ML20205S924
| ML20205S924 | |
| Person / Time | |
|---|---|
| Site: | Sequoyah |
| Issue date: | 03/27/1987 |
| From: | Russell Gibbs, Halverson R, Mckenzie L TENNESSEE VALLEY AUTHORITY |
| To: | |
| Shared Package | |
| ML20205S746 | List: |
| References | |
| 80203-SQN, 80203-SQN-R04, 80203-SQN-R4, NUDOCS 8704070164 | |
| Download: ML20205S924 (14) | |
Text
/
TVA EMPLOYEE CONCERNS REPORT NUMBER g.
SPECIAL PROGRAM 80203-SQN j
REVISION NUMBER:
' REPORT TYPE 4
Element Report PAGE 1 0F 11 TITLE:
Inspection Performance REASON FOR REVISION:
Revised to incorporate NRC comments. Revision indicators are show in the right margin of each affected f
L page.
Note:
Sequoyah Applicability Only PREPARATION PREPARED BY:
D. G. BARLOW /R. D. HALVERSON
~
~
An
/16t22K -
'(
Tort *
/"[
DATE REVIEWS PEER:
3-2o~87 r
. ctw W1 DATE J
Q SIGNATU18 k
TAS:
3 l'7 3b4/h7 k
SIGNATURE '
/ DA/k 4
CONCURRENCES C
1 h
T/w[S /
CEG-H :
SRP :
3-27-87 SIGNATURE DATE (S]GNATURE*
DATE
\\ /
APPROVED BY:
s.,
O,h.D N 3 Z1[M N/A SP MANAGER DATE
MANAGER OF NUCLEAR DATE POWER CONCURRENCE (FINAL REPORT ONLY) 1 l'
- SRP Secretary's signature denotes SRP concurrences are in files.
8704070164 870331 l
DR ADOCK 05000327 PDR p-.-._-.-
TVA EMPLOYEE CONCERNS REPORT NUMBER:
REPORT TYPE:
SPECIAL PROGRAM 80203-SQN Element Report REVISION NUMBER:
TITLE:
4 Inspection Performance PAGE 2 0F 11 1.0 CHARACTERIZATION OF ISSUES 1.1 Introduction The issues described below were derived from Employee Concerns generated as a result of the Watts Bar Employee Concern Special Program. The issues were specific to the Sequoyah Nuclear Plant.
L 1.2 Description of Issues 1
The conditions reported (Attachment A) by concerned employees are:
L a.
Inspection personnel were distracted by craf t personnel and did
(
not observe damaged cable insulation.
(00-85-005-003) b.
Craf t and inspection personnel falsified anchor pull tests and i
applicable documents.
(XX-85-023-X02) c.
Conax connectors in the containment did not always meet vendor wire bend radius instructions, connector installations with deficiencies were inspected and accepted by Sequoyah Quality
~
no action was taken by SQN QC management to investigate or document the deficiencies.
(I-86-101-SQN) d.
An item of equipment may not have been adequately inspected.
(SQM-6-009-001) h 2.0
SUMMARY
r-2.1 Sucimary of Characterization of Issues A
=
4 The issues raised by the employee concerns suggest that:
inspection personnel were distracted by craft personnel and did not perform their 3
required functions; test results and documents were falsified; inspection personnel did not perform an adequate inspection of an item; and QC Management failed to investigate or document identified deficiencies.
2.2 Summary of Evaluation Process y
The evaluation process consisted of a review of the Employee Concern files, Quality Technology Company (QTC) files, and Nuclear Safety Review Staff (NSRS) files to determine the scope and extent of the concerns identified.
The Nuclear Quality Assurance Manual, lower tier procedures and instructions, General Construction Specifications, Work Requests and other related correspondence and documents were reviewed to determine
-=
P o
TVA EMPLOYEE CONCERNS REPORT NUMBER i
SPECIAL PROGRAM 80203-SQN
?
REPORT TYPE:
REVISION NUMBER:
Illement Report 4
TITLE:
PAGE 3 0F 11 Inspection Performance the programmatic requirements and management directives related to the issue.
Discussions were held with Quality
- Control, Construction, and Modification personnel to obtain more specific. information regarding the issues.
The documents reviewed during the investigations and used in the evaluation are listed on Attachment D.
2.3 Summary of Findings 2.3.1 Issue - Inspection personnel were distracted by craf t personnel and did not observe damaged cable insulation.
,j The concern from which; this issue was extracted provided reference to a similar concern (00-85-005-014) which noted specific cable / conduit runs and identified the period in which 4
the incident occurred as 1977.
1 The records that were applicable to,the specific cable pulling A
operation were reviewed.
It was determined ' that the cables y
receive.d and passed High Iotential (Hi-Pot) tests. The cables N
have since been de-energized ' and the electrical circuit for the back flow gate hoist motors have been connected from a
9 automatic control to manual control.
R) 2.3.2 Issue - Craf t and inspection personnel falsified anchor pull
.q M
tests and reirted documentation.
.?
The investigation identified an Employee Response Team (ERT)
A dealing with the same issue.
The investigation also Report Q
produced a copy of a memorandum from the Office of the General Counsel which agreed with the ERT findings and took no further
- W~
action on the f alsification issue raised.
Based on the ERT Report, the interviews conducted, and the Quality Assurance Category Evaluation Group (QACEG) evaluation - of the results, the QACEG could find no cases where anchor pull tests were falsified.
a 4
" Investigation and evaluation of anchor pull testing concerns A
is covered in the Construction CEG Subcategory Report 11300,
,3 Revision 0, titled ' Anchorages'".
2-Issues -- Conax connectors in the containment did not always 2.3.3 vendor wire bend radius instructions; connector meet installations with deficiencies were inspected and accepted by-SQN QC; no action was taken by SQN QC management to investigate or document the deficiencies.
. -. ~. _
.--,---,,-,,,-.-m n,,-.-c en-.,,,-
-,.,-,.-w
,---,e..m-.m,-.
f TVA EMPLOYEE ' CONCERNS REPORT NUMBER:
M
- ~. REPORT TYPE:
SPECIAL PROGRAM 80203-SQN REVISION NUMBER:
Element Report 4
TITLE:
PAGE 4 0F.11 Inspection' Performance The NSRS investigated these issues and issued report No.. I 101-SQN dated February-1986 ( Attachment. B).
A Corrective Action Report dated February 1986 was also issued.
Two valves were found to have connectors'where wire bend radii were below minimum requirements - and workplans.were found to have - been written where work was performed and.' inspected;. however, the plans did not refer to the vendor manual for installation of the connectors.
Lack. 'of QC management 1 action. could not be verified since the QACEG could. find no evidence to. determine if the concerned-individual brought this issue to QC Management prior to the NSRS investigation.
The issue of the connectors not meeting the wire bend radius instructions and connectors being installed and accepted with deficiencies is valid.
A reinspection was initiated by TVA Management.
Specific corrective actions and the results achieved to date are discussed below.
2.3.4 Issue -- A item of equipment may not have been adequately inspected.
w i
This issue could not be evaluated since there was-insufficient.
information available to perform an investigation.
l I
2.4 Corrective Actions Taken and the Results Achieved to Date It could. not be determined if-cable insulation was improperly repaired.
However, - QACEG investigation has determined, through the issuance of Corrective Action Tracking Documents and Responses from the SQN Site Director, that the subject cables have been tested, 3,.
experienced worst case conditions, and been 'in service since 1977.
Engineering concluded 'if there was. insulation damage, it was not sufficient to impair the fuention of the cable and no further action f(
is needed.
j Conax connectors were installed outside the allowable limits.
A Corrective Action Report was issued causing for a QA Program revision, reinspections and rework.
This ' was completed in August 1986' and no further actions are required.
L.;
3.0 EVALUATORS d
in D. G. Barlow R. D. Halverson i
lf 4.0 EVALUATION PROCESS 1
l 4.1 Ceneral Methods of Evaluation n.,-.---
1 I
' TVA EMPLOYEE CONCERNS REPORT NUMBER:'
' REPORT TYPE:
SPECIAL PROGRAM 80203-SQN
- Element Report REVISION NUMBERi TITLE:
4 Inspection Performance PAGE-5 0F 11 i
Research of the files produced additional information to support the
. investigation by way of NSRS Reports and an additional concern.
?)
Construction specifications, procedures and instructions were reviewed to extract the requirements and determine adequacy of the details provided.
Microfilm records provided details of inspections and tests performed and personnel discussions were held to support the records reviewed.
d Corrective action records and supporting data were also reviewed to -
provide details on the deficiencies noted and the corrective actions i
taken.
4.2 Specifics of Evaluation A
4.2.1 Issue -- Inspection personnel were distracted by craft personnel and did not observe damaged cable instruction.
a fj In researching the files for additional information regarding craft distracting inspection persdhnel and cable insulation 3
damage, QACEG personnel reviewed a related concern (00-85-005-4 014) which identified the specific cable / conduit runs involved.
Four cables were identified.
That concern also identified the period of time as mid-1977.
f.
Microfilm records relating to-the above identified h
cable / conduit runs were reviewed (cable pulling
- cards, q
cable / conduit inspection
- cards, and Hi pot records) to 4
determine if inspectio'ns were performed and ' tests completed.
O An interview was held with an individual involved in the inspection of three (3) of the above noted cable pulls.
The q
interview centered around how an inspector may become 5
distracted and how an inspector can cover the inspections I
given the various areas cable is pulled through.
General Construction Specification G-38, Revision 1,. dated October 22, 1975 " Installing Insulated Cable Up to 15,000 Volt Inclusive", was reviewed to determine if instructions were provided for repairing damaged cable and/or insulation.
Likewise, Sequoyah Inspection Instructions Numbers SNP 11-28, a
" Cable Pulling Ins pection'.' Revision 0 (dated May 26, 1977),
Revision 1 (dated June 11, 1977),
Revision 2, (dated October 4, 1977);
SNP I1-10,
" Electrical Penetration and Interconnecting Cable Termination and Insulation Inspection" Revision 6 (dated. December 27, 1976),
Revision 7 (dated May 26, 1977), Revision 8 (dated June 11, 1977), Revision 9 (dated December 21, 1977); SNP II-26, " Exposed Conduit and
.=
r.
m
'4
- TVA EMPLOYEE CONCERNS REPORT NUMBER:
REPORT TYPE:
SPECIAL PROGRAM
.80203-SQN Element. Report REVISION NUMBER:
TITLE:
4 Inspection Performance PAGE 6 0F'11-Conduit Box Inspection", Revision 0 (dated May 26, 1977),
Revision 1 (dated June'.11, 1977),
Revision 2.(dated h
September 13, 1977), Revision.3 (dated October'14, 1977), were i
reviewed to determine inspection requirements and adequacy of those methods and acceptance criteria to enable an inspector to perform the intended functions.
A Construction Category Evaluation Group Element Report No..
C010900-SQN dated Nov. 1986 was also reviewed for additional information pertaining to the subject issue.
F 4.2.2 Issue -- Craft and inspection personne1' falsified anchor pull.
tests.and related documentation.
An Employee Response Team (ERT) Report (XX-85-023-X02, dated
-March, 1986)- (Attachment, C) was found to address the same issue.
The QACEG investigation attempted to secure a listing or the hangers in the Unit 2 Annulus area since the employee concern identified this area specifically.
A list of hangers by location does not exist, according to Engineering, and it was concluded that if records. were located it would be extremely difficult to establish if the test results-were falsified.
Therefore, emphasis was placed on locating and discussing the issue with personnel who were involved in anchor bolt installations / inspections in that period.
A review was performed of General Construction Specification G-32,
" Bolt Anchors. Set In Hardened Concrete" Revision 4 (dated April 21, 1976).and Revisio'n 5 (dated July 21, 1977) to determine the installation and test requirements. ' Inspection Instruction SNP 11-93, " Testing of. Expansion Anchors Set in Hardened Concrete", Revision 0 (dated February 14, 1977),
Revision 1 (dated March 15, 1977),
Revision 2 (dated November 2, 1977) were ~ also reviewed to determine testing 3
requirements and the sseociated documentation.
4.2.3 Issue -- Conax connectors in the containment did not always meet vendor wire bend radius instructions, connector installations with deficiencies were ' inspected and accepted by Sequoyah Quality Control (SQN QC); no action was taken by SQN QC management to investigate or document the deficiencies.
l
?
NSRS Report I-86-101-SQN dated February 1986 was written on g
the above issues along with a Corrective Action Report CAR-86-02-005 also dated February 1986 describing deficiencies on Conax connector bend radii.
The CAR and subsequent revision to Maintenance and Addition Instructions M&AI-19 (RI), " Installation of Conax Connectors" were reviewed to determine if adequate requirements-for i
l
. ~..
4
TVA EMPLOYEE CONCERNS REPORT NUMBER:
REPORT TYPE:
SPECIAL PROGRAM 80203-SQN hiement Report REVISION NUMBER:
TITLE:
4 Inspection Performance PAGE 7 0F 11 inspection of wire bend radii had been provided and if the CAR had been closed satisfactorily.
In ~ researching the
' issues concerning Conax connector deficiencies, the QACEG Evaluation Group interviewed the QC
' Electrical Supervisor.
A copy of Corrective Action Report SQ CAR-86-02-005 dated February 10, 1986 was furnished by this individual.
4.2.4 Issue -- An item of equipment may not have been adequately inspected.
Insufficient information available
-to perform an investigation.
(
5.0 FINDINGS 5.1 Findings on Issue - Inspection personnel were distracted by craft
{
personnel.
5.1.1 Discussion Concern No. 00-85-005-003 dealing with the inspector being
-a distracted and preventing him from noticing damage to cable insulation referenced Concern No.
00-85-005-014 which identified four specific cable / conduit runs.
That concern stated in part, " Insulation was mistakenly cut off of a 440 volt cable and the insulation was reattached with electrical i
tape."
The concern went on to identify the cables as the power feed to the Back Plow Gate Hoist Motors.
There are four such motors and*are.part of the Essential Raw Cooling Water-(ERCW) System. That same concern identified four cable / conduit runs as 1-PL-6370-B, 1-PL-6360-A, 2-PL-6370-B and 2-PL-6360-A and also identified the period of time as mid-1977.
Concern No. 00-85-005-014 is a reissue of Concern No. 00 005-001.
The reason for ' reissue was a correction of one of the cable numbers referenced in the concern.
This concern was part of the Construction Element Report No. C010900-SQN and-the particular issue is addressed under the heading
" Insulation Damage".
Inspection records show that two (2) inspectors were involved with the cable visual examinations of the identified cable / conduit runs in the period from June-September 1977.
An interview was held with an individual involved in the inspection of three (3) cable pulls (1-PL-6370-B, 1-PL-6360-A, and 2-PL-6360-A).
The interview centered around how an inspector may become distracted and how an inspector can cover 1
r
.(
i TVA EMPLOYEE CONCERNS REPORT NUMBER:
' REPORT. TYPE:
SPECIAL PROGRAM 80203-SQN
- Element Report REVISION NUMBER:
TITLE:.
4 Inspection Performance PAGE 8 0F 11 the inspections given the various areas' cable is. pulled through.
The. individual involved with cable puli 2-PL-6370-B inspection could not-be interviewed as he is no longer-employed by TVA.
The individual interviewed, who inspected-three of the four cables in question, stated that because of the various areas a cable may be ' pulled through the inspector could not always witness the - entire operation.
In his opinion, the point at issue could have happened.
In reviewing the records it was noted that the four (4) cable / conduit runs referenced are'non-CSSC and received acceptable installation inspection and 4
testing through the period June-September 1977.
These cables received and passed a.Hi-Pot Test.
It was also-found that-the cables have - been de-energized and per -ECN L5720, the electrical circuit for the Back Flow Gates have been converted from automatic control to manual control.
In discussions with the Design Engineering personnel and a E
review of the drawings associated with the motors and cables, it was found that the design drawinds 45N-751-1,
-2,
-5, and -
6 do not reflect that the cables have been de-energized and f
motors taken out of service.
h 5.1.2 Conclusion The issue of an inspector being deliberately distracted from noticing a cable insulation nonconformance and the same inspector being distracted while the cable was improperly I'
repaired and pulled into the conduit cannot be substantiated.
However, since the referenced cables have been de-energized the issue raise'd by.the concerned employee is invalid at this time.
2 5
Craf t = and inspection personne1' falsified anchor 5.2 Finding on Issue pull tests and applicable documents.
5.2.1 Discussion The SQN Inspection Supervisor provided the names of five (5) inspection personnel who were involved in anchor bolt j
inspections in' 1977.
These personnel were interviewed to determine their knowledge of falsification of test records or other wrongdoing involving records.
They all.said they had heard that falsification had happened at Watts Bar, but no one could recall an instance of falsification of test results having happened at SQN.
P The ERT report mentioned conducting interviews with 27 individuals involved in the installation and inspection of m-
'l l
.,_--_...__.-.___,,._-,,-,.-,-.m._--,
_.,~ __ __
TVA EMPLOYEE CONCERNS REPORT NUMBER:
REPORT TYPE:
SPECIAL PROGRAM 80203-SQN
$lement Report REVISION NUMBER:
TITLE:
4 Inspection Performance PAGE 9 0F 11 l
anchor bolts.
They too denied knowlege of falsification of test records.
j The Office of General Counsel (OGC), in their memorandum to l
the Manager of Nuclear Power dated April 30, 1986, concluded l
that in its review of the QTC investigation into the issue of craft and inspection personnel falsifying anchor pull tests i
and documentation there was
"...no collaborating / objective l
evidence
...found to allow substantiation."
The Office of General Counsel will take no further action on this issue.
In a phone conversation with the Office of the Manager of Nuclear l
Power, ONP advised that it has accepted the decision of the t
Of tice of General Counsel regarding this issue.
"The Construction CEG has performed an extensive investigation 4
and evaluation of the anchorage issues and has reported on their findings in Subcategory Report 11300 Revision O.
5.2.2 Conclusion r
Based on interviews, lack of data 'to support the issue, the ERT Report and the OGC memorandum, it is concluded that the issue of craft and inspection personnel falsifying anchor pull tests and applicable documents is not substantiated.
5.3 Finding on Issues - Conax connectors in the containment did not always meet vendor wire bend radius instructions, connector installations with deficiencies were inspected and accepted by Sequoyah Quality Control (SQN QC); no action was taken by SQN QC management to investigate or document the deficiencies.
5.3.1 Discussion The issue dealing with Conax connectors and deficiencies noted was the subject of a NSRS Report of " Installation of Conax Connectors", I-86-101-SQN dated February 1986 and a Corrective Action Report (CAR)
SQ CAR 86-02-005 dated February 10, 1986.
Two valves were verified to have wire bend radii below minimum allowed.
A sample was than taken from Units 1 and 2 and an additional 14 valves were found to have deficient wire bend radii.
Workplans were written to install the connectors, field installation was completed and inspections were performed.
Work plans did not contain steps e
to verify wire bend radius nor did they reference the vendor manual for installation.
(Reference Attachment G for general 4
arrangements details for Conax Connector.)
A review was made of the CAR and a subsequent revision to 4
Maintenance and Addition Instruction M&AI-19 (RI),
" Installation of Conax connectors".
It was determined that
~. - -.. - ~.
TVA EMPLOYEE CONCERNS REPORT NUMBER:
REPORT TYPE:
SPECIAL PROGRAM 80203-SQN
- Element. Report REVISION NUMBER:
TITLE:
4 Inspection Performance PAGE 10 0F'11 the requirements for inspection of wire bend radii have been added.
A 100% reinspection for the minimum bend radius and rework as necessary to all Conax connectors, and the~ EQ 4
Project Manager's concurrence with the vendor manual revision have been performed.
TVA QA ~ verified corrective action was taken and CAR 86-02-005 was closed in August 1986.
5.3.2 Conclusion The issue of Conax connectors installed in containment that do
?~
not meet the vendor wire bend radius instructions was substantiated.
However, this condition was documented in SQ CAR-86-02-005, reinspections have been performed, and corrective actions have been completed.
p The issue of connectors < being inspected and accepted by QC 4
with deficiencies is factual since there were. cases found l
where wire bend radii was inadequate.
Work Plans for the installation of the connectors did not address bend radii when q
issued.
General Construction Specification G-38 did. not L
address wire bend radii'either.
Iniipections were conducted to the requirements of the approved workplans.
It was the d
omission of minimum wire bend radius inspection criteria in the workplans which allowed the connector installation to be f'
accepted by QC.
The inclusion now, of vendor. instructions for minimum bend radius in the M&AI-19 (RI) will preclude the omission of bend radii inspections in the future.
r The issue ot no action being taken by SQN QC Management to investigate and document. the deficiencies prior to the NSRS investigation cannot be sushtantiated.
No evidence exists to determine if anyone knew there were deficiencies prior to the investigation.
a 4
5.4 Finding on Issue - An item of equipment may not have been adequately.
inspected.
In researching this issue the QACEG could not find any specific information to aid in a meaningful investigation.
5.5 Corrective Action Corrective Action Report CAR-86-02-005 was issued in February 1986 to document that Conax connectors were installed outside the allowable limits.
Corrective actions included Environmental Qualification (EQ) review and concurrence with the Conax Vendor Manual and issuance of Rev. I to Maintensuce and Addition Instruction M&AI-19 to included wire bend radii criteria.
Reinspections and rework was performed on all Conax connectors and verification by Quality Assurance (QA) was j
completed in August 1986. No further actions were required.
y TVA EMPLOYEE CONCERNS REPORT NUMBER:
REPORT TYPE:
SPECIAL PROGRAM 80203-SQN Element Report REVISION NUMBER:
TITLE:
4 Inspection Performance PAGE 11 0F 11 f
The ECSP Corrective Action Tracking Document Nc..
80203-SQN-01 (Attachment E) which was issued on September 18, 1986 was issued for Engineering to evaluate the long term effect on the cables being repaired with electrical tape.
The SQN Site Director has since responded by saying that records indicate acceptable installation and testing (Hi-Pot and Megger).
The cables have been in service since 1977 and it is likely that they have experienced the worst conditions including submergence during that time without any problems.
Engineering concluded that if there was damage, it was not sufficient to impair the function of the cable and no further action is needed.
With the additional information made available to QACEG and further.
research where it was found that Engineering did not reflect the status of the cables as being de-energized on the design drawings, QACEG has prepared CATD 80203-SQN-02 (Attachment F) for SQN to evaluate the problem condition in light of their response to CATD 80203-SQN-01.
The SQN Site Director has responded by stating:
" Design Drawings 45N751-1,
-2,
-5 and -6 do reflect the system status, however, the electrical circuit for the back flow gates had been converted from automatic control to manual control by the unit operator (ECN L5720) which he has authority to do.
The breakers tor the back flow gate hoist motors are being tagged with ' caution order' of the administrative operation."
r QACEG concurs with this response and no further action is required.
Attachment A identified,these issues as potentially safety related and safety significant.
- However, corrective measurn-which include procedural revisions rework and reinspection have been completed.
No further action is required.
6.0 ATTACHMENTS A.
List of Employee Concern Information Subcategory:
80203 Inspection Performance bi B.
NSRS Report I-86-101-SQN C.
QTC Employee Response Team (ERT) Report No. XX-85-023-X02 D.
Listing of documents and correspondence reviewed during the investigation ot these issues.
E.
CATD No. 80203-SQN-01 and SQN Memorandum dated October 29, 1986 (RIMS S03 861022 808)
F.
CATD No. 80203-SQN-02 and SQN Memorandum dated January 24, 1987 (RIMS l-S03 870123 803) 4 G.
General Arrangement Detail for Electrical Conductor Seal Assembly Conax.
ATTACilHENT A o
PRGE 13 'f TENIIESS VALLEY AUTHORITY RUll TIME - 13: 48:
- ECEREtICE
- ECPSI20J-ECPS121C OFFICE OF'llUCLERR POWER Rut! DATE - 10/16/
4 E EQUE!!CY
- REQUEST EMPLOYEE'CutlCERil PROGRAM SYSTEM (ECPS) i :llP - 1555 - RHt1 LIST OF EMPLOYEE CutlCERtl IllFORI1ATI0tl
.1EGORY: QA QA/QC PROGRAMS SUBCATEGORY: 80203 IllSPEQTION PERFORMANCE KEYHOP.D A j
i S
GENERIC KEYHORD B H
APPL QTC/flSRS P
KEYlIORD C l
C0tICERil SUB R PLT BBSH INVESTIG AT 1011 S
C0tlCERN KEYHORD D i
nut 1 DER CAT CAT D LOC FLQB REPORT R
DESCRIPTI0tl 101-SQtt QA 80203 !! SQtt it H 11 11 NS 1.CONAX C0ilNECTORS IllSTALLED IllSIDE i
SEQUDYAH HUCLEAR PLAllT ( SQti) UtlIT 1 K-FORM C0tlTAltit1EllT DO NOT ALHAYS MEET VENDO R HIRE BEllD RADIUS REQUIREMEilTS. 2.A l
l LLEGED DEFICIEllCIES III C0llAX CONilECT OR INSTALLATI0tl HERE IllSPECTED BY SQ l
il QUALITY CollTROL (QC) AtID ACCEPTED.
i 3.110 ACTI0tl IIAS T AKEli BY SQti QC MAN AGEMEllT TO IllVESTIGATE OR DOCUMEilt T HESE DEFICIEllCIES HHEli THEY HERE MAD I
l E AHARE OF THEM.
~
J asumumusussen y
t I
.......n
....n.
.r a..-
w SEQUDYAH: CRAFT FOREMAll (Kil0Hil) Af1D N0 tlc 0tlFORMANCE I
- G 005-003 QA 80203 N SQH YYNY OTHER MEMBERS OF THE CREW DELIBERATE CORRECTIVE ACTIDIL GEllERAL K-FORT 1 LY DISTRACTED All INSPECTOR TO PREVEll FOREMAN T50224 T THE INSPECTOR FR0t1Il0TICING A N0 tlc ONFORMAllCE REGARDItIG CABLE INSULATIO I
N DAt1 AGE.
THE IllSPECTOR HAS DISTRAC TED HHILE THE CABLE DAMAGE IIAS REPAI l
RED IMPROPERLY, AllD THE CABLE PULLED IllTO THE C013DUIT.
(SPECIFIC CABLE l
j CONCERil ADDRESSED III THIS FILE, C0 tlc i
ERtl 001) DETAILS Kil0 Hit TO QTC, HITHH ELD DUE TO C0tlFIDEtiTIALITY. 110 FURT i
HER INFORMATI0tl MAY BE RELEASED. CO NST. DEPT. CollCERil. CI HAS tl0 F
!!OilCallF ORMAllCE A PIECE OF EQUIPMEllT (NOT SPECIFIED)
IllSPECT I0tt 0M-86-009-001. QA 80203 H SQN N N N 11 I-86-242-SQti SS MAY llCT HAVE BEEli ADEQUATELY IIISPEC i
T50262 TED.
DETAILS KN0!!il TO QTC, HITHHELD QUALITY K-FORif DUE TO CONFIDENTIALITY. 110 FURTHER EQUIPMENT INFORMATI0tl MAY BE RELEASED. NUCLE AR POWER DEPARTMElli CollCERil.
)
I 14*P et
- t# 'd g-t e..
.L a i.
, 14 TElitlES E VALLEY AUTHORITY PAGE RUll TIME - 13:48:
'EFERE!!CE
- ECPSI20J-ECPSI21C OFFICE OF'llVCLEAR P0HER RUll DATE - 10/16/
REQUEST EMPLOYEE CutlCERil PROGRAtt SYSTEM (ECPS)
REQUEllCY itIP - ISSS - RHit LIST OF EMPLOYEE CollCERil IllFORMATI0ff
.T EGORY : QA QA/GC PROGRAMS SUBCATEGORY: 30203 IllSPEpT10tl PERFORMAtlCE KEYl!ORD A S
GENERIC KEYllDRD B Cot!CERII SUD R PLT D B S II INVESTIGATI0ll S
C0!!CERtl
- KEYHORD C H
APPL QTC/NSRS P
KEYll0RD D tlUltDER CAT CAT D LOC, FLQD REPORT R
DESCRIPTION FALSIFICAT10tl CRAFT AtlD IllSPECTI0tt PERSOffilEL FALSI RECORDS SS OC 023-X02 IH 00000 S SQti il !! Y !!
FIED AllCil0R PULL TESTS AllD APPLICADL OPERATI0tl3 T50135
,q A 80205 K-FORM E DOCUllEllTS. HID 1977.
UtlIT 8 2, Atitt AllCHORS
" DETAILS TO SPECIFICE CA ULUS AREA.
SE Kil0 Hit TO QTC AllD HITHELD TO NAlllT AIll C0!!FIDEll11 ALITY). C0tiSTRUCTI0tl DEPT C0!!CER!l. CI HAS HQ HORE IllFORilA j
T 10tl.
f I
t I
i L
1
~
t e
e O
O T
l
', TVA 4 (os-s-ess tomwAS sS)
UNITED tiTATES COVERNMENT ATTAClelENT B Memorandum TENNESSEE VALLEY AUTHORITY TO: H. L. Abercrombie, Site Director, Sequoyah Nuclear Plant
(
K. W. Whitt, Director of Nuclear Safety Review Staff. E3AB C-K FROM:
?
{ { @ 2 7 1986 I*
DATE:
SUBJECT:
NUCLEAR SAFETY REVIEW STAFF INVESTICATION REPORT TRANSMITTAL k
l A,
Transmitted herein is NSRS Report No.
T-86-101-SON l-(
Subject INSTALLATION OF CONAI CONNECTORS Concern No.
N/A
,and associated prioriti::ed recommendations for your
),
action / disposition.
~
a It is requested that you respond to this report and the attached Priority l,
f.
2 [P2] recommendation by April 28, 1986. Should you have any questione, u
1 l*
e,*
E please contact W. D. Stevens at telephone 6231-K b
5
' Recommend Reportability Determination: Yes
.No I
l s
f y
9 irector, NS m nesilfree
=ans ama mtsn vna me r :rceserre.
WDS:JTH Attachment cc (Attachment):
MAR 0FB6 W. C. Bibb, BFN W. T. Cottle, WBN James P. Darling, BLN
, j g R. P. Denise, LP6N40A-C J # 2 G. B. Kirk, SQN D. R. Nichols, E10A14 C-K jQ QTC/ERT, Watts Bar Nuclear Plant
-g E.'
Eric Sliger, LP6U48A-C J. H. SulliVan, SQU
-fig 7.
543U
=
..._. _. _. _._ _ Nm > =5 L
It /
)
r
- a..
~
w TENNESSEE VALLEY AUTHORITY NUCLEAR SAFETY REVIEW STAFF NSRS INVESTICATION REPORT NO. I-86-101-SQN N
IN5TALLATION OF CONAX CONNECTORS
' ~"~
4 SUBJECT r.
~
DATES OF s
INVESTICATION:
FEBRUARY 10-13,*1986 5
4 I
'^
u
'INVESTICATOR:
DATE 4
s N. T. EENRICH
.a s
I M
d 2!24 /M
..R$VIEWEDBY:
DATE I
L. E. BROCK
~
i 6!
A
)
p'N O/ 7 [b D
8 AA.~/
S APPROVED BY:
- w. D. STEVENG DATE /
d 0
8
- g g
i 44#i2 %
4 6
e e
o--
ww g
O w-mA.,,e,,jg
1 t
I 1
\\
1 I.
BACKCROUND A Nuclear Saf ety Review Staf f *(NSRS) investigatio 87-001.
the NSRS during the investigation of employee concern IX-85-0 The concern addressed by this report was not related to the concern dum from under investigation at that time and was outlined in a mesoran31, 1985 (Ref. 1).
C. E. Chmielewski to R. C. Sauer dated December id not come The employee concern addressed by this investigation report d A
through the Quality Technology Company (QTC)/Employea, Response Te Therefore, no Employee Concern Assignment Request Form is a
(ERT).
availabl,e summarizing the concern of record.
II.
SCOPE-f The scope of this investigation was determined from the concern o record as summarized in reference 1 to be that of three specific d
A.
ii j'
issues requiring investigation:
Conax connectors installed inside Seq'uoyah Nuclear Plant (SQN)*
i unit 1 containment do not always meeg vendor wire bend rad us y
L 1.
6.
requirements.
I.k Alleged deficiencies in Conax connector installation were t
inspected by SQN Quality Control (QC) and accepted.
2.
3..
il!
d' n
No action was taken by SQN QC management to NI 3.
f To accomplish this investigation, vendor manuals and environmental qualification data sheets were reviewed to determine Conax conne B.
~
Procedures governing the actual
. installation requir.ements.
installation of these connectors were reviewed and com
- q
- /
determine if Conax connector installation deficie these requirements.
h4
~~
.L deficiencies should they exist.
~
~
L s,
s III.
SUMMARY
OF FINDINGS Requirements and Commitments J
A.
}
Not applicable to this investigation.
~ '.,
- S B.
Findings Conax Corporation Manual, I_ nstallation Manual for Electric _
Conductor Se'n1 Assemblies with Lenz Body for Pipe Thrend_
1.
houlement Interfac_e, IPS-725, was originally issued June 26, ii "C" which The latest revision to this manual is rev s on 1981.
1 re
"***'-weae.as,%.p,,
was issued February 15, 1985 (Ref. A).
This manual provides and install'ation instructions for basic information. handling, Conax clectrical conductor seal assemblics type ECSA.
ifies the minimum wire bend radii
,Section 7.2 of the manual specBased on a review of the manual revision los, it appears that these requirements were identified in the original requirements.
issuance of the manual.
Reference 3 documents that Conax electrical conductor sea assemblies type ECSA are environmentally qualified for forty 2.
years with one design basis accident and 100-day postaccident t'
However, the initial installation.and subsequent reinstallation or replacement of the seal following maintenance operation.
must be performed in,accordance with Conax installation '
' instructions outlined in reference 4.
Workplans 11077 R1,11231, and 11335 (Ref s. 6. 7, and 8, respectively) were written to install Conax conne 3.
f Each of these workplans were prepared and worke These workplans did not.
installation of Conax connectors.
specify minimum connector wire bend radius requirements and d f
8 Each of not require-verification of installed
- wire bend radii.
these workplans had been reviewed and approved by SQN QC Werk was performed in accordance with the workplans, personnel.
and specified QC inspections were performed.
Discussions with QC personnel revealed that so f E'.
4.
QC inspectors training when it was offered to craf t personnel.
- ~
evaluated Conax connector installations asainst requirementsThe identified in approved workplans.
not include evaluation of wire band radii.
b,
- 5. Modifications and Additions Instruction M&AI-19 R0 (Ref s
and provides guidelines for initial d
approved April 12, 1985, SQN.
As
. field installation of electrical Conax connectors for radius requirements for these connectors nor did it' identify a ne.ed to inspect completed installations for acceptable wire bend radii.
Modification and Additions Instruct [on H&AI-19 was subsequently 26,1985 (Ref. 2b) and incorporated vendor 6.
revised July recommendations f or the minimum bend radius of elect pigtails as specified by Conax Corporation in reference 4.
s 2
~
- ~.. - _ - _.
\\'
i
^
3 Maintenance activities have confirmed that valves 2-PSV-43--310 7.
and 2-FSV-43-319 installed under wokplan 11077 R1 have wire bend radil which do not meet minimum requirements set forth in M&AI-19 R1 (Ref. 2b) and Conax manual IPS-725 (Ref. 4).
have been initiated to Work requests B-106737 and B-106242 inspect a sample of installed Conax connectors for. proper wire 8.
Preliminary inspections indicate that a number of bend radii.
valves using Conax connectors on both units do not meet' the -
specified wire band radii requirements.
y
~
10, 1986, SQN Corrective Action. Report (CAR)
On February 9.
SQN-CAR-86-02-005 (Ref. $) was-is' sued to identify an adverse.
' condition related to the installation of Conax connectors.
~ ' ~ ~ This CAR states:
Contrary to the requirements of M&AI-19 and the Conax vendor manual IPS-725, not all Conax connectors were installed with wire band radii within allowable limits. In addition, M&AI-19 is not consistent with the vendor manual revision referenced in the IQ binder.
j Adherence to these requirements is*necessary to maintain equipment environmental, qualification.
8 As written, M&AI-19 R1 (Ref. 2b) specifies a different torquing s
sequence and different final torquing values than Conax
. (,
installation manual IPS-725 (Ref. 4).
In addition, M&AI-19 R1
)
does not provide details regarding application of Grafoil sealant.
In accordance with SQN Administrative Insttvetion AI-12 10.
(Ref. 9) an evaluation of the root cause of the deficiency.
must be completed within 30 days 1
addressed by SQN-CAR-86-02-005 of the issuance of a CAR. This evaluation must also address
(
remedial corrective action, action to prevent recurrence, and '
an estimated schedule for completing the corrective action.
a S
QC has begun reviewing all workplans and/or work instructions 11.
for work affecting any equipment within the scope,of the
, environmental qualification program against vendor instructions to ensure compliance with vendor recommendations.
IV.
CONCLUSIONS AND REC 019tENDATIONS i
A.
Conclusions The first issue raised by the concern of record is 1.
substantiated in that several Conax connectors have been installed on both units 1 and 2 without meeting the minimum wire bend r'adii requirements set forth in Conax installation manual IPS-725.
~
s 3
N
"'-****%wwe s+g,
--mm---,~~,,,-~n-mm---a,,-,--r,-----r-~---w-nw.-,
-n----,--..,,m.--
e,
.-+n,- - -,,,-,,--
m-
~
'~
[
\\.
j d not be The second issue raised by the' concern o'f record coul Conax con,ncetors were installed in accordancef 2.
substantiated.
with approved workplans.QC inspectors were not directed to inspectIt sho approved by QC.Conax installations for proper bend radii.k l n l
however, that the wor p ainstallation recomendations identified in regarding minimum wire bend radii.
ld not be The third issue raised by the concern of record couhas been. issued to CAR SQN-CAR-86-02-005 A response.
5 3.
document Conax connector installation deficiencies.unless an exte substantiated.
d is required by March 12, 1986, Recomendations B.
I-86-101-SQN-01, Resolution of Deficiencies t
The deficiencies identified in corrective action repor in accordance i
should be addressed and resolved SQN-CAR-86-02-005 with SQN AI-12.
[P2]
1 t
3
.g k
s s
4 fyf....
- c p
et s
^
4 l
e e
I e
A L--
.u 1
(
.'.s DOCUMENTS REVIEWED I INVESTICATION 1*86-101-SQN-AND REFERENCES l
Infornal memorandum from C. E. Chmielewski to R. C. Sauec, "
85
(
1.
i f Conax Modifications and Additions Instruction H&AI-19 "Installat on o 2.
Connectors" R0 dated April 12, 1985
+
s, a.
b.
El dated July 26, 1985 t
Seal Assemblies SQN Environmental, Qualification Binder, "Conax Conduc or 3.
(ECSA)." No. SQNEQ-CSC-001 d t r Sea _1_
Conax Corporation, Installation Manual for Electrical Con uc ofor Pipe Thread Eou 4.
Body Assemblies with Lont 15, 1985 IPS-725 RG, dated February dated February 1, 1986 0
5.' SQN Corrective Action Report SQN-CAR-86-02-005 Valves Inside Workplan 11077 R1, " Installation of Conax Conne'ctors in PASF i
15, 1984
- 6.
Containment," prepared.0ctober x
d
.j
- 7. ; Workplan 11231, "Various Equipment Seals - NUREG-0588," prepare g
September 24, 1984
- f...# 'B. ~ Workplan 11335. "Various Equipment Seals - NUREG-0588," prepared P
November 7, 1984
- f d Correct.ivo SQN Administrative Instruction - AI-12, " Adverse Conditions an Actions," R20, dated August 2, 1985.
,',9.
f
~
8 g
du
<e>
=7\\
e
.t s
5
- -g Y9 x.4 S
og 5
N~.
w.
6
i 1
(s (1
i ATTACm1ENT C QUALITY TECHNOLOGY COMPANY g
(615)365 4414 Sweetwater. TN 37874
~P.O. BOX 600 PAGE 1 OF 4 L
ERT. INVESTIGATION REPORT 1
CONCERN NO:
XX-85-023-X02 falsified anchor j
h Craft and inspection personnel T
CONCERN: 'Sequoyah; (Mid-1977, Unit 2, Annulus).
, pull-tests and applicable documents, INVESTIGATION-PERFORMED BY:
T.
Hough DETAILS a
t PERSONNEL CONTACTED: (CONFIDENTIAL) i 2
h' g
- 4 6
f 1
s s
+
g h
s
.t OI k-
,,g, 5
N e -
b l'
d b
??
J l
6 9
i 9
1 c8*
c
(
e P
9 PALE 2 OF 4 ERT INVESTIG.; TION REPOllT CONCERN NO:
XX-85-023-X02 DETAILS, continueo DOCUMENTS REVIEWED:
Instruction - 93 (II-93)
" Testing of Expansion l
in Hardened Concrete and Grouted Anchors" l.-
SNP Inspection Anchors Set R-0 (2/22/77), R-1 (3/22/77), R-16 (8/1/84).
in Hardened G-32 " Bolt Anchors Set Concrete" R-0 (9/72),
R-4 (4/21/76),
R-5 (7/21/77),
R-6 2.
General Construction Spec.
(2 /17 /81), and R-10 (4/1/85).
(Support Typicals)
SNP 47A050 " General Notes" 3.
Craft Time Cards (1978) 4 4.
1
SUMMARY
OF INVESTIGATION:
substantiated. Interviews were conducted with (27) nsion anchors s
This concern was not individuals involved in the. installation of concrete expa No Sequoyah during the time frame specified in the concern. ev of y
( CEA 's ). at collaborating / objective conducted intermittently from 4
tpe' concern.
This investigation was j
13/25/85'to2/21/86.
+
3 FINDINGS:
review of a
The investigation of this conce'rn was approached in two ways;and intervi in CEA 1977.
As noted during the investigation of a
epplicable documentation applicable documentation proved y
installation during
( XX-85 -0 2 3- 0 01 )',
not This is due to the fact that work plans werewhen cc=bine related concer.n
.3 difficult to obtain.
utilized at SNP until 1981. This fact, exceptions to anchor pull-testing (Ref:
47A050 notes and 4e finding documentation documented and the unlikelihood of applicable procedures) the investigation proving falsification of pull-testing, dictated thateffort be co reviewed
- to J
Personnel records and cost accounting records were A list was developed personnel to interview. inspections of CEA's and appropriate determine personnel. certified to conduct a
comprising
('.
d PAGE 3 Or 4 ERT INVESTIGATION REPORT XX-85-023-X02 CONCERN NO.
DETAILS, continued FINDINGS, continued installation.
The list was narrowed by determining whom within the list are still employed locally (i.e.,
those persons involved in CEA for interview). Interviews were ccnducted to determine compliance immediately available (during specified time-frames),
and ascertain knowledge of wrongdoing verify involvement with procedural requirements, activities.
Results of the interview process are as follows:
with the. individual alleged to have been Acquaintance falsification activities could not be o
involved in
- t established, (even after prompting).
of alleged wrongdoing activities was limited to Several craft Knowledge was denied in relation to Sequoyah.
o reference to WBNP and personnel and a few inspection personnel made R
activities such as cutting off
" Re d.- He a d "
CEA 's,
welding etc.,
but only at
- WBNP, bolts to the backs of-base-plates,.(Reference various other ERT concerns).
.4 not at SNP.
exceotion, inspection personnel interviewed
-U.
o "47A050 Notes" With few concebn regarding the quantity of fhp'. o.
of the expressed and the ability of anyone to keep abreast (Reference various other 75 generated lj "050 Notes" and subsequent changes.
~ ~ ~
ERT concerns) i
- n CONCLUSIONS:
~-
?hh This concern is not substantiated.
\\
This conclusion is based on the following:
o The "47A050 Notes" allowed numerous exceptions
- n there were few personnel knowledet pull-testing, i.e.,
about exactly when a
pull-test absolutely had to be performed.
s.'
(.
(.
('
PAGE 4 OF 4 ERT IMVCSTICATION REPORT CONCERN NO. XX-85-023-X02 DETAILS, continueo CONCLUSIONS, continued-No documentation could be obtained that would support o
occurrence of this wrongdoing activity (falsifying. pull-test records) 4 o
No collaborating testimony was obtained from personnel involved in CEA installation in the Sequoyah Unit-2 Annulus during 1977.
s s
E f
s W
M.
r
- [7[80
' ~ PREPARED BY:
DATE
'v 4
M#
3bATM
" REVIEWED BY:
/
~
DATE s
(4 s.~
p,eh b
(
p
~
ATTACHMENT D t
List of Documents Reviewed in the Evaluation Process Element Report 80203 XX-Quality Technology Corportation Employee Response Team (ERT) Report No.
a.
85-023-001 (Revised 10/22/85) b.
Memorandum, SQN Site Director to Manager of Nuclear Manager's Review Group, April 24, 1986.
c.
Memorandum, General Counsel to Manager Nuclear Power, April 30, 1986 (Administratively Confidential) d.
Construction Specifications:
G-38, R1
" Installing Insulated Cable UP to 15,000 Volt Inclus ive" G-32, R4, R5
" Bolt Anchors Set in Hardened Concrete" Sequoyah Inspection Instructions:
e.
SNP-II-93, RO, R1, R2
- i SNP-II-10, R6, R7
?"
SNP-II-26, R0, R1,.R2, R3_
j SNP-II-28, R0, R1, R2
(
,f.
, Maintenance and Addition Instructions:
~
?
~
M&AI-4, R8 M&AI-7, R6 j
Construction QA Procedure, Const. QAP-10.01, R1 G
, g.
Ranger Drawing General Notes, 47A050 (latest issue of each page) h.
i.
NSRS Report I-86-101-SQN, February 27, 1986 Y
j.
Corrective Action Report, SQ CAR 86 02 005, 2/10/86 Construction CEG Element Report C010900-SQN, November 1986 k.
o e
s, D
4
""E v,.
i- -
j
)
1.
Pcgs 1 ATTACHMENT E
- TTAO:Z:NT
I'
,1 ECSP CORRECTIVE Action Tracking Document _
(CATD)
INITIATION
~
1.
Immediate Corrective Action Required:
/Y/ Yes // No 2.
Stop Work Recommended:
// Yes /X/ No 3.
CATD No.
80203-SQN-1 4.
INITIATION DATE 9/5/86 5.
RESPONSIBLE ORGANIZATION: QACEG
'h 6.
PROBLEM DESCRIPTION: /X/ QR /[/ NQN Engineering to determine by evaluation, the long term effect on cable where insulation was possibly repaired by the use of electrical tape.
440 volt cable feeding Back Flow Gate Hoist Motors (IAA, IBB, 2AA, 2BB)
.a a
n A
/1
,/////i/ //\\
./ / ATTACHMENTS _
L 7.
PREPARED BY: NAME D.G. Barlow
//#// //.4AJ DATE:
0-/f.//
f./ M /J'l/T 4
, DATE:
94 k-Y(,
i 8.
CONCURRENCE: CEG-H d
9.
APPROVAL: ECTG PROGRAM fiGR:
fY///d/d
-4_ DATE:
2/2/9) __
li CORRECTIVE ACTION e
u.
10.
PROPOSED CORRECTIVE ACTION PLAN:
.<y 4
~
NcML - Sf4 JamPicomo,J DJ NmteMm&rt /t c1= -
44 MEMO 24rDu/JJ B 26~ 9 (o e OI ? O '7 &
DMGD Oc'1 17; I9l(&
d PLsc 5 es.
en Y 7> a ra o N
213;;
2_f
,' d;
/ / /A/
/
/ /ATTACHMENIS 11.
PROPOSED BY: DIRECTOR /MGR: #4/W/7////4d/M/u DATE: /4/2/?/7 DATE:
12.
CONCURRENCE: CEG-H DATE:
SRP:
ECTG PROGRAM MGR:
DATE:
j
.c f.h j.
,$dc VERIFICATION AND CLOSEOUT,
13.
Approved corrective actions have been verified as satisfactorily implemented.
SIGNATURE TITLE DATE E
(
ATTACNiENT E Pega 2 S03 861022 808
- m kw.
7 pMOD STATES GOVERUENT TENNESSEE VALLEY AUTHORITY Memorandum ONP, Watts Bar W. R. Brown, Program Manager, Employee Concerns Task Group, To Plant H. L. Abercrombie, Site Director, ONP, O&PS-4, Sequoyah Nuclear Nuclear Plant FROM DATE October 29, 1986 ELEMENT
- EMPLOYEE CONCERNS TASK GROUP (ECT SEQUOYAH NUCLEAR PLANT (SQN) REPORT 802.
SUBJECT:
Your memorandum to me dated October 2, 1986, " Watts Bar Element Report Plant - Employee Concerns Task Group (ECTG)
Reference:
(T25 861002 871) 80203-SQN - Inspection Performance (Sequoyah)"
i h your I acknowledge receipt of your element report and in accordance w t viewed for.
request (see reference), Element Report 802.03 SQN has been re applicable corrective action.
i tion CAP and By way of this memorandum I am endorsing the sit i -
r Corrective Action Tracking Document 80203-SQN-1.
tfieECTGconcurrencespace If you agree with ths proposed CAP, please sigridbe king
'm checklist.
dlu4Whuwh H. L. Abercrombie
~
RCD:JDS:JB:CS RECEIVED Attachments cc (Attachments):
RIMS, MR 4N 72A-C (B25 '861017 076)
M308Y A. G. Debbage, ONP, ECTG Building, WBN
. Employce Ccnnms Task G* cup WBN 0221T o
w eiscier. nes, apo KLB C
'M e
L, N
a 1-H P
I d
M GL.~. xoc ;I 9Q Tdnw-s r
1-1 J y
-ECP i es es 7
~
Ro'<*nlariv nn Ihr Payroll.YicinisTPinh
~
Rear l' S. Snt iro ce floorrcis
'A
/
I
')
g Standard Practice Pagn 8 SQA166 Revision 8 Attachment A Page 1 of 2 Cerrective Action Plan of Employee Concern Investigation Tracking Checklist 702 o 3 -W.A> -- f ECTG Report /CATD Number FO 2 o 3-WN ff7h#
6W6./A/ Fan?-///h Lead Organization Responsible for Corrective Action Plan Initiation Date
/ 0 f4, CORRECTIVE ACTICN PIAN (CAP) ' corrective action?
Yes No I t
l
- 1. Does this report requiref (If yes, describe corrective action to be taken, if no, provide justification) oMFonmenoJ N 7NL RUtr4D Ce$ Win /suinnM 5iact TMr:L /S ao DEnnLLD 124/PtL 6V n+L u.sb cP fsla7usM. DtfL 20 er:tcir CH bl. tat:Esa FDL77tL TRf6 BEA+14. /!lfDitoS F0ff 7M f$) CMNL /&diowr* tesi$ M sause.*rt pczMitii346 7fstid (h'r-hr no 'mLGGEL). 77%JL C@WJ M*vl 6W os) Jee91ct.
tusrw W nod M O Arect 1917 MO id Att UrlL1 Hood Dufad 77f15 Uls/L YlM ffAno HPVL 8xf4 tite &
3
'1ML wouf codornosS fidCLRDos)G-Su6MLCWCE ) 71h+1~ 1NLY wr1Htuf MY P&obilms. Bi Mo n) 7M. RtkvL-4 Identify any similar item / instances and corrective action taken.
2.
a
$i
- +
Yes
)(
No
- 3. Will corrective actien preclude recurrence of findings?
- 4. Does this report contain findings that are conditions adverse to cuality (CAQ)
YES No X,
j as defined by AI-12 or NEP 9.l?
JF Si IF a CAQ condition e..ists, what CAQ document was initiated?
MlA
'"6. Which site sectir.,a/ organization is responsible for corrective action?
4
@d Mowf Yes No X.
d
- 7. Is corrective action required for restart?
(This determination is to be made using Attachment C of SQA166.)
,3
- 8. P2 zone number for restart corrective action? Zone tJ M
- 9. Eatimate completion date for correction action.
Wie
~
Completed By M,1 -
Date.
Def./f /98Io Approved By
~777 (f Mneuwdf///
Date
/o//f'/f6
//
6 U// //A // \\
Date
' /4422-R ECTG Concurrence ' -
vy To imima 7HL wenM y',
l 9 p g w e, a or S s tscs yw y yo fugTHff. RCDeJ IS J2f-@t//l4D.
o
'~
p
~_*
- I' i
i
,f -
/
,f. '
0206S/m1t M
- ~ -
m.
- - i
~
i t
~~
Standard practica Paga 9 SQA166 Revision 8 ATTACNIT A Page 2 of 2 i
~
CAP CLOSURE
- 10. Was your corrective action initiated and completed in accordance with step l?
Yes No
- 11. If step 10 is no, describe the corrective action taken.
L Yes No
- 12. Is the corrective action implementation complete?
Yes No
- 13. Is the corrective action documentation closed?
- 14. What documents were used to implement the corrective action?
Date Completed By:
Date s
Verified By:
Date ECIG Closure:
's d
Description (Step No.)
g 4
.N 14 -
Y~
h) u Y
?
s, 02065/n1t
( ~
e 808 861224 80s Cmren srares covenor.sr
Mcmorandum TENNESSEE VALLEY AUTHORITY To W. R. Brown, Jr., Program Manager, Employee' Concerns Task Group, ONP, Watts Bar Nuclear PJant FHO.T!
H. L. Abercrombie, Site Director, ONP, O&PS-4, Sequoyah Nt. clear Plant DATE December 24, 1986 SCHJECT:
SEQUOYAH NUCLEAR PLANT (SQN)
EMPLOYEE CONCERNS TASK GROUP (ECTG) ELEMENT REPORT 802.03 SQN - QUALITY ASSURANCE CATEGORY - CORRECTIVE ACTION PLAN (CAP)
/
Reference:
Your memorandum to me dated November 25, 1986, " Watts Bar Nuclear Plant - Employee Concerns Task Group (ECTG) Element Report 80203-SQN - Inspection Performance (Sequoyah)"
(T25 861125 891)
%j I acknowledge receipt of your element report and in accordance with your request (see referenco), Element Report'802.03 SQN has been reviewed for applicable corrective action.
By way of this memorandum I am endorsing the site line organization CAP, returning your Corrective Action Tracking Document No. 80203-SQN-02, and attaching the CAP for~your review / concurrence. This CAP is not a restart a
requirement.
s.
s g*
If you agree with the proposed CAP, please sign the ECTG concurrence space Fy below item 9 on the CAP tracking checklist and return the CAP tracking checklist.
[
q g
[
H. L..Abercrombie 4
P.E C E I V E D RCD:JDS:JB:CS
?
Attachments DEC 3 0 86 cc (Attachments):
RIMS, MR AN 72A-C.(B25 '861218 025)
. Em;'oyje Ccnar.9 Task T. C. Priee, 5-212 SB-K l
uroup W Bt:
Wie" Nob 0495T wte
"'.'e A
+
i 1
f{.-
~
ews V
z.3
.-. s
?4C l
t 1
+
t i
fbC - --
I
.t
, f r, co g sy L i
-~
~
~'
i :....
.g n.n-n,,,
I ~ C C,,,. i,.. e 1:1,,rle Ro~ upiin ris n,, r1,e Pn,.rn11 7avin ns Pinn ' W u l.
..m
. f.
\\
1 ECSP CORRECTIVE
~
Action Tracking Document (CATD)
INITIATION I
1.
Immediate Corrective Action Required:
/~/ Yes
// No
~
2.
Stop Work Recommended:
/ /' Yes /I/ Iio" 3.
CATD No.
80203-SQN-02 4.
INITIATION DATE 11/18/86 5.
RESPONSILLE ORGANIZATION:
Office of Nuclear Power 6.
PROBLEM DESCRIPTION:
/I_/ QR /~/ NQR Emplovee concern 00-85-005-003 was investigated by QACEG and D
COCEG.
COCEG investigation C010900-SQN indicates that cables 1-PL-6370-B 1-PL-6360-A. 2-PL-6370-B and 2-PL-6370 which supplies power feed to the ERCW Backflow Gate Hoist Motors have been de-energized and the motors r,armenately taken out of service.
QACEG invstigation reveals Design Drawings 45N-751-1,
-2,
-5, and -6 do not reflect this system status.
A
/
// ATTACHMENTS i
2 7.
PREPARED BY: NAME R. D. Halverson. @
DATE: 11/18/86 8.
CONCURRENCE:
CEG-H R. K. Maxon * /< /C it 11_ /, DATE: /I /]R/ Y G
^
' d-DATE:
7/1/F) 9.
APPROVAL: ECTG PROGRAM MGR: __ ff/s/M
- [
CORRECTIVE ACTION 10.
PROPOSED CORRECTIVE ACTION PLAN:
a 4
SEE~ TM CAP TPAWStr7/7tED
&}/ /??8MOR/MJLAuff 6
fr'77)?5 # 82 5 R6 /Z/2 Ozf n,c.+ e-t>
t 1 ': e s c.
^
- ~
m ji iii 5
/ / ATTACHMENTS
'd
~ PROPOSED BY: DIRECTOR /MGR: # 4!? #
4' f( ( DATE: /.J -A 9-/-/.
11.
DATE:
12.
CONCURRENCE: CEG-H y
N SRP:
DATE:
f ECTG PROGRAM MGR:
DATE:
. VERIFICATION AND CLOSEOUT as satisfactorily 13.
Approved corrective actions have been verified implemented.
2 4
5 SIGNATURE TITLE DATE l
~
(
t Standard Practice Page 8 SQA166 Revision 8 C
Attachment A Page 1 of 2 Corrective Action. Plan of Employee Concern Investigation Tracking Checklist D E, o 3 MM b W 70 WO-5 W ~O ECTG Report /CATD Number P&
Lead Organization Responsible for Corrective Action Plan Initiation Date
// - 2 6.%
s.
f CORRECTIVE ACTION PLAN (CAP) corrective action?
Yes No V
- 1. Does this report require (If yes, describe corrective action to be taken, if no, provide justification)k A 4' des.r d U &
M 4.en/ de 1be.
< w.+M m W.Jt m n wmw
-du wJt M C Ec Att 572.0).
Jhe. Ma -4v -eba d,a) 0
& %%%f.ei<t & asn M-e 2 % a a l u ifA 4 O u % 6 vd W '
-1/u a.tu.tlif au d/ M M PJ99~ w 3 Om C HE8 Plo 7 o 90/0. C l w'm M 62
-t/o Id6ntify any similar item / instances and corrective action taken.
2.
N/A i;
/
3 rence of findings?
Yes No
.3. Will corrective action preclude rec 4.' Does this report contain findings t at are conditions adverse to cualitv (CAQ)
~
j" d,
as defined by AI-12 or NEP 9.l?
YES No W. y ~
- 5. IF a CAQ condition exists, what CA ocument was initiated?
q,
,}
- 6. Which site section/ organization is sponsible for corrective action?
s.
- 7. Is corrective action required for estart?
Yes No 4
(This determination is to be made using Attachment C of SQA166.)
ej
- 8. P2 :one number for restarf., corre oive action? " Zone
- 9. Estimate. completion date for co ection action.
k.
Date
/2-/7-8d
{p,CompletedByApproved By #/6 ' k' ot' /Wf/h Date
/7- / T-k-L
~
~ ~'
Date ECTG Concurrence i
I A
C 0206S/mit
.. ( '
~
,1 I
Standard Practice Page 9 I
SQA166 Revision 8
.ATTAcafENT A Page 2 of 2 CAP CLOSURE
- 10. Was your corrective action initiated and completed in accordance with step 17 Yes No
- 11. If step 10 is no, describe the corrective action taken.
h Yes No
- 12. Is the corrective action implementation complete?
Yes No
- 13. Is the corrective action documentation closed?
- 14. What documents were used to implement the corrective action?
Date Completed By:
~
Date Verified By:
Date ECIG Closure:
)
s 5
Description (Step No.)
}
^
hi
(
f.,y
.+
4
'.?
91 b
$b,,
{ m Dj 4
L
~
0206S/mit
.s
l f
(~
P'lt D d 1 L. J 9 C) I a
[
3 mn;s unn:nsm:sr
~ morandum TENNESSEE VALLEY AUTHORITY fj l'
810717E0130 2.
no., useed t
n,
C. A. Chandley, Chie f, Hechanical Engineering Branch, W10D224 C-K JUL 8 1981 SEQUOYAH NUCLEAR Pl. ANT - DISPOSITION OF DESIGN CHANGE REQUE
~7 *,
SQ-DCR-891 CONDENSER CIRCULATING WATER SYSTEM (CCW) AND PREOP TEST -
L DEFICIENCY NO. PT-600 l
neuocantiuw from H. J. Green to H. N. Sprouse dated Dec, ember 6,
.w iu ca..ce :
1980 (DES-80-12-17-021), and DCR-971 We recom:: tend disapproval of SQ-DCR-891. The subject pressure switches for units 1 and 2; PS-0131 A and B, -132 A and B, and -134 A and B; were L
safety-related switches to activate the closure of the CCW backflow gates.
This functional requirement was deleted when the new essential raw cooling
}
watei pumping station was activated.
As long as these suitches are installed, they can activate the closure of the backflow gates and possibly trip the unit. Since the safety-related 4
closure requirement of the backflow gates no longer exists, the closure of the backflow gates and the shutdown of any CCW pumps shogld be under ths J,
. control of the unit operator and not automatically actuated.
h
.. 'Iherefore, we recom:nend the following:
y h.
3 Removal from both units of PS-027-131 A and B, -132 A and B, and -134 A 1.
/4 and B.
M 2.
Do not buy any replacement switches.
Revise the following drawings to delete the above pressure switches and f9 3.
their functional use:
D Contro1 Diagram 47W810-27-series Logic Diagram 47W611-27-series Instrumentation Tab 47B601-27-series Pumping Station 37W205-series Any other drawings for the If you are in concurrence, we will revise the scoping document preop test TVA-17.
I l
5 Buy ( *.S. Savin:p Burul> R gularly mu the Payroll Savings Plan
~
~
m.
l
\\
r --
(\\
(
I
~
2
)
,s, '
These Linted
- j.
JUL 8 1981 7
T (DCH)
SEQUOY AH NUCLEAR PLANT - DISPOSITION OF, DESICH CHANGE SQ-DCR-891 17 TEST CONDENSER CIRCULATING WATER SYSTEM (CCW) AN DEFICIENCY NO. PT-600 the reference drawing number 47W601-27-series instrumentation tabulacion to read 47B601-27-series on. drawin Plear,e correct 5
Please respond by July 31, 1981.
C. A. Chandley F. W. Chandler, W8Cl26 C-K
~
2 5
J. E. Holladay, W2D224 C-K J. A. Raulston, W10C126 C-K R. W. Cantrell, 204 GB-K
.g e
d JEM:JES M. N. Sprouse, W11A9 C-K fj
/} '
cc:
nuS:JES JULH. J. Creen,1750 CST 2-C - Please respond by J n 1981 31, 1981.
j g
. '~~
cc:
L3 IMEDS.E4B37C-_K in...'...
~h
~-
Q-
~
g.3 i
k8
~~
g,;
et
~:.y
' d' E81187.09 z..;
R$
$14 Jn i:o.
s
~
em
,V 4
va 4 I
NO. 2.o r z SHEET NO.
CLEARANCE SHEET
'[f.. '
SEQUOY AH NUCLEAR PLANT
. Gu t un ORDER
~
- 4ni, or s
E.- c u\\.t.h ld nTe c 3nA 7 6. C,' rte e
""^"*C e.... i,
,. r DATE REQUESTED BY EOUtPMENT CLEARED BY 4
l117
/7 54
/ / - T (3
~,Y. e o e, ck
- c. & h _ - m t ELD I '. L' %hIeeh LUben (k D tnn cdnow WORK TO BE DONE h e. AD,s n a e-n.,e = e U
i bC U I., N e,w br It'V s c[f<.el oN< A I"Dr-bk D e ic rn i
r
.a (in( 0\\biv
() t.s i/M CD?
bh t.
REMARKS AND INSTRUCTIONS g
ISSUE l
RELEASE ISSUED TO TIME DATE i
TIME DATE m
R s t:
In sM l-l R to a c ts f
{~
$/trf
/ **
l *<,;I';
W To 3
a,s '.s au.,.
',,,,*,% O c/erres.,s c c./*
, lJ) u,re, u < s c.e a " ' '
e)(.'a-csW/e'4s'o s~
a t,
a 6
// 9W l
/p*
q,.y ',
'O fv,4 p 96 /V' s ul* r. -
~
// 9 6 f f' '..
}j0*
3'.',
// AS/d
.~
.~,
?
s.
p 4. ar *. 3 I"E-Additional clearance sheets are a part of thle clearance and must be properly released.
O vas u Ue-*efounds have been placed in conjunction with this clearance.
YES C Attach Safety Ground Form CLEARANCE RELEASED BY TIME DATE
^ Wacm) t'ege i e
=
/
z e f.p_
CLEARANCE t..EET onoen,
no,S - u c /., w, e,., y,,
SEQUOYAH NUCLEAR PLANT C. e, d i e n Conc} enter C in e
- e. Nn - N cL e iJcth 9ow (- de c
^
y f
DETERMIN ATION OF 2nd PARTY (CHECK ONE) O REQUIRED
% bi3c % x VERIFICATION REQUIREMENT RELEASE OF CLEARANCE
/
g b
REMOVAL FROM SERVICE E
O VALVE DRAIN 2nd EQUIPMENT RETURN 2nd PERSOP CLOSED OR PERSON RELEASED TO NORMAL VERIFI-E nor U
BREAKER VENT VERIFI-E V ALVES. BRE AKERS. SWITCHES.
OR SWITCH OPEN CATION N
ALIGNED CATION OR FUSES HELD.
OPEN.
IF G
NORMAL 3p N
REOUIRE-C FUSE PULLED REQUIRED E
(LOCATION AS NEEDED)
Initials initials inillels NO.
Initials initials initiale N O.
lAln P OiC L/ C..m DCI E1CR
,n,n n, nu g c ~,, n i w a n ma w,$a w hQG Y. Sd nweda,u T
> dmn nx i
a R
.s-Ps.
q, a-9,,
44 M
- a.
vt l-
. )
s-.
e e*
e e8 1
_~
f
__~
.-4.
, !: a m
u,.. o A :_.
y yl
\\.
p gy y;,5g
...M y.
r ;. 1*h.$
5.f '
,; M y-r w "a. =... -_ N(
r.
[
f i
~
,s :
e-p--
,.j
.... a f
~.," 7. p % o
.r.
- t. y 3 s
Jk
/
. (rnY-o+ W<
w ;- A A s A no A
A aa ade.
fe.
l
- c i
JiS%syg pgs.;;c m_ 2:s. s.
s.
c.-
u 4..
w
. '.. g.. ": C u
u t -:
.g%%
=,
,g. ;;e.-
46.. r.,
.l a
s L51 M -
.j S,' u.%
S'.
.,I rg$
.,:7 c
' *~'_
v.
g:a[
4 Th '
/$, \\
- q.~g ;.
.y d-y.,w
,y s ;.. s
- 1.-
- r.
Meq17 g M, dW,--ly% _
7]_
p'.
,. n. - g,,..
s.. w -
y.
n m
w...
I ty.
~
g f&&.-@
- i. 3 i
kt
? $5'.Y N $
p
...- e pW'*Eyegg-sac 46%
.kh g
J..
I.;_..
.a
.. m5.,
t
.n
-....,Y 9......
< a * ;-
e
-d.
\\
w k.;
l p
-cn s ork % a.
a.9%
'Q pow 4n I
o (no 4 5..
ft-CrYM Typ)
=
j '..v.
4 e
I "amm.
F Io
^.
e*
~
m_.
g -
,hEh
- sm e*.ym ep
a._ma.--
u
-.---.-aa
,--m a
m 0*3 6
l
.Y 4
. - 4 e
-?
l i.'
m-.
=
t :, [. r)iildB.T ' '
=
ff p 4
a
-e
,..e,,.f W' '.m.:
- 'h.....'..
g.
- .r
-e 4 ' A h
[
/h
/
of W wint, &
.(7yYp A
no i
a..aa. u % t.
Ac.
.w
- b$E ' N.'.1 l
k,
- ; ;h:
.s.
p%!;.
.-4 1
- i..
. 2k,.......
NOT l.
4%,.;. ~11
- c r
[jU
-f m%~
- C 1;
.,. x.;
,'!.],;jY; W " *^-""
w L.
, m : ? - - 2 =:-
[i'
_ ~ ~ '
l;'
- e. = ~
iHs.fr ssp.
'1 g.
y.,
m
..m.,.,.
gg.
y 4.
.-w. " N w M4
- g. 3!q. pg
- f.~-
u p.~.1 ]
3 Ei@A s
C ~
e,..... m...
f;
.w..p,' w 'ac... a!
~ ~ ' ( 'j h
EW k
ljiliff gf,[ @
~j$
~
./_
m Y20) 26/2-
=-
f&YDe$ h (TYN. Q"
'Do w C
- Do & C, UK.-
(Typ)
.(
t I
y
.l t
i
'*M=.
f r_
~
- g Ef..MMv_w -
(
ODU
" * ~ ' '
. UNITED STATMs <;nVEltN31EST TENNESSEE VALLEY AUTilOI:lTY
'M...e,in ovan d um
?
V. R. Brown, Jr., Program Manager Employee Concerns Task Group, ONP, To Watts Bar Nuclear Plant H. L. Abercrombie, Site Director, ONP, O&PS-4, Seguoyah Nuclear Plant yno,y January 24, 1987 DATE
- EMPLOYEE CONCERNS TASK GROUP (ECTG) ELEMENT t
SEQUOYAH NUCLEAR PLANT (SQN)
REPORT 802.03 SQN R1 - QUALITY ASSURANCE CATEGORY - CORRECTI SCDJ ECT:
PLAN (CAP) REVISION 24, 1986, "Sequoyah L
Reference:
My memorandum to you dated DecemberEmployee Concerns Task Grou Nuclear Plant (SQN) -
Element Report 802.03 SQN - Quality Assurance Category -
Corrective Action Plan (CAP)" (S03 861224 806)
'~
Attached is my revised CAP for Element Report 802.03 SQN R1, Corrective Action Tracking Document No. 80203-SQN-02 for your review / concurrence.
This revised CAP supersedes the CAP previously transmitted to you (see reference) and h not a restart requirement.
If you egree with the proposed CAP, please sign the ECTG concurrence space
+
below item 9 on the CAP tracking checklist and return the CAP tracking s.
checklist.
y a.
a g,-
g'..
ggg H. L. Abercrombie p
~.
RCD:JDS:JB:CS
~
Attachment 4.-
-. REEIVED RIMS, MR 4N 72A-C (B25 '870123 037) ec:
ig*
T'. C.' Price, 5-212 SB:K (Attachment)
C-JE 26 T7
~
).}
0569T-Emplo :a Cener ns Tad 1
c..:
ws...
f.*..cSjdab
_g g, + <u.,, r ".
~--
n 4
__i
_g
~Wse
-a
--s p,
_ g
,n, c,,
l'* t
[t@~
e
-1,
~
~
c.m e
-f'.-'_!
t
-fp t_
$I'
_m R__lq)
G5103.iN
- )/
L
/l,lg-nuo, l'..t.7m ir. < R >nds Re ularly on the Payroll Savines Plan
- .5-. c'
\\
(
';j, uRDER~ './, -
x.>
SEOUOYAH NUCL sR PLANT' N o.S - v.. < L.
7 C.,, d, c. n ->-
1.3,,,c v
C ; n r.1 e n t o,,_ C i n a l. k h, ld e te r 1. ds %
(-. & c
. i DETECMINATION OF 2nd P ARTY VERIFIC ATION REQUIREMENT (CHECK ONE)
ED DE O REQUIRED S'S MgEWINED BW (SRO) 3e g
REMOVAL FROM SERVICE
/
RELEASE OF CLEARANCE U
VALVE.
DR AIN 2nd EQUIPMENT RETURN
~7ne CLOSED OR PERSON E
VALVES. BREAKERS. SWITCHES.
BREAKER VENT VERIF1-E RELEASED nor TO NORMAL.
L N
vtan C
OR FUSES HELD.
OR SWITCH OPEN CATION N
ALIGNED OPEN.
IF C
NORMAL C AT1' gp (LOCATION AS NEE 0ED)
NO.
Initials Initials initlels NO.
Initials Inillais initi:
lAln Ps Dht/ C Q DC I fh
' 'l
,a,a o, nav & vi
.k(M m
~
~
i I
c.i '
1818 k% 010Y bG D A /
mm a nwnda,c. i 'I fk]
.1 x
I i
i,.
,~ F J
.?
(
_7
.y p
i.
-r-c tj m.,,;
},_
De a'
,,.{s_
.; > 3
,e 8
, d,4 8
I J
,=
p
-g g
9
.i p
s -.
-
- c.'
f s
,,:q x
.r-p 8
l t
e
.-s f
.J
.~
~
4
,- = = -
.hm5 =
e 6
~
- 4..,
.s
~
[
.b., q. I,.,
.. lih
^
a;,'g
[,i
.'Pcgs 8 Standard Pecctics
- y. [.,
.e SQA166
~
Revision B
..l
'l C
- 4(Attachment A <.w..[';* if.
,.n Y~
'e ',
t
..s
. Page 1 of 2 Corrective Action Plan of Employee Concern Investigaticn
?
Tracking Checklist -
ECTG Report /CATD Number 80a.03 SGu R.I / onTD # 80 Z.a5 - S M - 0 2-de)(r-
. Lead Organization Responsible for Corrective Action Plan 7
- 3. Initiation Date II-3 8- % ' '
.. :. w,. :....n ;,, ;.W:
T,..
1 A.
CCRRECTIVE ACTION PLAN (CAP)* D;!.m#
.. i
~
ri 3
'V DY '
'V Yes No U[ s1. Does this report require corrective action? N (If yes, describe corrective action to be taken, if no, provide justification)
.;l )4 nnh -6 Dr MA.feT~ iM MrCm Sm w.s-Of > t&,J 0,1 mo,&S Mh) 77/ - / -l -S
~
'~
IMCT7Lf t srTL, <~4)culi"" F%t, r?tt. BKL ftce) (ht1T5 twD Nts }
inwfr*f.C -n+t t'o,A'EMi n Filem thirtmnnc. l'comu L-To mtMarth tervrnti. dr ?M uiJo i'~
Off b2tdOt: < FM 7/tC ct{rtmnt /Ecall 51x ) wmrH I L HM Bttt14citrW 10 OC.
J APct 1%) OmG IMT* mt.itM ML M& 17h'CCD u.' int 'Cmo nuJ ist0U ' ~~P TW-mrm( mf A 6 e c') (;'l c eI<- )
A9,,nmTitaw6 ( PP/mTn.d. PL(ML SCL rW MTwe+x0 3
4 C Lf ftfMf, %KET Pr h FKTU f Ls.l%6mirmo L tTw frm.ioc.A eM Identify any simil' r item /insta.nces and corrective action taken.
a 2.
.i /o tV l r1
' t '. ~
4 e
7 4,
ude recurrence of findings?
Yes No y.
O
."... $.. Will corrective action pre ndings that are conditions adverse to cuality (CAQ)
')
4r Does this report contain YES c, No 9 as defined by AI-12 or NE 9.17 y. j. q:
..,rj g Q' 3 g3 -
4.;
p
~
y
- 6. Which site section/organiza ion is responsible for. corrective action?
- 3..g ;+,.,.
q p'b
...jlg.
.9 < n. - m
,i.f.., ;.n c ws s
- j.
v e
Yes No
.1 : :.,.;7. Is corrective action requi ed for restart?
~
'Jf L (This determination is to e made using Attachment C.of SQA166.)
1
! v.s.
- 3 '.* 8. P2 :one number for resta corrective action? (Zone '"'
(,
- 9. Estimate completion dat for correction, action.;
ate 3/~b 7 i.'
Completed By i M Approved By K /g. M
." Date
/-23-f7
'i*Date L
ECTG Concurrence 4
.p g,
4..
6
. s :.,.,.
,3.
.s.
,.q.
~.,
>v-s '.
,a....l.
a
..j e
,s s'
p.
. '..'h.
- ',' [ ' :.hl ',L, 7 ';.
,=,
.. c. w
,s
- t
- n..
, u...,;y s s 4p n,': c :.,, s..
,, 4 v..;
. : t..
.7
- ..,1
.,3y*
. i;
-(
'g;,
- e
- _ f. G.
^ {.,-
f, ;;
,i.
]
}",.
02065/mit S81m=>-++%
mm
.. f Eg}j{gM'@f$'E,y%N.QI[.
' NTj-d( - t
. gf
.yjg..,..
~
........-.. s e. n.w. s r '
- ~ M.'; M. M'. M C.D' d y.,!,V.') U J D R
,: :. L.
e-s
- r. g...t
' J'J.V, U. :.s y.,. 7..r. %TENNESSEEtVALLEY AUTH 7M O Td H d M1?C.w 4
. W.
.a
- 2. c :
.; v.;.t:
r h.,. 1..;.nyg ^ v&*..810717E 013 r.)
- 2. j.
ya y
y 3.
m.euna,
.w t
.G l
C. A. Chandley, Chie f, Hechanical E,ngineering Dranch, W10D224 C-K
.(.
M L ' O 1981
.y, [
j,'( Qhj lM, N hy i
t 7
SEQUOYAH NUCLEAR PLANT.. DISPOSITION OF. DESIGN CHANGE REQUEST. (DCR) l'
- t. -
SQ-DCR-89 g-Q,%g, j j'gi;,
j '3 g,{ i 5..
~
m
.n.
CONDENSER CIRCULATING WATER SYST.EM (CCW),A.ND PREO.P TEST.'.TVA-17 TES!*',.
' N..'
DEFICIENCY NO. PT-600
-~
.)
y
.19 v. ',,
u v. : 9. t
.s 4
l r.
g..
u, f.c d.du r.::uc e : Heniocamluu from H. J. Green to M. N..Sprouse dated Dec, ember 6, f;
s 1980 (DES-80-12,17-021)e and DCR-971.,L--
c
.4,
- )-
,J.~'
l I..j.
1 We recommend disapproval of SQ-DCR-891.*The subject pressure switches for
}
units I snd 2; PS-0131 A and B, -132 A and B, and -134 A and B; were
^-l1 safety-related swite'es'to activate thc. closure of the CCW backflow gates.,4 ':
[
h 4
Ee
'Ihis functional requirement was deleted w water pumping station was activated.j,,,ve...he.n t,he n.ew ess.en,t.ial raw cooling
'f 5
. :.. s.
r
. ; y,j. ay c;;,pq ;'.. c,...
f 3
fp ~.'M y ' y Jrv.,
.t p:
f.
As long as these switches are installed.. they can' activate the closure of 4
,l R
,4 9
the backflow gates and possibly trip the unit. U Since the safety-related ' f 7.g,g g.
4, i-closure requirement of;the backflow gates no longer exists,~the closure of W i the backflow gates and.ethe shutdown of any CCW pumps should be ender the
- R@J,3
~
t control of the unit operator and not automatically actuated..
9 i
, N.l h.
. N Therefore, we reconnend the followingt ?'a V.7,,'#qk Q'Q..,
,y 3.
Ni'
- lLi.yry,j M % ~"
-:9 :
.g ;.'
4 7
f, t.n
- a. y,.. p
.a-mg y.w, r. g..:
a -
e
'.9 4,
{.
, ;.~
- 1. ", Removal from both units of PS-027-131 A and B, -132 A'and B, and -134 A y.((
. t, and B..'; fx. !).? M,.y y,; e,GT.4:GQjW y.&. 'p,w J)xq. &..,
i a,
s;.Wp. _ ;
e:., i. m... s..
. +v +.
.w
- c. ; *.n.q.
e N, s..
.ey p.. t.. ;,
n.. -
s 9
' f...... 2. ' Do not buy any replacement suieches. ")/p,,' !.Q!!
.M a
n.
e,. x n.,. n..p:..
E
=
5 s
.q.n. s c.
i..
l q}.M..;.g {[
5-4
~
9...
..g, v;. %g,g.f y./
y 9;
}
.,. 4..
/p-
- 3. ' Revise' the following drawings, co delete.the* above pressure. switches -and jhf t y j
}:!.
~~
'their. functional uses. W: r.sl @ ml $.. ~ $.+M.. Q,L+4 W T *(Q.?j'prp.
,'V.;. Y, y.d{ $ ^
4
- t.,.- 3 m..,..
.n v.,.
.. s.,
> Control Diagram 47W810-27-series h h.......,. :..
- w..,.i, r
..w i, [ h,.. :fh[.f: 4
....a a.
~
h!)
h
<(, '!]((
g
~
) Logic Diagram 47W611-27-series i
g.1.:?,f
.@'G".
b.
O t
Instrumentation Tab 47B601-27-series ".T.*/ A M.1%.k @
- Pumping Station 37W205, series j:
. ' $ } '$ I:
ch.*
If l
n Any other, drawings.:' 1
,. '.,d. ;.;I.Of '
1.
h p;. q :
i t.,. t.
n, v
W, If you are in concurrence, we will. revise the scoping document for the I:7,.'
r
".}
preep test TVA-17. -
g;. ( i'. '7 <, b,dp,p.7.;'.a.g,-
.l j.' 'f.] '
1 s.
1.
. :. s,,e m.... y.g., c.,cf m
).
.e,.
s
~.~
.m 3,
- p#.
.4 3
r
,, s. $..
.a
.s
...,.,e.
.....si..;
. e. 3
,.w ~.
.v.-
m.,~ #.,
m..,
a
.u
,'/k?N.{.,'/pg,'c)"O' 15 2O T.([3. N ' l; '..
-j
(, '
...J t
.t...,.
~
v..
t
. u. s
- c. n.. o.,. w. c.. le...w -
9.
i
., ~., -
,t s.
...s..
s
,.J,. e a[.m... u. Z s..
...a/ *,..
2.,
.. =.
q..
.m c
)
,t
.3i,g gg 2.-
3
.,:. t.
....t
- 4.,-
- a. r
..,.,1 z:..; e., %,
- ,..,.... m.m
,w-g,
. o.,. m,....u.... g..
~. n. :....g...
y,
- 0.,v.,c '. n, c.. m,.
y,.
',,e w.
.w
.sp.
~
- .,a..
r
^
t.
Buy I' V..Vau.in:p Bunuts Re ;;nlarly uns tire Payroll.Vaving Plan o
g.t u
_~_w
..,y.
..>. a
.,.... n.wQ *.
$m. p.
4, /c e f
.'n,
,.7.'.., j.g g.
. n..A.,..,..< [..,1 ( j_4.,., j;w f jy s
s v
w>o
..%-+
.w
.a.
5 m.
- n..
.4.,,
,y..
, g< -,. r,
. ate ~,y v
4 a...
e
+.
-, v..* s u.
m e
.g
.4.*
. A..#
^
s
. g.?
Those Listed
\\
^.
1 7,
J U L '. 81981 m.
"?
- L a.
m SEQUOYAll NUCLEAR PLANT -1DISPOSIT10N 0P DESIGN CllANCE REQUEST (DCR)
SQ-DCR-891.
- 4,.
n
~.,- cc,dt ;
p,..,,
. -n,
- p::ta.9...
'a
,p.
.s
, CONDENSER CIRCULATINC WATER. SYSTEM (CCW). AND PREOP TEST.- TVA-17 TEST '
. t.. " :
%q'.-
DEFICIENCY NO. PT-600
-4 0&
- J.. '
T :.: s... t f.'g..s o.. M.....
E Q_%.a t,v&. R,.%q,%gy.... q.1,.q%q*,..,..,..
.,i..
q g L.
. j
.c 3. p ? wy; e-
- g. Q< yef.. 3,.R..l p.
.t
?
M *, '.
- g.' L
~
n-Please correct the 're ference drawing number 47W601-27-series l
instrumentation tabulation to read 47B601-27-series on drawing 47W610-27-1.' -
k M....'
Please respond by July 31, 1981.
.t x.
.s,.,..
- e
.,f s
..,.e,-",.
~>
~ --
f.
/
/
. {
s
- t. -
..C..,A. Chandley.
.' 1.
~
e e..
, s r..
..,"..y
,' % ~ /O d,,.. ~,4 ;..%,' [,M T. W. Chandler, W8C126 C-K c,
j
~J. E. Holladay, W2D224 C-K
.T UMa, "h
~.?
J. A. Raulston, W10C126 C-K' %.m ' N M Y9.
9 E. m/*. df. 2 '.M*).
mJ ~
9)
- %f R. W. Cantrell, 204 GB-K?
.fS b
- a..
t...t.
.....g.
w-c.
y, s
y w
M..
O'M
^W
- 1]
JEH.JES
,s
- d.,'.. -
~U L
'AN M. If.' Sprous e, W11 A9 C-K.g<g..,...'.;c-
- 4. ',.
- n
.., p z..e.r.,
s s.
~
c I
-,' h'.
5-s u.s..
.' l.
3, /m(sy 4
W N 1 9 8 1. *'. '.' ". q' ',.e.'h "'
M.:.,.\\.M. M... t - E...,'. 4 0'
rM t
,,.l s.
. m,n..'".e,.Y. r. - 4,.4.
a.s%,v -V.
cc:
+v+ -
1..,
.,, m
- k.. <
..s.
g t
a.
- (
4 A...
]ll u
HNS:JES-V U
. U.,.{.
s,.
su g
H. J. Green,1750 CST 2-Cj Please' respond.b'y July. 31, ~ 1981, b....b.
cc:
.st..
M ED S. E4 B3 7 C-K '[.'4';.p, ;. g* e g,
. ' ^
- L.. - Q.y c '
- s. *
'.. -. Q '~M. j
- s
% e 5
c : t.,y; 6 3,..f,,,.N.'..
..s
-....;.. pp. @
1.1
, %. -l.pw.'.
> +. a r2
.m
,w
..;f~
v:
- ka. y.c t
.. g.
.. n
- t. ra.
.s. r v.
s
.s. -
ce :. o.. y. g..
5.
2.
-.r*....
v
,2
- ...,., r,.
.n y r.
1 a,,. c..,.7 n., u,. ;4,. P v. s c.. s. q At. uy,.og.. g,. m,
..g.,,
.M
- 3...r 4 w3
- . e
.,:3 pc
.,a
+ l. ~ n.:.# lN:f,%u%.tS.. c:p..
w~
.,L'.e <t
,W..
v,,..,
.c - -
v
- . V. p,; j< -mg;n,_@ ;,, a..
. +..:
.n.
.s
.,e*,
.s
'n.
,.. _ e f.,1 p g-e s
1,.
%c u',,g
- Q..Q'i.
2 t -
~ '
1 rs.
t &.~. s.1%r e <.$U je 2%W-.
. % :v.:1 s '
- U. ;
lA
.Qk' f Y.;. ),.n ' M.
i? W d. Q, K'f'j%.We,di jdf *.",
'.h }
W 2, '
g-c. 't 4
.. q; - ec n.,'
ar
,).
t..
1,
(> p., u. q... v. :..>.s.m.s.: 9.. t.;, t
, =.. n f.8 c 4.:,,....g y. t j.
s g.
+
m,.,. > ?. t e.f:
- y. p :. I :, s *
.Ja
.,.e -....
- y
'~
.,, ' c
.g
.s
',, *:j g ? "; -
j e.
s
. - )' 1, '
m y ly;g.J q '3M e y p,.l 3
- qp,. ?. '
1 *,
' t ',h y; ',[
w*
L
-.yjg.,y;q,j^y..,.3.,.
- 4. 'i Qi? f' s 5
$y.
- ,.j j '
3.-
g.
4
.b
.s g.., a y '..4.,, e.? - ' _. r y. s.
..f; ' p' f...% : *s.
g. 3,,,,
4
- 3.. ;~, 4, -
- y, cy;,.c j
,.i..
...n 'p~;wys.'..,,. {.m:. -
A
,~
> n c.,
i s;
)...,
-n g,. \\ q.+.. '.,s..r;./<.
a
.a
- 7. e. ',;g.M.,.1
,,n, e-
.-..6
.. r m.
~..,.,..
,p*
r t-.,.,...
e-.
s s
q
~.,,
e.,...
.6.-
...m.-
. y..,> e. s:.
- s. '.,
- g.,.
.. n,...
,o~.
1 J. :
.g -
.e
.j.
s
, W.
E81187.09
.F.,..
"..Y '
..L.....,..,.
..,ea, er....,
- ..' ' -;. 7 i,. ',
r.,.
Q
..?.'-
',; 3s c.'- egg. :
t g'.,*
. c. *.e., ' <
..6,y.
. n W..
q.,
a
,., p;. 1 f
, \\..;:
a.
c
(;.- w.'.
p..
~
'6a
- s h,'
a.
- ~; n, ).
- s [.y s "7;,1.
- nl.
.e
. I,
-t 2, ;
_ [ b 9,..Va.,s.
' ' d.../.
a
- / 'A. t'
$U.
[.
8
)*..'
s.,'.
.i
.,.,-...a y,
. *,.c...
4 m.
-. 6
's. y 1 ~.
.4,p.
.L
,. c*,)
a,
.,s
,T*s'>
,.q.3.A",4.,,.. s y
. s =. e
's
.e n_e*
r r
v.
}s..
'*Y'
,J -
e
.# a s
A
.*f**.*.*f' s.
. g.,
,v.
. '. /,,r,%,
. f..,,; *
,..t.*.
n,,p;.. '. c'
- c.i. { f,.y..
.# a. ;. g.e. ;t, g.,
'?1 b
3 -
> t.
w. /,* f
- 4;2 t. ry M:
. '. h.,4
>g:
.q.
'l, :
r s
c,.,
4 1... *.
,,',/,***.-C*
,7.
- '4.."
i9 M.. g.
1 6
., ob. i.
./.7 sf..-
,r l.
-r s
~.:
(4 -r i
b y
g
- u
. /
m.
+a..
..=**N-e-
~
8-.-'-******-=**.e.Bi e-owemmeg *
..=.-.=e-=*=*e.,-
.eme.
,=e-=.
a.s> %.
. ~ m,,,., - - g.
.,.,., r s.., y. a,.sx..
..,.m,.,..,,.:.
,....,,,,, r e..,1x.Q.
~
.y...
~-
.s
- 0.. i i;-.
.^**:,..
. *< - ?. "o?, *.. l, 4
-f '.
g.
CLEARANCE SHEET
,. 'r.e,p onDEn t,.T? -
"o.
L' i 2.
SHEET No.
i 3
SEQUOY AH NUCLEAR PLANT.
r 4
- in or g
A., n u ! l o r i
-M;*.
.ti$.1R A T US.., ' -
"'. ' ' k
- (..' *'
. 2pf IU C '. 9. k n e w 'k rn.' $
l. e..... I.s a. p..1*..#,4-uk'Y.'f.,h
'i n
'.a C,' '
tb t -
t (1) e c
' il?.:H t. ELD l q ~5 t.l a'.
/.
./.'/.*:7f.,......,b....
-g,e c
,L g' %.
c.,q g _.,
l DATE a"
'a.
REQUESTED BY -
EQUIPMENT CLEARED BY
'~
1
~
WORK TO BE DONE
~ ~ ~
-? /,
3 V-\\'p hIsk>
& l ne, c,{ nm d
LA) en (
P n e r-n n e
6 g
b t-'
In) s'ic l lc.cl D h,f.pmNI Tv %
- C. C LJ Ii, M
,w i
tn i...r a
kin C \\ b i *,'r h P. ' */ s '
G D'?
W bI REMARKS AND INSTRUCTIONS m Lc.f. w l-l O g f
- .fr.
- +
ISSUE RELEASE ISSUED TO TIME DATE TIME DATE
^'
~
/-.. /--
n fy "N -K 1
' ' v. 44.'
. Jr u
s.
s p.. I
,g q,,
's,
2
- 7.,.
. c,
.to.2a17 e
i.
,b.
2 ssf~i.; ' / ~~'. ; y '. --
- s, n
. :;~,.
- 'y y " y'
- r.. 4.*
. u.,.
a.
., y,
/c,
.e,.
- 7
/I'cyed,f
- tsA'ce n + # 6'
.j.
i..
k.
& I 4
s
'. p'
/.
, 5' '.
'G.,(
fy (:-
. C/dMs'*? C 'z l./ b g(.t,77,:,y u M*.<
- W'2'
,;l
.; cn s*/e ry, ' 4;g;,_.
C?!'
~
[v'/f.\\C:#.
//9dM.[).3
..d,o.
pc !Y. f, i 5. [ d., 'i rr.'..
..$/e*,
.' l. L,
i, :
v3 :
.t.,a*'e-M. - n '...i.'.'
.e..
c-
.8
.r-
.L'
- a. ;w
'.'i,'
et. '. * '
v s.. //
r-
.y
. s..
.,i
.,, h d...'.
i.
- 'L. "t.,,
.' & l l. [z.
lt
// 96 of2
. T i-
.v, og s
/ / l A d af f b,?:,
b.,,,. ; W y
. (:
,.q, ; -
- ?..,
,.:. -i ;.
.1...* "
-4
.i.
n
.. v...gA.y.
.< q,..
~
- y
.,p p,
t
- s. -
i-
- Q<}..?t;T ;&y ? '
/ g/
?n p n.,
4
- ~ '.
D.V....
7.m.
}&,
l2ff.yll.'.,,; '
- }*f.-
. i..'t
-* ".* a ; y.,. ~.
~,1 -
c7 c
- f g
p;e 4
5" I
i
.,. y e.r -,
.s2........
e
- 9
~f J,:
. 7-N.
. s.?
- 7:
j ?..
p; nn,..
- .v.
V.
,d j"***'E.'.t!ditional clearance sheets are a part of thla clearance an' must be properly release YES hi..I { ~
- 3 L.r 4,,
d ic c
,s, 1
..<..r.
s,
-s
- i. r
,.e.,, ff w -
v.:
e" d,
f.
.pr G.,e,.-*arounds have been placed in conjunction with this clearance. ' M.YES O Aiiaen saisir cround rar= -
CLEARANCE RELEASED BY TIME DATE
,(Tittrt) ga g g g 9 _-
- - - ~
+:b..
4 H&AI-19 Appendix A a
Page 1 Of 1 i
Revision 4
~
~
~.
f_
IP&.725 ntvis Ows IDENTIFIC ATION TAG (yp Og 5CRIPTION DATE APPROvtD (IF APPLICABLE)
A PER C,0. N8740 AR
'4'n W
l i
6.00(rep SHORT LONG
=
=
r r
TA M L
PIGTAILS (REF)
SEE TABLE
'4 PA6E'f l
FD,R WRENCH HPT NPT e
t l
qI
({0R CO 1,T SIZ E AT TACHMENT) j n,r.U2 W RIGI D CONDUli
'-=
=-
_ _ _,.-- g ~
.g ll I
II I-
-t v- _ m=
W t : :-- _- -.-. = 1'[
l
}
LW~ ~ ',!,-
--\\cotcOCT6RS NdMEERIO '
- j.
%.h,.g-g.*,,';--ey~,
-~
U k
/
j;
~~
M V
l.00 *-
SEQUENTIALLY ON BOTH MlN-
_ INSIDE '.... ENDS OF ASSEMBLY HEAT SHRINK TUBING DEVICE "
~
DEVICE
~SEE TABLE *B',
(REF)
FEEDTHRU SUS-ASSEMBLY
+
PAGE /.:, FOR.
y, le WRENCH SIZE SEAL BODY
~
SEAL BODY WIDLOCK FERRULE SUB-ASSEMBLY MIDLOCK CAP l
NUCLEAE s k
I DE SCRIPflO*f
' teAftA!AB.".
SPECIF8 CATION orv soo IDENTI ING NO.
PAwts test i
{
bett tss on+E mwist SPtCtFi&8 OR Aggie httiroPli[t, 9'M CORPOR AT SON g
74 e.se.e w.at.aesn ave. awe.
i ggg a
sie.
s..
==
U" y
GENERAL ARRANGEMENT DCTAILS
""$ ',',,,',, " t
,N O'.' k'I,d
FOR ELECTRIC CONDUCTOR urb h
%d' SEAL ASSEMBLIES
..o a. u n i.
s att PAhl$ i ff RURRS praff? h N oc f*Ll.,.
set cooi sosas ao
-6OO I 5
.....O****s...'****"
w-nit I. iR g
Da5M htNI A55V U5: 0 0N
.i 1
3..
gi a, 8
A*********
NO APPtlCA YlON
, O ff
,g g
.e,,
l l$Hgti l OF l 4
.y
...e..-.*.=*4Aa4*.*.
hM =. ** 3* M gW,,d,.,' ML..m.. J,,
,J., <_.- -._
4
'2D e $
..._._..s._-a--
I N--
- ' * * =
~
.