ML20204F306

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Discusses Insp on 850701-1015 & Forwards Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $75,000
ML20204F306
Person / Time
Site: Fermi 
Issue date: 07/29/1986
From: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Sylvia B
DETROIT EDISON CO.
Shared Package
ML20204F313 List:
References
EA-86-112, NUDOCS 8608040150
Download: ML20204F306 (4)


See also: IR 05000701/2010015

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July 29, 1986

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Docket No. 50 341

License No. NPF-43

EA 86-112

The Detroit Edison Company

ATTN:

B. Ralph Sylvia

Group Vice President-Nuclear

6400 N. Dixie Highway

Newport, MI 48166

Gentlemen:

SUBJECT: NOTICE OF VIOLATION AND PROPOSED IMPOSITION OF CIVIL PENALTIES

NRC INSPECTION REPORT NO. 50-341/85040(DRP)

This refers to the inspection conducted by the NRC during the period July 1 -

October 15, 1985, of activities authorized by NRC License No NPF-43 for

Fermi-2.

Inspection Report 50-341/85040 (DRP) identified violations of NRC

requirements and was

Some of the violations

were associated with'provided to you on January 7, 1986.

the July 1-2, 1985 roa pull error and subsequent events

and were the subject of separate correspondence.

The other results of this

inspection were discussed on July 17, 1986 during an enforcement conference

held at the Fermi-2 site between you and other members of your staff and

Mr. J. G. Keppler, Regional Administrator, and other members of the NRC staff.

Some of the incidents described in the inspection report were identified by

your personnel and reported to the NRC.

Item A of the enclosed Notice of Violation and Proposed Imposition of Civil

Penalties (Notice) involves the failure to provide a flow path during the

period July 23-29, 1985 for the Emergency Equipment Service Water (EESW) system

which is required to provide cooling water to the Division 1 emergency core

cooling systems and Division 1 emergency diesel generators. The Fermi-2

license contains a'special condition with which the licensee must comply until

its alternate shutdown capability in the event of a fire has been established.

This condition requires the removal of power from a cooling tower bypass valve

to prevent its spurious closure and interruption of the flow of the EESW.

In

this instance, a Reactor Building rounds operator who had been required to

stroke the bypass valve was not given clear instructions to leave the valve

open and he closed the valve. Although an alternate flow path would have

satisfied the license condition, the alternate flow path was also unavailable

because the valves used for the alternate flow path were closed.

Item B of the Notice involves a violation of primary containment integrity during

the period June 21 to September 2, 1985 as a result of conditions existing in

the containment monitoring system and the Division 2 hydrogen recombiner. On

September 2, 1985, the licensee determined that one valve in the containment

monitoring system had been left open after installation of the valve and the

CERTIFIED MAIL

iiETURN RECEIPT REQUESTED

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The Detroit Edison Company

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July 29, 1986

line had been left uncapped resulting in an open pathway between primary

containment and the reactor building.

In addition, on August 28, 1985, the

Division 2 hydrogen recombiner was discovered by the licensee to have leakage

in excess of allowable containment leakage limits.

This condition had been in

existence since June 21, 1985 when maintenance was performed on the system to

replace a blower seal. Both of these violations of primary containment

integrity had resulted from the sign-off on work orders that the work and

testing had been completed before leakage testing had been performed.

Item C of the Notice involves the removal from service of the Reactor Core

Isolation Cooling (RCIC)/ Core Spray System (CSS) room cooler from July 23 24,

1985, which made the RCIC system and Division 1 of the CSS inoperable. This

condition was caused by the placement of the control switch for the room cooler

in the off-reset position and was discovered by your personnel on July 24, 1985.

However, it is not clear what caused the placement of the control switch in the

off-reset position.

The root cause of the above violations appears to be inadequate work control

meatares to ensure that work activities are accomplished in a controlled manner

and in accordance with established procedures, work is fully completed,

applicable inspections are performed, and the systems are tested to ensure

that the system will function as intended.

In addition, Item C involved an

incident in which shift turnovers of control room personnel did not identify

the significance of the off-normal condition of the room cooler. On March 13,

1986, you were cited for a Severity Level IV violation related to the failure

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of control room personnel to identify that the seismic monitor was in an

off-normal condition. These violations and other findings in Inspection

Report 50-341/85040 indicate the need for increased management attention to

assure that control room personnel are aware of the operational status of plant

equipment at all times.

To emphasize the need for proper work control measures, including adherence to

work procedures and awareness of the status of work activities, and attention

to other than normal conditions by control room personnel, I have been

authorized, after consultation with the Director, Office of Inspection and

Enforcement, to issue the enclosed Notice of Violation and Proposed Imposition

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of Civil Penalties in the amount of Seventy-five Thousand Dollars ($75,000) for

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the violations set forth in the enclosed Notice.

In accordance with the " General

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Statemeat of Policy and Procedures for NRC Enforcement Actions," 10 CFR Part 2,

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Appendix C (1986) (Enforcement Policy), the violations described in the enclosed

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Notice have each been categorized as a Severity Level III violation. The base

value of a civil penalty for a Severity Level III violation is $50,000. The NRC

Enforcement Policy allows for reduction of a civil penalty under certain

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circumstances. These violations are symptomatic of the management weaknesses

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that led to the July 1-2, 1985 rod pull error and resulted in the proposed

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$300,000 civil penalty for that event.

In addition, the violations occurred

during the same time period (June-September 1985). You have taken extensive

actions to correct these violations during the past several months including

the implementation of:

a control room specific Reactor Operations Improvement

Plan; independent investigations of operating activities and communications by

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The Detroit Edison Company

3

July 29, 1986

an Independent Overview Committee; and a broad based Nuclear Operations

Improvement Plan. Accordingly, in recognition of your corrective actions and

the prior civil penalty for similar management problems, the base civil penalty

for each violation has been reduced by 50 percent.

Because you have already instituted extensive corrective action as described

above and we view these programs to have encompassed the problems identified in

this letter and Inspection Report 50-341/85040 (DRP), no response to the Notice

of Violation except for payment of the proposed civil penalty is required.

If

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you choose to respond to the Notice of Violation, you should follow the

instructions specified in the enclosed Notice when preparing your response.

The NRC will continue to monitor the effectiveness of your corrective action

programs in determining whether further enforcement action is necessary to

ensure compliance with regulatory requirements.

In accordance with Section 2.790 of the NRC's " Rules of Practice," Part 2,

Title 10, Code of Federal Regulations, a copy of this letter and its enclosure

will be placed in the NRC Public Document Room.

The responses directed by this letter and the enclosed Notice are not subject

to the clearance procedure of the Office of Management and Budget, as required

by the Paperwork Reduction Act of 1980, PL 96-511.

Sincerely,

kipinal s,1$ned by

Jess G. Kewt r

James G. Keppler

Regional Administrator

Enclosure: Notice of Violation

and Proposed Imposition of Civil

Penalties

cc w/ enclosure:

L. P. Bregni, Licensing

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Engineer

P. A. Marquardt, Corporate

Legal Department

Licensing Fee Management Branch

Resident Inspector, RIII

Ronald Callen, Michigan

Public Service Commission

Harry H. Voigt, Esq.

Nuclear Facilities and

Environmental Monitoring

Section

Monroe County Office of

Civil Preparedness

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The Detroit Edison Company

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July 29, 1986

Distribution-(continued)

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- JTaylor, IE

JGKeppler, RIII

JAxelrad, IE

HWong, IE

JLieberman, ELD

JSniezek, DED/ROGR

Enforcement Coordinators

RI, RII, RIII, RIV, RV

FIngram, PA

HDenton, NRR

BHayes, 01

SConnelly, 0IA

JCrooks, AE00

DCS

EDO Rdg File

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