- 4 n o unt er numn.
Runback initiated on circulatine water
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pump trip at 1308. Repairs completed and loading commenced for full power operation at 1348.
Attained 100% power at 1645.
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PART B PORV AND SAPETY VALVE
SUMMARY
None M
6 8612310185 860831 PDR ADOCK 05000483 CA-#804 R
PDR 04/10/85 QDP-Z"-04204 Page 1 of 4
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Part C AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-483 UNIT Callaway DATE 9/9/86 S. R. EVANS COMPLETED BY 314/676-8742 TELEPHONE MONTH AUcusT 1986 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net)
(MWe Net) 1096
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gy 1089 i
531 1090 2
gg 1026 1092 3
g, 1099 1096 4
1102 1094 5
21 1100 1091 e
22 1095 1093 y
33 1099 1088 8
24 1101 289 g
1074 0
-10 3
1083 32 33 gy 1102 497 12 3
1089 1055 13 3
1064 1098 94 gg 1080 1084 15 y
1084 15 I
Page 2 of 4 CA-#804 04/10/85 QDP-ZZ-04204
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e Part D
' OPERATING DATA REPORT 50-483 DOCKET NO.
r*m11 - I UNIT __.
9/9/86 DATE COMPLETED 8Y 314/676-8742 TELEPHONE CPERATING STATUS
( YTD CUM 744 (5831 14,893.5)
August 1986 GROSS HOURS IN REPORTING PERICO:
- i. REpORTiNo PEmico:
3411 Max. OEPENO. CAPACITY (MWo.Ned:
1120
- 2. CURRENTLY AUTHORIZED POWER LEVEL (mwd:
1171*
- At stretch power level which is not currently DESsGN ELECTRICAL RATING IMWo.Ned:
authorized under the Operating License.
100%
- 3. POWER LEVEL TO WHICH RESTRICTED tlP ANY) (MWo.Nell:
- 4. REASONS FOR RESTRICTION (IP ANYh THIS MONTH YR TO DATE CUMULATIVE 697.7 4379.0 12,842.5 S. NUMSER OF HOURS REACTOR WAS CRmCAL 0
0 0
- s. REACTOR RESERVE SHUTDOWN HOURS 687.9 4198.3 12.385.7
- 7. HOURS GENER ATOR ON UNE............
O O
n
- 8. UNIT RESERVE SHUTDOWN HOURS
..........2,,236,572 13,200,714 39,218.267
- s. GROSS THERMAL ENERGY GENERATED (MWH1 to. oROSS ELECTRICAL ENERGY GENERATED (MWHI............ 748. 806 4.428.667 13.2A2.610
.............710,711 4,200,894 12,569.681 t1. NET ELECTRICAL. ENERGY GENERATED (MWHI 93 8%
75.I7 R6 ??
- 12. REACTOR SERVICE P ACTOR.........
... 93.8%
75.1%
86.27'
- 13. REACTom AVAILAstuTY PACTOR..................
72.0%
81.??
- 14. UNIT SERVICE P ACTOR,............................. 2.2. 5 %
................4?5*'
77 O*/
A 't P'
- 15. UNIT AVAILAsluTY PACTOR........
............. 85.37 64.1%
75.47 is. UNIT CAPACITY PACTOR (Uene MOCl.
61.5%
72.1%
- 37. UNIT CAPACITY P ACTOR (Using Desen MWei.........,...... 81. 6%
i 7.5%
9.8%
7.4%
- 18. UNIT PORCEO OUTAG E RATE.........................
f None
- 19. SHUTOOWNS SCHEDULED OVER NEXT $ MONTHS (TYPE. OATE. AND Ol/MATION OF EACHl:
- 20. IP SHUT DOWN AT END OP REPORT PERICO. ESTIMATED DATE OF STARTUP:_
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l CA-#804 Page 3 of 4 04/10/85 QDP-ZZ-04204
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I Part E DOCKET NO.
50-483 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME Callaway DATE 9/9/86 COMPLETED BY S. R. EVANS,
REPORT MONTH AUGUST 1986 TELEPHONE 314/676-8742 METHOD OF TYPE
$6AATTING DOWN F: F06CED DURATION THE REACTOft On NO.
DATE S: SCHEDULED IHOURSI REASON REDUC 8NG POWER CORRECTIVE ACTIONSEOuteENTS 17.
8/1/86 S
0 B
4 Power reduced to 45% for repair of EHC leak, WTP, and intake repairs.
18.
8/25/8f F
56.1 A
2 Manual reactor / turbine trip due to turbine runback and rod control failure.
LER 86-029-00 l l i
19.
8/31/81 F
0 A
4 Reduction in power to 75% due to turbine runback on loss of circulating i
water pump "B."
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.l SuasMARY:
6 REASON 9ET400 A: EQUltteENT FAILURE (LEFLA804 8: BAANUAL 4
R: ta480tT.OR TEST 2: bdADIUAL SCRAes.
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DCn C: REFUEtJNG 3: AUrce84 TIC SCRAM D: REGULATORY.RESTRact 006 4: OFIER(EsptAsse y G.
Po E: GFERATOR TkA8 MING AND l M R "O L8CDesE EXAbd8 MAT 90N I cn F: ADtRNESTRAllVE i
O" C: OPERATIONAL ERROR (EEFLAIN)
H. OfIIER(EEPLAlfft Page 4 of 4
,!~ Umon Etscraic s
Ca#away Ptant September 12, 1986 Director, Resource Management Nuclear Regulatory Commission Washington, DC 20555 ULNRC-1370
Dear Sir:
DOCKET NUMBER 50-483 CALLAWAY PLANT UNIT 1 FACILITY OPERATING LICENSE NPF-30 MONTHLY OPERATING REPORT AUGUST 1986 The enclosed Monthly Operating Report for August 1986 is submitted pursuant to section 6.9.1.8 of the Callaway Unit 1 Technical Specifications.
okt G. L. Randolph Manager, Callaway Plant UNS #h he MET /RDA/
$/
/drs Enclosure cc: Distribution attached N
I a l MaRog A06tess: P.O Box 620 Fulton, MO 652S1
cc distributionL for ULNRC-1370 with enclosures Mr. W. F. Forney, Chief Project Section lA U. S.: Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Mr. Paul O'Connor
' Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission Mail Stop P-316 7920 Norfolk Avenue Bethesda, MD 20014 Director Office of Inspection & Enforcement U. S. Nuclear Regulatory Commission
' Washington, DC 20555 NRC Resident Inspector Manager, Electric Department Missouri Public Service Commission P. O. Box 360 Jefferson City, MO 65102