ML20204E861

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Monthly Operating Rept for Sept 1988 for Fermi 2
ML20204E861
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 09/30/1988
From: Anthony P
DETROIT EDISON CO.
To:
Shared Package
ML20204E865 List:
References
NUDOCS 8810210463
Download: ML20204E861 (3)


Text

____ _ _ - _ _ _ _ _ .

' OPERATING DATA REPORT

  • P. M. Anthony DICKETNO. 50-341 COMPLETED BY DATE October 15, 1988 TELEPHONE (313)586-1617 OPERATING STATUS
1. UNIT NAME: Fermi 2 l Notes: l
2. REPORTING PERIOD: September 1988 l l 3 LICENSED THERMAL POWER (MWt): 3292 l ' To be determined l
4. NAMEPLATE RATING (GROSS MWe): 1154 l l
5. DESIGN ELECT RATING (Net MWe) ,1093 l l
6. MAX DEPENDABLE CAP (GROSS MWe):
  • l l
  1. l
7. MAX DEPENDABLE CAP (Net NWE): l
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS: None
9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (HWe Net): None
10. REASONS FOR RESTRICTION, IF ANY: Nono THIS MONTH YR TO DATE CUMULATIVE
11. HRS IN REPORTING PERIOD 720 6037 6037
12. HRS REACTOR WAS CRITICAL 0 3072.3 3072.3
13. REACTOR RESERVE SHUTDOWN HRS 0 0 0
14. HOURS GENERATOR OW-LINE 0 2850 2850
15. UNIT RESERVE SHUTDOWN HOURS 0 0 0
16. GROSS THERMAL ENERGY GEN (MWH) 0 7,214,612 7,214,112
17. GROSS ELECT ENERGY GEN (MWH) 0 2,316,048 _2,316,048
18. NET ELECT ENERGY GEN (MWH) 0 2,183,980 2,183,980
19. UNIT SERVICE FACTOR 0 ' 47.2 47 2
20. UNIT AVAILABILITY FACTOR 0 47.2 47 2
21. UNIT CAP FACTOR (USING MDC NET)
22. UNIT CAP FACTOR (USING DER NET) 0 33.1 33 1
23. UNIT FORCED OUTAGE RATE 100 22.4 22.4
24. SHVTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, DURATION OF EACH)

None

25. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: 10/06/88
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

FORECAST ACHIEVED INITIAL CRITICALITY N/A N/A INITIAL ELECTRICITY N/A N/A N/A '

COMMERCIAL OPERATION N/A i.ih 41 h R PDC

l .b.

  • 1 l AVERACE DA1LY UIllt POWER LEftL i

l '

l  :.

i DOCKET NO. 50-341 l

UNIT FERMI 2 I

l DATE October 15. 1988 COMPLETED BY P. M. Anthony l

I TELEPHONE (313) 586-1617 1

! Nonth September, 1988 i l

! DAY AVERAGE DAILY POWER LEVEL DAY AVERACE DAILY POWER LEVEL

! (NWe-Net) (NWe-Net) 1 0 17 0 i

2 0 18 0 3 0 19 0 i

4 0 M 0 [

i 5 0 21 0 [

t 6 0 22 0 ,

i l

7 0 23 0 t

8 0 24 0 9 0 5 0

! 10 0 _

26 "0 11 0 27 0 f 12 0 28 O_ l 13 0 29 0 [

r 14 0 30 _

0 l t

15 0 31 N/A  !

16 0 l i

t i

[

?

UNIT SHUTDOWNS AND POutO REDUCTIONS ',

e DOCmET NO. 50-341 DATJ Octcbee 95. 1988 UNIT NawE per=* 2 COwPLETED SW P2 _w. Anthony YELEPHONE (313)586-1617 REPORT WONTH 5epte=cer. 1988 1 I I I I I , i I l l  ! l  ! 1 wtTHO3 OF l LER I Sv5 Coup I CAUSE & CORRECT!vE j N3. I DATE l TvpE l DUR 1 REASON I SMUTTING DOwN l NO. CODE CODE l ACTION TO PREVENT l l l (1) 1 (HRS)l (2)  ! THE REACTOR I (4) l (5) i RECURRENCE I I I I I f (3)  ! I

!  !  !  ! I i  !

I I I i i i I j 88-006 1 08/29/88 i F 1 720 l 8 I 4 108-032 ! BO , V l LPCI Loop Select togic still inop- 1 I l } l  ! l l L l 1 oracle cue to inability to close l l l l l  !  ! l l 831-70318. Found torque settch l l l  ! 1 j l l l not prcperty reset foltostog l l l l l I l l i j replacement of operator in 1984. I I I l I i 1 1 1 I

!  !  ! I f I I I I I

'  !  ! I f  ! f I 1 I I (1) F: FORCEO (2) REmSON: (3) wETHOD: (4) EXHIBIT G - INSTRUCTIONS 5: SCHEDULED A - EQUIPvtNT FAILURE (EXPLAIN) 1 - MANUAL F OR PREPARATION OF DATA 8 - MAINTENANCE OR TEST 2 - wANUAL SCRAW ENTRY SHEETS FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAW EVENT REPORT (LER) *ILE D - REGULATOCV RESTRICTION 4 - CONTINUED (NUREG-0161)

E - OPEnATOR TRAINING & LICENSE ExAw! NATION 5 - REDUCED LOAD F - ADw!NISTRAT!vE 9 - OTHER G.- OPERATIONAL ERROR (EmpLAIN)

H - OTHER (ENPLAIN) (5) ExHISIT 1 - SAwE SOURCE 6

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