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Category:TECHNICAL SPECIFICATIONS
MONTHYEARML20217D7961999-10-12012 October 1999 Proposed Tech Specs Pages,Removing Turbine EHC Low Oil Pressure Trip from RPS Trip Function Requirements in TS Sections 2.2 & 3/4.1.A ML20210R8281999-08-13013 August 1999 Revised Bases Page B.3/4.9-6 to TS Section 3/4.9,providing Clarity & Consistency with Sys Design Description in UFSAR Sections 8.3.2.1 & 8.3.2.2 ML20209J2321999-07-16016 July 1999 Proposed Tech Specs 3/4.7.D Replacing Limit for Any One Msli Valve of Less than or Equal 11.5 Sfch with Aggregate Value of Less than or Equal 46 Scfh for All MSIVs ML20209C2951999-06-29029 June 1999 Proposed Tech Specs Section 3/4.3.C, Reactivity Control - Control Rod Operability ML20205L2631999-04-0505 April 1999 Tech Spec Page B 3/4.5-2 to TS Section 3/4.5, ECCS, to Clarify Requirement Discussed in ML20205J9321999-03-30030 March 1999 Proposed Tech Specs 3/4.6.E Changing SRs 4.6.E.2 to Allow one-time Extension of 18 Month Requirement to Pressure Test or Replace One Half of MSSVs to Interval of 24 Months ML20205J9911999-03-30030 March 1999 Proposed Tech Specs Allowing Alternative Methodology for Quantifying RCS Leakage When Normal RCS Leakage Detection Sys Is Inoperable ML20205J9741999-03-30030 March 1999 Proposed Tech Specs,Deleting Various License Conditions That Have Been Completed,Making Editorial Changes & Providing Clarifying Info ML20199L7741999-01-21021 January 1999 Proposed Tech Specs Bases for Sections 3/4.10.K & 3/4.10.L, Provides Description of Design & Operation of RHR SD Cooling Subsystem ML20199L6921999-01-21021 January 1999 Proposed Tech Specs Section 3/4.6.I,relocating from Chemistry TS Requirements to UFSAR ML20196H4571998-11-30030 November 1998 Proposed Tech Specs 3/4.8.J, Safe Shutdown Makeup Pump, Reducing Current AOT from 67 Days to 14 Days ML20196F6451998-11-30030 November 1998 Proposed Tech Specs 3/4.1.A,3/4.10.B & 3/4.12.B,proposing Changes to Relocate Requirement to Remove RPS Shorting Links Which Enable non-coincident Scram for Neutron Instrumentation,To Licensee Controlled Document ML20155D8091998-10-29029 October 1998 Proposed Tech Specs Bases Sections 3/4.2.D & 3/4.5.D, Providing Clarity & Consistency with Sys Design Description Contained in UFSAR Section 5.4.6.2 ML20151S7991998-08-31031 August 1998 Proposed Tech Specs,Increasing Max Allowable MSIV Leakage from 11.5 Scfh to 30 Scfh Per Valve When Tested at 25 Psig, IAW SR 4.7.D.6 ML20236W8401998-07-31031 July 1998 Proposed Tech Specs Bases 3/4.7.C & 3/4.7.12.C,clarifying Testing Requirements for Primary Containment Excess Flow Check Valves ML20247D7761998-05-0505 May 1998 Proposed Tech Specs Page B 3/4.4-1,changing Administrative Error.Bases for Net Quantity of Gallons for Solution Is Changed from 3254 (Correct Quantity) to 3245 ML20246Q3481998-04-29029 April 1998 TS Page B 3/4.5-3,reflecting Change to TS Bases for Section 3/4.5.C ML20217G1481998-03-27027 March 1998 Proposed Tech Specs Bases Section 3/4.5.A,reflecting Design Info Contained in Rev 4 to Ufsar,Dtd Apr 1997 ML20216C6381997-08-29029 August 1997 Proposed Tech Specs,Incorporating New Siemens' Methodologies That Will Enhance Operational Flexibility & Reducing Likelihood of Future Plant Derates ML20196G0271997-05-0101 May 1997 Proposed Tech Specs 4.9.A.8.b Revising Load Value for Diesel Generator to Be Equal to or Greater than Largest Single Load & Revising Frequency & Voltage Requirements During Performance of Test ML20138G3321997-04-29029 April 1997 Proposed Tech Specs,Permitting Loading of ATRIUM-9B Fuel in Plant Unit Core for Operational Modes 3,4 & 5.Modes Will Support Refueling Activities Such as Fuel Load,Vessel re- Assembly & Single Rod Timing ML20138B3231997-04-21021 April 1997 Proposed Tech Specs,Requesting That NRC Grant Exigent Amend to TS 2.1.B & 6.9.A.6.b to Support Plant Unit 2 Cycle 15 Operation Scheduled to Begin 970519 ML20137G3981997-03-26026 March 1997 Proposed Tech Specs 3/4.7.P Re Standby Gas Treatment & TS 5.2.C Re Secondary Containment ML20135F7321997-03-0303 March 1997 Proposed Tech Spec Bases 3/4.9.E,clarifying Purpose of SR 4.9.E ML20135D9461997-02-24024 February 1997 Proposed Tech Specs,Clarifying Bases for TS Surveillance 4.8.D.5.c ML20138L4011997-02-17017 February 1997 Proposed Tech Specs Section 2.1.B Re Thermal Power,Section 3/4.11 Re Power Distribution Limits,Section 3/4.6 Re Primary Sys Boundary,Section 5.3 Re Reactor Core & Section 6.9 Re Reporting Requirements ML20138L3701997-02-17017 February 1997 Proposed Tech Specs 4.9.A.8.h Re Diesel Generator Endurance Test Surveillance Requirements ML20134D2191997-01-27027 January 1997 Proposed Tech Specs Deleting marked-up Sentence from TS Bases for Section 3/4.7.K ML20129C2391996-10-16016 October 1996 Proposed Tech Specs for Dresden 2 & 3 & Quad Cities 1 & 2, marked-up to Show Transition Verbiage ML20129D3981996-09-20020 September 1996 Proposed Tech Specs 3/4.6.K,updating Pressure-Temp Curves to 22 Effective Full Power Yrs & TS Bases ML20113C3571996-06-25025 June 1996 Proposed Tech Specs Re Upgrade Program ML20113A7861996-06-10010 June 1996 Proposed Tech Specs,App A,To Reflect Transition of Fuel Supplier from General Electric to Siemens Power Corp ML20117D7121996-05-0606 May 1996 Proposed Tech Specs,Implementing New LCO & SR Re Revs to TS for 10CFR50,App J,Lrt ML20107A1881996-04-0404 April 1996 Proposed Tech Specs 3.4/4.4 Re Standby Liquid Control Sys ML20101H1381996-03-25025 March 1996 Complete Version of TS Upgrade Program Pages That Reflect Current Configuration of Plant & Specifies SRs That Will Not Be Current Upon Implementation of Tsup Project ML20097D9231996-02-0808 February 1996 Proposed Tech Specs,Upgrading Existing TS 3/4.5, Eccs ML20098A3821995-09-20020 September 1995 Proposed Tech Specs,Revising TS Upgrade Program & Improving Plant Submittals ML20086D4741995-06-30030 June 1995 Proposed Tech Specs Re TS Upgrade Program for Dresden Units 2 & 3 & Quad Cities Units 1 & 2 ML20087H8651995-05-0202 May 1995 Proposed Tech Specs Re TS Upgrade Program Section 3/4.10 ML20082H7481995-04-10010 April 1995 Proposed Tech Specs,Revising SR for HPCI & RCIC Sys ML20080K8171995-02-23023 February 1995 Proposed Tech Specs,Changing Name of Iige to Reflect Results of Merger Between Iige,Mid American Energy Co,Midwest Power Sys Inc & Midwest Resources Inc ML20078E2051995-01-20020 January 1995 Proposed Tech Specs Re Snubber Visual Insp Intervals ML20078Q6061994-12-12012 December 1994 Proposed TS Section 3.4/4.4 Re Standby Liquid Control Sys ML20064J3181994-03-11011 March 1994 Proposed Tech Specs Re Snubber Visual Insp Intervals ML20059A7321993-12-20020 December 1993 Proposed Tech Specs 1.1/2.1-1 Increasing MCPR Safety Limit from 1.06 to 1.07 for Units 1 & 2 ML20059A8301993-10-21021 October 1993 Proposed Tech Specs Deleting Requirements for Demonstrating Operability of Redundant Equipment When ECCS Equipment Is Found Inoperable or Made Inoperable for Maint ML20125D6381992-12-0808 December 1992 Proposed Tech Specs 3/4.1 Re Reactor Protection Sys ML20116J7091992-11-0606 November 1992 Corrected Proposed TS 3.2/4.2-8 Re Administrative Changes ML20106A6221992-09-15015 September 1992 Proposed TS 2.0, Safety Limits & Limiting Safety Sys Settings & 3/4.11, Power Distribution Limits ML20099D7791992-07-29029 July 1992 Proposed Tech Specs Sections 1.0, Definitions, 3/4.0, Applicability & 3/4.3, Reactivity 1999-08-13
[Table view] Category:TECHNICAL SPECIFICATIONS & TEST REPORTS
MONTHYEARML20217D7961999-10-12012 October 1999 Proposed Tech Specs Pages,Removing Turbine EHC Low Oil Pressure Trip from RPS Trip Function Requirements in TS Sections 2.2 & 3/4.1.A ML20210R8281999-08-13013 August 1999 Revised Bases Page B.3/4.9-6 to TS Section 3/4.9,providing Clarity & Consistency with Sys Design Description in UFSAR Sections 8.3.2.1 & 8.3.2.2 ML20209J2321999-07-16016 July 1999 Proposed Tech Specs 3/4.7.D Replacing Limit for Any One Msli Valve of Less than or Equal 11.5 Sfch with Aggregate Value of Less than or Equal 46 Scfh for All MSIVs ML20196K1941999-06-30030 June 1999 Rev 2.0 to Chapter 11 of Quad Cities Offsite Dose Calculation Manual ML20209C2951999-06-29029 June 1999 Proposed Tech Specs Section 3/4.3.C, Reactivity Control - Control Rod Operability ML20211C3311999-04-30030 April 1999 Rev 2.0 to Generic ODCM for Dresden,Quad Cities,Zion, Lasalle,Byron & Braidwood ML20205L2631999-04-0505 April 1999 Tech Spec Page B 3/4.5-2 to TS Section 3/4.5, ECCS, to Clarify Requirement Discussed in ML20205J9741999-03-30030 March 1999 Proposed Tech Specs,Deleting Various License Conditions That Have Been Completed,Making Editorial Changes & Providing Clarifying Info ML20205J9321999-03-30030 March 1999 Proposed Tech Specs 3/4.6.E Changing SRs 4.6.E.2 to Allow one-time Extension of 18 Month Requirement to Pressure Test or Replace One Half of MSSVs to Interval of 24 Months ML20205J9911999-03-30030 March 1999 Proposed Tech Specs Allowing Alternative Methodology for Quantifying RCS Leakage When Normal RCS Leakage Detection Sys Is Inoperable ML20199L6921999-01-21021 January 1999 Proposed Tech Specs Section 3/4.6.I,relocating from Chemistry TS Requirements to UFSAR ML20199L7741999-01-21021 January 1999 Proposed Tech Specs Bases for Sections 3/4.10.K & 3/4.10.L, Provides Description of Design & Operation of RHR SD Cooling Subsystem ML20196H4571998-11-30030 November 1998 Proposed Tech Specs 3/4.8.J, Safe Shutdown Makeup Pump, Reducing Current AOT from 67 Days to 14 Days ML20196F6451998-11-30030 November 1998 Proposed Tech Specs 3/4.1.A,3/4.10.B & 3/4.12.B,proposing Changes to Relocate Requirement to Remove RPS Shorting Links Which Enable non-coincident Scram for Neutron Instrumentation,To Licensee Controlled Document ML20196K5861998-11-0505 November 1998 Rev 3 to Qcap 0280-01, Process Control Program for Processing of Radioactive Wet Wastes at Quad Cities Nuclear Power Station ML20155D8091998-10-29029 October 1998 Proposed Tech Specs Bases Sections 3/4.2.D & 3/4.5.D, Providing Clarity & Consistency with Sys Design Description Contained in UFSAR Section 5.4.6.2 ML20195J9041998-09-24024 September 1998 Rev 0 to TR-VQ1500-02, Clean ECCS Suction Strainer Head Loss Test Rept ML20151S7991998-08-31031 August 1998 Proposed Tech Specs,Increasing Max Allowable MSIV Leakage from 11.5 Scfh to 30 Scfh Per Valve When Tested at 25 Psig, IAW SR 4.7.D.6 ML20236W8401998-07-31031 July 1998 Proposed Tech Specs Bases 3/4.7.C & 3/4.7.12.C,clarifying Testing Requirements for Primary Containment Excess Flow Check Valves ML20247D7761998-05-0505 May 1998 Proposed Tech Specs Page B 3/4.4-1,changing Administrative Error.Bases for Net Quantity of Gallons for Solution Is Changed from 3254 (Correct Quantity) to 3245 ML20246Q3481998-04-29029 April 1998 TS Page B 3/4.5-3,reflecting Change to TS Bases for Section 3/4.5.C ML20217G1481998-03-27027 March 1998 Proposed Tech Specs Bases Section 3/4.5.A,reflecting Design Info Contained in Rev 4 to Ufsar,Dtd Apr 1997 ML20216C6381997-08-29029 August 1997 Proposed Tech Specs,Incorporating New Siemens' Methodologies That Will Enhance Operational Flexibility & Reducing Likelihood of Future Plant Derates ML20196G0271997-05-0101 May 1997 Proposed Tech Specs 4.9.A.8.b Revising Load Value for Diesel Generator to Be Equal to or Greater than Largest Single Load & Revising Frequency & Voltage Requirements During Performance of Test ML20138G3321997-04-29029 April 1997 Proposed Tech Specs,Permitting Loading of ATRIUM-9B Fuel in Plant Unit Core for Operational Modes 3,4 & 5.Modes Will Support Refueling Activities Such as Fuel Load,Vessel re- Assembly & Single Rod Timing ML20138B3231997-04-21021 April 1997 Proposed Tech Specs,Requesting That NRC Grant Exigent Amend to TS 2.1.B & 6.9.A.6.b to Support Plant Unit 2 Cycle 15 Operation Scheduled to Begin 970519 ML20137G3981997-03-26026 March 1997 Proposed Tech Specs 3/4.7.P Re Standby Gas Treatment & TS 5.2.C Re Secondary Containment ML20135F7321997-03-0303 March 1997 Proposed Tech Spec Bases 3/4.9.E,clarifying Purpose of SR 4.9.E ML20135D9461997-02-24024 February 1997 Proposed Tech Specs,Clarifying Bases for TS Surveillance 4.8.D.5.c ML20138L4011997-02-17017 February 1997 Proposed Tech Specs Section 2.1.B Re Thermal Power,Section 3/4.11 Re Power Distribution Limits,Section 3/4.6 Re Primary Sys Boundary,Section 5.3 Re Reactor Core & Section 6.9 Re Reporting Requirements ML20138L3701997-02-17017 February 1997 Proposed Tech Specs 4.9.A.8.h Re Diesel Generator Endurance Test Surveillance Requirements ML20134D2191997-01-27027 January 1997 Proposed Tech Specs Deleting marked-up Sentence from TS Bases for Section 3/4.7.K ML20129K3321996-10-18018 October 1996 Cycle 15 Startup Test Results ML20129C2391996-10-16016 October 1996 Proposed Tech Specs for Dresden 2 & 3 & Quad Cities 1 & 2, marked-up to Show Transition Verbiage ML20129D3981996-09-20020 September 1996 Proposed Tech Specs 3/4.6.K,updating Pressure-Temp Curves to 22 Effective Full Power Yrs & TS Bases ML20216H8841996-06-30030 June 1996 Revs to ODCM for Quad Cities,Including Rev 1.8 to Chapters 10,11,12 & App F ML20116F3971996-06-30030 June 1996 Rev 1.8 to ODCM, Annex,Chapters 10,11,12 & App F ML20113C3571996-06-25025 June 1996 Proposed Tech Specs Re Upgrade Program ML20113A7861996-06-10010 June 1996 Proposed Tech Specs,App A,To Reflect Transition of Fuel Supplier from General Electric to Siemens Power Corp ML20117D7121996-05-0606 May 1996 Proposed Tech Specs,Implementing New LCO & SR Re Revs to TS for 10CFR50,App J,Lrt ML20107A1881996-04-0404 April 1996 Proposed Tech Specs 3.4/4.4 Re Standby Liquid Control Sys ML20101H1381996-03-25025 March 1996 Complete Version of TS Upgrade Program Pages That Reflect Current Configuration of Plant & Specifies SRs That Will Not Be Current Upon Implementation of Tsup Project ML20097D9231996-02-0808 February 1996 Proposed Tech Specs,Upgrading Existing TS 3/4.5, Eccs ML20100C0441996-01-24024 January 1996 Secondary Containment Leak Test Summary ML20093K7721995-10-12012 October 1995 Quad-Cities Nuclear Power Station Unit 2 Cycle 14 Startup Test Results Summary ML20098A3821995-09-20020 September 1995 Proposed Tech Specs,Revising TS Upgrade Program & Improving Plant Submittals ML20086D4741995-06-30030 June 1995 Proposed Tech Specs Re TS Upgrade Program for Dresden Units 2 & 3 & Quad Cities Units 1 & 2 ML20087H8651995-05-0202 May 1995 Proposed Tech Specs Re TS Upgrade Program Section 3/4.10 ML20082H7481995-04-10010 April 1995 Proposed Tech Specs,Revising SR for HPCI & RCIC Sys ML20080K8171995-02-23023 February 1995 Proposed Tech Specs,Changing Name of Iige to Reflect Results of Merger Between Iige,Mid American Energy Co,Midwest Power Sys Inc & Midwest Resources Inc 1999-08-13
[Table view] |
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ATTACHMENT B Marked Up Technical Specifications Pages 1 SVP-99-038 (Page1of1) 3/4.6-10 B 3/4.6-4 J
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9904120285 990330 I l
PDR ADOCK 05000254 l P PDR '
PRIMARY SYSTEM BOUNDARY Lcakage Detection 3/4.6.G 3.6 - LIMITING CONDITIONS FOR OPERATION 4.6 - SURVEILLANCE REQUIREMENTS G. Leak' age Detection Systems G. Leakage Detection Systems The following reactor coolant system The reactor coolant system leakage leakage detection systems shall be detection systems shall be demonstrated OPERABLE: OPERABLE by:
- 1. The primary containment atmosphere 1. Performing the leakage determinations porticulate radioactivity sampling of Specification 4.6.H.
system, and
- 2. Performing a CHANNEL CAllBRATION
- 2. The drywell floor drain sump d e APPLICABILITY: '
ddec45^
OPERATIONAL MODE (s) 1, 2 and 3. h Icad Astre e W$on 4 yee er 18 t*oN4
ACTION: _
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- 1. With the primary containment atmosphere particulate radioactivity sampling system inoperable, restore the inoperable leak detection radioactivity sampling system to OPERABLE status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; otherwise, be in HOT SHUTDOWN within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in COLD SHUTDOWN within the l following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
(mec1 W $
- 2. With the drywell floor drain sumpJ ~
s stem inoperable,(rsst a -
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(
rjrnpih sufntVsvit tGsfwithin o [j hourct,sttherwise, be in at least HO SHUTDOWN within the
. /gt;d no oAktMkd- -
( 4 g gwrang i
next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> nd in COLD / gUj gg,,, argin 5,q SHUTDOW within the following . w, S ( I s r be. y?U mo44orsrg
(? Sloor dMe g sgw r *,
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QUAD CITIES - UNITS 1 & 2 3/4.6-10 Amendment Nos.
[h
F PRIMARY o. TEM BOUNDARY B 3/4.6 ;
w-- l BASES hhe' Leakage from the reactor coolant pressure boundary insid the drywell is detected by at least one or two independently monitored variables, such as sum evel changes and drywell atmosphere i radioactivity levels. The means of quantifying leakage in the drywell is the _drywell floor dr '
sump pumps. With the drvwell floor drain sumo .ystem inoperable 9/pf 7gMfprgi(
(Mo#itArAg'ghp dg(4d fy(g(u/idlWidf6stnMdsfdhlbdeGd/ondsfi/ containment atmannhere l sampling for radioactivity can provide indication of channes in leakage rates.MaWeen.Q men
$6nk e 5 me s s ew s w for Y*d I'*bse "al he *MW ged 4'er up
[Q. So dass uude,g sump r*a tia***.A.. .s +v.4 eve a 5 c entret s . Pr'5*$
3/4.U.H unerational Leakaos The allowable leakage rates from the reactor coolant system have been based on the predicted and experimentally observed behavior of cracks in pipes. The normally expected background leakage due to equipment design and the detection capability of the instrumentation for determining system leakage was also considered. The evidence obtained from experiments suggests that for leakage somewhat greater than that specified for UNIDENTIFIED LEAKAGE the probability is small that the imperfection or crack associated with such leakage would grow rapidly. However, in all cases, if the leakage rates exceed the values specified or the leakage is located and known 'to be PRESSURE BOUNDARY LEAKAGE, the reactor will be shutdown to sidow further investigation and corrective action.
An UNIDENTIFIED LEAKAGE increase of more than 2 gpm within a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period is an indication of a potential flaw in the reactor coolant pressure boundary and must be quickly evaluated.
Although the increase does not necessarily violate the absolute UNIDENTIFIED LEAKAGE limit, IGSCC susceptible components must be determi~ui not to be the source of the leakage within the required completion time.
l 3/4.6.1 Chemistry The water chemistry limits of the reactor coolant system are established to prevent damage to the reactor materials in contact with the coolant. Chloride limits are specified to prevent stress corrosion cracking of the stainless steel. The effect of chloride is not as great when the oxygen 4 concentration in the coolant is low, thus the 0.2 ppm limit on chlorides is permitted dunne POWER OPERATION.
Conductivity measurements are required on a continuous basis since changes in this parameter are an indication of abnormal conditions. When the conductivity is within limits, the pH, chlorides and other impurities affecting conductivity must also be within their acceptable limits. With the conductivity meter inoperable, additional samples must be analyzed to ensure that the chloridos are not exceeding the limits.
Action 1 permits temporary operation with chemistry limits outside of the limits required in OPERATIONAL MODE 1 without requiring Commission notification. The surveillance requirements provide adequate assurance that cnneentrations in excess of the limits will be detected in sufficient time to take corrective action.
QUAD CITIES - UNITS 1 & 2 B 3/4.6 4 Amendment Nos. ma
E 1
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ATTACHMENT C Information Supporting a Finding of No Significant Hazards SVP-99-038 (Page 1 of 2)
Comed has evaluated this proposed amendment for Quad Cities Station, Units 1 and 2, and has determined that it involves no significant hazards consideration. According to 10 CFR 50.92(c),
a proposed amendment to an operating license involves no significant hazards consideration if operation of the facility in accordance with the proposed amendment would not:
Involve a significant increase in the probability of occurrence or consequences of an accident l previously evaluated; Create the possibility of a new or different kind of accident from any previously analyzed; or Involve a significant reduction in a margin of safety.
]
Pursuant to 10 CFR 50.90, Comed proposes to change Appendix A, TS Section 3/4.6.0, Leakage Detection Systems, for Facility Operating Licenses DPR-29 and DPR-30. The purpose of this proposed change is to allow an alternate methodology for quantifying reactor coolant system (RCS) leakage when the normal monitoring system is inoperable. This change is consistent with NRC guidance provided in letter L. Olshan (USNRC) to T. Kovach (Comed) dated August 21,1990, concerning Generic Letter 88-01, "NRC Position on IGSCC in BWR Austenitic Stainless Steel Piping."
The determination that the criteria set forth in 10 CFR 50.92 are met for this amendment request is indicated below: l Does the change involve a significant increase in the probability or consequences of an l accident previously evaluated?
The current Technical Specifications require a periodic measurement of RCS leakage. The ,
normal method for quantifying RCS leakage is to use the DWFDS and DWEDS flow totalizers. !
The proposed TS change would allow an attemate method for quantifying RCS leakage when a flow tota:izeris not available. The proposed change has no impact on the frequency for monitoring RCS leakage and would only be used for a maximum of 30 days while the normal leakage monitoring system is being restored to an operable condition. The alternate methodology for quantifying leakage has a measurement sensitivity that is consistent with the normal method. The proposed change does not impact any system structure or component used I to mitigate the consequences of an accident and there will be no change in the types or j significant merease in the amounts of any effluents released offsite.
Therefore this proposed amendment does not involve a significant increase in the probability or
. consequences of an accident previously evaluated.
ATTACllMENT C Information Supporting a Finding of No Significant flazards
( SVP-99-038 (Page 2 of 2)
Does the change create the possibility of a new or difrerent kind of accident from any accident previously evaluated? !
The proposed change involves no physical modifications to any system, stmeture or component used to mitigate the consequences of an accident. The operation of the DWEDS and DWFDS are not being altered in any way that could affect their ability to function during an accident condition.
l Therefore, the proposed changes do not create the possibility of a new or different kind of l accident from any previously evaluated.
l Does the change involve a significant reduction in a margin of safety?
The current TS's require a periodic measurement of RCS leakage. The normal method for l quantifying RCS leakage is to use the DWFDS and DWEDS flow totalizers. The proposed technical specifications change would allow an a' ternate method for quantifying RCS leakage when a flow totalizer is inoperable. The proposed change has no impact on the frequency for
! monitoring RCS leakage and would only be used for a maximum of 30-days while the normal leakage monitoring system is being restored to an operable condition. The proposed alternate methodology for quantifying leakage has a measurement sensitivity that is consistent with the
- normal method.
l Therefore, these changes do not involve a significant reduction in the margin of safety.
l Therefore, based upon the above evaluation, Comed has concluded that these changes involve no significant hazards consideration.
l
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- l. .
l ATTACHMENT D Information Supporting an Environmental Assessment SVP-99-038 l (Page 1 of 1) l l
Comed has evaluated this proposed operating license amendment request against the criteria for identification of licensing and regulatory actions requiring environmental assessment in l accordance with 10 CFR 51.21, Comed has determined that this proposed license amendment request meets the criteria for a categorical exclusion set forth in 10 CFR 51.22(c)(9) and as such, has determined that no irreversible consequences exist in accordance with 10 CFR 50.92(b).
This determination is based on the fact that this change is being proposed as an amendment to a license issued pursuant to 10 CFR 50 that changes a requirement with respect to installation or use of a facility component located within the restricted area, as defined in 10 CFR 20, or that changes an inspection or a surveillance requirement, and the amendment meets the following specific criteria:
(i) the amendment involves no significant hazards consideration.
As demonstrated in Attachment C, this proposed amendment does not involve any significant hazards consideration.
(ii) there is no significant change in the types or significant increase in the amounts of any effluent that may be released offsite.
As documented in Attachment C, there will be no change in the types or significant increase in the amounts of any effluents released offsite.
(iii) there is no significant increase in individual or cumulative occupational radiation exposure.
The proposed changes will not result in changes in the operation or configuration che facility. There will be no change in the level of controls or methodology used for processing of radioactive effluents or handling of solid radioactive waste, nor will the -
proposal result in any change in the normal radiation levels within the plant. Therefore, there will be no significant increase in individual or cumulative occupational radiation exposure resulting from this change.
l 1