ML20203D175
ML20203D175 | |
Person / Time | |
---|---|
Site: | Millstone |
Issue date: | 02/23/1998 |
From: | Schopfer D SARGENT & LUNDY, INC. |
To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
References | |
9583-100, NUDOCS 9802250367 | |
Download: ML20203D175 (164) | |
Text
.
t Sor'Gont S LuncJy -
.y
(:
Don K. $thopfer
!.mma vge hes0nt 312 ?O M78 February 23,1998 Project No. 9583100 Docket No. 50 423 Nonheast Nuebar Energy Company h4 llstone Nuclear Power Station, Unit No. 3 indeperylent Corrective Action Verification Program United States Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C, 20555 Enclosed are discrepancy reports (DRs) identified during our review actisities for the ICAVP.
These DRs are being distributed in acccrdance with the Communications Protocol, PI hip 3 01.
<e enclosed the er.e (1) DR that has been detennined invalid. No action is required from h thea:t Utilities for this DR. The basis for its invalid determination is included on the document.
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~""'" -
DR No. DR-MP3 1069 I have also enclosed the following sixty three (63) DRs for which the NU resolutions have been h-reviewed and accepted by S&L R-
- =R' DR No. IA MP3-0049 DR No. DR MP3-0298 DR No. DR-MP3 0083 DR No. DR MP3 0299 DR No. DR MP3 0084 DR No. DR-MP3 0304 DR No, DR MP3-0989 DR No. DR-MP3-0317 j DR No. DR-MP3-0107 DR No. DR-MP3 0320 i i DR No. DR-MP3-0124 DR No. DR-MP3 0134 DR No, DR MP3 0337 DR No. DR MP3 0347
%09ij//
DR No. DR-MP3-0175 DR No. DR MP3 0396 DR No. DR-MP3-0195 DR No. DR-MP3-0397 DR No. DR-MP3 0217 UR No. DR MP3-0404 DR No. DR-MP3 0227 DR No. DR MP3 0419 DR No. DR MP3-0239 DR No. DR MP3-0420 DR No. DR MP3-0260 DR No. DR-MP3-0421 hhf23 t a Chicago. IL 60603-5780 USA
- 312 269-2000 P PDR
United States Nuclear Regulatory Commission February 23,1998 Document Control Desk Project No. 9583-100 Page 2 DR No. DR MP3-0424 DR No. DR MP3-0650 DR No. DR MP3 0429 DR No. DR MP3 0652 DR No. DR MP3-0439 DR No DR MP3-0661 DR No. DR-MP3 0449 DR No. DR MP3-0689 DR No. DR-MP3-0460 DR No. DR MP3-0715 DR No. DR-MP3 0462 DR No. DR MP34718 DR No. DR MP3 0504 DR No. DR MP3 0720 DR No. DR-MP3 0516 DR No. DR MP3 0721 DR No. DR MP3-0517 DR No. DR MP3 0722 DR No. DR-MP3 0519 DR No. DR MD 0743 DR No. DR MP3 0521 DR No. DR MP3 0 790 DR No. DR MP3 0562 DR No. DR MP3 0820 DR No. DR MP3 0577 DR No. DR MP3 0825 DR No. DR MP3 0603 DR No. DR MP3 0828 DR No. DR MP3-0621 DR No. DR MP3 0838 DR No. DR-MP3 0634 DR No. DR MP3 0848 DR No. DR-MP3 06?~- DR No. DR MP3-0868 DR No. DR-MP3 0636 DR No. DR MP3-0869 DR No. DR MP3-0975 1 have also enclosed the seven (7) DRs for which the NU resolutions have been reviewed but not accepted. S&L comments on these resoluoons have been provided.
DR No. DR-MP3-0072 DR No. DR MP3 0509 DR No. DR-MP3-0122 DR No. DR-MP3 0556 DR No. DR-MP3-0483 DR No. DR MP3 0638 DR No. DR MP3 0915 Please direct any questions to me at (312) 269-6078.
Yours very truly, C 1) C D. K. Schopfer g Senior Vice President and ICAVP Manager DKS:spr Enclosures Copics:
E. Imbro (1/1) Deputy Director, ICAVP Oversight T, Concannon (1/l) Nuclear Energy Advisory Council J. Fougere (1/1) NU i miavg%c\91Iw022M &w f
l DR N). DR-MP3 0049 Northeast Utlinies ICAVP Millstone unk 3 Discrepancy Report Review Oroup: syetem 03 RESOLUTION ACCEPTED A'# I IM*'" Potential OperstdlNy issue D6ecipune: Structural Design O Yw D6screpancy Type: Calculeton 4g systerVProceae: SWP MC signifW ence level: 4 Date F Axed lo NU:
Date Published: 9/2247 D6*ctopency: Pipe support calculation NP(F) Z19B-071 discrepancy DescriP#on: We have reviewed the Pipe Support Calculation No NP(F).
219B-071 Rev. $ . Based upon this review we have noted the following discrepancies:
(a) On page no. 24 vf the above calculation, applied forces and momeilts are computed at center line of the spdce (Point B) as follows:
Fxb = Fx/2 sides = 7,798#
Fyb = Fy/2 sides = 8,971#
Fzb = Fz/2 sides = 6,$77#
The above forces are discrep* '. because they do not include the contributions from the applied moments at pipe center line.
The correct forces ara as follows:
Fxb = Fx/2 sides a 7,798# ( No Change)
Fyb = Fy/2 sides 4 Mz / 2Lz = 9,580#
' Fzb = Fz/2 sides + My / 2Lz = 7,078#
(b) On page no. 29, the allowable shear for 1" Diameter A 325 SC bolts used is 13.40 k. This is in error. The bolt allowable shear should be based upon Shear Tension interaction for slip-critical connection per section J.3 of AISC manual,9th edition.
The correct value is 6.58k.
Review Val 6d inval6d Needed Date 8 7/S7 inM6etor: Patel. A. O O O S'$SS7 VT Lead: Nerl. Anthony A O O O 9/1897 VT Mgrt schopfer, Don K Q Q Q 8'5SS7 IRC Chmn: sin 0h AnandK O O O Deio:
WVAuo:
Date: 2/18/98 REs0LUTION: NU has concluded that Discrepancy Report, DR MP3-0049, has identified a condition not previously discovered by NU which requires correction This discrepancy meets the criteria specified in NRC letter B169ui , '.17010 it has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR MS 97 3868 has been written to develop and track resolution of this item per RP 4.
Prev 6ously identthod by NUf Q Yes @ No Non D6een ;2nt CondM6on?O Yes @ No Page 1 or 2 Printed 2/23/98 9.65.16 AM
__ _ - . .- . - . .-. . .-- _ _ _ - _ _ _ - - __ - - . . ~ . - - - _ . - . . . - - - - . . - . _ .
DR N2. DR-MP34049 (
Northeast Utilities ICAVP l Millsione Unit 3 Discrepancy Report .
n uion un, ev.er u v.e (e) wo n =*auPweetu v.4
- ) we neview M$# M Mc$2 W No
! insig. ,,3 p,i.i, A.
O O O m VT L.ed: Non, Arthony A O O O m VT Mer: Sdepfw DonK R O O m mc chmn: smn, Anand K D D 0 osie: 2/18/98 st Cwwnents: NU resolution is acceptable per review of CR M3 97 3666.
i I
9 l
i Page 2 of 2 Printed 2/2W96 9%20 AM .
1 _ -
Systern'Procese: 0f4 Date F A,Ked to NO:
NRC Shinifbcarece level: 4 Date Pubhshed: &?497 DI6erePancy: ESAFfTables 1.91 & 1.9-2 are inconsistent with FSAR Section 6.5.2 with respect to SRP 6.5.2.
D*6ctlMkm: FSAR Tables 1.91 & 1.9-2 are inconsistent with FSAR Sectica 6.5.2 wth respect to SRP 6.5.2.
Table 1.91 under SRP 6.5.2 states:
Containment splay system requirements are not discussed in Section 6.5.2.
Table 1.9 2 under SRP 6.5.2 51ates:
A. The containment spray system reguliements of SRP 6.5.2 are not discussed in FSAR Section 6.5.2.
D. No credit for containment spray fission product removal is taken in the Millstone 3 design.
However, fission product removal by the containment spray systems is specificaly addressed in FSAR Section 6.5.2.
Affected System Requirements:
OSS 384 RSS 329 Rev6ew VsM Invahd Needed Date O S?oS7 initiator: Feingold. D. J. O O VT Lead: Nort. Anthony A C O D S?nS7 O &?2/97 VT Mgr: Schopfer. Don K O O O &7697 IRc Chmn: sngh, Anand K Q C wie:
l' VALID:
Wie: 2/18/98 RESOLUTK)N: Disposition:
This discreoancy in the FSAR was previously discovered. FSAR CR 97.MPS 95 was initiated to correct the inconsistency, therefore no CR will be written.
Conclusion:
The discrepancy reported on S&L DR MP3-0083 was previously identified. FSAR CR 97 MP3 95 will correct the inconsistency.
For your information, a copy is attached.
Pepe 1 of 2 PrWed 2/21981007.44 AM
l ICAVP DR No. DR MP3 0083 Northeast Utliks Millstone Unit 3 Discrepancy Report Previously identihed by NUF (@~Yes O No Non D6screpent Condaion?C Yes @ No Resolution PondiaetO Ve. (6; No R. iioion unroeoiv.dr O v e. + No Review loatletor Feingold, D. J.
VT Lead: Nori, Arthaty A O O O **
i VT Mgra Schopfer, Don K IRC Chmn: $1ngh, Anand K
- e, sL Comments 1 Printed 2/2396 to 07.46 AM Page 2 of 2
I i
ICAVP DR No. DR-MP3-0084 Northeast UtilHies Millstorie Unit 3 Discrepancy Report Review Group: system DR RESOLUTION ACCEPTED A #I PMential Operetnitty leeue Diecipl6ne: Mechwket Desig" O va Discrepency Type: Drewlng
%) No systerrvProcess: Oss NRc signHncence level: 4 Date faxed to NU: <
Dale Published: 11/1&et Diecrepency: Interlock discrepancy between P&lDs EM 104A, EM 112A, & EM-113A. and FSAR Section 7.3.1.1.5 Dactlption: The suction valves to the charging pumps from the Refueling Water Storage Tank (RWST) are motor operated valves 3CHS*112D and 3CHS*112E. These valves are shown on P&lDs EM 104A Revision 26, EM 112A Revision 25, and EM-113A Revision 14.
According to FSAR Section 7.3.1.1.5, valves 3CHS*1120 and 3CHS*112E shall be interlocked to open on a safety injection signal (SIS). However, these P&lDs show no interlocks between SIS and these valves. Furthermore, the P&lDs shows no controls for 3CHS*1120 and 3CHS*112E.
Rev6ew Vol6d invol6d Needed Date initiator: Feingo6d, D. J. O O O $ 5/4/87 VT Lead: Neri, Anthony A Q ] Q 11/497 155S7 vi Mori schopfw, De K O O O O O 15'1i/97 1Rc chmn: singh. Anend K O Date:
WVAuo:
D*Ie: 2/6/98 Resol.UTION: Dispositlon:
NU has concluded that DR MP3-0084 does not represent a discrepant condition. P&lD EM 113A, Revision 17 and EM 104A, Rev 32 provides a cross reference to PalD EM 104D, Revision 20, dwg. locetion D 11 that show the controls and interlocks for valves 3CHS*1120 and 3CHS*112E. This section includes all controls and signals that these two valves receive and is consistent with FSAR section 7.3.1,1.5. Additionally, the latest revision of EM 112A is Rev 32 not Rev 25 as Indicated on DR.
MP3-0084 and valves 3CHS*112D and 3CHv112E do not appear on the current revision of EM 117.'..
Conclusion:
NU has concluded that Discrepancy Report DR MP3 0084 does not represent a discrepant condition. As detailed in the disposition, the proper controls and interlocks for valves 3CHS*112D and 3CHS*112E are indicated on EM 104D, Rev 20 which is cross referenced by both EM 104A and EM 113A.
Valves 3CHS*112D and 3CHS*112C are not indicated on the current revision of P&lD EM 112A. Current revisions of EM.
Printed 2/239610:11:18 AM - Pege 1 of 2
_ _ . ---. . .- - _ . - . _ . - _- . = - _ - _ _ _ - _ . _ . -
ICAVP DR N3. DR MP3 0084 J Northeast Utilities Millstone Unk 3 Discrepancy Report !
I 104A, EM 104D, EM 112A and EM 113A are included with this IRF. Significance level criteria does not apply as this is not a discrepant condlilon.
Previously klentified by NU7 O Yes fG) No N* D6screpard CondN6on?O Yes f#i No Resolut6on Pending?O Yes +> No Renoiuiion un eaoived?O Y . 'W) No Review Acceptatde Not Acceptable Needed Date inn W F M ,D.1 VT Leed: Nort. Anthony A VT Mgt: Schopfer. Don K IRC Chmn: singh. Anand K Date: 2/6/98 sL commerds: The drawing revisions applicable at the cut off date of 5/27/97 are as follows:
12179 EM 104A Revison 26 12179 EM 104D Revison 16 12179 EM 112A Revison 25 12179-EM 113A Revison 14 Drawing 12179-EM 113A Revision 14 does reference c'rawing 12179-EM 104A and 12179-EM 104D for control infor, nation on valves 3CHS'1120 and 3CHS*112E. Drawing 1217's-EM 104D Revision 16 does show controls for the subject valvt* '.id shows that the valves open on a safety injection signal. The discrepancy is that drawing 12179 EM-104A Revision 26 does not show any control information for valves 3CHS*112D and 3CHS*112E and does not cross reference drawing 12179 EM-104D Revision 16 or drawing 12179-EM 113A.
A review of drawings P&lD EM 113A, Revision 17, dated 12/22/97 and EM 104A, Rev 32, dated 11/3/97, show the coiTect cross references.
Consequently, this discrepancy report is valid and the implemented change to P&lD EM 113A Revision 17 is an acceptable resolution.
Printed 2/239610.11:21 AM Page 2 of 2
DR No. DR-MP3 006v Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Revirsf Otoup: System DR REs0LUTK)N ACCEPTED Rev E : s@ W Potential Operatety issue D6scip66ne: Structural Design O v.
Discrepency Type: C*deten O No sysiwn' Process: QSS NRC sign 6f6cence level: 4 Dele Faxed to NU:
Deie Published: 9/22/97 D6*crepancy: Pipe Support Calculation Discrepancy Descript6on: We have reviewed Pipe Gupport Calculation # 12170 NP(F).
2790127 R1, CCN1 Based on this review, we have noted the following discrepancies.
- 1. Calculations on Page 17, Loading 104 Joint 16 Load Force Y should ba 650(not 350).
- 2. Calculations on Page 58, the factor fa/Fs should be 0.0197 (
not 0.274 ). The value of fa did not consider the erea in denominator.
The above discrepancies are not significant for the final design.
Review Val 6d invol6d Nooded Date
- Initiator: Patel,A. O O O S'17/87 VT Lead: Nort, Anthony A O O O S'17/87 O S7/87 VT Mgr Schopfw, Don K O O S'17/87 1RC Chmn: Singh, Ahend K O O O Dete:
IWALID:
Date: 2/20/93 RESOLUTION: NU has concluded that Discrepancy Report DR MP3-0089 has identified a condition not previously discovered by NU which requires correction. Calculation NP(F) Z790127 has been revised to correct the discrepancies of item 1 and 2. This is a documentation change only, No changes in the field are required. Condition Report (CR) M3 97 3524 has been written to provide the necessary corrective actions to resolve this issue.
Previously identified by NU7 O vos @ No Non D6scropont Condition?O vos @ No Resolution Pend 6ng?O vee @ No ResolutionUnresolvedtO ve. @ No Review initletor: Petel. A.
O m VT Leed: Neri, Anthony A VT Mgri Schopfer, Don K 1RC Chmn: Singh. Anand K
-e sL Comments:
Page 1 of 1 Printed 2/23/9e 10.12:o4 AM
DR No. DR MP3 0107 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Revb .1 Group: Syenem DR RESOLUTION ACCEPTED ,
Rev6ew Element: System Doengn need OperdsN#y kaue D6sciphne: Electrical Design O s*
Dioctopency Type: Drowin0 gg System?rocese: Rs3 NRC SlgntAconce level: 4 Date faxed to NO:
Date Published: 9/1497 Dieuepency: Logic Diagram Discrepancy foi Valves 3RSS*MOV38A & B, Descripilon: General Notes drawing LSK-0 38, note 6,1 Indicates that *When torque seating is required, the logic diagram will so stat).*
Schematic diagrams ESK-6AFL and ESK-6AFM indicate that 3RSS*MOV38A & B will close on torque, since the torque switch le not bypassed during the final 15% of valve travel in the closing direction. The associated logic diagram, LSK 2711H, does not Indicate valve closure on torque, Review I Vend invend Nooded Date 8'6S7 initiator: Marion, R. O O O S'897 VT Lead: Nerl, Anthony A @ [ Q *SS7 VT Mor schopfw, Don K O O O O *SS7 Ntc Chmn: Singh. Anand K G O Date:
INVALID:
Date: 2/9/98 REs0LUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3 0107, has identified a condition not previously discovered by NU which has been conected. Logic diagram LSK 2711H has been revised per Design Change Notice (DCN) DM3 001060 97, dated August 29,1997 to depict the
- Torque Seated
- requirement for 3RSS*MOV38A & B, Condition Report CR 97 3245 has been written to document this discrepancy.
Coi.clusion:
NU has concluded that Discrepancy Report, DR MP3-0107, has identified a condition not previously discovered by NU which has been corrected. Logic Diagram LSK 2711H has been revised per Design Change Notice (DCN) DM3-001060-97 to depict the
- Torque Seated
- requirement for 3RSS*MOV38A&B. No field changes are required, Condition Report CR 97 3245 has been written to document this discrepancy.
Previously identined by NU7 Q Yes I$8) No NonDiscrepentCondition70 Yes (9) No ResolutionPending?O vos (*J No Renoiuemuaronoive470 vos (*D No Review Acceptable Not Acceptable Needed Date inMietor Mon, Ri b b b VT Lead: Nort, Anthony A D D m VT Mgr: Schopfer, Don K Pope 1 of 2 Printed 2/23Se 1o.13.18 AM
--e.- - - _ _ . _ _ . _ _ _ -._____._______________._.________m_
1 ICAVP DR No. DR MP3 0107 Northeast UtilMks Millstone Unn 3 Discrepancy Report
. . , . . . . . , ' ~ '
O O mia
- MC Chmn: Shgh, Anand K Date:
1 SL Comments:
l i
4-i l
4 J
s i
Printed 2/239610:13.22 AM Page 2 of 2
DR No. DR MP3 4124 Northout Utiliths ICAVP Millstone Unit 3 Discrepancy Report Review Oroup: System DR RESOLUTION ACCEe TED
"*
- Potentlel Operet,.Jty losue D6ecipline: Elemal Des $n O ve.
D6screpency Type: DreMng @ No systerrWrocess: $WP NRC sigrdftcence level: 4 Date faxed to NU:
Date Putd66hed: 9/1497 D6*cr*Pency: Logic and Schematic Drawing Discrepancy in Auxiliary Rela /
Designation Descript6on: Schematic diagrams ESK-6AAA,6AAB,6AAC, & 6AAD identifies the thermal overtoad auxillary relay as p *49X' device.
The logic diagram LSK 2711E Identifies the thermal overtoad auxiliary relay as a '74' device.
Review Val 6d invellf Needed Date Q 2 97 initiator: Morton, R. Q Q "S7 VTLeed: Neri, Anthony A G O O O SS7 VT Mgi: Schopfu, Don K O O Q M97 IRc chmn: singh, Anand K Q Q D d.:
WVALO:
Date: 2/17/98 RESOLUTON: Disposition:
NU has concluded that Disc epancy Report DR MP3-0124, has identified a condition previously discovered by NU which has been corrected. A comparative review of the LSK drawings and ESK drawings was performed as part of the 50.54f program. As a result of this review, Condition Report (CR) M3 971711 was initiated on May 29,1997. As part of the corrective action for this CR, Design Change Notice (DCN)DM3 00-0854 97 was prepared and issued which included the revision of LSK 2711E to show 49X as a sourca in lieu of 74.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0124, has identified a condition previously discovered by NU which has been corrected. Design Change Notice (DCN) DM3 00 0854 97 has been prepared and issued which revisad drawing LSK 27-11E to show 49X as a source in lieu of 74.
Previously identifled by NUf @ vos Q No Non D6ecrepent Condetion?O vos @ No ResolutionPendingtO vs. @ No ResolutionunresolvedrO yes @ wo Review Acc8Pteble Not Acceptable Needed Date Miete Mort % R.
VT Leed: Nort. Anthony A O O mm VT Mgr: Schopfer, Don K IRC Chmn: $1ngh. Anand K D.e, n a..
Page 1 of 2 Printed 2/239610:15:30 AM m
DR No. DR-MP3 0124 Northeast utilitie, ICAVP unistone Unit 3 Discrepancy Report PrWed 21239610.15 43 AM
DR No. DR MP3 0134 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Rev6ew Geog: System DR RESOLUTION ACCEPTED Review fierr.ard: Systern Desigi Potential OperebHNy issue Dixipane: En dricalDesiga O vs.
D6screpancy Type: Drewing @) No SystenVProcess* SWP NRC Significence level: 4 Date faked to NU-Date Publ6shed: 1/1G98 Discr*p*ncy: Discrepancy between schematic drawings and FSAR figure 7.3-4 (typical test circuits).
Descripuon: The logic diagrams (LSK 2711E Rev,9 & 11L Rev. 9 and LSK.
91G Rev.11,70 Rev. 9 & 7E Rev. 9) and schematic diagrams (ESK-6AAF Rev. 9, AAG Rev.10, AAH Rev,8. AAJ Rev, f!,
AAK Rev. 9, AAL Rev.8, AAM Rev. 9, and AAN Rev. 8) indicate that a *No . No* Equipment test circuit is part of the circuits for 3SWP'MOV50A & B,54A, B, C, & D, and 71 A & B. FSAR section 7.3.2.2.5 and figule 7.3-4 provides typical detalls for the
- No . No* test circuit in bcth 120 Vac and 125 Vdc circuit applications. The typical details in FSAR figure 7.3 4 Indicates that a varistor is used in 125 Vdc applications and does not indicate the use of a varistor in 120 Vac applications. These schematics (listed above) Indicate the use of a varistor in 120 Vac applications.
Rev6ew Voi6d invalid Needed Date 12/18/97 initiator: Morton, R. ] Q Q VT Leed: Nort, Anthony A g Q Q 12/1897 O in/2297 VT Mget schopfer, Don K O O
' 1Rc chmn: singh, Anand K O O O 12'31/S7 Deio:
INvAllo:
D*Ie: 2/11/98 ResOLUTON: Dlsposltjon:
NU has concluded that Discrepancy Report, DR MP3-0134, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter 816901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0512 has been written to develop and track resolution of this item per RP 4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0134, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0512 has been written to develop and track resolution of this item per Pope 1 or 2 Printed 2!23/9e 10,16:15 AM
DR N3. DR MP3 0134 Northeast Utiinies ICAVP Millstone UnN 3 Olscrepancy Report RP4, Previously klont6fied try NU7 U Yee 79) No Non D6screpent Condn6on?U Yes % No ResolutionPend6ng?O Yee (6) No RenosuisonunresoevedtO vee
- No Rev6ew Acceptable Not Accogdebie Needed Date hMWw: W R.
O O O wa VT Leed: t4ert, Anthony A O O O **
VT Mgt: ScMpfer, Don K 1RC Chmn, Singh, Anand K
-e SL Comments:
l l
Pope 2 of 2 Printed 2/23W 10:16:19 AM
~ - ..
DR N1 DR-MP3 0175 N:rtheast Utilities ICAVP Milistone Unit 3 Discrepancy Report Review Oroup: splom DR RESOLUTION ACCEPTED i
Reybew Eternent: Sptem Des 6gn P lOWWh Discipline: Electrical Desgn Om Discrepancy Type: Licermng Documord ,g systerWPetgess: SWP NRC $6gnirmarco level: 4 Date F Axed to NU:
Date Publi6hed: 9/2297 Di$crepancy: FSAR Description of MCC & rod control area booster pump operation does not match drawing information De6ctlpuon: The description of the MCC and rod control area booster pump operation does not match the logic rnd schematic drawings.
FSAR Section 9.2.1.2 pages 9.2 4 & 5 state:'MCC and rod control eres bootter pumps, one on each service water header, provide the additional head required to circulate service water through the MCC and rod control area air conditioning units when chilled water flow to these units is lost. In the event of a high temperature in the retum duct to the MCC and rod control area air handling unit, or an Loss of Offsite Power (LOP), the pumps will automaticall/ statt if the associated air conditioning unit is operatir$g ."
This description does not match the schematic and logic drawings. Based on the drawings the pumps will not start if booster pump suction pressure is low for greater than 20 seconds along with the conditions defined in the description.
This was verified by a reviow of the following drawings:
ESK 06SM Rev 11 Elem Diag 480V MC MCC Rod & Cable Vault ACU [3HVR*ACU1 A.1B]
ESK 06ALG Rev 07 Elem Diao 480V MC MCC & Rod Control Area Booster Pumps [3SWP*P3A,3B)
LSK 09-10E Rev 17 Logic Diagram Service Water System LSK 22-CiK Rev 08 Logic Diagram Reactor Plant Ventilation Review Val 6d inval6d Needed Dats 8/15S7 initiator: Wamet, I O O O Q 9/1597 VT Lead: Nort, Anthony A Q Q S 7/S7 VT Mgr: schopfer, Don K O O O 4 % 97 IRC Chmn: singh. Anand K Q Q Q D.ie:
INVAll0:
Date: 2/19/98 RESOLUTION: NU has concluded that the issue reported in Discrepancy Report, DR MP3-0175, does not represent a discrepant condition. The MCC and Rod Control Area air conditioning units are normally supplied with chilled water from the chilled water system.
Page 1 of 2 Prtnted 2/239610.17:27 AM
l DR No, DR MP3 0176 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report ,.
Dackup cooling to these units is provided by the service water system. Specifically, two independent booster pumps provide service water to these units under the following conditions:
On LOP signalif the cooling units are running, OR On high I.imperature in the retum duct to the MCC and rod control ares air handling unit if the unit is running.
The above information is reflected in the design basis and appropriately reflected in the lleensing basis as described in the FSAR. The additional feature in the design which shuts off the booster pumps if there is not sufficient suction pressure for 20 seconds is provided for equipment orotection only since one booster pump will always be available for a transient condition.
Specifically,if one assumes a single failure of an electrical train, the other train will be available and it is not necessary to postulate a second f ailure associated with the booster pump suction pressure.
In summary, the logic diagrams and the FSAR have been reviewed and it has been concluded that both are consistent and correct and no further action is required. it should also be recognized that in the overall context of the FSAR it is not necessary to discuss every design feature of a system, particularly when the discussion does not Impact the safety analysis.
Significance Level criteria do not apply here as this is not a discrepant condition.
Conclusion:
Nu has concluded that the issue reported in Discrepancy Report, DR MP3 0175, does not represent a discrepant condition. The low suction pressure for 20 seconds is a trip of the service water booster pump not a start permissive. In addition, the trip is for equipment protection only. The automatic starts of 3SWP*P2A/B are well described in the FSAR and accurate. In the context of the FSAR,it is not necessary to discuss every design feature of a system. Significance Level criteria do not apply here as this is not a discrepant condition.
Previously identifned by Nu? O Yes (#1 No Non D6screpent Condotion?(*) Yes O No ResolutionPend6ng?O vos @ No ResolutionUnresolvedrO vos @ No Review inmator: wenw,i.
- "A***** ""d'd D*
VT Lead: Nort. Anthony A VT Mgr: Schopfer, Don K IRC Chmn: Skgh, Anand K Dete: 2/19/98 sL conwnents:
Pope 2 or 2 l Printed 2/2196 to 17.31 AM
DR N3. DR MP3-0196 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Rev6ew Oroup: Confgurets DR REs0LUTION ACCEPTED Rev6ew Eiernent systern D@ Potent 6el Operablisty issue
() m
' Diecipline: Pp6n0 Do66pn Discrepancy Type: Drew 6ng 4 po systerr#rocess: Oss i NRc signifkence level: 4 Date faxed to NU:
1 Date F utillehed: k?k97 D6scr*Pency: OSS/RSS Upper fier to Lower Tier Drawing Discrepancies for Containment Bldg:
Descript60n: The following drawing discrepancies were found in reviewing the PalD with the as built isometric drawings-
- 1. On Cl OSS 30 Sht 6 Rev 15 safety telated valve 3OSS*V979 as shown on PalD EM 115A Rev 18 (L 7) should be designated with (*).
- 2. On Cl OSS 30 Sht 10 Rev 15 safety related valve 3OSS*V978 as shown on PalD EM 115A Rev 18 (L 8) shot.id be designated with (').
- 3. On Cl RSS 504A Sht 5 Rev 5 safety related valves 3RSS*V950, 'V991, and 'V995 as shown on PalD EM 116A Rev 18 (L 7) should be designated with (*).
- 4. On Cl RSS 502B Shi 3 Rev 4 safety related valves 3RSS*V952,'V993. 'V989, and 'V6 as shown on P&lD EM 115A Rev 18 (J 5) should be designated with (').
- 5. On Cl RSS 504B Sht 4 Rev 4 saftty related valves 3RSS*V953,'V992,'V988, and 'V3 as shown on PalD EM 115A Rev 18 (L 4,L 5) should be designated with (').
Review Val 6d invol6d Needed Date O 8'1 '87 inttletor: Reed. J. W. O O VT Lead: Nori. Anthony A O O O S/15/S7 O 222r97 VT Mgr: schopfw Don K O O O *?5S7 1RC Chmn: singh, Anand K O O Dele:
INVALlO:
Dele: 2/17/98 RESOLUTION: Disposillon:
NU has concluded that Discrepancy Report, DR MP3-0195, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 Pl-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 97 3374 has been written to develop ar.d track resolution of this item per RP4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0195, has identified a condition not previously discovered by NU which Pope 1 of 2 Printed 2,739610.16.31 AM
-- . - . _ _ - . .. --. _ . _ _ ~ _ - . - - - . - - - .- --
DR No. DR-MP34196 Northeast Utilhies ICAVP Millstone Unn 3 Discrepancy Report requires correction. This discrepancy meets the criteria Specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concerns and inJets the Unit 3 deferral criteria. CR M3 97 3374 has been written to develop and track resolution of this item per RP-4.
'97 No NonDe6ctopentCorHNt60n?O Yes @ No Prevk>usly identifM by NU? O Yes Renoiviion unce.oiv.drO Yo. (v>No R4oolut60n Pend 6ng?O Ye. (v No Rev6ew Acceptable Not Acceptetdo Nooded Date g g O O O m VT Leed: Neft. Anthony A VT Mgri Schopfer, Don K IRC Chmn: $6ngh. Anand K Dele:
$L Comrnents:
Page 2 of 2 PrWed 2/239e 10.16 34 AM
DR No. DR MP3-0217 k Northeast Utilities ICAVP l Millstone Unit 3 Discrepancy Report l Review Group: System DRREsOLUTION ACCEPTED
- Potential Operabinety istue mocipiw i a e D.'* O Yo.
Discrepency Type: Drewing
- No systerr#rocess: Rs3 NRC sbgnihcance level: 4 Date faxed to NO:
Date Published: 11/2/97 Discrepancy: Drawing Discrepancy . LSK 2711 A,0 J,K
Description:
Condition for Pump P1D on LSK 27118 should be chan0ed from
- Bus 340 Bus Diff, Lockout Relay Reset to
- Bus 34D Bus Diff. Lockout Relay Operated" to be consistent with the Condition for Pumps P1 A, P1B and P1C. Bus Diff, Lockout Relay Operated is one of the Conditions requlted to trip the pump.
Rev6ew Val 6d inval6d Needed Date
^
50'17'87 initletor: Pinelas, H. O O O VT Lead: Net, Anttony A g Q Q 10/17/97 1D7S97 VT Mgt: Schopfw, Don K Q Q Q O 'o'3357 BRC Ctwnn: &lngh. Anand K O O Date:
INVALID:
Date: 2/9/98 RESOLUTION: 0;sposition:
NU has concluaed that Discrepancy Report, DR MP3 0217, has identitled a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010, it has been screened per U3 Pl-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-96-0164 has been written to develop and track resolution of this item per RP 4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0217, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0164 has been written to develop and track resolution of this item por RP 4.
Prov60usly identnrwd by Nu? U Yes (@ No NonDscrepantCondition?O Yes (el No ResoluuonPend6ng?O ve. @ No Resuuuonunr savedtO vos @ No Review initiator: Hindie, R.
VT Lead: Nort, Anthony A O m VT Mgt: Sctopfer Don K nRC Ctwnn: Singh, Anand K b
Page 1 of 2 Printed 2/2396 to 1909 AM
DR No. DRWP3 0217 Northeast Utilities ICAVP Millstone unk 3 Discrepancy Report
- . , , , - ~ "
O O O Date:
SL Comnseds:
l 4
PrWod 2/239010.19:13 AM Pm2W2
_. __ _ - - . _ _ _ - -__ -= . - _ _ - - . _ __
DR No. DR-MP34227 Northeast Utilities ICAVP Miiistone Unit 3 Discrepancy Report Review Oroup: Confguraten DR REsOLt/ TION ACCEPTED
- " Potentiel Operab666ty leeue D6scipl6ne: I & C Dee$n g D6screpency Type: Insteheten implementaten ~ No SysterrWProcess: sWP NRC Sign 6acance levet: 4 Date faxed to NU:
Date Published: 12/2097 06*ct*Pency: Instrument Sealing Desertpoon: The sealing of instruments to preclude moisture intrusion or the introduction of foreign material / contaminates into the device thereby rendering it inoperable is provided by specification and vendor instrument manuals. The following inconsistencies between the installed conditions and the requirements of the referenced documents were noted during the system walkdowns
- 1. l&C Technical Bulletin #102,
Subject:
'Use of Teflon Tape (Corrective Action for ACR M3 96-0067T and Specification SP.
EE 212,' instrumentation Installation, Piping and Tubing
- set forth requirements for use of thread sealant. SP ME 570, *Fleid Fabrication and Erection of Piping and Supports
- Sections 1B.1.4 and 10.1.4.1 also contaln requirements. These documents indicate that Teflon tape should not be used.
Contrary to this requirement, the following instruments have Teflon tape applied to their threads:
l SSWP FIS41A 3SWP Pl4dA 3SWP Pl23D 3SWP Pl45A 3SWP Pl23B 3SWP Pl46C 3SWP Pl23A 3SWP Pl45B 3SWP Pl23C 3SWP Pl45B 3SWP PDl164B The following material conditions were observed during the walkdown. These items are not configuration management related issues.
- 1. Pressure switch 3SWP'PS278 shows signs of galling of a housing plug. The electrical pipe plug used to seal an used port is excessively corroded to the point that leakage may occur.
- 2. Pressure Transmitter 3RSS PT43D service cap is very loose. The 0-ring seal appears to be the wrong size or broken -
a large gap between the service case cover and the fixed case housing exists which creates an inleakage potential.
- 3. Drawing BK 16P-05 Rev.13 Sheet 1 of 1 shows proper instrument installation for 3RSS-PT24. This Instrument is not securely mounted and not sealed.
Review Valid invalid Needed Date initiato': Server. T. L G O O 12/t<$7 VT Lead: Nort, Anthony A O O O 12/5'87 D D 12iiti97 VT Mgr: Schopfer, Don K D O O 2itas7 IRC Chmn: singh Anand K O Page i of 2 Printed 2/239610.59.36 AM
DR No. DR MP3 0227 Northeast UtilHies ICAVP Millstone Unit 3 Discrepancy Report om:
twAuD:
D*: 2/20/98 ntsoLUTioN: Disposition:
NU has concluded that Discrepancy Report, DR.MP3 0227. has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 Pl.
20 criteria and found to have no operability or reportability concems and meets the Unit 3 defctral criteria. CR M3 98-0$11 i has been written to develop and track resolution of this item per RP 4.
Conclusion:
NU has concluded that Discrepancy Report DR MP3 0227. has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC setter B16901 and 17010. It has been screened per U3 Pl.
20 criteria and found to have no operability or reportability g
concems and meets the Unit 3 deferral criteria. CR M3 98-0511 has been written to develop and track resolution of this item per RP 4.
< Prev 6ously iderdined by Nut () vos Y No Non D6ecrepent Condition?O vee foi No Resolut6on Pending70 vee (*) No neeoiuinoaunteeoivedrO vee
- No Pev6.w
- * ***# "**#*d "*
insinator: Wwne,1.
VT Leed: Nort, Anthony A VT M9r: Schopfer, Don K 1RC Ctwnn: s6ngn. Anand K D*: 2/20/f8 sL Crwnmente:
Printed 2/239810.19 42 AM Page 2 of 2
DR No. DR MP3 0227 Northeast UtilNios ICAVP Millstone UnR 3 Discrepancy Report Review Group: Contgweten DR REsoLUTsoN ACCEPTED Rev6ew Elemord: syenem inoteheton p ,
D6scipl6ne: 14 C Do64pn Om D6ecreparwy T ype: Irwtstaton trnplementate ,g system 9tocees: sWP NRC signif6conce level: 4 Dele F Axed to NU:
Deee Putd6ehed: 12/2097 twoctogencIinstrument Sealing Descrg46oi.: The sealing of instruments to preclude moisture intrusion or the introduction of foreign materist/ contaminates into the device thereby rendering it inoperable is provided by specification and vendor instrument manuals. The following inconsistencies between the installed conditions and the requirements of the referenced documents were noted during the system walkdowns 1, l&C Technical Bulletin #102,
Subject:
"Use of Teflon Tape (Corrective Action for ACR M3 96 0067)" and Specification SP-EE 212,' Instrumentation Installation, Piping and Tubing" set forth requirements for use of thread sealant. SP ME 570,'Fleid Fabrication and Erection of Piping and Supports
- Sections 18.1.4 and 18,1.4.1 also contain requirements. These documents indicate that Teflon tape should not be used.
Contrary to this requirement, the following instruments have Teflon tape applied to their threads:
3SWP-FIS41A 3SWP Pi46A 3SWP Pl23D 3SWP Pl45A 3SWP Pl23B 3SWP Pl460 3SWP Pl23A 3SWP Pl45B 3SWP Pl23C 3CWP Pl458 3SWP PDl1648 l
The following material conditions were observed during the
' walkdown. These items are not configuration management related issues.
1, Pressure switch 3SWP'PS278 shows signs of galling of a housing plug The electrical pipe plug used to seal an used port is excessively corroded to the point that leakage may occur.
are Transmitter 3RSS-PT43D service cap is very
- 2. Pr, } he O ring seal appears to be the wrong size or broken loose.1 a targe gap between the service case cover and the flxed case housing exists which creates an inleakage potential, 3 Drawing BK 16P 05 Rey,13 Sheet 1 of 1 shows proper instrument installation for 3RSS PT24. This instrument is not securely mounted and not sealed.
Rev6ew Valid inval6d Nooded Date intilator: server, T. L O O O 12/i/97 VT Lead: Nort, Anthony A O O O i:5S7 O O $2/it'S7 vi por: schapter Don K O IRC Chmn: Singh, Anand K @ Q O 12/1&S7 Page 1 or 2 Printed 2/23961o.19.S5 AM
ICAVP DR No. DR MP3 42E Northeast UtilMies Millstone UnN 3 Discrepancy Report D*:
puAuo:
D*: 2/20/98 ResoLUTloN: Disposition:
l NU has concluded that Discrepancy Report, DR MP3 0227, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the enteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportaNfity concems and meets the Unit 3 deferra' criteria. CR MS 98-0511 has been written to develop and track resolution of this item per RP4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3 0227, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability Concems and meets the Unit 3 deferral criteria. CR M3 96 0511 has been written to develop and track resolution of this item per RP-4.
Prevkuly identmed by NU? O Yen (GI) No Non D6screpent CondM60n?Q Yes IG) No Resolution Pend 6ngtO vos (6) No MesolutionUnresolvedf0 vs. (4) No Revlow Accepteble Not Accepteble Needed Date gny,,; g, t VT Leed: Nort. Anthony A O O **
VT Mgr: schopfer, Don K IRc chmn: Singh, Anand K Dele: 2/20/98 sL Comments:
Pege 2 of 2 Printed 2/259610:19 56 AM
DR No, DR MP3 0239 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report \
Rev6ew Group: SyWorn DR REs0LUTION ACCEPTED l ReVl'* El*'"*t: System Desgn Potent 6al Operabmty 166ue I
Discipline: 1 & C Dodgn ({py y,,
D6screpency Type: Dremang O No SysterWProcess: SWP NRC $6gnifbcance level: 4 Date Faxed to NO:
Date Published: 10/1&97
' Disc'*P*ncy: Drawing Discrepancy . Schematics 3SWP 060A,B Descript6on: Per Section 12.6.1 of the Design Basis Summary Document, 3DBS BOP 001,'A radiation monitor shall be located on the outlet of each RSS Heat Exchanger...". This disagrees with P&lD EM 133B which shows two radiation monitors:
3SWP'RE60A at the discharge header of 3RSS*E1 A, E1C and 3SWP'RE600 at the discharge header of RSS'E18 E1D. Loop Schematics 3SWP 000A, Rev 4 and 3SWP 0608 Rev 3 agree with the above P&lD In addition, FSAR Secilon 6.2.2.2 System Design, Subsecilon on the Containment Recirculation System dated S/97 states 'The service water from each pair of the recirculation coolers is monitored by a radiation monitor ..,*.
PalD EM 1338 shows local alarms for high radiation and failed channel and a control room common high radiation alarm; the Loop Schematic does not show these 6: arms.
Review V666d invalid Needed Date O o/2ss7 initiator: Pinelas. H. O O VT Lead: Nert, Anthony A O O O 10/1/97 VT Mor schopfer, Don K O O O 10/12S7 O io'i+S7 INC Chmn: Skgh, Anand K O O Dei.:
Oh/ Allo:
Date: 2/9/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0239, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified
- in NRC letter B16901 and 17010 It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-97 3928 and 3929 have been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0239, has identified a condition not previously discovered by NU which requires correc41on. This discrepancy meets the criteria specified
- In NRC letter B16901 and 17010 It has been screened per U3 Pi-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral r 'teria. CR M3 97 3928 and 3929 have been written to develop a.1d track resolution of Page 1 of 2 Pnnled 2/219610.21:21 AM
DR No. DR MP34239 Northeast Utilhies ICAVP Millstone Unit 3 Discrepancy Report this item per RP-4, Non(Noct:;-tConet6on?U Yes IG) No ;
Previously idenOfted by NU7 U vos (Gi No ResolutionPoneng70 vee <*? No Re.oiotion un,. iv.de o v., re; No Review Acceptable Nc4 Acceptable Needed Date inkW: He, R.
VT Leed: Neri, Anthony A O O ma VT Mgt: Schopfer, Don K IRC Ctenn: Shgh, Anand K
- e. ,
$L Commerds:
1 1
I l
i Page 2of 2 l Prtr#ed 2/239810.21:25 AM
ICAVP DR No. DR MP3 0239 Northeast Utilities Millstone Unit 3 Discrepancy Report Review Group: Syntom DR RESOLUTION ACCEPTED
'# II N poterdialOperstdidy lasue Discipline: 1 & C Design 4g D6screpency Type: D1'** O No systemProcese: sWP NRC sigenconce level: 4 Date FAKod to NU:
Dele Putd6ehed: 10/1&T7 Descrepancy: Drawing Discrepancy . Schematics 3SWP 060A.B Descript6on: Per Section 12.01 of the Design Basis Summary Document, 3DBS BOP 001, *A radiation monitor shall be located on the outlet of each RSS Heat Exchanger...". This disagrees with P&lD EM 133B which shows twa radiation monitors; 3SWP*RE60A at the discharp, newer of 3RSS*E1 A, Eic and 3SWP'RE60B at the discht ~1 header of RSS'E1B, E10. Loop Schematics 3SWP 060A, f W 4 and 3SWP 0608, Rev 3 agree with the above P&lD. In adoni>n, FSAR Section 6.2.2.2, System Design, Subsection on the Containment Recirculation System dated 5/97 states ihe service water from each pair of the recirculation coolers is monitored by a radiation monitor ...".
PalD EM 1338 shows local alarms for high radiation and failed channel and a control room common high radiation alarm; the Loop Schematic does not show these alarms.
Review Vol6d invalid Needed Date W2697 initiator: Paneles. H. @ Q Q VT Lead: NorI. Anthony A @ [ Q 10/1/97 VT Mor: Schopfer. Don K O O O 10/12S7 O O 10S7 IRC Chmn: Singh. Anend K O Dei.:
INVAuoi Date: 2/9/96 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0239, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 anu 17010 it has been screened per U3 PI-20 criteria and found to have no opernbility or reportability concems and meets the Unit 3 deferral criteria. CR M3-97 3928 and 3929 have been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0239, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 1701011 has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 97 3928 and 3929 have been written to develop and track resolution of Page 1 of 2 Printed 2/219610.21:36 AM
DR No. DR-MP3 0239 Northeast Utiliths ICAVP Millstone Unit 3 Discrepancy Report this item per P,P-4.
~
Previou.ly identified by NU7 U Yes (#) No Nor[kscrepentCondM6on?U Yes (#1 No Rs.olut60n Pending?O Ye. 1@ No Re.oiution unre.oivedtO i ss 5) No Review Accerchk Not Acceptable Needed Date initiator; iirda, R. 2/$SS8 VT Lead: Nort, Anthony A O O O O 2/S S*
VT Mgt: Schopfer, Don K Q O O 2f41/98 IRC Chmn: Singh, Anand K O O O Cate:
SL Comments:
Page 2 of 2 Printed 2/239610:21:41 AM
ICAVP DR No. Dit-MP3-0260
, N::stheast Utilitle3
- Millstone unit 3 Discrepancy Report Review Group
- Contguraton DR RESOLUTION ACCEPTED Review Element: system Design NWWmW W Discipline: Piping Design Discreparcy Type: Drawing Om
% No System / Process: Co*
NRC Signincance levet: 4 Date faxed to NU:
Date Published: 9/29?J7 Discrepency: Upper tier to Lower Tier Drawing inconsistencies for SWP in Auxillary Bldg.
Descripuon: The following drawing discrepancies were found in reviewing the P&lD with the as built Isometrics:
- 1. On Cl SWP-22 Sht 4 Rev 8 safety related valves 3SWP*V972, 'V198, 'V973,*V29(*MOV71 A), 'V62(*MOV718),
and 'V199 and instruments *PS89A, *PS70A, *PS69B, and
- PS70B as shown on P&lD EM 1338 Rev 34 (C-6,7,8) should be designated with an (*).
- 2. On Cl SWP 22 Sht 4 Rev 8 the continuation line 3-SWP-030-56-3 should be 3-SWP-018-99 3 per the isometric drawing itself and P&lD EM 1338 Rev 34 (D 8).
- 3. On Cl SWP-95 Sht 4 Rev 10 line 3-SWP-030-396 3 is called out.This line is not on P&lD EM 133B Rev 34.
- 4. On Cl SWP 95 Sht 4 Rev 10 flow element 3SWP* FE43B as shown on P&lD EMA338 Rev 34 (G 5) should be designated with a (*).
- 5. On Cl-SWP 23 Sht 6 Rev6 safety related valves 3SWP*V316,
- V209, *V317, 'V208, *V315, and 'V207 as shown on P&lD EM.
133B Rev 34 (F-5, F-6, F-7, E 5,E-6.E 7) should be designa'.ed witt a (*).
- 6. On Cl-SWP-23 Sht 5 Rev 7 safety related valves 3SWP*V70,
- V71, *V40, 'V41, *V67, 'V66,*V39, 'V38, *V35, *V34, 'V212,
'V221, *V211, *V220, 'V210, and *V219 as shown on PalD EM-133B Rev 34 should be designated with a (*).
- 7. On Cl SWP b8 Sht 4 Rev 6 safety related valve 3SWP'MOV130B (*V875) and restricting orifice 3SWP*RO133B as shown on P&lD EM-133B Rev 34 (G-2) should be designated with a (*).
- 8. On Cl-SWP-158 Sht 5 Rev 6 safeiy related valve 3SWP*V808 as shown on P&lD EM 133B Rev 34 (F 2) should be designated with a (*).
- 9. On Cl SWP-16 Sht 5 Rev 7 safety related valve 3SWP*V700 as shown on P&lD EM-133B Rev 34 (D-9) should be designated with a (*).
- 10. On Cl-SWP-24S Sht 5 Rev 9 safety related valves 3SWP*V65, *V66, *V68 *V69, *V33, *V34,*V36, and*V37 as chnwn nn Pain FM 1%%R Rnv MyQ.4 in TLM thnntet he
NS99 i
i DR No. DR-MP3-0160 l Northeast Utilities '4AVP l Ministone unk 3 Discrepancy Report designated with a (*).
- 11. On CI SWP 56 Shi 3 Rev 11 the drawing continuation line 3-SWP 004102 3 should bo 3-SWP 004-405-3.
- 12. On Cl SWP 149 Sht 3 Rev 7 safety related restricting onfice 3SWP*RO133A as shown on P&lD EM 133B Rev 34 (G 10) should be designated with a (*).
- 13. On Cl-SWP 97 Sht 4 Rev 9 safety related flow element 3SWP*FE43A as shown on P&lD EM-133B Rev 34 (F-6) should be designated with a (*).
Review Valid invalid Needed Date 9/1CNI initiator: Road, J. W. Q Q Q VT Lead: Neri, Anthony A G O O st23/97 O 8'2387 VT Mgt: schopfer, Don K G O 9/2497 IRC Chmn: singh, Anand K Q Q Q Date:
INVALlO:
Date: 2/20/98 RESOLUTION: Disposition; NU has concluded that Discrepancy Report, DR MP3-0260, has identified a condite not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 97 3351
& 3499 have been written to develop and truck resolution of this item per RP-4.
Conclusion:
NU has co aluded that Discrepancy Report, DR MP3-0260, has identified i .ondition not previously discovered by NU which requires correction. This cliscrepancy meets the criteria specified in NRC letter B16901 ano '*010. It has been screened per U3 PI-20 criteria and found to ha no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-97-3351
& 3499 have been written to develop and track resolution of this item per RP-4.
Previously identified by NU7 O Yes (9) No Non Discrepant Condition?O Yes @ No Resolution Pendmg?O ve. @ No Re.oiution unre.oiv.d70 ve. @ No Review initiator: Road. J. W.
VT Lead: Nort, Anthony A VT Mgr: schopfer, Don K IRC Chmn: singh, Anand K Date:
sL Comments:
Page 2 of 2 Printed 2r23/9e 10.22:37 AM 1
DR No. DR-MP3-0298 l Northe::t Utilities ICAVP Millstone Unit 3 Discrepancy Report Review Group: Conhguration DRREsOLUTION ACCEPTED Rev.ew Element: system Design Potential Operability lasue Digipenne: Piping Design O vn Discrepancy Type: Drawing (#3 No systemfrocess: sWP NRC signincance level: 4 Date faxed to NU:
Date Published: 10/10/97 Discrepancy: Upper Tier to Lower Tier Drawing Review for SWP in Control Bldg.
Ducription: The following drawing discrepancies were found in reviewing the P&lD with tne as built Isometrics:
- 1. On isometric Cl SWP P2A/B Sht i Rev 3 drain lines with valves 3SWP V984 and 3SWP-W85 are shown to be capped but not on P&lD EM 133D Rev 24 (M-3 and M 7). These valves are designated u safety related per the P&lD and ...ould be designated on the ;sometric drawing with a (*).
- 2. On Cl SWP 226 Cht 2 Rev 8 a 3 in, welded plug is shown on line3-SWP 006 ?62 3 and not on P&lD EM-133D Rev 24. The isometric also has a call out for continuation on drawing Cl SWP-368 for this plugged line that is no longer needed.
- 3. On isometric Cl SWP 30S Sht 5 Rev 9 safety related components 3SWP*TE35B and 3SWP*EJ10B per P&lD EM-133D Rev 24 (L 2) should be designated with a (*). Also continuation line 3-SWP 750-398-3 should be 3-SWP-750-410-3 per P&lD EM 133D Rev 24 (L 2).
- 4. On isometric Cl-SWP 31 A Sht 4 Rev 7 safety related components 3SWP*EJ10D and 3SWP*FIS36B per P&lD EM-133D Rev 24(K-2) should be designated with a (*).
- 5. On CB-839508 Sht 3 Rnv 10 line 3-SWP-002-416-3 should be 3-SWP 002 288-3 per P&lD EM 133D Rev 24 (K-5).
Review Valid invalid Needed Date Inittetor: Reed, J. W. O O O 8/23/97 VT Lead: Nort. Anthony A Q Q Q 9/23/97 0/1/S7 VT Mgt: Schopfer, Don K G O O 10'2/97 IRC Chmn: Singh, Anand K G O O Date:
INVALID:
Date: 2/17/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-029P, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 andM 17010. It has been screened per U3 PI-20 criteria and fornd to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-97 3709 has been written to develop and track resoletion of this item per Page 1 of 2 Prtnted 2/23/9610.23:12 AM
DR No. DR-MP3-0298 I N:rtheast Utilities ICAVP MinistDne Unit 3 Discrepancy Report RP4.
Conclusion:
NU has concluded that Discrepancy Report, DR-MP3-0298, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 andM 17010. It has been screened per U3 PI 20 criteria and found to have no operability or reportability concerns and meets the Unit 3 deferral criteria. CR M3-97-3709 has been written to develop and track resolution of this item per RP-4.
Previously identifbed by NU? O Yes (s)No NonDiscrepentCondition?Q Yes (#) No Resolution Pending?O ve. @ No newutionunresoevedrO vee @ No Review initiator: Road, J. W.
VT Leed: Nort, Anthony A VT Mgt; schopfer, Don K IRC chmn: s@, At snd K Date:
SL Conenents:
l Page 2 of 2 Printed 2/23/9810:23:15 AM
1 l DR ND. DR-MP3-0299
} Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Review Group: Contguraten DR RESOLUTION ACCEPTED Review Element: system instanaten p Discipline: Piping Desig" Diserepa.cy Type: Installaton trnplementaton Om 4~
System / Process: sWP NRC Significance level: 4 Date faxed to NU:
Date Published: 10/10"J7 Discrepancy: Walkdown Discrepancies for SWP in Control Building Descripuon: The following discrepancy items were found during the walkdown of the piping and mechanical equipment of the SWP in the Control Building:
- 1. Lines 3-SWP 006 32 3 and 3 SWP-006 35-3 are inside the 48 in, cover pipe but not insulated as required by spec. SP ME 691,
- 2. Line 3-SWP-006-398-3 is insulated but not required to be insulated por spec. SP-ME-691.
- 3. Expansion joint 3SWP*EJ100 has no NU component tag.
- 4. Line 3-SWP-002 314-3 is missing insulation as is required by spec. SP ME-691.
- 5. Lines 3-SWP-006-263-3 and 3-SWP-006-50-3 have insulation missing after the lines enter the 48 in, cover pipe. Insulation is required by spec. SP-ME-691.
- 6. Line 3-SWP 006-397 3 is insulated but not required to be insulated per spec SP-ME-691.
- 7. Valve 3SWP*TV35B (*V47) has incorrect sesial number per vendor drawing 12179-2472110.185 312 Rev D.Per GRITS, no DCNs are shown to be outstanding against the vendor drawing.
- 8. Line 3-SWP-002 315-3 is not insulated as required by spec SP-ME-691.
The followlPg material condition item was found during the walkdown of the piping and mechanical equipment of the SWP in the Control Building:
- 1. Pump 3SWP*P2A seal shows leakage.
Review Valid invalid Needed Date initiator: Read. J. W. O O O S' 5/S7 VT Lead: Nerl. Anthony A B O O 9/2s/97 VT Mgr: schopfer, Don K Q O O 10/1/97 IRC Chmn: singh, Anand K Q Q Q 10/2/97 Date:
INVAll0:
Date: 2117/98 RESOLUTION: Disposition:
Printe12/23/9610:23.43 AM Page 1 of 2
ICAVP DR Ns. DR-MP3 0299 I N:rthenst Utilities Millstone unit 3 Discrepancy Report NU has concluded that Discrepancy Report, DR MP3-0299, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-97 3778 and 3779 have been written to develop and track resolution of this item por RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR-MP3-0299, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B'6901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-97 3778 and 3779 have been written to develop and track resolution of this item per RP-4.
?:eviously identined by NU7 O Yes @ No Non Discrepant Conditkm?Q Yes @ No Resolution Panding70 vos CE - Re.oiuiion unr...ev.dro v.. @ No Review ceMaW NM AcceMable Needed Date initiator: Road. J. W. 2m VT Leed: Neri, Anthony A O O O G O O zu VT Mgr: schopfer, Don K IRC Chmn: singh, Anand K O O 221/98 Data:
SL Comments:
Printed 2/236s01o23 47 AM Page 2 of 2
DR No. DR-MP3 0304 Northeast utilities ICAVP MillstDne Unit 3 Discrepancy Reix>rt Review Oroup: System DR RESOLUTION ACCEPTED N'*
- 6M'* Potonnel Operability issue D6scip66ne: Mechanical Design O ve.
D6screpancy Type: Component Date @ No System / Process: RSs NRC significance level: 4 Date faxed to NU:
Date Published: 11/2/97
+
Discrepency: Containment recirculation pump design pH is inconsistent with FSAR Section 6.5.2.1..
Descripuon: FSAR Section 0.5.2.1 identifies the containment recirculation fluid to have a pH of 7.0 to 10.5. However, the containment recirculation pump oesign specification 2214.802-044 through Revision i shows the pump to be designed for a pumped fluid pH range of 5.0 to 7.5.
d According to specification 221,.802 044, the quench spray pump wetted parts are made of Type 304 stainless steel. These materials are suitable for the design pH range of 7.0 to 10.5.
Review venid invahd Needed Date O 10/'3S7 initiator: Feingold, D. J. O O 1o/1697 VT Leed: Neri, Anthony A @ ] ]
1o"2097 VT Mgt: Schopfer, Don K @ Q O IRC Chmn: Singh. Anand K G O O 10~30S7 Dete:
INVALID:
Date: 2/20/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0304, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI 20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria CR M3-97-3983 has been written to uevelop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0304, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-97-3983 has been written to develop and track resolution of this item per RP-4.
Previously identined by NU7 O Yes @) No NonDiscrepentCondition?O Yes @ No Resolution Pending?O ve. @ No Resoiutionunre.oived?O ve. @ No Review Page 1 of 2 Printed 2/23/9e 1o-24:14 AM
~~ - -----_ ____
DR No. DR-MP3-0304 l N:rthe:st Utilities ICAVP l Miliatone Unit 3 Discrepancy Report _
initiator: Feingold, D. J.
O N 17 Lead: Nerl, Antnony A O O VT Mgt: Schopfer. Don K IRC Chmn: $4ngh, Anand K oate: 2/20/98 sL conents: The intended corrective action is apparent from condition report CR M3-97 0383. According to the coiidition report, A DCN will be written against the pump specification to correct the discrepancy, Page 2 of 2 l Prtnted 2/23/9910.24.18 AM
~~ -
DR Ns. DR-MP3-0317 N:rthea:t Utilities ICAVP f
Millstone Unit 3 Discrepancy Report _
Review Group: splom DR REsOLu tt ACCEr"ED rem EW: sptem W Potes 1 Operability Isrue Discipline: Mechanical Design ;g Discrepancy Type: Componert Data * - No SystenVProcess: HVX NRC Signincance level: 4 Date faxed to NU:
Date Published: 10/2397 Discrepancy: Emergency Generator Enclosure Supply Fan Performance
Description:
During the review of component data for the Emergency Generator Enclosure Ventilation System supply fans 3HVP*FN1 AltB/1C/1D discrepancies regarding the fan model number, motor nameplate rating, and fan total pressure rating were identified.
FSAR Section 9.4.6.2 states that each emergency generator enclosure supply fan provides 60,000 cfm of supply air.
Specification 2170.430-140 indicate that the fans are Buffalo Forge model number 48B5 rated at 60,000 cfm and 2.95 ive total pressure. The f an horsepower requirements at the rating point is 37.2 hp. The fan motor data sheet contains conflicting information on the nameplate rating of the motor Under horsepower by fan mfg; it states 60 hp, while in the column that contains performance data for the motor it Indicates that the motor has a 40 hp rating.
The Plant Design Data System (PDDS) database indicates that the f an brake horsepower required is 38.5 hp and that the motor has a 40 hp nameplate rating.
The vendor drawing for the fan,2170.430-140-100, states that the fan is a Buffalo Forge model number 48B9 rated at 60,000 cfm and 2.5 iwg total pressure with a 60 hp motor.
The fan performance curve dated 6/21/82 for the fan states that the fan is a Buffalo Forge mode! number 48B5 rated at 60,000 cfm and 2.95 iwg total pressure.
Review Valid inval6d Needed Dats initiator: stout, M. D. Q Q Q 10/ % 7 So/SS7 VT Leed: Neri, Anthony A Q O O So/13S7 VT Mgr: schopfer, Don K O O O
'o'18/S7 IRC chmn: singh, Anand K G O O Date:
INVAL!O:
Date: 2/17/98 RESOLUTION: NU has concluded that Discrepancy Report, DR MP3-0317, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral critera, CR M3-97-3880 Page 1 of 2 Printed 2/239610:24 49 AM l
DR N2. DR-MP3-0317 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report has been written to develop and track resolution of this item per RP4, Attachments:
CR M3-97 3880 Non Diecrepent Condition?() vee (e'> No Previously identmed by NU7 (.) vee I No Resolution Pendmg?O vee tv No Renoivi6onuareeoived70 vee @ No Review init6etor: stout, M. D.
VT Leed: Neri, Anthony A VT Mgr: schopfer, Don K IRC Chmn: singh, Anand K Date: 2/17/98 st Conenente: CR M3 98-3880 wes added to the Config Management bin, The motor data sheet in specification 2170.430140 also needs to be revised as part of the corrective action for CR M3-97 3880, 4
i Pope 2 of 2 PrWed 2/23961tr.24.53 AM
DR N3. DR MP3-0320 N:rtheast Utilities ICAVP Millstone Unit 3 Discrepaticy Report Review Group: Confguraton DR RESOLUTION ACCEPTED Rev6ew Element: System instanation PoteMiel Opwebimy Issue Discipline: Pipino De8490 C Yes Discrepancy Type: Instenation implementaten @ No System / Process: SWP NRC Significance level: 4 Date faxed to NU:
Date Published: 1o/1&97 Discrepancy: Walkdown Discrepancy for Service Water Supply to Water Treatment at the Pumphouse
' Ducript6on: T ne following discrepancy item was found during the walkdown of the piping and mechanical equipment of the SWP scope items in the pumphouse:
- 1. Line 3 WTC-003-42 3 which includes the isolation valves to the SWP was included in the SWP walkdown scope up to the isolation valves, This line requires insulation per spec SP ME-691 but was verified to not have insulation.
Review Valid invalid Needed Date initiator: Road, J. W. O O O n/27/97 VT Lead: Nort, Anthony A B D 0 1o/2/97 O O 10/1 F VT Mer: schopfe, Don K O 10/1'S7 IRc Chmn: singh, Anand K O O G Date:
INVALID:
Date: 2/17/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR-MP3-0320, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-97 3679 has been written to develop and track resolution of this iterii per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR-MP3-0320, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and fosmd 'a have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-97 3679 has been written to develop and track resolution of this item fer RP-4.
Previously identifled by NU7 Q Yes @ No Non Discrepent Condition?O yes (8) No Resolution Pending7O v @ No R.soiuiion unr. eved70 vee @ No Review Acceptable Not Acceptable Needed Date initiator: Reed, J. W.
VT Lead: Nort, Anthony A O O 2'2o/9e O 2':'oS8 VT Mgr: schopfer, Don K g c;..... L vh,An W K e n O 2/21/9e Page 1 of 2 p ,
)
DR Ns. DR4AP3-0320 Northea:t Utilities ICAVP Millstone Unit 3 Discrepancy Report . _ . _
4 im, o. . . .. -vi. ^"* "
O D D o .:
SL Commerds:
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4 Page 2 of 2 Printed 2/23/9610:25 58 AM i
DR No. DR-MP3-0337 Northeast Utilitloo ICAVP Millstone Unit 3 Discrepancy Report Review Group: system DR REs0LUTION ACCEPTED W'* Potential Operability issue Discipline: Mechanica! Design Ow Discrepency Type: Calculation gg SystemProcess: Rss NRC Significance level: 4 Date faxed to NU:
Date Published: 10r23/97 Discrepancy: Calculation P(R)-1020 D!screpancies De6cription: Calculation P(R) 1020, Rev. O," Verification that RSS Pumps have Sufficient Head to Provide Containment Sump Water to SSP System for Sampling." The calculation uses the pump head and the piping friction losses to estimate the flow rate to i
the sampling system during Recirculation Mode. The flow rate l
through the sample system is required to be between 0.3 and 1.0 i gpm. The calculation concluded the flow rate should be approximately 0.75 gPm.
j The length of pipe from the pump to the cooler included only the '
vertical piping and the fittings. The horizontal piping is approximately 50% of the length of the vertical piping. This results in an additional 1 psi pressure drop and decrease the flow rate.
The length of pipe from the cooler to the 8" x 10" reducer j
included only the horizontal piping and the one tee. The vertical piping is approximately 100% of the length of the vertical piping and there is another tee. This doubles the resulting head loss and decreases the flow rate. i The dP coefficier.t (0.000216) was incorrectly transposed f j
(0.00216). The result reflects the correct coefficient was used in )
the calculation.
The length of 8" pipe is given as 103.75 feet. A review of the I references indicates only about 72 feet of pipe. This decreases i the head loss and increases the flow rate. l The sample lines are tubing. Tha ielative roughness for tubing is j
.00013 resulting in a friction factor of 0.028 which is less than O.037 used for the same size pipe. This decreases the head loss and increases the flow rate.
The dP from Point D to E is incorrect. The value of 0.18 psi was included in the equation as 0.018. This value was carried throughout the calculation; however, because of its size compared to the overall pressure drop (174.1 psi), it has no impact on the results.
The equation to calculate the angle for a reducer is incorrect.
The angle is based on half the diameter iifference and the length of the reducer. The equation uses half the length of the reducer. This overestimates the head loss and increases the flow rate.
3g y The 50cd !ccc for the 10" x46*-reducerc i:cc the ince regg
ICAVP DR No. DR-MP3-0337 Northeast Utilities Millstone Unit 3 Discrepancy Report for K. The numbers were not transposed correctly; however, the results reflect the correct number.
The approach indicates that the losses will be calculated across Train D. Trains A, B and C have 16' X 10' Reducers at the outlet of the Coolers. Train D has a 16' X 10' reducing flange.
This is better approximated by a sudden contraction. This does not impact the overall results of the calculation.
The dimensions for the sample lines could not be confirmed.
The referenced drawings did not have all the dimensions nor were the drawings legible. Any gross overestimation of the tubing length will be offset by the conservatisrn used by assuming a higher friction factor.
The calculation states, "No pressure drop is associated with elevation since the water being pumped starts from and retums to the same place." However, the calculation starts at the pump discharge and ends at the end of the sample line. The sample line drains into the sump. Since the dimensions and elevations for the sampic lines could not be verified, the elevation loss cannot be determined.
Overall, the comments associated with this calculation do not appear to affect the conclusions of the calculation.
Review Valid invalid Needed Date Initiator: Langel. D. O O O 10/1SS7 VT Leod: Nert, Anthony A B O O 10/15S7 10/15'87 VT Mgr; schopfer. Don K O O O IRC Chmn: Singh. Anand K O O o8S7 G
Date:
INVALID:
Date: 2/17/98 RESOLUTION: Disposition; NU has concluded that Discrepancy Report, DR-MP3-0337, has identified a cond; tion not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI 20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-97 4369 has been written to develop and track resolution of this item per RP 4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0337, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16301 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-97 4369
~
Printed 2/239810:26A0 AM Page 2 of 3
ICAVP DR No. DR-MP3-0337 Northea:t Utilities Millstone Unit 3 Discrepancy Report has been written to develop and track resolution of this item per RP-4, Previously identified by NU7 () Yes (n) No Non Discrepent Condet6onK) Yes fy) No Resolution Pend 6ng70 Yes @ No no.oiuiion unt.ooiv.dro Yes @ No Revkw ACC*Plable Not Acceptable Needed Date inh: WA VT Lead: Nort, Anthony A VT Mgr: Schopfer, Don K iP.C Chmn: Sltsh, Anand K
! Dele: 2/17/98 SL Conants: CR M3 97 4369 recommends revising or canceling the Calculatimi 33 appropdate.
l Printed 2/234610:26:51 AM Page 3 of 3
ICAVP L.8t No. DR-MP3-0347 NErtheast Utilities Millstone Unit 3 Discrepancy Report Review Group: System DR RESOLUTION ACCEPTED
'" 8Y '* Potential Operability Iscue Discipl6ne: Structural Design Om Discrepancy Type: Calculaton g g, SysterrWProcess: SWP NRC significance level: 4 Date faxed to NU:
Date Published: to/1&S7 Discrepancy: Pipe support calculation NP(F) Z79D-454 discrepancy
- Descrtpuon
- We have reviewed the Pipe Support Calculation 12179-NP(F).
Z79D-454, Rev.3, CCN #1 and note the following discrepancies.
- 1. On page 28, the Fx lor.d component for load cases OBEl and SSEl is not based on t. latet,t load from Pipe Support Summary (page 24). The latest loads are, Fx=1877# (not Fx=1287#) for OBEl and Fx=2105# (not Fx=1863#) for SSEl.
- 2. On page 48, moment MYL should be 3555 In-# (not 6185 in-#)
and moment MZL should be 29584 in-# (not 26928 in-#). This will change the member stresses.
- 3. On page 49, moment Mc should be 3555 in-# (not 6185 in-#)
and moment ML should t:e 29584 in-# (not 11886 in-#). This will change the weld size Ratio to 1.46.
' Review Valid invalid Needed Date O 10/3S7 initiator: Patel, A. O O VT Lead: Neri, Anthony A Q O O io/7S7 VT Mgr: Schopfer, Don K O O O 10'isS7 O O 10/1'S7 IRC Chmn: Singh. Anand K O D.t.:
INVALlo:
Date: 2/18/g8 RESOLUTION: NU nas concluded that Discrepancy Report, DR MP3-0347, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 It has been screened per U3 Pl-20 critena and found to have no operability or reportability concems and meets the Unit 3 deferral criieria. CR M3-97-3973 has been written to develop and track resolution of this item per RP-4.
Previously identifled by NU7 O Yes @ No Non Discrepant Condition?Q Yes @ No Resolution Pending?O ve. @ No Re.oimion uareeoived70 ve. @ No Review Acceptable Not Acceptable Needed Date gg.g p VT Lead: Nort, Anthor'y A VT Mgr: Schopfer, Don K IRC Chmn: Singh, Anand K Dete: 2/18/98 st comments: NU resolution is acceptable per review of CR M3-97 3973.
1-nnted 2/23S61o'.27:27 AM Page 1 of 1
DR No. DR-MP3-0396 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Review Group: System DR RESOLtJTION ACCEPTED IN'* " Potential Opereldlety lasue Discipline: Mechanical Design Ow Discrepency Type: CeleutetLet gg SysterrvProcess: SWP NRC Significence level: 4 Date faxed to NU:
Date Published: 11/1W97 DisCf*Pency: Calc. 90-0691116-M3 rev. O through CCN 02 contains several unaddressed issues.
Ducription: Calculation 90-069-1116-M3 rev. O through CCN 02 determines the Service Water System (SWP) minimum available cooling water flow rates under design basis accident scenarios. This calculation uses the Westinghouse PEGISYS SWP model. The following discrepancies were noted in this calculation:
- 1. A nodal diagram is needed to verify the inputs and outputs of the PEGISYS model. However, there is no nodal diagram included in the calculation. Thus the PEGISYS outputs (results) can not be correlated to SWP system components.
- 2. CCN 02 dated 5/27/97, states on the enver sheet that calculations NM-061 SWP, HYD H9, HYD-H10 and 12179-2330.110 are superseded by this calculation. On page 2 of this CCN, calculations P(T)-1005, P(T)-1092,3-ENG-164 and NM-021 SWP were hand written in following the above calculations.
- Pages 3-5 of this CCN does not included these four additional calculations as being superseded. It is unclear whether or not these additional calculations are superseded by CCN 02.
- 3. CCN 01 dated 3/31/97, stetes at the bottom of page 2 that this calculation is SUPPLEMENTED by calc. 90-0691097-M3, rav. O through CCN 02 which contains the latest service water PEGISYS model. Calc.1097 was not one of the references that were added by this CCN. It is not documented what affect this latest model will have on the results of this calculation. The model should have been re-run to verify that the system changes incorporated by calculation 1097 were included and the resultant minimum flows did not change adversely as a result of the model revisions.
- 4. Pages 47 and 48, state that the surveillance limits for the CCP heat exchanger and the HVQ ventilation units were reduced from 19 to 15 psid and from 6 to 4.5 psid respectively. There is no justification stated or documents referenced to quantify how these ney; limits were derived. The surveillance curves in procedure SP 3626.13 reflect these values, however, the calculations that develop the surveillance curves (cales. 90-069-778GM and 90-069-776GM for CCP and HVQ respectively) still maintain the original surveillance limits. Calculations -778GM and 776GM were not superseded by CCN 02.
- 5. Page 49 and 50 contain the table that summarizes the results of the PEGISYS runs. There is no conclusion stated that validates or invalidates the values listed. The margin in some t nene le nanntlug ~
nnri thle le nnt nridracewt (f't'N 81 inwSIS.t,he_
Printed 2/23/9610:2e:48AM Page 1 of 3
1 ICAVP DR N2. DR MP3 0396 Northeast Utilities Millstone Unit 3 Discrepancy Report minimum required flow for the equipment that previously )
4 reflected negative margin.) A statement should be made to !
address the results from the model runs,
- 6. The PEGISYS output for all the cases evaluated is included in this calculation. There were several cases in which the output stated that the pump flow rates exceed run-out. This occurred for the cases titled: case (page 78), case 5cep (page 280) and c5cepa (page 406). This was not addressed in the body of the calculation for acceptability of the model results. This could impact the results of this calculation and any other document that references these results.
The overall affect of the discrepancies noted for calculation 90-069-1116-M3 rev. O through CCN 02 can not be determined without revising the calculation.
Review Valed invalid Needed Date initinfor Dionne, B. J. O O O 15' -
VT Leed: Nori, Anthony A O O O 'in/87 O O 1'n/87 VT Mgr: schopfer, Don K O O O 1'n/S7 IRC Chmn: sangh, Anand K O oei.:
WVALID:
Dese: 2/20/98 REsoLUThoN: Dl$positjon:
NU has concluded that the issue reported in Discrepancy Report, DR MP3-0396, has identified a condition not previously discovered by NU which requires correction. The corrective actions necessary to resolve the issues detailed in DR MP3 0396 will be implemented and tracked under the auspices of Condition Report M3-97-4774, The approved corrective action plan for Condition Report M3 97 4774 will correct this issue by determining if calculation 90-069-1116-M3 rev. O through CCN 02 is superseded by the current SWP flow model (Proto Power Calculati in 96-001) or if active to update consistent with the discrepancies of this DR. These corrective actions will be performed post startup.Proto Power Calculation 96-001 was transmitted to S&t. by IRF-00401, TRA-00118. NU has determined that this discrepancy does not impact the drsign ur licensing basis of MP3, The calculation in question,00-069-1116-M3, was assessed undar the PI 31 program and CCN 01 was issued Page 1 of CCN 01 presents the summary of results and states in01 this information is also presented in calculation 90-069-1065-M3, Calculation 1065 has been verified by the current SWP flow model 96-001. NU has concluded that this discrepancy is a Significance Level 4
Conclusion:
NU has concluded that the issue reported in Discrepancy Report, DR-MP3-0396 has ident!fied a condition not previously Prtnted 2/23/9610:28.52 AM Page 2 of 3
l I
DRF DR-MP3-0396 l Northeast Utilitiea ICAVP I Millstone Unit 3 Discrepancy Report discovered by NU which requires correction. The approved corrective action plan in CR M3 97-4774 will determine if calculation 90-069-1116 M3 should be superseded by the current SWP flow model(Proto Power Calculation 96-001). As Proto Power Calculation 96-001 is the current SWP flow model there is no impact on the design or licenslag basis. NU has concluded that this discrepancy is a Significance Level 4.
Previously identifled by NU? O Yes (9) No NonD6screpentCondition?O Yes (#') No ResolutionPendingtO vos @ No Renoiutionunresoev.drO Yee @ No Review Ir itiator: Dranne. 8. J.
VT Lead: Neri, Anthony A VT Mgr: schopfer, Don K 1RC Chmn: singh. Anand K
~
Date: 2/20/98 sL commente: The significance level of this discrepancy has been reduced to level 4 from level 3 based on the current SW hydraulic model (Proto Flo Calc 96-001) having been compared with test data and shown to be adequate. This calculation should not impact the design or licensing basis.
Printed 2/23/961028:53 AM Page 3 of 3
ICAVP DR N:. DR-MP3 0397 Northeast Utilities Millstone Unit 3 Discrepaticy Report Review Group: System DR RESOLUTION ACCEPTED Potential Operability issue Discipline: Mechanical Design Discrepency Type: calculation Om
(#) No SystemProcess: SWP NRC Signifk *vs level: 4 Date faxed to NU:
Date Published: 11/20/97 Discrepency: Calculation 95-ENG 1177-M3 rev. O, CCN 1, has several unjustified values.
Description:
Reviaw of calculation 95-ENG 1177 M3 Rev. O through CCN 01 identhied the following discrepancies:
1.) The calculation uses design inputs which are documented inclusively in calculation 90-0691130-M3. However, Design input #6 of the calculation (95-ENG-1177) references a portion of calculation 90-069-1130 M3 which has been superseded by calculation 95-ENG 1177 M3. Therefore, no valid reference for design input #6 is documented in the calculation.
2.) Design input #12 is based on Reference 6. However, the number of passes in the heat exchanger is not contained in Reference 6.
3.) Assumption 1 of the calculation,"no subcooling in the condensor", contradicts the 8 'F of subcooling assumed by the vendor suppling the heat exchanger data as documented in Reference 6, Attachment 1, item 7.
4.) No reference orjustification for the Correction Factor, F=1.0 for the heat exchanger is documented in the calculation.
These discrepancies are not expected to have a significant effect on the calculational conclusions.
Review Val 6d invalid Needed Date initbior: Dionne. B. J. O O O 11'1SS7 V7 Leed: Nort, Anthony A O O O 1 t'13'S7 O O $ 1'1'S7
'/T Mgr: Schopfer, Don K G IRC Chmn: Singh, Anand K O O O 15'17/S7 Date:
INVALID:
Date: 2/20/98 RESOLUTION: Disposition:
NU has concluded that the issue reported in Discrepancy Report, DR-MP3-0397, has identified a condition previously discovered by NU for another issue which resulted in superseding calculation 95-ENG-1177-M3. CR M3-97-1667 was issued because the calculation evaluating Control Building Water Chiller Condenser (3HVK*CHL1 A/B) performance contained incorrect
- assumptions. The corrective action resulted in a new calculation (Proto Power 97-123) which now supersedes 95-ENG-1177-M3.
Printed 2/23/9810:50:53 AM Page 1 of 2
DR N . DRMP3-0397 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report
Conclusion:
NU has concluded that the issue reported in Discrepancy Report, DR MP3-0397 has identified a condition previously discovered by NU which required correction. Issues raised in CR M3 97-1667 resulted in an approved corrective action plan which has superseded 95-ENG 1177 M3 with Proto Power 97123, R lon Po ? Yes ( No ?O Yo ( No Review Instletor: Denne, B. J.
VT Lead: Neri, Anthony A VT ugr: Schopfer, Don K IRC chmn: Singh, Anand K Date: 2/20/98 SL Comments:
4 Printed 2/239810:5o:57 AM Page 2 of 2 s
DR N2. DR-MP3 0404 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Review Orcup: system DR RESOLUTION ACCEPTED Review Element: system Doogn PotenM OpereWiny issue Diecipl6ne: Mechanical Design O vee Discrepancy Type: Calculeton g go System / Process: SWP NRc Significance level: 4 Date faxed to NU:
Date PuM6shed: 10/2397 D6screpancy: Calculation 714P(T) does not completely evaluate the design pressure of the Service Water System, Descr6puon: Calculation 714P(T) rev, O through CCN 02, " Service Water System Design Pressure", does not calculate or reference all of the design pressures of the piping in the SWS as the title and purpose dictate, The calculation dcas not address the portions of the SWS that have a design pressure of 145 psig or 97 psig, No other calculations could be found to justify the 145 psig and DR MP3-0398 should be referenced regarding the 97 psig, CON 02 for this calculation is locomplete. The description of change & technincal justification section (section 6) is left with an incomplete statement (partially complete sentence) to justify the change noted. Also, reference 3 of this CCN does not contain a valid calculation number as stated, Review Valid invalid Needed Date initiator: Denne, B. J- 0 0 0 1oS'S7 VT Lead: Neri, Anthony A O O O 10/10/S7 O 10/1'S7 VT Mgr: schopfer, Don K O O 1RC Chmn: srgh, Anand K O O O 10/18/S7 Date:
INVAllo:
Date: 2/20/98 RESOLUTION: Disposition-NU has concluded that the issue reported in Discrepancy Report, DR MP3-0404, does not represent a discrepant condition.
Prior to start up design pressures and temperatures for systems were stated on the system flow diagrams (FSKs) and listed in the line designation table (LDT), Design pressures and temperatures, along with their reference, are also stated in the stress data package (SDP), The FSKs have since been retired but the values remain in the LDT and SDPs. The SDPs have been reconciled with system calculations under the 50.54(f) effort. FSK 9-10J (retired) inoicates a design pressure of 145 psig for the lines on the discharge side on 3SWP*P3A&B. SDP-SWP 01370M3," Service Water Stress Data Package" page 29 of 71 states that " isolated sections of piping in the service water cubicles, control bul! ding, and ESF building have a design pressure of 97 psig for hydro test reasons. Lines downstream of
- he MCC and rod control area booster pumps have a design pressure of 145 psig, Calc P(T)-974," Maximum Sustained Pressure of Service Water System"is referenced for the 97 psig Page 1 of 2 Printed 2/23/9810:s1:23 AM 2
1
DR No. DR MP3-0404 Northeact Utilities ICAVP Millstone Unit 3 Discrepancy Report design pressure and P(T)-1125 " Maximum Discharge Pressure of 3SWP*P3"is referenced for the 145 psig pressure As such, s the calculations for the pressures do exist and can be located through reference from the SDP.
CCN 02 to calculation 714P(T) contains two ' typos
- as discovered by S&L. Block 4 of the CCN form states SWEC calculation but does not list a number. The attached Calculation Tracking Program (CTP) data sheet lists all the reference calculations. This page is considered part of the CCN and is used to maintain the QA CTP database. Block 6," Description of Change and Technical Justification" does contain an unfinished sentence, however a review of the previous block indicates a clear technical Justification. Because all of the information has been provided on the CCN form, these " typos
- do not compromise the results of the CCN. CCN 04 was issued to correct these items.
Significance Level criteria do not apply here as this is not a discrepant condition.
Conclusion:
NU has concluded that the issue reported in Discrepancy Report, DR MP3-0404, does not represcr.t e discrepant condition.
Calculations P(T)-974 and P(T)-1125 support 97 psig and 145 psig respectively. These pressures are also provided in stress data package SDP-SWP 01370M3. CCN 02 to calculation 714P(T) provides the calculation reference on page 2.
Significance Level criteria do not apply here as this is not a discrepant condition.
Previously identitled by NU? O Yes @ No Non D6screpent Condetion?O vos @ No ResolutionPend6ng?O vos @ No Resoiution unresoived?O vos @ No Review initiator: Dionne. B. J.
VT Lead: Neri, Anthony A VT Mgr: Schopfer, Don K 1RC Chmn: Singh, Anand K Date: 2/20/98 sL commente:
Printed 2/23rS610:51:27 AM Page 2 of 2
l DR N;. DR-MP3 0419 Northeast Utilities ICAVP ;
Millstone Unit 3 D;screpancy Report l Review Group: system DR RESOLUTION ACCEPTED
'" II ** Potential Operabiety issue Discipl6ne: Mechanical Design Om Discrepancy Type: Calculation g system / Process: SWP NRc $69nif6cance level: 4 Date faxed to NU:
Date Published: 11/1197 D6*cr*P*acy: The wrong methodology was used for the orifice bore calculations.
D**ctlPt60n: The methodology for flow metering devices was used instead of the that for restricting orifices in Calculations NE-024 SWP, rey, 0 and NE-025-SWP, rev. O which applies to 3SWP*RO122A, B and 3SWP*RO125A, B, C and D respectively. These orifices are located on the Containment Recirculation Coolers Service Water outlet header (3SWP*RO122A & B) and on the Containment Recirculation Coolers Service Water outlet lines (3SWP*RO125A, B, C & D).
Also the calculations did not include references for the design inputs used to determine the bore diameters, therefore, the bases for these inputs could not be validated. These errors could Impact the calculational results.
Review Valid invalid Needed Date O 10'3 /S7 initiator: Deonne, B. J.
O O VT Lead: Neri, Anthony A y O O 1G'31/97 O '1/5/S7 VT Mgr: schopfer, Don K G O IRc Chmn: singh, Anand K B O O 11/7/S7 Deie:
INVALID:
Date: 2/20/98 RESOLUTION: Disposition:
NU has concluded that the issue reported in Discrepancy Report, DR-MP3-0419, has identified a condition not previously aiscovered by NU which requires correction.The approved corrective action plan for Condition Report M3-97-4774 will correct this issue by determining if calculations NE 024-SWP and NE-025-SWP need to be superseded by the current SWP flow model (Proto Power Calculation 96-001) or if active to update them consistent with the discrepancies identified in this DR. These corrective actions will be performed post startup.
Proto Power Calculation 96-001 was transmitted to S&L by IRF-00401, TRA-00118.
NU has determined that this discrepancy does not impact the design or licensing bcsis of MP3, These calculations are historical in that they were used to size the restrictive orifices.
The resulting flowrates for system limiting conditions have been verified to be acceptable. The calculations in question, NE-024-SWP and NE-025-SWP were assessed under the PI-31 program and determined to be satisfactory, Proto Power Calculation 96-Printed 2f219610:51:s3 AM Page 1 of 2
DR No. DR-MP3-0419 Northeast Utilities ICAVP Milistone Unit 3 Discrepancy Report 001 is the current SWP flow model. Therefore, NU has concluded that this discrepancy is a Significance Level 4
Conclusion:
NU has concluded that the issue reported in Discrepancy Report, DR-MP3-0419 has identified a condition not previously discovered by NU which requires correction. The approved corrective action plan in CR M3-97 4774 will be completed post startup to determine if calculations NE 024 SWP and NE 025-SWP should be superseded by the current SWP flow model (Proto Power Calculation 96-001). As Proto Power Calculation 96-001 is the current SWP flow model there is no impact on the design or licensing basis. NU has concluded that this discrepancy is a Significance Level 4.
Previously idenuaed by NU? O vos @) No Non D6screpent Condellon?O ves (*) No J
Resolution Pending?O ve. @ No ReeduuonUnreedveJ70 ve. @ No Review Intuator: Ocnne, B. J.
VT Lead: Nort, Anthony A VT r r:
e schopfer, Don K lac ctwnn: singh, Anand K Dete: 2/20/98 sL conwnents: This calculation was reduced to significance level 4 based on the model being benchmarked to test data.
Printed YA9e 10:51:57 AM Fage 2 of 2
l 1
i DR No. DR-MP3 0420 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Repoft Review Oroup: System DR RESOLUTION ACCEPTED Rev6ew Elemort Operatin0 Procedure D6ecipl6ne: Muhanical Deo*" O vee 4 Discrepancy Vype: calculaten @ No System / Process: SWP ,
NRC Siwnificance level: 4 p,q, F Ax,4 go Ng; Date Publishe(.- 1/2590 Diecrepency: Incorrect values were used in determining the degraded pump' curves for SWS pumps.
Descr6puon: Calculation NM-022 SWP rey, O determines the minimum acceptable SW pump curve for ASME XI degredation acceptance. This calculation was reviewed and several discrepencies were found as follows:
Page 5: The calculated minimum required flow includes a
- measured flow rate to SW Pump lube water which was removed from service. Although a calculation change notice should have been written, this flow is small (3.4 gpr,1) and can be considered negilgible. The 3 SSP *SCL3 (sample pass cooler) flow rate has been updated per calculation 90-0691065M3 and should be changed in this calculation.
Page 9: The SWS Pump 'TDH' was calculated for flows of 6000 and 3600 gpm using an incorrect factor in the equation. A curve fit coefficient of 183.1 was used in place of 182.9 for the determination of both of these values. The correct value was used in calculating the TDH for 10,000 gpm. This error does not affect the calculated results.
Review Valid invelid Needed Date 1' 5'S8 initiator: Dionne, B. J. O O O 1/169e VT Leed: Ned, Anthony A @ ] ] /10/S8 VT Mgt: Schopfer, Don K O O O O t/2irse IRc Chmn: Singh. Anand K 8 O Date:
INVALID:
D*: 2/20/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR-MP3-0420, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 it has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 98-0653 has been written to develop and track resolution of this item per RP-4,
Conclusion:
NU has concluded that Discrepancy Report, DR-MP3-0420, has identified a condition riot previously discovered by NU which Page1 of 2 Pnnted 2/23/9e 10:s3.05 AM
DR N DR MP3 0420 Northeast Utilities ICAVP Millstone tinit 3 Discrepancy Report requires correction This discrepancy meets the criteria specified in NRC letter B16901 and,17010 It has been screened per U3 PI-20 crtierta and found to have no operability or reportability concems and meets Ine Unit 3 deferral criteria, CR M3-96-0653 has been written to develop and track resolution of this item per RP 4.
Previously iderdif6ed by NU7 O vos @ No NonD6screpentCondM6on?O vos (!') No ResolutionPending70 vee (f)No Resouionunre.aved70 ve. @ No Review initiator: Denne, B. J.
VT Leed: Nort, Arttony A VT Mgt: Schopfer, Don K IRC chmn: Singh, Anand K Date: 2/20/98 SL Corrynords:
f Page 2 of 2 Printed 2/23/96 lo.s3M AM
DR N3. DR-MP3 0421 Northeast Utilities ICAVP Millstone Unh 3 Discrepancy Report Review Oroup: system DR RESOLUTION AC.:EPTED Rev6ew Element: System Des $n Potential Operatdisty issue Discipl6ne: Mechancal Des $n O ve.
D6screpancy Type: Calculaton (e) No systerWProcess: $WP NRC s'.gnificance level; 4 Date Faxed to NU:
Date Published: 11/2/97
~ ~~ Discrepency: Incorrect fluid properties were used/ interpolated in various calculations.
Description:
Several calculations that were reviewed wt,te found to be using incorrect fluid properties. These discrepancies are as follows:
Calculation 94 ENG 1036-M3 rev. O, Page 19: The density for water @ 95'F is 62.05 lbm/cu. ft. not 62.2 as stated. Pages 22, 23,32 and 33: The dynamic viscosity determined for both shell and tube side parameters varied from the given reference for the temperatures notod. The tube side peperties for sea water were not consistent with the reference for the given temperatures.
Also the density determined on pages 32 and 33 for the shell sidc were incorrect for the given temperatures.
Calculation 94 ENG 1037 M3 rev. O, Page 14: The density used for water @ 130*F is not correct from the noted roferences in the calculation. Page 16: The dynamic viscosities noted for the shell l and tube side parameters do nM coincide with values interpolated from the reference
- Calculation 94 ENG 1038 M3 rev. O, Page 14: The density used for water @ 130'F is not correct from the noted references in the calculation. Page 16: The dynamic viscosities noted for the shell and tube s6ae parameters do not coincide with values
'nterpolated from the references.
Cai s aion 91 BOP 783-ES rev. 2, Page 3: The tube side fluid properties do not coincide with those interpolated froin the references.
Calculation 91 BOP 789-ES rev. 2, Pages 19 and 20: The tube and shell side fluid properties d J not coincide with those interpolated from the references at the given temperatures.
Review Val 6d invalld Needed Datt Q 10/1497 initiator: Dionne, B. J. Q Q VT Lead: Nort. Anthony A Q Q Q 1G'1497 VT Mgr: Schopfer, Don K O O O 1o?nS7 IRC Chmn: Singh, Anand K O O O 1S'33S7 Date:
INVALID:
Date: 2/20/98 RE SOL'8'lON: Oisposit!Dn:
NU has concluded that Discrepancy Report, DR MP3-0421, has Pnnlad 2/219815.s3 32 Au P o. i oTr
' DR No. DR MP3 0421 Northeast Utilities ICAVP Ministone UnM 3 Discrepancy Report ,
identified a condition r<>t previously discovered by NU which requires corredion. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 Pl.
20 criteria and fcund to have no operability or repor* ability concems and meets the Unit 3 deferral criteria. CR M3-98-0138 has been written to develop and track resolution of this it3m per RP 4.
Conclusio't:
NU has concluded that Discrepancy Report, DR MP3-0421, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets tile criteria specified in NRC letter B16901 and 17010. It has been screened ger U3 PI-20 criteria and found to have no operability or reportsbility concems and meets the Unit 3 deferral criteria. CR M3-98-0138 has been written to develop snd track resolution of this item per RP4.
Prev 60uely identmed try NU7 Q Yee @ No NonDiecrepentCondellon?O Yee @ No Resolut6onPerdng?O ves @ No ReeauilonunteedvootO vee @ No Review ACCoPtatde Not Acceptatde Needed Date inhor: Dm B. A O 2m VT Lead: Neri, Anthony A O
VT Mgr; Schopfer, Don K inc chmn: singh, Anand K Dele: 2/20/98 SL Corronents:
s Page 2 or 2
'Prvded 2/239610 53:36 AM
DR No. DR-MP3-0424 Northeast Utlinies ICAVP
/
Ministone Unit 3 Dist:repancy Report Review Oroup: Confgurabon DRREsot.UTKhACCEPTED Review Element: Ikadtfcaton insteheton p , ,
Discipline: Piping Doo6p" Dluropency Type: Insts'letlon Irnplementaten Om No SystemProcess: SWP NRC sigrdf6conce level: 4 DMe FMed to NU:
Date Publ6thed: 11/1197 D6*c m ancy: Modification PDCR MP3 88136 : Add pipe couplings to line 3 SWP 150-072 3 Descriptio. The sketch and note in the PDCR calls for a coupling to be added to line 3-SWP 150-072 3 within one ft.(C in.) from an elbow in the hortzontal run of the pipe. The coupilng was measured to be about 27 in. from the centeriine of the elbow.
This discrepancy does not affect the pipe t, tress calculations.
Review Val 6d invalid Needed Date i'#3SS7 inittetor: Reed. J. W. O O O ^ #3i'87 VT Lead: Nort, Anthony A O O O VT Mgr: Schopfer, Don K O O O 11/6S7 IRC Chnwi: $1ngh, Anand K O O O 11/7'87 Dei.:
INVALID:
Dets: 2/17/98 REs0LUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0424, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B18901 and 17010. It has been screened per U3 Pl.
20 criteria and found to have no operability or reportability ,
concems and meets the Unit 3 deferral criteria. CR M3 97-4017 has been written to develop and track resolution of this Mm per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0424, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 97-4017 has been written to develop and track resalution of this item per RP-4.
Previously identitled by NUP Q Yec @ No NonDescrepentConomontO ves @ No ResolutbonPend6ngv0 vee @ No ResoiuiionUnresoived?O vec @ No Review Acceptable Not Acceptable Needed Date ,
M RM m VT Lead: Neri, Anthony A VT Mge: schopfer, Don K '
IRC Ctwnn: Srigh. Anand K DMe, KL t'u. .='n Printoa 2/23/0610.s4 28 AM Page 1 of 2
l DR No. DRMP3 0424 Northeast Utilities ICAVP Millstone UnN 3 Discrepancy Report o
Page 2 of 2 PrWed 2/219010 54 32 AM
bR No. DR MP3 0429 Nonheast Utilities ICAVP Ministone unk 3 Discrepancy Report Review Group: System DR REs0LUTKW ACCEPTED Review Elenwnt: system Dngn Potential Operptwnwy issue Diecipim: MKhankM Deoyt Q y,,
Discrepancy Type: Calev.eten (e) No system' Process: SWP NRC signinconce level: 4 Date F Axed to NU:
Date Publ6shed: 11/1397 D'ureP*ncy! PEGISYS Computer Model showing pump curves exceeded, without follow up tn analysis.
Ductlption: Calculation FSE/SS NEU 1922, Revision 1, Dated 5/30/97,
Millstone 3 SWS Rerun of Test Cases for Uncertainty Calc. has computer output from PEGISYS 3.0 shown in pages A1 thru A104. On pages A26, A57 and A71 there is a note describing that flow. ate exceeds runout and that the NPSH curve has been exceeded. These computer generated automatic comments are not addressed in the body of the report nor in the NU review of the calc., leaving the acceptability of the computer resdits uncertain.
This cou'd significantly impact the results of this calculation and that of other calculations which this output was used as a basis.
This output was used in calculations FSE/SS-NEU 1924 and 90-0691116 M3, both of which would impact the results of calc. 90-0691065-M3 which is the GL 8913, item IV Summary Document.
Review Val 6d involui Needed Date initletor: Omnne, B. J. O O O ior27/97 VT Lead: Neri. Arthony A Q Q Q 1o/27/97 Q 10'2&97 VT Mgt: Sctopfer, Don K Q Q IRC Ctwnn: Singh. Anand K O O O 55/1/97 Date:
INVALID:
Date: 2/20/98 RESOLUTION: Disposition:
NU .1as concluded that the issue reported in Discrepancy Report, DR MP3-0429, has identified a condition not previously discovered by NU which requires correction. The approved corrective action plan for Condition Report M3 97 4774 w'll correct this issue by determining if calculation FSE/SS NF.U.
1922 needs to be superseded by the current SWP flow piodel (Proto Power Calculation 96-001) or if active to update it consistent with the discrepancies of this DR. These conective actions will be performed post startup.Proto Power Calculation 96-001 was transmitted to S&L by IRF-00401, TRA 00118.NU has determhed that this discrepancy does not impact the design or licensing basis of MP3. This calculation is active only to maintain a basis for identifying the most limiting service water system lineups. The flow results are historical. Proto Power Calculation 96 001 is the current SWP flow model. Therefore, NU has concluded that this discrepancy is a Significance Level 4.
Page 1 of Y Printed 2/219610 54 57 AM
1 l
DR No. DR-MP3-0429 Northeast Utilities ICAVP l
Millstone Unit 3 Discrepancy Report
Conclusion:
NU has concluded that the issue reported in Discrepancy Report, DR MP3-0429 has identified a condition not previously discovered by NU which requires correction. The approved corrective action plan in CR M3 97 4774 will be comr!eted post startup to determine if calculation FSE/SS-NEU 1922 should be superseded by the current SWP flow model(Proto Power Calculatloa 96-001), As Proto Power Calculation 96-001 is the current SWP flow model there is no impact on the design or licensing basis. NU has concluded that this discrepancy is a Significance Level 4.
Prev 60usly identifbed by NU? U Yee (9) No Non D6scr6 rent CondM6on?O Yee @ No Resolution Pend 6ngtO tee '3) No Resoiutt.a.uareceivedtO vee @ No Review inNielori Dionne, B.J.
VT Lead: Nort, Anthony A VT Mgt: Schopfw, Don K b
IRC Chmn: singh, Anand K D*: 2/20/98 sL conerwnte! Acceptable to deferr based on CR M3 97-4774. Modeling of the Service Water System has been performed and tested to the current model (calc. 96 001), this calculation would not pose a design or licensing basis problem and can be reduced to level 4 fron6 significance level 3.
Pege 2 of 2 Printed 2/2196 to 55:01 AM
I ICAVp DR NO. DR-MP3 0439 Northeast Utilities Millstone Unit 3 D'screpancy Report Rev6ew Group: system DR RESOLUTION ACCEPTED Revfp13ement: Wks$feston Des 6pn Potential Operab6hty issue D scien n.: ueci nu oeson O ve.
D.urepancy Type: Instanaton Irnpnementaten 4g systern' Process: SWP NRc significance level: 4 Date F Axed to NU:
Date Published: tr2590 D'screPancy: Information not fully documented in modification PDCE MP3 140.
Descript6on: Modification PDCE MP3 90140, Install Piping Mods to "A* Train SWP at 3HVK' ACUS 1 A. Several discrepencies were noted with the documentation supporting this modification. The supporting documents reviewed with this modification included, DCN DM3-P 07190 and DCN DMS P 000-90.
This modification replaced schedule 10 piping spools with schedule 80 pipe, which reduced the Inside Diameter (1D) of the piping. The hydraulle model / calculations should have been revised and referenced in this modification to reflect the reduction in the pipe ID.
DCN DM3-P 07190 which consists of only one page, states that the *as built dimensions of spool tnd spacer plate to be attached to this DCN", were not included with this DCN. The dimensions of the spool to be replaced could not be verified.
Revlew Valid invalid Needed Date iiir,9s initiator: Donne, B. J- O O O 1'1SS8 VT Lead: Nort, Anthony A O O O 1/1498 VT Mgt: schopter,00n K @ O O ir2iro8 IRC Chmn: singh. Anand K O O O Date: 1/15/98 INVALID:
Dete: 2/20/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0439, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 It has been screened per US PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. OR M3 98-0655 has been written to develop and track resolution of this item per RP4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0430, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 ar.d.17010 it has been screened per U3 Pl.
20 criteria and found to have no operability or reportability Page i of 2 Pnnted 2/239810 $s 28 AM I
l N:stheast Utilities ICAVh DR N3. DR-MP3-0439 t
Millstone Unit 3 Discrepancy Report concerns and meets the Unit 3 deferral criteria. CR M3 98-0655 has t+ eq wntlen to develop and track resolution of this item per RP4.
Previously klentif6ed by NU7 O Yes iti No Non Descrepent Condetkm?O Yes f*I No Resolution Pend 6ngtO ve. *> so RenoiuilonuaremoivoorO ve. + No Review inittetori Dxrine, R. J.
VT Leod: Nort, Anttany A O O O m VT Mgr Schopfer, Don K b h b IRC Chmn: Singh, Anand K Date: 2/20/98 SL Conenents:
PrWed 2/23961055 32 AM Pope 2 of 2
DR N2. DR MP3 0449 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Rev6ew Group: sptern DR RESOLUTION ACCEPTED Review Element: Syetem Doogn Potentiel Operetdisty lasue 06sc6pline: Mechanical Do61gn O vee Descrepency Type: Calculaton fe) No systerrvProcess: $WP )
NRC s6gnificence level: 4 Dele faxed to NU:
Dele Publishad: 11/1597 D6screpency: Calculation 92 0801014ES Incorrectly Applied Hydraulic Data
Description:
The purpose of Calculation W2 0801014ES was to evaluate ),ow rete changes in the 3HVQ' ACUS 1B and 3CCI'E1B piping lines as a result of modl0 cations made by DCN DM3 S 034 93 and DCN DM3-S 0050-93 The approach taken was to evaluate the form loss coef0clent, K, before and after the modifications to predict changes in the flow rates. Table 1, page 7, identifies the tJD for all of the components in the 3HVQ' ACUS 1B line before and after the modl0 cations. The values listed in the UD coluren cre actually the values of K, where K = f*(UD). This error is propogated all the way through the calculation such that changes in K are being compared to changes in UD, which are not meaningful and probably not intended.
The 'Altemate Check Calculation'(included as Attachment A) assumes the information in Table 1 of the original calculation is correct and uses it in the attemate check calculation without verifying it. The change in the form loss coef0cient, detta K, for the 3HVQ' ACUS 1B branch is calculated on page A2. Here delta K is determined by multiplying f times delta UD Since the referenced delta UD value was actually detta K, multiplying it again by f Inv:lidates the results of the calculation as this error is propagated through to the final result.
The percent UD reduction for the HVQ branch was Incorrectly determined to be 0.09%. Had this analysis been done correctly, the percent UD reduction for the HVQ branch would have been approximately 5% and the percent UD reduction for the CCl branch would have remained as 4%. Therefore, the conclusion that percent UD reduction for the HVQ is less than the percent L.iD reduction for the CCl branch is incorrect. The difference between the two branches is minor (5% vs. 4%).
Review Vol6d invalid Needed Date initletor: Diontw, B. J. g [ Q 11/397 O t iS7 VT Leed: Nort. Arthony A S O iirin97 VT Mgr schopter, Don K S O O IRC Chmn: Singh, Anand K O O O 15'11/97 Date:
INVALID:
D*: 2/20/98 RESOLUTON: Disposition:
Page 1 of 2 Printed 2/239e to 51.36 AM
f DR N2. DR-MP3 0449
! N:rthea;t Utilities ICAVP
} Milistone Unit 3 Discrepancy Report l NU has concluded that Discrepancy Report, DR MP3 0449, has identified a condKlon not previously discovered by NU which requires correr' tion. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 P.-
20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 98-0138 has been written to develop and track resolution of this item per RP-4,
Conclusion:
NU has concluded that Discrepancy Report, DR MP3 0449, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been sc eened pe. U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria, CR M3 98 0138 has been written to develop and track resolution of this item per RP 4.
Previously iderdined by NU7 O Yes (ei> No Non D6screpent Conditkm70 Yes it) too Resolut6onPending?O Yes @ No Resolution unresolved?O Yo. @ No Review ACC'Ptab6e Not Acceptable Needed Date inmor: Dm, e4 O O O m VT Leed: Nort, Anthony A VT Mgt: Schopfer, Don K IRc chmn: Singh, Anand K Date: 2/20/98 SL Coeronents:
Printed 2/23/96 to 57;42 AM Page 2 of 2 l
l DR No. DR MP3 0460 Northeast Utilities ICAVP
( Millstone Unit 3 Discrepancy Report Review Group: Jystem DR RESOLUTION ACCEPTED
""** """*"': Sr**"' D'**' roi.nu oper.t.uy i..ue oi.cien ne: u.a.nu De.*' O ve.
Di.crepancy Type: calculaton Sy.tenvProcess: SWP NRC significance leveh 4 Date F Axed to NU:
Date Put>h6hed: 1VM97 Dacrepency: Insufficient reference and incomplete methodology identified in Calculation 88-BOP 677 GM, Rev 0.
Description:
The purpose of calculation 88 BOP-677 GM. Rev 0 was to analyze the effects on the Millstone Unit 3 service water system after replacing certain short radius small bore pipe elbows with 4D and SD pipe bends located in the HVQ, CCI, and CCE portions of the system.
The approach taken by this calculation was to multiply the difference in the 1/D values for the affected lines before and after the modifications by the worst case flow to predict the change in pressure drop.
The worst case flow rates were taken from Reference 6, Millstona Ur.;t 3 Service Water Phase I & 11 Test Report. The worst case flow rates usod in the calculation could not be verified because the reference is insufficient. Reference 6 does not include a date when the tests were condus *1d nor does it include a number to identify it.
Assumptions and approximations are made in the calculation to determine the 110 values for the affecteo lines before and after the modifications. The methodology section does not indicale what assamptions and approximations will yield conservative and non conservative results. For example, it is not clear if an assumption that ovsr estimates llD for the pre-modifications condition is conservative or non-conservative. An approach to determine conservative llD values for pre and post modification conditions should have been established.
Page 12 of the calculation contains a sentence that trails off:
"These slightly larger pipe ID's are not expected to cause . ? ?
The discrepancies identified in the calculation are not expected to effect the conclusion of the calculation that the modifications will have an insignificant impact on the service water system operation.
Review Val 6d inval6d Needed Date intuator: Donne, B. J. O O O 10/$oS7 VT Lead: Nett, Anthony A Q Q Q 10/11/97 Q to/1s/97 VT Mgr: schop'er, Don K @ Q IRC Chmn: singh, Anand K Q Q Q 10/22/97 Date:
INVAllD:
Page 1 of 2 Printed 2/219810 t.8.11 AM
DR No, DR MPo 0460 Northeast Utilnies ICAVP Milletone unn Discrepancy Report D*: 2/18/98 REsOLUTeoN: Disposition; NU has concluded that Discrepancy Report, DR MP3 0460, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter 816901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 97 3810 has been written to develop and track resolution of this item per RP-4,
Conclusion:
NU has concluded that Discrepancy Report, DR-MP3-0460, has identif;ed a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B18901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unt',3 deferral criteria. CR M3 97 3810 has been written to develop and track resolution of this item per RP4.
Previously klent6f6*d by NU7 O Yes (e) Ns Non Discrepent Corwestion?Q Yes @ No Resolution Petwitng70 ve. @ No Re.oiuiion une. eved70 ve. @ No Review initle'.or: Dionne, B. J.
i VT Leed: Nort, Anthony A VT Mgt: Schopfer, Don K NtCChmn: singh, Anand K Date: 2/18/98 sL comrnents: CR M3 97 3810 will track the resolution of this DR and after reviewing this CR was deemed to be appropriate.
Printed 2/239810017 AM Pope 2or 2
DR N . DR-MP3 0462 Northeast Utilities ICAVP Mitistone unit 3 Discrepancy Report Review Group; system DR RESOLUTION ACCEPTED Potenttal Operstety issue Discipilne: Mechancal Desgn Om Discrepancy Type: Calculaton system' Process: SWP NRc signmcance level: 4 Date F AKed to NU:
Date Published: in?697 Discrepancy: Required component flow rates in Calculation 17273.161P(T) were not able to be verified oescript6on: The purpose of Calculation 17273,1tr1P(T) was to predict Individual component flow rates in the service water system using degraded service water pump conditions and compare them to required flow rates established from several referenced sources.
The approach taken by this calculation was tc use the HY 06C hydraulic model, using the degraded pump curves, to predict the flow rates to several components in the service water system.
The predicted flow rates were then compared to required flow rates referenced from several sources.
The required flow rates for tiie components analyzed are shown on Page 43 of the calculation along with their respective references. These references were not incicded in the Reference Section of the calculation on Page 4 of the calculation.
The referenced required flow retes identified on Page 43 could not be verified for (3) reasons. The first is that many of the references have been superseded. Referenced calculations 90-FAC-094GF,12i?9-P(T) 1100 and P(R) 1168 have been s.perseded. The second reason !s that the required flow rate was not referenced from a particular operating condition, References, such as the FSAR, contain several required flow rabs for a component under differer.t operating conditions. And lastly, the comparison does not Indicate the quantity of each component operating when comparing the required flow rate and model predictions. For example, is the required flow rate for the CCP heat exchanger based upon 1,2 or 3 operating, and are the predicted flow rates for the CCP heat exchanger based upon 1,2 or 3 operating so a direct comparision can be made?
The discrepancies identified in this calculation are not expected to impar:t the results of this calculation or the functionality of the service water system, in fact, the objective of ;his ca.lcu!ation is also addressed by calculation 90-069-1116 M3 using the PEGISYS hydraulic model to demonstrate minimum component flow requirements will be met.
Review Val 6d inval6d Needed Date 10/15S7 init6ator: Dionne, B. J. O O O O iotiSS7 VT Lead: Nort, Anthony A O O Q t07G97 VT Mgt: schopfer, Don K Q Q O O io'nS7 IRC Chmn: Singh, Anand K O ennied m9e to se.4s AM eage i or 3 )
I
ICAVP DR N . DR-MP3 0462 Northeast Utilities Millstone Unh 3 Discrepancy Report ;
Date:
WWALID:
pele: 2/20/96 RdsowTION: Disposition:
NU has concluded that Discrepancy Report DR MP3-0462 represents a discrepant condition not previously identified, in that Calculation 17273.161P(T), which is no longer the calculation of record, was not identified as superseded or volded, and other calculations referenced within are now out of date. Conditlen l Report (CR) M3 97 3897 has been approved to correct this condition. The new calculation of record is 90 069-1065M3, Rev. O, dated 10/06/94, *MP3 Service Water System . NRC GL 6913, item No. IV Design Basis Summary Report?
Implementation of this change did not identify P(T) 1 as canceled or superseded.
Calculation 90-0691116M3, noted by S&L in DR MP3 0462, was prepared as Westingheuse Calculetion FSE/SS-NEU 1956 to determine minimum available flow rates during accident scenarios. This portion of the calculation has been superseded by calculations PROTO-POWER 97 035 Rev. O dated 08/14/97, PROTO-POWER 97 041 Rev. O dated 09/05/97 and 97 ENG-01427D3, Rav. O. This change was documented in CCNs 1 through 6 of Calculation 90 0691065M3 Rev. O.
As part of the corrective action for condition report M3-97 3897, service water system design basis flow calculations will be reviewed to verify that no references contained therein have been volded or superseded. With reference tc steps 5.2.6 and 5.3.4 of the Desion Control Manual, which require a review of child or parent interactions when preparing changes, item 4 of the corrective action plan requires that a siniilar change be made to Section 6.1 of the DCM to direct the same review when superseding or volding calculations.
Difficuttles in determininq required and available flow raus, as identified by DR MP3 0462, have been corrected by the revisions described above. The remaining corrective action is to revise Calculation P(TF1 to identify that it is volded or superseded. Based on calculation 1065M3 being the calculation of record, the discrepancy a sociated with not voiding calculation 1P(T) is considered an administrative issue, and as such, NU considers this a Significance Level 4 issue.
Calculations PROTO-POWER 97 035 Rev. O PROTO-POWER 97 041 Rev. O and 97 ENG-01427D3 were sent to S&L on 10/24/97 in response to RFl MP3-0641.
Conclusion:
NU has concluded that Discrepancy Report DR MP3-0462 represents a discrepant condition not previously identified, in that Calculation 17273.16-1P(T) has not been identified as superseded or voided Condition Report (CR) M3-97 3097 has PrEted 2f2N96 loM49 AM Page 2of 3
DR No. DR-MP3 0442 Northeast Utilities ICAVP Milintone Unit 3 Discrepancy Report been approved to correct this condition. Service Water flow rate issues of DR MP3-0462 have been addressed by calculations 90-0691065M3, Rev. O, PROTO-POWER 97 035 Rev. O PROTO-POWER 97 041 Rey,0 and 97 ENG-0142703. Based on calculation 1065M3 being the calculation. of record, the discrepancy associated with not voiding calculation 1P(T) is an administrative issue, and as such NU considers this a t'qnificance Level 4 issue., Chapter 5 of the Design Control Manual has been revised to require that child and parerit interactions with other cf.culations be reconciled when other calculations are revised. This is implemented through use of the tracking tool provided by CTP/ Passport Calc tracking,
~
Previously identihed by NUF Q Yes Ti No Non 06screpent Conditkm?O Yes (GI No Resolutkm Per. ding?O vs. @ No Reeduuon unre.wv.d?O ve. @w Review inNietor: Dkwm.B.J.
VT Leed: Nort. Anthony A b O O VT Mgri Schopfer, Don K mc chmn: Shgh, Anand K =
Date: 2/20/98 SL conwnents: Agree with corrective action and that significance level should be reduced to level 4.
Pege 3 of 3 Printed 2/219610.5e 50 AM
DR No. DR-MP3 0604 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Review Group: Confgureten DR REsOLUT10N ACCEPTED
'# I Potential Opershiefty Leue Discipi4ne: Electrieel Deeign O va Diecropency Type: DrW (0) No systerr#tocess: SWP NRC signanconce level: 4 Date Faxed to NU:
Date Published: ta'31/97 4 Di* crop *ncy: Vendor Data not in agreement nameplate data.
De*ctlPtion: Vendor drawing 2332.516 063-005, Rev. B indicates the motor speed for strainer motors 3SWP'STRI A thru 1D is 1800 rpm and the horsepower to be 1.3. Single line EE 1 AE Rev. 35 also shows a horsepower of 1.3. The nameplate indicates a speed of 1700 rpm and a horsepower of 1.4.
Review valid inv.ind Needed Date O O 10/'S7 initletor: server, T. L. O 105S7 VTLead: Nort. Anthony ^ O O O O O in2of c VT Mgt: schopfer, Don K O 1RC Chmn: singh. Anand K Q Q Q 1a'2&97 Dei.:
INVAllo:
DW: 2/7/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy F.eport, DR MP3 0504, has identified a condition not previously discovered by NU wtilch requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the UnN 3 deferral criteria. CR M3 97 3899 has been written to develop and track resolution of this item per RP4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3 0504, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 Pl.
20 criteria and found to have no operability or reportability concems and meets the Uillt 3 deferral criteria. GR M3 97 3899 has been written to develop and track resolution of this item per RP-4.
Previously ider tthed by NU7 O vos @ No Non Discrepent Cond4 Hon?O Yee @ No kesolution Pending?O ve. @ Na Resoiuison unt..oiv.orO vee @ No Review initiator: Werner, l.
VT Lead: Neri, Anthony A VT Mgr: Schopfer. Don K Pnnled 2/2198 to 69 21 AM Pope 1 of 2
ICAVP DR No. DR MP34604 Northeast Utiliti:s "
Millstone unH 3 Discrepancy Report RC Ctvem: Legn, Anand K a -
" a z?2m O J O Dele:
SL Ccwmerde:
I Printed 2/239610 59 25 AM Page 2 of 2
DR No. DR-MP34616 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Review Group: sptom DR REsDLUT6oN ACCEPTED Rev6ew Eierrwnt: sptem Design PMk1 Operabilty hm Dkcipline: lAscherucal Design Q y,,
Dacropency Type: Calculaton < ,3 y, syeterr#rocess: sWP NRc significance level: 4 Date F Axed to NU:
Date Published: 11/E97 066crepancy: Calculation P(T) 0938 rev. O has several inconsistencies.
Descriptkm: Calculation P(T) 0938, rev. 0 ' Service Water System Flow Balancing for Normal Operation" determines the butterfly valve throttling positions and orifice size for balancing the service water system in the nomial operating mode.
The piping referenced in this calculation is class 158 (ref 9). For 24" and 30" class 158 pipe, the well thickness should be 3/8" thick. This would result in pipe ID's of 23.25' and 29.25
respectively. This calculation uses 23.27' and 28,75' which does not coincide with the referenced document.
The factor DP/ttio is used in calculating c(d) (used to determine valve choking) for the outlet valve on pages 11,12 and 28. The values used for the f actor DP,rno are not consistent with the data noted and are not referenced. This questions the valid" the values being calculated.
The f actors DP (units of psi) and r" . (units of feet) are being interchanged in the analysis without account for the conversion factor between units. Thus the values used are not correct and the flow coefficients being determined are not correct.
The resistance coefficient for 3-way valves is not consistent with the referenced document. A value of k=10.21 is being used and a value of k=10.00 is noted in the reference 1. However, the value should be k=1.35 based on the document that reference 1 used as a basis, Crane Technical Paper No. 410. This affects the pressure drop being evaluated.
Page 29 references a pressure of 33 77 psl with an associated equivalent length of 142.02'. This value is not consistent based on the typical conversion factor of 2.32 ft/ psi which would yield an equivalent length of 77.19'. This affects the head differential that is determined using this value.
There were new nodes defined in this calculation that were to be incorporated into calc P(T) 935. This information was not included in P(T) 935 through CCN 02.
Due to the uying degree of the inconsistencies found throughout this calculation the overallImpact on the results can not be determined without re-calculating the model used.
Review Vel 6d inval6d Needed Date initletor: Deonne. B. J. Q Q Q 10/27/97 10,'27/97 VT Lead: Nort, Anthony A Q Q Q erni.d2/2mowsWW W'
- siW
DR No. DR MP3 0516 Northeast Utilit es ICAVP Millstone UnN 3 Discrepancy Report
~' 1 W 97 VT Men 6desder, Don K Q Q Q O 15S7 mc chmn: sngh, Arund K O O Date:
WVALID:
D*: 2/20/98 REs0LUTION: Disposition' NU has concluded that Discrepancy Report DR MP3 0516 has identified a condition not previously discovered by NU which requires correction. Condition Report MS 97 4255 has been written to address this issue. The corrective adlons outlined in Condition Report MS 97 4255 necessary to correct this issue are:
a
- 1) to review and revise as necessary Calculations P(T) 0938 and P(T) 0935; 2) to determine the relevence of P(T) 0938 ar.d P(T) .
0935 and supercede them in accordance with the Design Control Manualif it has been made redundant by Proto Power Calculation 96 001. These corrective actions will be performed Post Startup.
NU has concluded that this discrepancy does not impact the design or !icensing basis of MP3. The calculation in question P(T) 0938, was assessed under the PI 31 program and confirmed by Test Procedure T.3326-P, " Service Water Test Phase
- between 7/30/85 and 8/13/85. The assessment performed under the Pl 31 program did not require a line by line review of calculation P(T) 0938 sirsce the results were verfied by test. The actual modeling of the Service Water System has since been reperformed by Proto-Power Calculation 96-001, therefore calculation P(T)-0938 is historical in nature and does not represent the current Service Water System design or licensing basis. Based upon this reasoning, NU has concluded
- that this discrepancy has a significance level of 4.
Conclusion:
' NU has concluded that Discrepancy Report DR MP3 0183 has identified a condition not previously discovered by NU which requires correction. The corrective actions necessary to resolve the issues detalled in DR MP3 0516 will be implemented and tracked undet the auspices of Condition Report M3 97 4255.
The corrective actions outlined in Condition Report M3 97 4255 necessary to correct this issue are: 1) to review and revise as necessary Calculations P(T) 0938 and P(T) 0935; 2) to determine the relevence of P(D-0938 and P(T)-0935 and supercede them in accordance with the Design Control Manualif they have been made redundant by Proto Power Calculation 96-001. These corrective actions will be performed Post Startup.
NU has concluded that this discrepancy does not impact the design or licensing basis of MP3. The calculation in question P(T)-0938, was assessed under the PI 31 program and confirmed by Test Procedure T 3326 P,
- Service Water Test Phase" between 7/30/85 and 8/13/85. The assessment nerformad urvtar the PI M nrDQram did nnt ranntra a lingthyJne_.
Page 2 of 3 Prwed 2r239610Ws7 AM
l ICAVP DR Ne. DR MP3 0616 l Northeast Utilities Millstone Unit 3 Discrepaficy Report review of calculation P(T) 0938 since the results were verfied by test. The actual modeling of the Service Water System has since been reperformed >y Proto Power Calculation 96 001, therefore calculation P(T)-0938 is historical in nature and does not represent the current Service Water System design or licensing basis. Based upon this reasoning, Nu has concluded that this discrepancy has a signif)cance level of 4, Provlou.ty identihed by NUP O Yes if No Non D6.cropont condulon?Q Yes @ No Re.oiunon un,e.oev.d?O v.. (6; o Re.olution Pend 6ng?O ve. <u; No Review Acceptable Not Acceptetdo Needed Date inNW Dm B. A VT Leed: Nort. Anthony A VT Mgt; Schopfer, Don K IRC Chmn: singh. Anand K Del *: 2/20/98 st comments: Acceptable to defert based on CR M3-97-4774. Modeling of the Service Water System has been performed and tested to the current model(calc.96-001) this calculation would not pose a design or licensing basis problem and can be reduced to level 4 from significance level 3.
s Printed 2/2198 to 59 59 AM Page 3 of 3 ,
l
- - - -~--%-._ ~ _ _ . _ . _ , _ _ _
ICAVP DR No. DR-MP3 0617 Northeast UtilMies Millstone Unit 3 Discrepancy Report l Review Group: SyWom DR RESOLUTION ACCEPTED j Rah EW: SyWorn W Potential Operstmay issue <
D6ecipl6ne: Mechanical Doongn O va D6ecrepency Type: Calculaton
@' No SyslernProcess: SWP NRC Signinconce level: 4 Date faxed to NU:
Date Published: 11/2497 D6*crepeacy: Severalinconsistencies were found in Calculation SDP SWP.
01370-M3 rev.10.
Descr6pt60n: Calculation SDP SWP 01370M3, Revision 10, dated 5/23/97, This calculation is the stress data package for the service water system.
On page 29 of the s data package, the service water design pressure is notr .100 psig. However, calculation 714P(T) determines the so 'ce water design pressure to be 101 psig.
On page 29 of the c..culation a value of 145 psig is listed in the temperature and pressure table, with calculatic1, P(T) 1125 as the source reference. Calculation P(T) 11251,sts a value of 132.7 psig which appears on page 2. Therefore, there is a discrepancy between the value used in the stress data package and the referenced calculation.
On page 29 of the calculation, for 3HVR*ACU1 A/B discharge lines reference MCE SA 93 362 is cited for a temperature of 98'F. This reference does not show nor discuss the 98'F value.
On page 29 of the calculation, the temperature of 125'F was noted for the discharge piping of 3CCP'E1 A/B heat exchanger.
This temperature was referenced from ER 96-0326. This document was requested from NU and was noted as nct in NU system by IRF MP3-0496.
These discrepancies could impact the stress ar.d piping calculations that use this Information from the stress data packa08.
Review Val 6d inval6d Needed Date s
inittetor: D60nne, B. J. G O O 1 '" 3'S7 VT Lead: Neri, Anthony A O O O $ 5'17'87 VT Mer Schooter, Don K Q Q Q 11/17/97 IRC Chmn: singh. Anand K Q Q Q 11/20/97 4
Date:
INVALID:
Date: 2/20/98 RESOLUTION: Dj$pos)(jon:
NU has concluded that issue #3 reported in Discrepancy Report DR MP3-0517 has identified a condition previously discovered Printed 2/239e it o0.29 AM Page 1 or 3
ICAVP DR N3. DR-MP3 0517 l Northeast Utilities Millstone Unit 3 Discrepaticy Report by NU which requires correction.
- 3. Reference giver. 'n RDP does not confirm 98F design temperature for certain lines.
The issue of adequate justification of pressures and temperatures used for piping analysis of the service water system was recognized and documented in CR M3 971598 dated 5/22/97 (attachod). The corrective action plan for the CR required reconsideration and update as required of all service water piping downstream of equipment.
As part of the corrective action, Enginect, ..,,M,a Correspondence 25212 ER 97 0242,1att d 10/27/r 7 (attached) was issued. The memo confirmed that'.ie 98F i ,nperature enveloped the operating temperatures. '.hanp' Notice #1 dated 11/27/97 (attached) to SDP SWP 01370Mdevision 10 incorporated the results of the memo.
NU has concluded that the issues #1,2 and 4 reported in DR M3-0517 are non-discrepant for the following reasons.
- 1. SDP states 100 psig as general design pressure, calc.
714P(T) gives 101 psig, in general, the Line Designation Table (LDD and SDP are the definitive source for design and operating conditions. The design conditions calculations were prepared as required to confirm that the selected design values were adequate. A strict correspondence from the calculations to the LOT is not required as long as there is no significant loss of conservatism.
The difference in pressure values between the LDT and the calculation can be attributed to differences in numerical rounding. T'-e calculation used a value of 1.03 for the density of seawater ans wived at a calculated pressure of 100.7 psig.
Using a more precise value for seawater density of 1.025 taken from the CRC Handbook of Chemistry and Physics (copy of page attached), the calculated value at the pump discharge would be 100.24 psig, which rounds to 100 psig and is consistent with the LDT The difference of 0.5 psig is insignificant and there is no need to revise the LDT. Therefore NU considers this item to be non-discrepant.
- 2. SDP states 145 psig as design for lines downstream of booster pumps, P(T) 1125 gives 132.7 psig.
The calculation determines a predicted pressure based on pump heads and elevation differences. The LDT design pressure is about 10% higher than the result of the calculation. 'is stated in the response to item 1, there is no requirement for a strict match between this confirmatory calculation and the value listed in the LDT The design pressure listed in the LDT is consistent with the
. relief valve 3SWP*RV132A.B setpoint of 145 psig for this piping. In accordance with the original S&W design procedure, the deslori;vessure must not be less than the relief valve Printed 2/239811:00.33 AM Page 2 of 3
ICAVP DR No. DR4AP3 0517 Northeast Utilities Mllistone Unit 3 Discrepancy Report setpoint.
Since the listed design pressure is consistent with the relief valve selpoir.t t'vl hinhar l'::..e the calculated pressure, NU considers this item to be non-discrepant.
- 4. Reference given in SDP was not provided to S&L A copy of the reference memo ER 96-0326 Rev.1 dated 2/23/97 is attached. Footnote 2 on page 2 of the memo describes the basis for the 125 F temperature listed in the SDP. The stated temperature has been reconfirmed in memo 25212 ER 97 0242 dated 10/27/97 (attached).
NU considers this item to be non-discrepant.
In summary of the above, NU believes that there is one discrepant item (#3) that has been pre discovered and three items that are non-discrepant. The pre-discovered discrepant item was corrected based on the action plan of CR M3-971598 and no further action is required. Further, the discrepancy of item #3 is with respect to documentation and not in Information used to satisfy the design basis of the plant. Therefore the discrepancy should be Significance Level 4.
Previously identined by NUP (Gi Yes O No Non Discrepent Condition?O Yes @) No Resolution Pending70 Yee
- No Resoiunon unreedved7O Vee @ No Review Acceptatile Not Acceptable Neled Date ineustor oionne,s.a, VT Leed: Nort, Anthony A O O O 2r:orse G O O VT Mgt: Schopfer, Don K O O mm 1Rc Chmn: Singh, Anand K O O O oste: 2/20/98 sL commente: The resolution given is agreeable and the resolution appears to be adequate for tisis discrepancy given the justifications noted.
The significance level was reduced from level 3 to level 4.
Printed 2r219e 11:00-34 AM Page 3 of 3
- - --- - - _ - . _ _ - _ _ _ _ = _ - _ _ - _ _ -- -. - _ .
DR No. DR MP3 0619 Northeast Utilities ICAVP Millstone unit 3 Discrepancy Report Rev6ew Group: system DR REs0LUTION ACCEPTED Reylew Element: System Des 4O" Pc' int 6elOperetary issue Disc 6pl6ne: *)ochencel Dot 7 Q y,,
D6screpency Type: Calculation (9) No systemerocean: sWP NRC s6gninconce level: 4 Dele faxed to NO:
Date Publ6shed: 1/2598 D6scr*Peacy: Calculations 94 ENG 1037 M3 and 94 ENG 1038 M3 contained various similar errors.
Description:
Calculation 94 ENG 1037 M3 rev. O determines the required SW flow with a 78'F SW temperature to the Charging Pump Coolers 3CCE'E1A & B. Calculation 94 ENG 1038 M3 rev. O determines the required SW flow with a 77'F SW temperature to the Safety injection Pump Coolers 3CCI'E1 A & B. These calculations contaln the following si..,ilar errors:
Data was transposed incorrectly from laputs/ equation to equation 1 in various places throughout the calculation. i.e, Page 21 -
LMTD is noted in energy transport equation as 47.49'F, however, the LMTD is stated in the result table on page 15 as '
l 47.69'F. The density of seawater was noted as 64.15 lbm/ft3 at a temperature of 77'F based on reference K. Thl's referer.ce (page 68) refers to a density of 64,00 lbm/ft3 for seawater at 77'F.
The nomenclature used for the tube radius (page 7) contains incorrect units. The units should be ft not ft'.
Page 13 refers to reference Z in the calculation as the stress calculation, however this reference is the Generic Letter 8913 summary report.
The above noted discrepancies do not greatly impact the conclusions of these calculations. However, calculation 1037 evaluates the service water supplied to the Charging pump coolers at 78'F, calc.1036 evaluates the reactor component cooling water heat exchangers at 78'F, and calc 1038 evaluates the safety injection pump coolers at 77'F. There doesn't seem to be a consistent evaluation of the SWS components at elevated SW inlet temperatures. The Technical Specification refers to an UHS Umperature up to 77'F but does not cddress 78'F as used in calculations 1036 and 1037, Review Vol6d invol6d Needed Date initletor: D6onne. B. J. O O O 1'15S8 O O $6S$
VT Lead: Nerl. Anthony A G VT Mgr schopfer, Don K O O O iiin9e O O i/2iros IRC Chmn: singh, Anand K G Dele:
INVALID:
Date: 2/20/98 RESOLUTION: Disposition:
Pnnted 2/239e 11:0050 AM Page i of 2 e y-1i---F& -- - e-
_- . _ - - _ _~ - _ .
ICAVP DR No. DR MP3 0619 Northeast UtilNies Millstorw UnN 3 Discrepancy Report NU has concluded that Discrepancy Report, DR MP3-0519, has identified a condition not previously discovered by NU which requires ce 1ction. This discrepancy meets the criteria specified in NRC letter B18901 and.1701011 has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 96-0809 has been written to develop and track resolution of this item per
)
RP-4. ,
4
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0519, has identified a condition not previously discovered by HU which requires correction. This discrepuncy meets the criteria specified in NRC letter B16901 and.1701011 has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-96-0809 has been written to develop and track resolution of this item per RP-4.
Prevlously identined by nut U Yes (9) No Non Discropont CoruHt6on?O Yes (9) No Roeolut6on Pending70 Yu @ No Reedut% UnroedvedtO Ya @ No Review intteetor: Dionne, 8. J.
VTLead: Neri, Anthony A b VT Mgr: schopfer Don K O O O m IRC Chmn: Singh, Anand K Dde: 2/20/98 SL Commente:
PrNed 2/2T9611:01:o3 AM Pege 2 or 2
! ICAVP DR No. DR MP3 0621 Northeast Utilities Millstone Unit 3 Discrepaficy Report Review Group; system DR RESOLUTION ACCEPTED Review Elonent: system Desgn p ,
Discipl6ne: Moctancel Des *'
Discrepancy Type: Calculatxt Ow systerWProcess: sWP NRc signthcence level: 4 Date faxed to NU:
Date Published: 11/597 D'*cr*F*ncy: Calculation 577MB) rev. O through CCN 01 hart several discrepancies.
D**ctlPt60n: Calculation 577P(B) determines the Control Building Service Water Booster Pump Head.
The conversion factor used from ft. to psig was not consistently used throughout this calculation.
Equivalent lengths noted for fittings are not consistent with values from Crane Technical Paper No. 410 or cameron Hydraulic Data (referenced documents). Values used were lower than those referenced and no more specific information was given.
The differential pressures for the flow element and control valve are not noted its the referenced specifications (2472.21019n and 2472.110-185). Estimated losses from the data sources are different than those values listed in the calculation.
These discrepancies are not significant enough to affect the pump operabillty, Review Vol6d inval6d Needed Date initletor: Dionne. B. J. O O O to/15S7 VT Lead: Nort, Anthony ^ O O D 1o27/97 iS?SS7 VT Mgr: schopfer, Don K O O O IRC Chmn: singh, Anand K Q Q Q iG"J1/97 D.i.:
INVAllo:
Dele: 2/20/98 REs0LUTION: Disposition; Nu has concluded that Discrepancy Report DR MP3-0521, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B 16901 and 17010. It has been screened per U3 PI 20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criterio CR M3-98-0138 has been written to develop and track resolut 6n of this item per RP4,
Conclusion:
NU has concluded that Discrepancy Repor1, DR-MP3-0521, has identifled a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B 16901 and 17010. It has been screened por U3 Printed 2/2x981001:29 AM Page 1 or 2
Northeast Utilities ICAVP DR No. DRMP3 0621 Millstone UnN 3 Discrepancy Report PI 20 criteria and found to havn no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 96-0138 has been written to develop and track resolution of this item per l RP4, 1 Previously identshed by NUF Q Yes M No Non D6ecreperd CondN60n?O Yes % No Roeoiotion Pend 6ng?O Ye. + No ne.oi iion unte.oev.drO Yo. (e.> No nev6 w Acceptob6e Not Accydebec Nooded Date ham > al VT Leed: Nort, Arthony A 4
VT Mgt: Schopfer, Don K mC chrevu see, Anend K =
Date: 2/20/98
)
SL Correnents:
i Pivded 2/739611:01:33 AM Pege 2 or 2
. . - . _ _ . -___- - - _ - . _ _ _ = _ - - . - _ _ - --- _-. ._
Northeast Utilities ICAVP DR No. DR MP3 0662 Millstone Unit 3 Discrepancy Report g,y6,w Group: sye4rtn DR RESOLUTION ACCEPTED Review Element: Byelem Desi0n D6scipl6ne: Electncel Design potential Operebouty issue Discrepeney Type: calculetran O y ,,
systwwProcess: DGX it) No i NRC significance level: 4 Date faxed to NO: 1 Date Published: 11/1197
_Di*c'*P*acy: Ampacity of Emergency Diesel Generator Cables in Duct Bank
, (Calculation PA91019-556E3, Revision 1)
D**ctir*on: Calculation PA91019 508E3, Revision 1 calculates the ampacity of several cables that are installed in underground duct banks.
The review of this calculation was limited to Duct 915, which l
caries cables from the emergency diesel generator,
{
The data for the cable at Row 1, Column 1 of Duct 915 is shown as a 3 conductor feed in the input data table on page A10-2, but as a single conductor feed in the computer run on page B10.
Since there is no retum feeder show,, the feeder is logically 3 r:onductor The effect of including the missing two cables will be to ralse the temperature of the cables in the duct bank, /,lso, the conductor resistance is listed as 52,5 microohm per foot on page A10 2, but is shown as 52.4 micoohm per foot on page B10.
However, this feed is very lightly loaded, so the additional heating will be slight, The valua of cable insulation thermal resistance til the 2000 MCM cable is not consistent between page A10-2 and page B10.
The Value on page 810 is lower, A reference should be given for this item.
Review Va46d invalid Needed Date initletor: Blosthe, G. William VT Lead: Neri, Anthony A O O O 10'3 '87 Q Q Q 1W31/97 VT Mgr schopfer, Don K O O O 11 5 S7 IRc chmn: singh, Anand K O O O 51/7/97 Dm.:
INVAUD:
Dde: 2/8/98 RESOLUTION: Disposillon:
NU has concluded that Discrepancy Report, DR MP3 0562, has identlfled a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter 816901 and 17010, it has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 98-0138 has been written to develop and track resolution of this item per RP-4.
Conclusior,:
.-rWed 2/219e 11:08.11 AM Page 1 of 2
DR N3. DR MP3 0662 Norths::t Uti!! ties ICAVP Millstone Unit 3 Discrepancy Report rid has concluded that Discrepancy Report, DR MP3-0562, has identified a condition not previously discowred by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found f o have no operability or reportability m
concems and meets the Unit ? deferral criteria. CR M3 98 0138 has been written to develop and track resolution of this item per RP-4.
Previously identined by NU? O Yes 197 No Non Discrepent Condet6on?U Ye. it) No Resolut6on Pendir.g70 ve. (*> wo Re.oiuiionunre.oivedrO Ye. (6) No Rev6ew N'
h4ttetor: Werner, l.
O O ma VT Lead: NoI, Anthony A VT Mgr: Schopfer, Don K b b b IRC Chmn: SinDh , Anard K Date:
SL comments:
t Page 2 of 2 Printed 2r23/9811:08:15 AM
ICAVP DR N3. DR-MP3-0677 N rthea:t Utilities Millstone Unit 3 Discrepancy Report Review Group: Contguraton DR RESOLUTION ACCEPTED Rev6ew Element: System Insteheten p Discipl6ne: Electtteel Design O ve.
D6scropency Type: Instanatkwi Regulrorr ents g -
Systerr#rocess: DGX NRC Signif6cence level: 4 Date faxed to NU:
Date Published: 11497 D6*cr*pency: In:,:elled conduit type not in agreement with design doctanent.
Description:
Conduits 3CH406PA, B, and C, and 3CH4070A, B, and C, which carry the emergency diesel generator output cables, are listed in the Cable and Raceway Program (TSO2) as comodity type CAC 10. This comodity type is for 4 inch rigid aluminum condult; the installed condults are 4 inch flexible conduits.
Review Valid invehd Needed Date inWietor: server, T. L O O O to/2ero7 VT Leed: Nort, Anthony A g Q Q 10/27/97 VT Mgr: Ses pfer, Dw) K O O O 53/3aS7 IRC Chmn: Sin 0h. Anand K O O O 11/5/97 Date:
INVALID:
D*te: 2/7/98 RESOLUTION: Dispositjon; NU has concluded that Discrepancy Report, DR MP3-0577, has identified a condition noi previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0513 has been written to develop and track resolution of this item per RP4.
Conclusion:
NU has concluded tuat Discrepancy Report, DR-MP3-0577, has identified a condition not previously discovered by NU which require'; correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 it has been screened per U3 PI- +
20 criteria and found to h9ve no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0513 has been written to develop and track resolution of this item per RP-4.
Previously identif6ed by NU7 O Yes (9) Nc Non Discrepent Condition?O Yes (OTNo Resolut6ove Pending70 ve. 4)No Pasolution Unresolved 70 ve. @) No Review initiator: We,ner,1.
G O O mm VT Lead: Nerl. Anthony A VT Mgr: Schopfer, Don K Printed 2/23/9e 11.0e.50 AM Page 1 of 2
ICAVP DR Ns. DR MP3 0677 Northeast Utilities I
Millstone Unit 3 Disntapancy Report -
,,.~,7,,,. v.
RC Chmn: $1ngh, Aners o.ie:
EL C h s:
5
(
Pnnted 2/219611:08:53 AM Page 2 of 2
Noethe:st Utilities ICAVP DR N3. DR-MP3-0603 Millstone Unit 3 Discrepancy Report Review Oroup: system DR *tESOLUTION ACCEPTED RwMW: S#em W Potential Operability issue Discipline: Em o"*"
D6screpancy Type: Cam O va
@ No SystemProcess: N/A NRC Significance level: 4 Date faxed to NU:
Date Published: 11/15/97 Discrepency: Dierepancies in Calculation #64E
- Cable Sizes for Feeders to MOVs*
Ducript60n: The review of Calculation #64E identified miscellaneous discrepancies lit the calculation. 'i he specific items are as '
follows:
- 1) Interoffler. Correspondence C-02 attached to the calculation identifies installed cable length: which differ from the lengths used in the calculation for the feed from the load center to the MCC, For the calculation of MOV feed ccble lengths from MCCs with a running voltage oN1v V (Table A), the cable length used in the calculation (page 3) is 479 feet. The installed length according to the memo is 550 feet.
.55(LRA @ rated voltage) as referenced in ETG IV 41. A review of the reference did not identify this basis.
- 3) Page 2 of the calculation identifies empacities for #12 and
- 10 cables taken from IPCEA P-46-426. A revievt of the subject reference did not identify these ampacities.
- 4) Page 3 of the calculation identifies the bl;ek load of MOVs at 3 MCCs. Reviewing the latest revision of the one line diagrams for the affected MCCs yields values approximately 20 hp higher than those used in the calculation.
- 5) Interoffice Correspondence C-02 attached to the calculation states that page 5 of the calculation should reference
' Calculation #74E' instead of " Calculation #62E" as a basis for short circuit considerations. A review of Calculation #74E did not identify any basis for short circuit considerations.
- 6) A review of the calculation did not identify any basis for why the three MCCs analyzed in the calculation were chosen i.e.,
whether or not they are limiting. Also, no basis could be identified for th6 load current of the MCCs (150 A or 300 A) and it.e MCC running voltage (418 V or 422V).
- 7) On pages 13,14, and 15 of the calculation, no basis could be identified for choosing a grid voltage of 331 KV in order to determine the load center voltage.
Some of these discrepancies are non conservative; however, there are other conservatisms in the calculation which would ensure adequate sizing of MOV power feeds. Most notably is the conservative acceptance criteria for starting voltage of safety reintad MOVc Tha unVe nrn t nnnhin nf sinriinn at 7004 rntad Printed 2/23/961109:57 AM Page 1 of 2
ICAVP DR N3. DR-MP3-0603 Northea:t Utilities Millstone Unit 3 Discrepancy Report ,
voltage, but a criteria of 80% is used in the calcwmion.
Therefore, the plant's licensing and design basis is stKi met and this discrepancy is rated a Significance i.evel 4.
Review Velid involid Needed Date initletor: Kleh, J. g Q O 11/1097 VT Lead: Neri, Anthony A O O O 11/10/87 VT Mgr: schopfer, Don K O O O 11' ins 7 1RC Chmn: singh, Anand K @ Q Q 11/11/97 Date:
IPNALIO:
Date: 2/18/98 RESOLUTION: Disposillon:
NU has concluded that Discrepancy Report, DR MP3-0603, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0138 has been written to develop and track resolution of this item per RP-4.
Conclusion:
Disposition:
NU has concluded that Discrer ancy Report, DR MP3-0603, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-93-0138 has been written to develop and track resc'ution of this item per RP-4.
Previously identifled by PA'? O Yes (#) No Non D6ecrepent Condition?O Yes T No Resolution Pending?O ve. @ No Resoiuiionunre.oived?O v @ No Review initletor: Wamer, l.
VT Lead: Neri, Anthony A VT Mgt: Schorder Don K 1RC Chmn: sin 0h, Anand K Date:
SL Conwnents:
Printed 2/239811:10.01 AM Page 2 of 2
l DR N3 DR-MP3-0621 I Northeast Utilities ICAVP Mi! stone Unit 3 Discrepancy Report f DR F,EsOLUTION ACCEPTED Review Group: system
- *
- Y' # Potedial Operability issue Discipline: Mechanical Desgr . O ve.
Discrepancy Type: Component Data @' No systern/ Process: Rss NRC signifncance level: 4 Dale faxed to NU:
Date Published: 11/20/97 Discrepancy: Specs 2214.803-020 & 2214.802-044 are not in agreement with FSAR Section 6.5.2.1 w/ respect to pH.
Descripuon: FSAR Section 6.5.2.1 states that the containment recirculation spray system is designed to contain a solution with a pH of range of 7.0 to 10.5. However, the following are desi0ned for a pH range inconsistent with the range specified in the FSAR:
- 1. C'.ntainment recirculation coolers design specification 2214.803-020 through Addendum 5, page 1-4, states that the solution on the shell side will have a pH range of 8 to 10.5.
- 2. Containment recirculation spray pump design specification 2214.802-044 through Addendum 6, page 15 states that the pumped solution w'll have a pH range of 5 to 7.5.
F.eview Val 6d inval6d Needed Date 11' * 'J7 inNietor: Feingold, D. J. 8 O O 0 11/
- 7 VT Lead: Neri. Anthony A B D VT Mgt; schopfer. Don K G O O 11/10/97 IRC Chmn: singh. Anand K G O O 11'17/S7 Date:
INVAllD:
Date: 2/20/98 REs0LUTION: Dispositjon:
NU has concluded that Discrepancy Report, DR-MP3-0621, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the ciiteria specified in NRC letter B16901 and 17010. It has been screened per U3 Pl.20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-97-4391 has been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0621, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter 816901 and 17010. It has been screened per U3 Pi-20 criteria and found to have no operability or repostability concums and meets the Unit 3 deferral criteria. CR M3-97-4391 Page 1 of 2 Printed 2/2*/9611:12:00 AM
ICAVP Dbo.hd-MP3-0621 Northe:st Utill!!es Millstone Unit 3 Discrepancy Report has been written to develop and track resolution of this item per RP-4, Previously iderdined by NU? O Yes (89 No NonD6screpardCondellon?O Yes (O') No Resolution Pending?O Yo. r*J> No Re.oiuiion unre.oivedtO Ye. @ No Rev6ew inatletor: Feingold, D. J.
l VT Lead: Noti, Anthony A VT Mgr: Schopfer. Don K b lRC Chmn: Singh, Anand K oste: 2/20/98 st Comments: The Intended corrective action is apparent from condition report CR M3-997-4391, According to the condition report, a DCN will be issued to correct to discrepant condition with the design specifications.
i Pnnted 2/23/9011:12:12 AM Page 2 of 2 4
ICAVP DR N . DR-MP3-0634 N:rtheast Utilities l Millstone Unit 3 Discrepancy Report Review Group: Systern DR RESOLUTION ACCEPTED Potential Operststy issue Discipline: Electrical Design Disciepancy Type: Calculaton Om g~
SystemfProcess: N'A NRC significance level: 4 Date faxed to NU:
Date Publishsd: 11/15/97 Descrepancy: Discrepancies in Cable Ampacity Calculations Descr'.ption: The review of Calculation #143E
- Determine the impact of Derating Cable Ampacity for Cables Routed in Conduit Bank' and Calculation #195E ' Verify Cable Selection fc ' 9 kV and 4.16 kV Loads' identified miscellaneous discrepancies in the calculations. The specific items are as follows:
- 1) On page 5 of Calcul.ation #143E, the transposed valla for ampacity of #10 cable is identified es 41 instead of 40. This discrepancy has no impact on the calculation's output.
- 2) Table-2 on page 6 of calculation #143E identifies cable sizes for L-tray. According to Calculation #67E, #4 and #2 cables can be routed in L tray. If these cables can be validly routed in L-tray, they should be addressed in Table-2.
- 3) Page 12 of Calculation Change Notice #3 of Calculation
- 195E, identifies a derating factor of .85 for 3 conduits spaced horizontally. A redew of the appropriate reference identifies this derating factor as .91. A more conservative value was used; therefore, this discrepancy does not adversely impact the calculation's output.
These discrepancies are not considered to adversely impact the output of the calculations. Therefore, the plant's licensing and desi0n basis is still met, and this discrepency report is rated a Significance Level 4.
Review Valid Invalid Needed Date 11/6/97 initiator: Klsh, J. @ [ Q VT Lead: Neri, Anthony A y ] ] 11/tV97 VT Mgr: schopfer, Don K @ Q Q 11/10/97 O 'i'11/S7 IRC Chmn: singh, Anand K G O Date:
INVALID:
Date: 2/8/98 RESOLUTION: Disposition:
NU has concludet that Discrepancy Report, DR MP3-0634, has identified a conGion not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 Pl.
20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0138 has been written to develop and track resolution of this item per Prtrited 2/23/9611:14:14 AM Page 1 of 2 l
ICAVP DR N3. DR MP3-0634 l N::rtheast Utilities Millstone Unit 3 Discrapancy Report RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR-MP3-0634, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0138 has been written to develop and track resolution of this item per RP4.
Previously identined by NU7 O Yes (@ No Non Discrepent CondM6on?U Yes (@ No Resolutto Pendmg?O ve. (@ No Resolution Unresolved 70 ve. (@ No Review inMlator: Warner, L VT Lead: Neri. Anthony A VT Mgr: Schopfer, Don K IRC Chmn: Singh, Anand K Date:
st Comments:
Printed 2/23/9811'14:18 AM Page 2 of 2
( N:rtheast Utilities ICAVP DR No. DR-MP3-0635 Mitistone unit 3 Discrepancy Report Review Group: System DR REsOLUTK)N ACCEPTED Potential Operabilty issue Di6cipline: Mechanical Design Discrepancy Type: Component Data Ow g~
Systern/ Process: Oss NRC significance level: 4 Date faxed to NU:
Date Published: 12/21/97 D(screpancy: Inconsistency between FSAR Sec 6.1.1.1 & design documents with respect to ASME Section ll materials.
Ducripuon: FSAR Section 6.1.1.1 states that mechanical proporties of the materials used in the engineered safety features (ESF) are in accordance with ASME Boiler and Pressure Vessel Code, Section 11.
The FSAR statement in Section 6.1.1.1 clearly apphes the requirement for materials to all safety-related piping and components. However, application of this requirement to pressure boundary materials appears more appropriate.
Since the FSAR Section 6.1.1.1 does not specify that the mechanical properties of pressure boundary materials, only, are in accordance with ASME Section ll, all safety related quench spray system materials are evaluated against the mechanical properties in ASME Section 11.
All materials in safety related components are designated "SA" or "SB' from ASME Section 11, Parts A and B except for the following:
A 193 GR B8 A 194 GR 8F A 276 TP 304 Cond A A 276 TP 316 Cond B A 296 CF8 A-296 CF8M A 307 GR B/CD B-438 GR 1 B-584 AL 836 According to ASME Section 11, Parts A and B, the specifications for ASTM A193, A194, A-307, and B-584 have equivalent mechanical properties to ASME Section 11, Parts A and B, Subsections SA193, SA194, SA-307, and SB 584. Therefore, components made from materials complying with these specifcations are considered acceptable.
However, specifications B-438, SA-276 and SA-296 are not listed in ASME Section 11. Therefore, components constructed from materials designed to specifications B-438, SA 276, SA-296 A 276, and A 296 do not have mechanical properties in accordance with ASME Section 11. Quench spray system components constructed from these materials are:
3QSS*P3A,B3 nnnn+unvut n Printed 2f23,9611:14.54 AM Page 1 of 3
DR No. DR-MP3-0635 l
Northeast Utilities ICAVP Miiistone Unit 3 Discrepancy Report SOSS V4, V8 30SSN976 V979 3QSS*V50-58 30SS*V940, V941 30SS*V948-V951 30SS*V968-V975 30SS*V933-V936 30SS*V957 V959 3OSS*V964 V967 3QSS*V986, V987 3QSS*V42, V43 Review Valid invW6d Needed Date O 12/i/97 initiator: Feingold. D. J. O O VT Leed: Nett. Anthony A g Q Q 12tS97 O O 12titis7 VT Mgr: schopfer, Don K O 12tii57 IRc ctoim: singh, Anand K G O O Date:
INVALID:
Date: 2/20/98 RESOLUTION: Dispositio9:
NU has concluded that Discrepancy Report DR-MP3-0635 has identified a condition not previously discovered by NU v411ch requires correction. Condition Report ( CR ) M3-97 4699 was written to provide the necessary corrective actions to resolve this issue. The corrective action to correct this issue is Create a FSARCR for clar;fication of appropriate applicability of the material property statement made in FSAR Section 6,1,1,1, pertaining to the Boller and Pressure Vessel Code, in particular with respect to pressure retaining components, as noted in ICAVP discrepancy DR-MP3-0635. This issue is viewed as an enhancement to the FSAR to clanfy plant configura'.lon. Based upon the preceding discussion, the LB /DB of MP3 is not impacted by this discrepancy therefore NU considers this issue to be a level 4 discrepancy.
This corrective action will be performed Post MP3 Startup.
Conclusion:
NU has concluded that Discrepancy Report DR-MP3-0635 has identified a condition not previously discovered by NU which requires correction. The corrective action necessary to resolve the issues detailed in DR-MP3-0635 will be implemented and tracked under the auspices of condition report M3-97-4699. The corrective action outlined in Condition Report M3-97-4699 necessary to correct this issue is: Create a FSARCR for clarification of appropriate apolicability of the material property statement made in FSAR Section 6.1.1.1, pertaining to the Boller and Pressure Vessel Code in particular with respect to pressure retaining components, as noted in ICAVP discrepancy DR MP3-0625. This issue is viewed as an enhancement to the FSAR to Page 2 of 3 Printed 2t23/9e 11:14.57 AM
ICAVP OR N3. DR-MP3-0635 N:rtheast Utilities Millstone Unit 3 Discrepancy Report clarify plant configuration. Based upon the preceding discussion, the LB /DB of MP3 is not impacted by this dircrepancy therefort NU considers this issue to be a level 4 discrepancy.
This corrective action will be performed Post MP3 Startup.
Previously identified by Nur O Yes ($1No Non Discrepent Condn6on?O Yes (f) No Resolution Pending?O Ye. @ No ResdubonUnresdvedrO Yes @ No Review int'letor: Feingold, D. J, VT Load: Neri, Anthony A VT Mgt: Schopfer, Don K IRC Chmn: Sin 0h, Anand K Date: 2/20!98 SL Comments:
4 Printed 2/2MB 11:14 59 AM Page 3 of 3 {
l
DR N3. DR MP3-0336 l Northert Utilities ICAVP MillstDne Unit 3 Discrepancy Report Review Group: System DR RESOLUTION ACCEPTED Review Element: system W Potential Operability issue Discipline: Mechanical Design O ve.
D6screpancy Type: Component Date
(@ No System / Process: RsS NRC signiricence level: 4 Date faxed tu NU:
Date Published: 12/7/97 DI*crePancy: Incenststency between FSAR Sec 6.1.1.1 & design documents with 'espect to ASME Section ll materials.
Descrlpuon: FSAP Section 6.1.1.1 states that mechanical properties of the materthls used in the engineered safety features (ESF) are in accordance with ASME Boller and Pressure Vessel Code, action 11.
The FSAR statement in Section 6.1.1.1 clear 1y applies the requirement for materials to all safety related piping and components. However, application of this requirement to -
pressure boundary materials appears more appropriate.
Since the FSAR Section 6.1.1.1 does not specify that the ,
mechanical properties of pressure boundary materials, only, are in accordance with ASME Section ll, all safety related containment recirculation spray system materials are evaluated against the mechanical properties in ASME Section ll.
All materials in safety related components are designated "SA" or "SB* from ASME Section 11, Parts A and B except for the following:
A 36 A-193 GR B8 A 194 GR 8F A 276 TP 304 Cond A A 276 TP 316 Cond B A-276 TP 410 A-296 CF8 A 296 CF8M A 307 A-351 TP CF8 A 351 GR CF3 A-479 TP 316 A 563 A 582 GR 416 A 703 A 705 GR 630 B-145 Alloy 836 B-438 GR 1 TP ll B-584 Alloy 836 According to ASME Section 11, Parts A and B, the specifications for ASTM A 36, A193, A194, A-307, A-351, A 479, A-563, A 703, A-705, and B-584 have equivalent mechanical properties to ASME Section 11, Parts A and B, Subsections SA-36, SA193, SA194, SA 307, SA 351, SA-479, SA 563, SA-703, SA-705, and RRAAA Thorninen t nmnnnante mnda imm matadak t nmnlym' g_,
Page1 or 3 Printed 2/23/9e 1122:00 AM
O DR N3. DR-MP3 0636 f Northeast Utilitin ICAVP Ministone Unit 3 Discrepancy Report with these specifcations are considered acceptable. .
However, specifications B-438, A 582, SA 276 and SA 296 are not listed in ASME Section 11. Therefore, components constructed from materials designed to specifications B-438, A-582, SA 273, SA 296, A 276, and A296 do not have mechanical properties in accordance with ASME Section 11. Containment recircu'ation spray system components constructed from these materials are: .
3RSS*MOV20A,B,C,0 3RSS*MOV23A,B,C,D 3RSS*V3, 6, 9,12 3RSS*V35,36 3RSS*V32 33 3RSS*V58 59 3RSS*V62 63 3RSS*V66-07 3RSS*V913 3RSS*V916 3RSSN920-931 3RSS*V946 953 3RSS*VS88-995 3RSS*V958-959 3RSS*V961932 3RSS*V26-29 3RSS*V64-65 3RSS*V68-69 3RSS*V912 3RSS*V970-971 3RSS*V973 3RSS*V977 978 3RSS*V984 3RSS*V967 968 3RSS*V980-981 3RSS*V911 Review VaHd invaNd Needed Date 11/17S7 initiator: Feingold. D. J. O O O VT Lead: Neri, Anthony A G O O 11'1S'S7 VT Mgt: Schopfer, Don K 8 O O 12 itis 7 O 12iss7 IRC Chmn: Singh, Anand K O O D.i.:
INVALID:
==
Date: 2/20/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report DR-MP3-0636 has identified a condition not previously discovered by NU which requires correction. Condition Report ( CR ) M3-97 4668 was written to provide the necessary corrective actions to resolve this issue. The corrective action to correct tnis issue is : Evaluate the applicabi!!!y of FSAR section 6.1.1.1 to non pressure Page 2 of 3 Prtuted 2/239811:22:03 AM
DR N3. DR-MP3-0636 f Northeast Utilities ICAVP l Millstone Unit 3 Discrepancy Report re! Ining valve parts and revise the FSAR if n9cessary. This is an administrative task for FSAR clarification only. Based upon the preceding discussion, the LB IDB of MP3 is not impacted by this discrepancy therefore NU considers this issue to be a level 4 discrepancy.
This corrective action will be performed Post MP3 Startup.
Conclusion:
NU has concluded that Discrepancy Report DR MP3-0036 has identified a condition not previously discovercd by NU which requires correction. The crirtective action necessary to resolve the issues detailed in DR-MP3-0636 will be implemented and tracked under the auspices of condition report M3 97-4668. The corrective action outlined in Condition Report M3-97 4668 necessary to correct this issue is: Evaluate the applicability of FSAR section 6.1.1.1 to non-pressure retalning valve parts and revise the FSAR if necessary. This is an administrative task for FSnA clarification only. Based upon the preceding discussion, the LB /DB of MP3 is not impacted by this discrepancy therefore NU considers this issue to be a level 4 discrepancy.
This correc*ive action will be performed Post MP3 Startup.
Previously identined by NU? O Yes @ No Non Discrepent cendition?O Yes (*) No~
Resolution Pending?O v.. @ wo Re.oiuiion unre.oived?O Ye. (s) No Review ACC8M8 ACCeMaW W Date initiator: Feingold, D. J.
O O -
VT Leed: Neri, Anthony A mia S O O VT M0r: schopfe , Don K mia O O IRC C'imn: singh. Anand K O O O Date: 2/20/98 SL Conwnents:
Page 3 or 3 Printed 2/239611:22:05 AM
ICAVP D"4 N). DR MP3-0650 N:rtheast Utilities Millstone Unit 3 Discrepancy Report Review Group: Confguraten DR RESOLUTION ACCEPTED Review Element: System Ostion PotentialOperabety lasue Discipl6ne: Pip 6ng Design O Yes Discrepancy Type: Drawin0 (M No System /Procese: DGX NRC Signifkance level: 4 Date Faxed to NU:
Date Published: 11/2G97 Discrepancy: Upper Tier to Lower Tier Drawing Review for DGX D*6ctlP tion: The following drawing discrepancies were found in reviewing the P&lD with the as built Isometrics for the Emergency Diesel Generators (DGX):
1 On isometric CP 360258 Sht 4 Rev 6 line 3-EGA 500-613 should be 3-EGA 500-64 3, line between valve *V995 and downstream reducer should be labeled 3-EGA 500-913, and line between air receiver 3EGA*TK1 A and first downstream flange should be labeled 3-EGA 500-90-3 per P&lD EM-116B Rev 28 (1-6).
- 2. On isometric CP 360259 Sh 4 Rev 8 the line between air receiver 3EGA*TK2A and first downstream reducer should be labeled 3 EGA 500-88-3 and the line between valve 3EGA*V994 and first downstream reducer should be labeled 3 EGA 500-89 3 per P&lD EM-116B Rev 28 (I-8, H 9).
- 3. On support drawing BZ-60R 63-1 Sht 1 the supported line called r" as 3-EGA 375-25 3 should be 3-EGA 375-17-3 per P&lD LL 1168 Rev 28 and CP-360259 Sht 4 Rev 8.
- 4. On isometric CP 360257 Sht3 Rev 4 line 3-EGA-250-62 3 should be 3-EGA 500-62 3 in the line list box. Line 3-EGA 375-19-3 should also be listed.
- 5. On isometric CP 360260 Sht 4 Rev 5 the line between air receiver 3EGA*TK1B and first downstream reducer should be labeled 3-EGA 500-86-3 and line between valve 3EGA*V982 and first downstream reducer should be labeled 3-EGA 500-87 3 per P&lD EM 116D Rev 9 (1-6). Also the drafth.g symbol for the excess flow check valve 3EGA*V984 is shown as a standard check valve (sea CP 360258 Sht 4 'V986)
- 6. Flex hoses 3EGA* Hose 1B/28 are not listed in GRITS.
- 7. Valves 3EGA*V9, 3EGA*V995,EGA*V5, 3EGA*V13, 3EGA*V4, 3EGA*V11,3EGA*V16, 3EGA*RV24 A1/A2, SEG A*V30, 3EGA*V37, 3EGA*V38, 3EGA*V31, 3 EGA*V981,
,%CA*V982,3EGA*V42,3EGA*V35,3EGA*RV24B1/82 and
?'EGA*V994 are not listed in GRITS and hence no vendor drawings could be identified.
- 8. On isometric Cl-EGD-501 Sht3 Rev 2 safety related equipment 3EGD*EJ2A,*EJ2B,*EJ2C, und EJ2D per P&lD EM-116E Rev 2 should be designated with a (*).
p , 9. On ! cmetdc C! EGD 505 Sht 2 Rev 3 00fety-re! ted g g 3
ICAVP DR No. DR-MP3.C660 Northeast Utilities Millstone Unit 3 Discrepancy Report.
3EGD*V2, 'V1, and diesel generator 3EGS*EG-A/B per PalD EM 116E Rev 2 (17, F 7) should be designated with a (*).
- 10. On isometric CP 360503 sht 3 Rev 8 the embedment should I not be shown on line 3 EGF-002 7 3 until after connection to line 3-EGF-002-43-3 per PalD EM-117A Rev10 (F 3).
- 11. On isometric CP 360503 Sht3 Rev8 line 3-EGF 001 15-3 4
should not show embedment per P&fD EM117A Rev10 (G 2) and the isometric should be continued through line 3-EGF-002-43 3 as shown on CP360503 Sht 1 Rev 8.
- 12. On isometric CP 360530 Sht 10 Rev 1 restricting orifice 3EGF*RO39A is shown but not labeled as per P&lD EM 117A Rev 10 (L 3). Also not listed in GRITS.
- 13. On isometric CP 360533 Sht 19 Rev 8 restricting orifice j 3EGF*RO39B should be labeled as per PalD EM 117A Rev 10 (L 7) Also not listed in GRITS.
- 14. On isometric CP 360534 Sht3 Rev 7 line labeled 3-EFG 001-213 should be 3-EGF 001213 per P&lD EM 117A Rev 10 (H.
8).
- 15. Valves 3 EGO *V986A, *V989A, 'V990A, 'V982A, 'V16A,
- V981 A, 'V18 A, *V988A, *V980A, *V987A, 'V991 A, 'V985A,
'V984A, 'V983A, 'V17A, 'V992A, 'V986B, *V989B, 'V9908,
'V982B,'V168,'V981B,*V188,'V9888,'V9808,*V9878,
'V991B, 'V9858, 'V984B, *V9838, 'V178 and *V992B, 'V208 are not listed in GRITS and hence no vendor drawings could be identified.
- 16. On isometric CP 360264 Sht 4 Rev 5 line between flex hose 3EGS* Hose 4A and the downstream tee should be labeled 3-EGS-375-113 per P&lD EM 116A Re's 30.
- 17. On isometric CP-360700 Sht 3 Rev 5 the line between the Diesel A and first coupling on line 3-EGS-375-9 3 should be labsled 3-EGS-500-22 3 per P&lD EM 116A Rev 27.
- p. view venid invalid Needed Date initiator: Rrad, J. W. O O O 11/2 /S7 VT Lead: Neri, Anthony A y Q Q 11/11/97 VT Mgt: schopfer, Don K G O O 11/17/97 IRC Chmn: Singh, Anand K 8 0 0 1 /17/87 Date:
WVAuD:
Date: 2/19/98 AESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0650, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 Pl.
Printed 2/23/9e 11:22A0 AM Page 2 of 3
DR N2, DR-MP3 0660 N:rthea:t Utilities ICAVP 1
Millstone unit 3 Discrepancy Report 20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-96-0164 has been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR-MP3-0650, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 96-0164 has been written to develop and track resolution of this item per RP-4.
Previously identifned by NU? O Yee @ No NonDiscrepentCondM6on?Q vos @) No ResolutionPending70 vee @ No Recoiuiionunteeoiv.d?O vee @) No Review CC* N M Act$aW Needed he initletor: Reed, J. W.
9 O O m VTt.ead: Nort, Anthony A mia VT Mgr: Schopfer, Don K O O O IRC Chmn: Singh, Anand K O O mia O O O ,
Dais:
SL Comments:
Printed 2/219611:22:42 AM Page 3 of 3 ,
ICAVP DR NO. DR-MP3 0652 N::rthext Utilities Millstone Unit il Discrepancy Report Review Group: Confguraten DR RESOLUTION ACCEPTED Review Element: System Installetxrt Discipl6ne: Ppng Doeng" Discrepancy Type: Installation imp 6ernentation Om g"
SystemProcess: DGX NRC Signmcence level: 4 Date faxed to NU:
Date Published: 11/2097 D6screpancy: Walkdown Discrepancy for the DGX Descript6nn: The following discrepancy items were found during the walkdown of the piping and mechanical equipment of the Emergency Diesel Generators (DGX):
- 1. Line 3-EGA 750-13 3 is not insulated as required by spec SP-ME-691.
- 2. Line 3-EGA-375-30-3 is not insulated as required by spec SP.
ME-691.
- 3. Flow element 3EGF*FE31 A mfg. data (bore) is illegible due to label being painted.
- 4. Restricting orifice 3EGF*RO20C mfg. data (bore) is illegible due to the label being painted.
- 5. Restricting orifice 3EGF*RO20A mfg. cata (bore)it lilegible.
- 6. Flex hoses 3EGS* Hose 3A and 3EGS* Hose 4A- NU labels should be jnterchanged to be consistent with isomelric CP-360264 Sht 4 Rev 5 and PalD EM-116A Rev 27,
- 7. Flex hose 3EGS* Hose 6A has no NU label.
- 8. Pipe support CP-360530-H005 shown on drawing BZ-60R 40 Rev 2 has two additional iln x iln bars welded to the support to provide lateral restraint to the pipe that are not shown on the drawing. Unincorporated E&DCR T-J-06448 (copy obtained from NU's drawing vault) has incorrect subsequent pages attached to its cover page and harce could not be used to determine if the additional bars are correct.
The following material conditlan items were found during the walkdown of the piping and mechanical equipment of the Emergency Diesel Generators (DGX);these items are not censidered configuration management issues:
- 1. Valves 3EGF'V996 and 3EGF*V097 packing shows leakage.
- 2. Valves 3EGF*V25, 'V26 and*V22 stems and bodies are rusted.
- 3. Valves 3EGF*Vi1 and *V14 packing show leakage. Also the mfg. label are not legible and not all of the data could be verified.
- 4. The threaded connection on line 3-EGF-150-48-3 to the diesel
- 'p'; tree ; Of valv0 3 EOF *V990 ch0ws !00h0g0. p,9, , ,, 3 g
ICAVP DR N3. DR MP3-0652 Northea:t Utilities Miiistone unit 3 Discrepancy Report
- 5. The threaded connection on line 3-EGF 00159-3 to the diesel upstream of valve 3-EGF'V969 shows leakage.
- 6. The threaded connection on line 3-EGF 150-49 3 to the diesel downstream of valve 3 EGF'V989 shows leakage.
- 7. The threaded connection on line 3-EGF-150-45-3 to the diesel upstream of union shows leakage.
- 8. Tubing connections at valve 3EGF'V986, at tee upstream of instrument mcnifold for LS-41B, and at instrument manifold for LS-40B show leakage.
- 9. Threaded connections on stralr.ers to valves EGO *V985B,
'V9848 and 'V9833 show leakage.
Rev6ew Valid invol6d Needed Date
'1/15/S7 initietor: Reed, J. W. O O O VT Lead: Neri, Anthony A g Q Q 11/11/97 15'17/S7 VT Mgr: schopfer, Don K O O O BRC chmn: Singh, Anand K Q O O 15/17/S7 Date:
INVALID:
Date: 2/17/98
,, RESOLUTION: Disposition: '
NU has concluded that Discrepancy Report, DR MP3-0652, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98 0511 has been written to develop and track resolution of this item per RP 4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0652, has identlfied a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 It has been screened per U3 Pl.
20 criteria and found to have no operability or reportability concems end meets the Unit 3 deferral criteria. CR M3-98-0511 has been written to develop and track resolution : ' this item per RP-4.
Previously identined by NU? O ies (#1 No Non Descrepent Conditkm?O ves () No Resolution Pend 6ng?O ve. - @ No Resolution Unresolved?O ve. @ No Review
^*** ^#* * *
- initiator: Reed, J. W.
VT Lead: Nort, Anthony A VT Mgr: Schopfer, Don K IRc Chmn: Singh, Anand K Date:
Printed 2/23/9611:23.33 AM Pai, 2 of 3
DR N3. DR-MP3-0662 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report sL Comments:
k i
i j
i s
i j
f 1
PrWed 2/23S811:23:35 AM Pe3W3
DR No. DR-MP3-0661 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Review Oroup: system DR RESOLUTION ACCEPTED Reh EW: s#em W Potential Operability issue Discipline: Electrical Design O va Discrepancy Type: Calculation
@ No Syste:WProcess: DGX NRC Significance level: 4 Date faxed to NU:
Date Published: 1/1oS8 Descrepency: First Level Undervoltage Relay Setting (Calculation NL-040)
Descriptioe . Calculation NL-040 determines the sett!ng of the first level undervoltage relcys. These relays detect the complete loss of
' power to a bus. (Calculation NL-042 determines the setting of the second level undervoltage relays that respond to sustained low bus voltage. See DR-MP3-0542.)
The first level undervoltage relays operate with a 1.8 second time delay, while the bus overcurrent relays take about 1,7 seconds to clear a line to line fault. The margin of 0.1 second is short, and may result in a loss of coordinatioit between the two relays. A margin of 0.3 second is allowed for coordinating overcurrent relays at Millstone 3, which provides margin to ensure that the relays operate as intended. A longer time delay setting of relay 62V would provide greater assurance that the ma,,1 circuit breaker has had a chance to clear the bus fault and lock out the feed from the RSST, thus preventing exposing the RSST source to a fault. Therefore, a coordination margin of 0.3 second is appropriate here, also.
The calculation cites information from General Electric on the characteristics of Typo NGV undervoltage relays. However, this information is contained in an unverified telephone memorandum, According to the telephone memorandum, General Electric was to follow up the telephone conver' . tion with a letter. The letter is not included in the calculation.
f The casu, ion includes a description of the closing of the feed frot.. .. e RSST on undervoltage. No reference for this is given.
Both Calculation NL-040 and Calculation 420CB set time delay relay f'P. While the proposed setting is the same in both calculo..ons, any given relay should be set in only one calculation to ensure consistancy.
Review Valid Invalid Needed Date hittiator: Bloethe, G. William O O O 12/23 s7 VT Lead: Nort, Anthony A O O O 52/23S7 VT Mgt: schopfer, Don K G O O 52/23/97
$2/31,97 IRC Chmn: singh, Anand K G O O Date:
INVAUD:
i Date: 2/10/98 RESOLUTION: Disposition; Printed 2/23Se 55:24 05 AM Page 1 of 2 l
i
DR N2. DR-MP3-0661 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report NU has concluded that Discrepancy Report, DR MP3-0661, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 it has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria CR M3-98-0515 has been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0661, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.1701011 has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0515 has been written to develop and track resolution of this item per RP-4.
Previously identined by NU? O Yes () No Non Discrepent Cond6 tion?Q Yes @ No Resolution Pending?O ve. @ No ResolutionUnresolved?O ve. @ No Review initiator: Womer. l.
VT Leed: Nort, Anthony A b N vi mor: senopter, con x B O O IRC Chmn: singh, Anand K Date:
SL Cortments:
1 1
Printed 2/23/96112409 AM Page 2 of 2
ICAVP DR No. DR-MP3 0689 N:rthe:st Utilities utilstOne Unit 3 Discrepancy Report j Review Group: system DR RESOLUTION ACCEPTED Rev6ew Clement: system Des 6gn Potential Operability issue Discipl6ne: Electrical Desen O ves D6screpancy Type: Calculaten (O') No Systern/ Process: HVX NRC Significance level: 4 Date faxed to NU:
Date Published: 12/B/97 D6screpency: Discrepancies in Cable Calculations for Heater Feeds
Description:
The review of Calculation #69E
- Maximum Cable Lengths for Heater Feeders to Heaters with 'Aotor Driven Fans' and Calculation #127E
- Sizing Cables for Heater Branch Circuits
- HVR*FLT 1 A,1B,2A,28,3A, and 3B' identified miscellaneous discrepancies in the calculations. The specific items are as follows:
- 1) Page 2 af Calculation #69E identifies IPCEA P54-440, Table 27 as a design input for K-Tray ampacities. Table 11 should also be listed.
- 2) The actual diameters used in Table A on page 2 of Calculation #69E correspond to the maximum guaranteed values identified in the cable specification. This is non-conservative with respect to using the minimum guaranteed values identified in the cable specification.
- 3) Assumption #2 of Calculation #127E states that the cables are sized based on ampacities and that voltage drcp is not a goveming criteria. Because of the cable length discrepancies identified in item #7 and the fact that some of these lengths do not meet the criteria for maximum cable lengths established in Calculation #69E, the validity of the assumption is not readily apparent without more in depth analysis. For this reason this attribute should be addressed in the calculation by more than just an assumption, A preliminary review indicates that voltage drop may not be a concern due to the relatively high degraded voltage values at the associated buses.
- 4) Assumption #3 of Calculation #127E assumes no more than two conduits running in parallel. A review of the conduit plan drawings (e.g. Drawings EE-48A and B) has concluded that at the power feed panels for heaters 1 A,2A, and 28 there are cases of three power condults in parallel.
- 5) Assumption #' of Calculation #127E assumes no additional power cables will be installed adjacent to the analyzed conduits.
A review of the electrical Installation drawings has not identified any note or direction ensuring this limitation is maintained.
- 6) Calculation #127E states that the heater power feeds being analyzed are run in 4 inch condult. A review of the cable raceway oata report has identified that some of the conduit runs are 3 inch condult. Also, the calculation identifies all the heater feeds as #4 AWG. A review of the cable schedule data report has identified some of the feeds as #2 AWG. These differences p g in ceb! Ond-conduesize v"! affect the pertiene of the p g3
DR No, DR-MP3 0689 N:rthe:st Utilities ICAVP Millstone unit 3 Discrepancy Report calculation which analyze conduit fill.
- 7) Calculation #127E lists cable lengths for the different nicater power feeds analyzed in the calculation. These lengths are sigriif!cantly less than those lengths listed in the cable schedule data report.
- 8) A review of Calculation #127E did not identify any considerations for the portions of the power fceds which are run in cable tray.
These discrepancies are not considered to adversely impact the output of the calculations. There iire conservatisms in the calculations ensuring adequate sizing of heater power feeds. For this reason this discrepancy is rated a Significance Level 4.
Review Valid invalid Needed Date 518/97 initiator: Kleh, J. O O O 11/24/97 VTLeed: Nat. Anthony A Q Q Q VT Mor: schopfw, Don K G O O 12/i/97 12/4/87 IRC Chmn: singh, Anand K O O O Date:
INVALID:
Dele: 2/8/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0689, has identified a condition not previously discovered by NU which requires correction. This Oscrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteda. CR M3-98-0138 has been written to develop and track resolt.t.On of this item pe:
RP-4,
Conclusion:
NU has concluded that Discrepancy Report, OR-MP3-0689, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria sper ified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability creacems and meets the Unit 3 deferral criteria. CR M3-98-0138 has been written to develop and track resolution of this item per RP-4, Previously Identmed by NU7 O Yes @ No Non D6screpent Condition?Q Yes (#1 No ResolutionPending70 vos @ No Resoiutionuressoiv.d70 vos @ No Review AcceP t m M Acc$m W Me inMietor: Wernw l.
VT Leed: Neri, Anthony A 2t2ii98 wr u.,. mm O O O Page 2 of 3 Printed 2/23/9811T4:47 AM
i ICAVP DR No. DR-MP3 0689 Northea:t Utilities Millstone Unit 3 Discrepancy Report
. . - . . ~ . , . . . _
O O O -
IRC Chmn: Singh, Anand K O O O Dele:
i SL Comments:
4 a
. PrWed 2/23/9611:24 49 AM Page 3 of 3
ICAVP DR N3. DR-MP3 0715 N:rthert Utilities Millstone Unit 3 Discrepancy Report Review Group: System DR RESOLUTION ACCEPTED
- Potential Operability issue D6scipune: Electr6 cal "*"
Discrepancy Type: Calcuistxx)
O va f@ No SysterrvProcess: N/A NRC Significance level: 4 Date faxed to NU:
Date Publishea: 12/1497 D6screpancy: Discrepancies in Control Cable Ampacity Calculation Ducripuon: The review of Calculation #173E 'To Determine Ampacity of 'C' Cables Installed in Tray or Condult' identified miscellaneous discrepancies in the calculation. The specific items are as follows:
- 1)Section I.A.2 of the calculation states that for loads greater than 7.5 A a cable is assigned a *K' service. The source for this design input (i.e., installation or design document) could not be identified. CCN #1 page 1, paragraph 3 implies that the subject calculation is the design basis for this input. This same CCN (page 2) identifies instances of 'C' cables exceeding, 7.5 A.
- 2) Section 8 of the calculation identifies the equation for the correction factor due to number of cables, but omits the ratio of cable diameters from the equation. This omission is editorial in nature since the correct equation was used in the body of the calculation.
- 3) CCN #1 uses a methodology which uses 50% of calculated cable area since the loading of cables in the trays is assumed to be 50% of the allowed load. A basis for this methodology could not be identified. Also, an adjustment in direct proportion to the reduced loading is not conservative due to non-uniform heat intensity in the cable tray.
These discrepancies are not considered to adversely impact the 2 output of the calculation. There still appears to be enough conservatism in the sizing of 'C' cables to ensure adequate ampacity. For this reason this discrepancy is rated a Significance Level 4.
Review Valid invalid Needed Date initiator; losh, J- O O tr2497 G
VT Lead: Neri, Anthony A g ] Q 11/29/97 VT Mgr: schopfer, Doa K G O O 12/s97 IRC Chmn: Singh. Anand K G O O 12/s/9T Date:
INVAUD:
Date: 2/8/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0715, has identified a condi' ion not previously discovered by NU which requires correction. This discrepancy meets the criteria specified Printed 2/239811:25:17 AM Page 1 of 2
DR NS, DR-MP3-0716 Northeast Utilities ICAVP 4 Millstone Unit 3 Discrepancy Report in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or repertability concems and meets the Unit 3 deferral crit, ia. CR M3-98-0138 has been written to develop and track resolution of this item per RP-4,
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0715, has identified a condition not previously discovered by NU which requires correctinn. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-t 20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 98 0138 has been written to develop and track resolution of this item per RP-4.
Previously identified by nut U Yes ~ @ No Non Diecrepent Condet6ontO Yes @ No Resolution PendingtO ve. @ No Resolut6onUnresolvedtO vee @ No Review "Y *
- Initiator: Womer, I.
8 D D =
VT Lead: Nort, Anthony A 9 O O **
VT Mgr: schopfer, Don K IRC Chmn: singh, Anand K Date:
i SL Comments:
Yrtnted 2/23/9e 11:25.21 AM Page 2 of 2
DR No, DR-MP3 0718 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report ReviewGroup: Accoortlenaton DR RESOLUTION ACCEPTED Review Enerrent: Systern desyn Discipline: fAech6hkal Desy9 "
Discrepancy Type: Lkensing Document Ilystern' Process: N/A NRC significarne level: 4 We FMed to NU' Dete Publ6shed: 1U2G97 D6*crepancy: Natural Circulation Flow Data Cited in FSAR is Not Used in Accident Analyses.
Descrylon: The ICAVP reviewed FSAR Sections related to natural circulation subsequent to reactor trip and reactor coolant pump coastdown. The specific sections reviewed were:
- 4) Complete Lo:s of Forced Reactor Coolant Flow (FSAR
$15.3.2.2).
In these sections Table 15.2 2 is cited as the justification for natural circulation flow that is s afficient to provide adequate core decay heat removal following a reactor trip and reactor coolant pump coastdown and therefore, seceptable rapability to respond to the accidents.
IRF 01099 which responded to RFl 689, provided a Westinghouse letter (NEU 97 305E) which states *The values presmnted in Table 15.2 2 are estimates of the amount of natural circulation flow that is expected under these conditions, however, they are not used in the non-LOCA safety analysis in any way.'
Specific sections of the FSAR where credit is taken for natural circulation for non LOCA analysis are discussed below; a) FSAR $15.2.6.3 for accident 1) above states ' Conclusions .
Analysis of the natural circul,: lion capability of the RCS has demon.=trated that sufficient heat removal capability exists following reactor coolant pump coastdown to prevent fuel or clad dama,e.'
b) FSAR $15.2.7.2 for accident 2) above states ' Method of Analysis. Assumptions mede in the analysis are as follows. 3. ,
For the case with a loss of off. site power, a heat transfer coefficient in the steam generator associated with RCS natural circulation.'
c) FSAR $15.2.8.2 for accident 3) above states
- Method of Analysis . The code describes the plant thermal kir stics, RCS inriuding naturel circulation, . .* Also this sectiore states
'Followine '- trip of the reactor coolant pumps, there N a flow coastaenn until flow in the loops reaches the natural circulation value.'
rn F.q$ 'll 9 9 fnr nerMant_d@y@tet 'The rnAr9nr Page 1 of 3 Printed 2/2T9611M44 AM
DR No, DR-MP3-0718 l Northeast Utilities ICAVP Millstor.e Unit 3 Discrepancy Report coolant pumps continue to coastdown, and natural circulation flow is eventually established, as demonstrated in Section 15.2.6.'
Nu should compare the Millstone 3 fuel reicad analysis of record with FSAR $$ 15.2.6,15.2.7,15.2.8 and 15.3.2 to determine if the values in FSAR Table 15.2 2 are used.
Review Vdd invahd Needed Date .
$2/a/97 InMetor: Peetnet, W. R. O O O VT Leed: Ratoja. Raj 0 0 0 0 12 taro 7 ,
VT Mgt: schopfer, Don K O O O 12/11/97 12/ifd97 1RC Chmn: singh, Anand K Q Q Q 0.ie:
INVAUo:
Dete: 2/20/98 RESOLUTION: Disposition: NU has concluded that the issue reported in Discrepancy Report D,' MP3-0718 does not represent a discrepant condition.
Westinghouse Letter NEU 97 30$E, dated Novembnr 21,1997, responded to Sergent and Lundy questions regarding the adequacy of FSAR Table 15.2 2 for use in the analysis of the feedline break event by desutbing the purpose of FSAR Table 15.2 2. This letter states the values presented in FSAR Table 15.2 2 are not utilized in any non LOCA safety analysis.
Westinghouse, as the Fuel Vendor for Millstr.,ne Unit 3, has reviewed the request for NU to compare the Millstone 3 Fuel Reload Analysis of record with FSAR Sections 15.2.6,15.2.7, 15.2.8 and 15.3.2 to determine if the values in FSAR Table 15.2
? are used. Westinghouse responded to this request in Letter NEU 98 510, dated February 6,1998 and again stated the data is not used in any of the non LOCA transient analyses.
Westinghouse Indicates the informction in the subject table is used to validate the analytical model used to perform this portion of t5e Chapter 15 safety analysis. This letter states that by showing that the actual natural circulation flow determined from the startup tests met or exceeded the values in Table 15.2 2 at inillal startup, the validity of the transient analysis natural circulatso model is confirmed. The letter further states that the emount of natural circulation flow for these events that assume a loss of forced reactor coolant flow is calculated by the computer code (LOFTRAN) based on transient conditions.
Westinghouse Letter NEU-98 510 indicates that changes were made to FSAR Section 15.2.6, via FSAR change 97 MP3-42, in order to clarify the application of this table. Additionally, Westinghouse provided proposed wording that can be incorporated in the FSAR if NU determines that the discussion on natural circulation flow within the FSAR requires additional clarification.
CR M3-98-Of.,87 was written on 2-6 98 as an enhancement CR to Page 2 of 3 Pnnted 2/23% is M 48 AV
DR No. DR4AP3-0718 Northeast Utilities ICAVP Miiistene unit 3 Discrepancy Report request that the FSAR clarifications, provided by Westinghouse, be evaluated forincorporation into the FSAR if NU review determines they are necessary.
Conclusion:
NU has concluded that the issue repurted in Discrepancy Report DR MP3 0718 does not represent a discrepant condition. Westin0 house Letter NEU 98 510, dated February 6th,1998, confirmed again that the data contain0d in FSAR Table 15.2 2 is not used in any of the non LOCA transient analyses but rather was L'tllized to validate the analytical model used to perform this portion of the Chapter 15 safety analysis.
The letter states that the amount of natural circulation flow for these events that assume a loss of forced reactor coolant flow is calculeted by the computer code (LOFTRAN) based on transient conditions.
Westinghouse has provided additional clarification, via this letter, that can be added to the FSAR to ensure the purpose of Table 15.2 2 is not misunderstood by those not familiar with non-LOCA tr6nsient analysis methodology, CR M3 98 0687 was written on 2 6-98 as an enhancement CH to request the recommended clarifications be evaluated for incorporation into the FSAR if NU review determines they are necess'.ry.
Attachments:
Westinghouse Letter NEU-98 510, dated February 6th 1998 CR M3 96-0667 Previously identired t>y Nu? O Yes @ No Non Discrepant CondNionfU Yes (@ No Reso:utkm Pending?O ve. @ No Re.oiutkmunreso#vedrO v . @ No Review Acceptable Not Accepable Needed Date initiator: Peebles. W. R.
G O O m VT Lead: Raheia.RajD O O O m VT Mgr schopter. Don K O O mm 1RC Chmn: singh, Anand K O O O Date: 2/20/98 sL ce ments: Bn:ed on the information contained in the Westinghouse letter, NEU 98 510, ICAVP agrees with the resolution of tr.Is item.
However, because the FSAR is NU's design basis for the olant, ICAVP resommends that the FSAR revisions provided Iri NEU 510 be incorporated into the FSAR.
Further, based on NU's response, ICAVP is changing the severity level from 3 to 4.
Page 3 of 3 i Printed 2/239e 1t25 50 AM l
DR No. DR MP3-0720 Northea4t Utilities ICAVP Millstone Unit 3 Discrepancy Report Rev6ew Group: Confguraten DR REs0LUTION ACCEPTF.D
'# # Poteistial Operabilny issue Discipline: I & C Des 6pn Om D6screpancy Type: Drawing 4 g, system' Process: N/A NRC signincance level: 4 Date Faxed to NU:
Date Pubilshed: 12/1497 Discrepancy: Drafting / Drawing Errors
Description:
- he following drawing discrepancies were noted during the documentation review for the systems.
- 1) Drewing EK 26A Rev.14 inconectly identifies 3SWP FT59C as 3SWP PT 590.
- 2) Drawing 2J72.710-392 336, for Foxt '"+rument Cabinet 3CES IPNLl12 erroneously associates 4C 1. urr,ents to a 3CWS loop by the title of the drawing.
- 3) Test loop diagram 25212 00348, Sheet 1. Rev. 2, erronaously identifies instrur:6ent 3RSS TY21 A, Iccated in Cabiaet 3CES-IPNLl12. as 3RSS-TY21.
Review Val 6d invol6d Needed Date
$ 5'25'87 inattetor: server, T. L O O O 11/2B97 VT Lead: Nort. Anthony A Q Q Q 12s57 VT Mgr: schopfer Oc.;K O O O 42/s57 IRC Chmn: Singh. Anand K O O Date:
INVALID:
Dete: 2/8/98 RESOLUTION: Disposition; NU has concluded that Discrepancy Repod, DR MP3-0720, has identified si condition not previoutly discovered by NU which regelret, correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 Pl.
20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0164 has been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0720, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability i concems e.nd meets the Unit 3 deferral criteria CR M3-98 0164 has been written to deveiop and track resolution of this item per RP-4.
Page i of 2 Printed 9./7%811:26:16 AM
. _ . - . __ - . ._.__-_ __ _ _ _ . . ,__ _ - _ _ _ . . . _ _ = - . _ . . . __._
1 1
DR No. DR MP3 0720 Northea st 0:ihtles ICAVP Minstow thR 3 Discrepancy Report Prev 60usly identifbed ley nut O Yes (c) No Non Descrepent Candet6ontO ves @ No Resolullon Pending?O ve. (6) No Re.oiuiian unre.oevedtO vee c6) No Review Inlinator: Womer,L VT Leed: Nort, Anthony A VT Mgr: Schopter. Don K 1
IRC Ctwnn: Singh. Anand K Dele SL Comments:
Page 2of 2 PrW 2/239011:26:20 AM
ICAVP DR N . DR 6..P3 0721 Northeast Utliities Millstone Unit 3 Discrepancy Report Review Group: Confguraton DR RESOLUTKW ACCEPTED Review Eternent: System installaton Discipl6ne: I & C Des 6pn Discrepancy Type: Instolisten trnplementsten Om SysterrvProcess: SWP NRC Signinconce level: 4 Date F AKed to NU:
Date Published: 12/1497 D6screpancy: Grounding not in accordance with specification D**ctlption: ElectricalInstallation Specification SP E 350, Rev. 9 sets forth installation / condition requirements for grounding of instruments and raceways connect 5g to instruments / field devices, in addition, instrurnent vendor manuals provide for the grounding requirements and maintenance of grounds. The following cond!tions not consistent with the above referenced requirements were observed during the system walkdowns.
- 1. Instruments 3SWP'PDIS 24A, B C, D, and pressure transmitters 3SWP PDIS 110A, B, C, D located in intake structure / pump house have instrument grounds which, in general, show considerable oxidation and lack the necessary 3-Inch ' slack loop
- In the ground wire required by SP E 350 3.3.11.
- 2. The required 3-inch ' slack loop
- in the ground cables required by Specification SP E 350-3.3.11 has not been provided for the following instruments:
3SWP FIS41 A00 Drawing BK 16F 651 3SWP PS152800 Drawing BK 16P-67 6 The following material conditions were noted during the walkdown. These are not confouration management .ssues.
- 3. The ground wire for instrument 3SWP*PS152B, reference BK-16P-67-6. shows excessive signs of oxidization / corrosion.
- 4. Instrument ground wire cable for 3SWP'PS152A, reference drawing BK 16P-67-6, is disconnected from flex condult.
Review Valid inval6d Needed Dtte initiator: server, T. L G O O ti/2s97 VT Lead: Nort, Anthony A y D ] 11/2997 VT Mgt: sctwpfe , Don K g g O 12/597 O 12/a97 IRC Chmn: singh, Anand K O O Dei.:
INVAUD:
Date: 2/8/98 RESOLUTION: Disposition:
NU has concluded that Discrt:pancy Report, DR MP3-0721, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter 816901 und 17010. It has been screened per U3 PI-Pnnted 2/239611:26 46 AM Page 1 of 2 1
Northe:st UtilHies ICAVP DR No. DR-MP3 0721 Millstone Unit 3 Discrepancy Report 20 criteria and found to have no operability or reportability concems and meets the Unit 3 r'eferral critetta. CR M3 98-0165 has been written to develop ano track resolution nf this item per RP-4.
Conclusion:
NU has conclude:I that Discrepancy Report, DR MP3-C721, hLs identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter 816901 and 17010. It has been screened per US Pl.
20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 98-0165 has been wntien to develop and track resolution of this item per RP-4.
Prev 6ously Hentined by NUF V Yes (S) No Non Descrepent Condet6ontO Yes (e) No n..oivison Pendiner O ve. (i>No Re.owon unresoev seO Yen (5) No Review initiator: Warnst,l
^** ***
- VT Leed: Nort, Anthony A O O O **
VT Mgr Schopfer, Don K IRC Chmn: Singh. Anand K om.:
sl conwnents:
Printed 2/219611:26.5o AM Page 2 of 2
~ -
DR No. DR MP3 0722 Nintheast Utilities ICAVP Millstone Unit 0 Discrepancy Report
( DR RESOLUTION ACCEPTED Review Group: Confguraten I M
- Potent 6al Operability issue Discipline: I & C 006199 O Ya Discespancy Type: Installstkm implementaten M No systerr#rocess: DGX NRC significance level: 4 Date F Axed to NU:
Date PuMished.12/14s7 biscrepancy: Grounding not in accordance with specification
?
Description:
Electrical Installation Specification SP E 350, Rev. 9, Section 3.3.11 sets forth Installation /condulon requirements for grounding of instruments and raceways connecting to instruments / field devices. These "equirements includs a 3-lach ' stack loop
- In the ground wire. Contrary to this requirement, the following installations do not have the 3 inch slack loop:
3EGF.LS28A 3EGF.LT29A 3EGD-PDIS25A Review Valid inval6d Needed Dole O ist2ssT initletor: Server. T. L O O ist2SS7 VT Lead: Nort. Anthony A B O O 12/sS7 VT Mgr: Schopfer. Don K O O O
$2/$S7 1Rc Chmn: Singh, Anand K O O O D.i.:
INVALIO:
Date: 2/20/98 RESOLUTION: Disposition: .
NU has concluded that Discrepancy Report, DR MP3-0722, has identified a condition not previously discovered by NU which requires correction. This d;screpancy meets the criteria specified in NRC letter B16901 and 17010. it has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets '.he Unit 3 deferral criteria. CR M3-98-0165 has been written to develop and track resolution of this item per RP / .
Cone.lusion:
NU has concluded that Discrepancy Report, DR MP3 0722, hrs identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 Pl.
23 criteria and found to have no operability or reportability concems and meets the Unit 3 deferr1il criteria. CR M3 98-0165 has been written to develop and track resolution of this item per RP-4.
Previously identifed by NU7 Q Yes @ No NonDiscrepantCondetkm?O Yes @ No Page 1 of 2 Prtried 2/23s011;32.40 AM l
ICfVP DR No. DR-MP3-0722 Nertheast Utilities Milistone Unit 3 Discrepancy Report Resolut6on Pend 6ng?U Yes (9) No ResoM6onUrwesolved7U Yes ie) No Review inttnetor: Womer. l.
VT Load: Nwl, Arthony A VT Mgri Gchopfer Don K b IRC Chmn: SWgh, Anand K Date:
$L convrants:
Printed 2/239811:32.44 AM Page 2 oE
DR N2. DR MP3 0722 Northeast Utilities ICAVP l Millstone Unit 3 Discrepancy Report Rtview Group Confguraten Re view Elemerd: System tratahation D66cipl6ne: I & C Dt+ign Discrepancy Type: Instanaten implorrentaten Date Faxed to NO:
Discre;*ncy: Grounding not in accoidance with specification D**ctlptkm: Electrical Installation Specification SP E 350, Rev. 9, Sedion 3.3.11 sets forth Installation / condition requirements for grounding of instruments and raceways connectin0 to instrumontr./fleid devices. These requirements include a 3-inch ' stack-loop
- in the ground wire. Contrary to this requirement, the follouing installations do not have the 3 inch stack loop:
DR No. DR MP3 0743 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Rev6ew Group: system DR RESOLUTION ACCEPTED Rev6ew Nnem spern W Potential Operability lasue Discipline: I & C des 6gn Ow Discreparty Type: Drawing No System?rocess: DGX NRC s6gnirmarge level: 4 Date faked to NO:
Date Publishn*: 1I1D98 DiscreParwy Drawing Discrepancy . LSK 8-9A, Rev 9 Descripuon: Refstences:
1, Loop Schematic 3EGF 040A, Rev 3 for Transfer Pump 3EGF*P1 A Control
- 2. Loop Schematic 3EGF 0400, Rev 4 for Transfer Pump 3EGF*P1B Control
- 3. Loop Schematic 3EGF-041 A, Rev 4 for Transf er Pump 3EGF*P1C Control
- 4. Loop Schematic 3EGF 041B, Rev 5 for Transfer Pump 3EGF'P1D Control Per references 1 through 4 above, the Emergency Generator Fuel System Fuel Oil Transfer Pump will stop automatically !f the control switch is in ' auto *, the day tank level is high and the bypast selector switch is in *on" (not in ' bypass"). The logic diagram does not show a ' control action" of the control switch in
' auto" position to the pump stop logic.
Per references 1 through 4 above, the presence of a motor thermal overload will prevent a pump start or trip the pump if it is running. The absence of a motor thermal overload is a prer<.quisite for pt,mp r, tart; the logic diagram shows two (2) signals from the motor thermal overioad relay 49, both Qoing to the pump stop logic; there is no signal from the motor thermal overioad relay to the pump start logic.
Escutcheons for pump 3EGF*P1C control switch and bypass selector switch are missing.
Review Valid inval6d Needed Date initiator: Pnetss,H. g
O $2/it/97 VT Lead: Nort, Anthony A O O O 12/15'S7 VT Mgt; schopfer, Don K g Q Q 12/2197 D i2/stis7 1RC Chrnn: Sngh Anand K D D Date:
INVALID:
Date: 2/18/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0743, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 it has been screened per U3 PI-20 Criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 98 0514 P6ge i of 2 Printed 2/219611:36.22 AM
i i
DR No. DR-MP3 0743 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report has been w.itten to develop and track resolution of this item per RP 4, k
Conclusion:
NU hLs concluded that Discrepancy Report DR MP3-0743, .Tas identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified
!n NRC letter 816901 and.1701011 has been screened per U3 PI-20 criteria and founc' to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 96-0514 hos been written to develop and track resolution of this item per RP-4, Prev 6ously klerdift;d by NUf U Yes si No NonD6screpardCondalon?Q Yes (97No Resolut6on Poneng70 Yu @ No RuolW6onUnresdved?O va @ No Rev6ew ACColdable Not Acceptande Needed Date gng; gg VT Lead: Nort, Anthony A VT Mgr Schopfer, Don K IRC Chmn: singh, Anand K Cate:
SL Cornments:
e r
Page 2 of 2 Printed 2/23s411:3t3 26 AM
ICAVP DR No. DR MP3-0790 N:rthe:st Utilities bilistone Unit 3 Discrepancy Report Rev6ew Group: System DR RESOLUTION ACCEPTED
'** l M Poterdlel Operet46#y issue D6scipl6ne: Mechanical Design O Yo.
Diecrepency Type: Componerd Date g g,
~'
Sy 4 err #rocess: Oss NRC $6gnificence level: 4 Date faxed to NU:
Date Publ6ehed: 1/1096
~
D6*cteP*acy: ' Missing venooi~ drawing for valve 3OSS*V032
Description:
The plant computer data base, GRITS, identifes the drawing for valve 30SS*V032 as drawing number 25212 29153-00022. The com,ntter data base cross referen:es this drawing number to voiidor drawing number B 51319. Neither of thesa drawings are found in the drawing system.
Rev6ew venid invei6d Needed Date O O '2/i2/97 initiator: Feinpoid, D. J. O O O 12/isS7 VTLead: Neri, Anthony A O VT Mgr: Schopfer Don K O O O $2/23/s7 IRC chmn: Singh, Anand K O O O 2tst/s7 Date:
INVAUD:
D*: 2/20/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0790, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI 20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferrol criteria. CP M3 98-0495 has been written to develop and track resolution of oils item per RP-4, 4
Conclusion:
NU has concluded that Discrepancy RepM, DR MP3-0790, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0495 has been written to develop and track resolution of this item per RP-4.
Previously 6dentifled by NU? O Yes @ No Non Discrepent CondMion?Q Yes (ei No ResolutionPend6ng?O Yee @ No Resolut6on unresolved?O ve. @ No Review initiator: Feingold D.J.
VT Leace : Neri, Anthony A B D D =
VT b; Schooler DonK Printed 2/239811:37:19 AM ,
Page 1 of 2
ICAVP DR N3. DR4AP3-0790 Northeast Utilities Millstone Unit 3 D screpancy Report mcc : sh, [
Date: 2/20/98 sL corrmnts: The intended corrective action is not apparent from the Northeast Utilities dispositian or from condition report CR M3 98-0495.
However, the corrective action is apparent from the discrepancy report. This corrective action should be to obtain a vendor drawing or prepare a vendor drawing for valve 30SS*V032 and to verify that the drawing is consistent with system requirements, Printed 2/239611:3022 AM Page 2 of 2
DR Nr. DR MP3 0870 Northeast Utilities ICAVP Mllistone Unit 3 Discrepancy Report Review Group: System DR RESOLUTION ACCEPTED Review Element: 3fstem Design Potentiel @ebimy issue Disctrine: Electrw De'*" O Yes Discreperry % ype: Componerd Data
@ No System / Process: MA NRC $6gnifncence level: 4 Date faxed to NU:
Date Published: 1/1D96 Descrepency; Calculation Discrepancies in Nomenclature and in Representing Data Descr6ptlon: A. Calculation SP M3 EE 342 (Rev.1)
The equipment number'3HVR*FLT 3B JB3B'is incorrectly shown as '3HVR*FLT 33 JB3B' throughout the calculation.
B. Calculation NL 025 (CCN #8, ReV. 3)
The equipment number *3HVR*FLT3B'should be
'3HVR*FN138'in Attachment 4 Page 15.
Review Val 6d inval6d Needed Date O 12/ias7 intilator: Kendall. 0. J. O O VT i eed: Neri, A:dhony A g Q [ 12/1&97 O 12r2297 VT Mgr: Schopfer, Don K O O IRC Chnwn: $1ngh, Anand K g Q Q 12/31/97 Date:
INVALID:
==
Date: 2/18/98 RESOLUTION: Dispositlon:
NU has concluded that Discrepancy Report, DR MP3-0820, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria spec,ified in NRC letter B16901 and.17010 It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0515 has been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0820, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 ft has been screened per U3 PI-20 criteria and found to hs.ve no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0515 has been written to develop and track resolution of this item per RP-4.
Previously identifled by Nu? O Yes (8) No Non Discrepent Condit6on?Q Yes (8) No Resolution PendingtO ve. @ No Re.oiuiion unr..oiv.d?O ve. @ No Review Acceptab6e Not Acceptable Needed Date w-am u nJ Printed 2/239611:36:33 AM Q"Mr2
ICAVP DR N3. DR MP3 0820 Northeast Utilities
[ Millstone Unn 3 Ditorepancy Report VT Leed: Heri, Areony A O O O $$ $*
O O O r2iS8 v r u,n setope,, % g mm RC Chmn: Grgh, Arend K J O O J O w .:
EL Conants:
PrWed 2C19611:36 37 AM P 2 of 2
Northeast Uti'ities ICAVP DR N3. DR MP3 0825 Millstone Unit 3 Discrepancy Report Review Group: System DR RESOLUTION ACCEPTED Review Eles.wnt: System Design p mscipl6ne: tiem Deson D6screpency Type? Dravang O ve.
g g, systerWProcess: DLX NRC signifgence level: 4 Date faxed to NU:
Date Pubinshed: 1/1096 Discrepency: AC Elementary / Schematic diagrams do not rnatch the wiring diagrams.
Descripuon: a) There are cases where the AC Elementary Diagrams do not match the wiring diagrams in regards to the connections of the current transformer secondary, as examples:
AC Elementary Diagram EE 21R, for Service Water Pump 3SWP'P1 A Indicates that terminal point B3 is connected to point 5 of the 3000/5 current trans'ormer (item ZC as identified in the wiring diagram). Wiring dia0 ram 25212 39010 sht.447 Indicates that the terminal point B3 is connected to po'nt 5 of the 100/5 current transformer (item ZB as identified in the wiring
~
diagrams). The wiring diagram does Indicate the correct wiring at the respective current transformer terminals, but not at the terminal blocks. Similar conditions exist on the Service Water Pump 3SWP'P1C tenninal point C2 (on the 50/5 current transformer) and on the CVCS Charging Nmp 3CHS*P3A terminal point B2 (on the 3000/5 current transformer).
Other similar conditions are located on the 3000/5 current transformer connections for 3CCP'P1C (terminal point B4) and for 3CHS*P3B (terminal point B2). Ref. AC Elementary Diagrams EE 21N, EE 21V, & EE 21Y.
b) AC Elementary Drawing EE 21W indicates a 2300 ohm grounding resistor for the 4200/120 Vac potential transformer 34D-2H. The wiring diagram 25212 39010 sht. 491 indicates a resistance value of 223 ohms, c) AC Eleraentary Drawing EE 21X indicates th1t the directional overcurrent relays (67NTB & 67NAR), in the Diesel Generator Neutral CT circuit, are connected in series with
- terminal 5' of 67NTB connected to the X1 terminal of the Aux CT and " terminal 6' of 67NTB connected to
- terminal 5' of the 67NAR relay. The corresponding wiring diagrams indicate that
- terminal 6* of 67NTB is conhected to the X1 terminal of the CT and ' terminal 5' of 67NTB is connected to
- terminal 6* of 67NAR, d) Schematic diagram ESK SDS Indicates that contact 15 from Agastat timing relay 62W 3ENSB02 is connected in between contacts from lockout relay 66HGB 3ENSB07 (contact 11) and from the 'DG Ready to Load' relay 3 3EGSB05 (contact 8 2).
The corresponding wiring diagrams indicates that contact 8-2 (3-3ENSB05) is wired in-between contacts 1 5 (62W 3ENSB02) and contact 11 (86HGB-3ENSB07).
Review Valid invalid Needeo Date l
trilietor: Morton. R. 12/1897 i 8nnted 2/219611:3017 AM Page 1 of 2
Northecst UtilHies ICAVP DM No. DR-MP3 0826 Mllistone UnN 3 Discrepancy Report _ _
insi6etor: Morton, R.
VT Leed: leert, Artwy ^
O Q-Q 12d&S7 R O O 12nas7 i l
i VT Mgr: Schopfer, Don K Q Q Q 127197 1RC Chmn: Sinch. Anand K Q _
Q __Q 1/sse Date:
twAuo:
Date: 2/18/98 RESOLUTION: Djsposition:
NU has concluded that Discrepancy Report, DR MP3-0825, has identified a condition not previously discovered by NU which requires correction. This discsepancy meets the criteria specified in NRC letter B16901 and.17010 it has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3 98-0514 has been writtt ' to develop and track resolution of this item per RP 4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0825, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.1701011 has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria, CR M3 98-0514 has been written to develop and track resolution of this item per RP4, Previously identified by NUF O Yee @ No ten Discrepent Condit6on?O Yee @ No Resolut60n Pend 6ng?O Yee @ N. Re.o uiionunrenoi<edrO vee @ wo Review inilletor: Merton. R.
- "Y
~ e:
]
sL Commente:
1
~
Printed 2/2M811:3921 AM Pope 2 of 2
ICAVP DR No. DR MP3 0828 Northeast Utilitie.
Millstone unM 3 Discrepancy Report Review Group: system DR RESOLUTION ACCEPTED Review Eternent: System Design p Discipline: Electrical Deongn O va D6screpancy Type: Drewing g system?rocess: DGX NRc signifbconce level: 4 Date F Axed to NU' Date Published: t/1098 Discrepancy: 4.16 KV wiring diagram discrepancies.
Descript6on: a) AC Elementary drawing EE 21W Indicates an electrical connection between the NGV undervottage relay (de'.lce 270) terminal point 5 and the synchronizing relay (GXS) terminal point
- 6. This connection is made through terminal block KK point 9.
Terminal point KK 9 indicates a connection to the undervoltage relay, device 27D point 5 (ref. drawing 25212 39010 sht. 491).
The undervoltage relay (device 270) does not indicate a connectiori to Terminal point KK 9 (ref. drawing 25212 39010 sht. 492). A similar condition exists on drawing 25212 39010 sht 440 tetween terminal pnint KK 9 and the HGA alarm relay 74D terminal point 5 (ref, AC Elementary drawing EE 21P).
b) Wiring diagram 25212 39010 sht. 493 Indicates a connection from terminal block G points 7 & 8 to handswitch (device 43) points 14C & 18C. Synchronizing handswitch (device 43) is shown on wiring dia0 rum 25212 39010 sht. 494. Wiring diagram 25212 39010 sht. 494 does not indicate a connection at device 43 points 14C & 18C.
Review Valid invalid Needed Date initiator: Morton, R. O O 12/iaS7 O
O O $2/sas7 VT Lead: Nort. Anthony A O VT Mgr: schopfer, Don K O O O 12/2sS7 IRC chrnn: singh, Anand K O O O i2rsiis7 Date:
ItNALID:
De;e: 2/17/98 REs0LUTION: Disposillon:
NU has concluded that Discrepancy Report, DR MP3-0828, has identified a condition not previously divovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 It has been screened per U3 PI-20 criteria and found to have no operability or reportability concems snd meets the Unit 3 deferral critoria. CR M3 98-0514 has been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy > port, DR MP3-0828, has identified a condition not previously .mvered by NU which requires correction. This discrepancy meets the criteria specified in NRC letier B16901 and.17010 N has been screened per U3 PI-Prinled 2/229011:39.49 AM Page 1 of 2
N:rtheest Utilitic , ICAVP DR No. DR-MP3 0828 Millstone Unit 3 Discrepancy Report 20 criteria and found to have no operability or reportability concerns and rneets the Unit 3 deferral csiteria, CR M3 98-0514 has been written to develop and track resolution of this itern per RP 4, Prev 6ously identif6ed by NU7 (,) Yes iti No MDiscrepent Condetkwi?O Yes if No Resolution Pending?O Yee v No a. oiutumunre.oived70 Yes 'M No Rev6ew Acceptable Not Acceptable Needed Date gngg,; gg g, VT Leed: Neri, Anthort/ A VT Mgr: Schopfer, Don K IRC Ctann: Singh, Anand K O O mt*
oeio:
O O O SL Conenents:
V Printed 2/239811:39 53 AM Page 2 of 2
Northeast Utliities ICAVP DR No. DR MP3 0838 Mllistone Unit 3 Olscrepaficy Repont Review Groge System DR RESOLUTION ACCEPTED Potential Operatilisty issue Diecipiene: Doctrical Design Discrepancy Type: Drawing Om 4g systerWProcess: DGX ~-
NRC signinconce levof: 4 Dete faxed to NU:
Date Putdiohed: 1/1096
! 06screpancy: Schematic diagrams and logic diagrams do not match.
Descrir4 kin: a) Schematic diagram 25212 39241 sht. 4 (12179-2447.300-004) indicates that the services shown are applicable to both i 3EGS*EG A & D. The same services are shown on schematic
%agr.l.n 25212 39241 sht.169 (12179 2447.300169).
Schematic diagram 25212 39241 sht 169 indicates that the services shown are applicable a only 3EGS'EG B. Hence, there appears to exist two separate drawings for the same 'B' services, b) Scherc,3 tic diagram ESK 8KJ indicates contact A8-B6 (mcIntenance contact) from handswitch 43-EGS*EG A is in parallel with the series combination of contacts from devices TSR (Test 6 tart Relay), XK 90 (sequencer contact for LOP / SIS /CDA), and conta. cts 26 & 27 (remote contact) from i
bandswitch 43FT EGS*EG A. The corresponding logic diagram '
l LSK 24 9.3J does not account for the remote contacts (26 & 27) l from handswitch 43FT EGS*EG-A. l c) Logb diagram LSK 24 9.3J Iridicates the inputs from PushbuttonWB1, PB2, PB3, PB4, along with lockout relays ,
86HBU & 8' HBP provides a signal to the Shutdown Relay, both directly ano through the 140 second timer, via 'OR* logic. The schematic diagram ESK 8KJ indicates the signal from the pushbuttons and lockout relays, to the shutdown relay, is through the 140 second timer only. See similar circuit on LSK 24 9.3P d) Logic diagram LSK 24 9.2A for the Emergency Diesel Generator breakers (3 ENS'AC'3 G A & B) indicates two bus undervoltage inputs in the breaker closing circuit. The logic diagram indicates the two bus undervoltage inputs are made from a *2 out of 4' logic scheme using four NGV undervoltage relays (27A, B, C, & D) and the bus undervoltage relay 27R-3ENSA18, the two inputs come from a variation of these five relays. The corresponding schematic diagram ESK SDR indicates a single bus undervoltage relay (27R 3ENSA18) contact is used as a permissive in the breaker closing circuit.
The schematic does not indicate a *2 out of 4' undervoltage logic scheme is associated with the DG breakers. Similar for schematic ESK SDS (3 ENS *ACB-G 8),
e) Logic diagram LSK 24 9.3L Indicates that a 'not' Manual Start Block permissive is required for the DG panel feed breaker close circuit and that a LOP / SIS /CDA permissive is required for the breaker trip. The logic diagram does not indicate any thermal over%ad/ loss of control power permissive. The schematic diagram ESK-6ABP does not indicate a Manual Start Printed 2/239811:40:24 A'M W oge 1 of 2
ICAVP DR No. DR MP3-0838 Northeast Utilities Millstone Unit 3 Discrepancy Report schematic indicates the permissive required for both a close and trip of the breaker is a L.OP/ SIS /CDA signal and thermal overload.
Review Ved inv ed Needed Date 12/iaS7 initnetor: Morton, R- 0 0 O
- S7 vit.ed: Nwt,ArewyA O O O O 12/2ss7 VT Mgt: Schopfw, Don K O O O '2/3'/97 IRc chmn: Singh, Anand K O O Dei.:
INVALID:
Date: 2/18/98 RELOLUT10N: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0838, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B18901 and,1701011 has been screened per U3 PI-20 criteria and found to have no operaNitty or reportability concems and meets the Unit 3 deferral criteria. CR M3 98-0514 has been written to develop and track resolution of this item per RP4.
Conclusion:
NU has concluded that Discrepancy Report, DR-MP3-UB38, has kjentified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B18901 and.17010 it has been screened per U3 PI-20 criietta and found to have no operability or reportability concemi and meets the Unit 3 deferral criteria. CR M3 98-0514 has been wrt ten to develop and track resolution of this item per RP-4, Previously identined by NU7 O Yes ($ No Non D6screpent condet60n?O Yes (#1 No Resolut6on Pend 6ng70 Ye. @) No Re.oiviion unre.oiveerO ve. @) No Review initletor: Morton, R.
VT Leed: Neri, Anthory A na VT Mgri Schopter, Don K O O IRC Chmn: Singh, Anand K Date:
sL Comments:
^
Page 2 of 2 PrWed 2/239611 Ao.26 AM l
l
- - _ - _ _ ~ _ _ . _ _ _ - _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ___ _____ __ __
7 P
N:rtheast Utilitier ICAVP DR N3. DR-MP3-0443 I
Millstone unk 3 Discrepancy Report Review Group: Systern DR RESOLUTION ACCEPTED Review Elernent: System Dea 69n Pm6M Opermy luue D6ecipline: Electrical Desgn Discrepancy Type: DrawinD O vee (g) No systernProcess: HVX NRc signthcance level: 4 Date faxed to NU:
Date Published: 1/1096 DiecrePancy: Schematic diagram does not match the Electrical Timer Sett.oint Database.
Ducr6pt6on: Timing relay setpoints and ranges are typically provided in the schematics and on the Electrical Timer Setpoint Database.
inconsistencies between these two documents are identified as follows:
a) Schematic diagram ESK-6SD Rev. 8 identifies the setpoint for Agastat relay 62-3HVR*FN14A as 10 seconos. The Electrical Timer Setpoint Database (SP EE 321 Rev. 0) indicates that the setpoint is 20 seconds. Similar for relay 62 3HVR*FN140 on ESK-6SE Rev.10.
b) The model number, as provided on the schematic diagrams, for Agastat relays 62A 3HVR*FN6A (ESK-6SB Rev.10) and 62-3HVR'ACU1A (ESK-6SM Rev.11) do not match SP EE 321 Rev. O.
c) The Agastat relay type,(TDDO versus TDPU) are not consistent for relays 62A 3HVR*FN6B (ESK 6SC Rev.12) and 62 3HVR*ACU1B (ESK 6SM Rev.11).
Review Valid invalid Needed Date inittetor: Mortor' R- 0 0 0 12/1r S7 VT Lead; heri, Anthony A @ Q Q 12/1&S7 12/23,97 VT Mgr: schopfer, Don K Q Q Q IRc Chmn: singh. Anand K Q Q Q 12/31/97 D.te-INVALID:
Date: 2/18/S8 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR MP3-0848, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 It has been screened per U3 Pl.
20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0495 has been written to develop and track resolution of this item per RP 4.
Conclusion:
NU has concluded that Discrepancy Repert, DR MP3-0848, has identified a condition not previously discovered by NU which Printed 2/225311:42.31 AM Pope 1 of 2 l
ICAVP DR N3. DR MP3 0848 l N:stheast Utilities Millstone unit 3 Discrepancy Report /
requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 it has been screened per U3 Pl.
20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria, CR M3 98-0495 has been written to develop and track resolution of this item per RP4, Previously identifed by NU? C) Yet iti No NonD6ecrepentCondet6on?O Yes @ No Resolution Pend 6ngtO veo <*) No Resoiuisonunresoeved?O ve. 4) No Review <
lnutetor: Morton, R.
VT Leed: Nort, Anthony A VT Mgri Sc.hopfer, Don K IRC Chmn: Singh, Anand K Date:
SL Correm..is:
}
Printed 2/2T9811:42.35 AM Pege 2 of 2
DR No. DR MP3 0468 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Review Group: system DR RESOLUTION ACCEPTED
'
- M** '
Potential Operab6fety issue D6scipline: Pip 6ng Depgn D6screpancy Type: Calculaton Om j"
syeterr#rocess: HVX NRC signincance level: 4 Date faxed to NU:
Date Published: 1/17/98 06screpancy: Pipe stress analysis has unverified assumptioni, and drawing incorporation anomalies
Description:
During review of HVR system i & C tubing stress analysis, NP(F) EK515003 XD REV. O we noted the following discrepancies:
Assumption 8 on page 14 requires confirmation.
Change Request Notices ICRNs EK 515003-1010 to 1015 were incorporated in isometric EK 515003 Rev. 4, but in the process the following anomalies were created:
ICRN 1012 specifies a safety class break before valve V149.
PalD EM 148D-8 and isometric EK 515003-5 s.sth show the safety class break after the valve.
Dimensions shown on isometric EK 515003 5 do not match the dimenslens specified on ICRN's 1010 and 1012.
Review Valid inval6d Needed Date
$2/22/97 inittetor: Jaln, R. C. O O O VT Leed: Neri. Anthony A g [ O 12/20/97 O i2/2sS7 VT Mgr: Schopfer, Don K O O 5'13/98 IRC Chmn: 56ngh. Anand K O O O Date:
INVALID:
Date: 2/20/98 RESOLUTION: Disposition: Response ID: M3-IRF-01704 NU has concluded that Discrepancy Report, DR MP3-0868, has identified a condition not previously discovered by NU which requires correction. This d!screpancy meets the criteria specified in NRC letter B16901 and.1701011 has been screened per U3 PI-20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0515 has been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0868, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.1701011 has been screened per U3 Pi-20 criteria and found to have no operability or rtportability Printed 2/239611:43.o7 AM Page 1 of 2
DR No. DR MP3 0868 Northeast U'.llitias ICAVP Millstone Unit 3 Discrepancy Report concerns and meets the Unit 3 deferral criteria. CR M3 98-0515 has been written to develop and track resolution of this item per RP 4.
Previously identified by NU7 (.) Yes fel No Non D6screpant Cond6tkm?(.) Yes (Oi No Resolution Pend 6ng?O Ye. +) No Resolut6on Unresolved?O ve. *) No Review
^** * **' *
Date: 2/20/98 st Conenents: This DR was issued for calculation and drawings deficiencies.
The corrective action required should be completed.
Page 2 of 2 Printed 2/2%811:43.11 AM
ICAVP DR No. DR-MP3-0669 Northeast Utilitl2s Millstone unit 3 Discrepancy Report Rev6ew oroup: Sptem DR RESOLUTION ACCEPTED N'# # Potenttal Operab64Ny issue Discipl6ne: Peng Design Discrepancy Type: Calculaton Om No systern' Process: HVX NRc signihcarece level: 4 Date F AXedio NU:
Date Published: 1/17/98 Discrepency: Pipe stress analysis calculation has unverified assumptions.
Descripuon: In the process of reviewing Calculation 12179-NP(B) X54002, Rev. O, we noted the following discrepancy.
The calculation dated 1982 contains the following assumptions which are stillidentified as requiring confirmation:
- 1. Drain lines leadin0 from filters 3HVR
- FLTR .1 A,18,2A, 28,3A & 3B operate at ambient temperature ( 70 F ).
- 2. ANSI Tees are used at all tee connectic'1s in this problem.
SIF for ANSI Lateral Tees are per I.O.M. from J. Goldberg, Dated 04 20 77 (EMTM 608 ).
Review Val 6d InveI6d Needed Date initiator: singh, R. O O O $5sS8
/*8 VT Lead: Nort, Anthony A O O O VT Mgr: Schopfer Don K Q Q Q 1/12/90 IRc chmn: singh, Anand K O O O 158 Date:
INVALID:
Date: 2/10/98 REs0LUllON: Response ID: M3-lRF 01705 Disposition:
NU has concluded th'e t Discrepancy Report, DR MP3-0869, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 ard 17010. It has been screened per U3 Pl.
20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0515 has been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0869, has
- dentified a condition not prevluusly discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B10901 and 17010. It has been screened per U3 Pl.
20 criteria and found to have no operability or reportabDty concems and meets the Unit 3 deferral criteria. CR M3-98 0515 has been written to develop and track resolution of this item per RP-4.
Previously identified by NU7 O Yes @ No Non Discrepant Condition?Q Yes @ No Pnnted 2/2MB 11:43 38 AM Peg,1 of 2
DR No. DR4AP3 0369 Northeast Utilities ICAVP Miiistone Unit 3 Discrepancy Report Resolut'on Perdng?Q Yes (*) No Resolutkmunresolved?Q Yes (e> No Review inttletor: Prekas',,A.
O O O mm VT Lead: Nort, Anthony A VT Mgr: Schopter, Don K 1RC Ctwnn: Sngh, Anand K =
Dete:
SL Conynents:
~
page 2 of 2
~Prtrted 2/21'9611:43 42 AM
DR Ns, DR-MP3-0975
- N2rthea:t Utilitbs ICAVP Millstone Unit a Discrepancy Report Review Orwp: Cc.nrigurohon DR RESOLUTION AccErTED Potent 6el Operab4Hty lasue rMacipline: Nph0 De.iD "
O va o Discsopency Type: Drawing (g g Systerr#rocess: SWP NRC Sigt.;f6cence level: 4 Date Faxed to NU:
Dete Published: 1/2G/98 Disc <epency: Upper Tier to L.ower Tier Drawings Review for SWP in the ESF
, Building h
Description:
The Upper Tier to Lower Tier drawing' review found the following draw'.ng discrepency on the as built isometric drawings for the ESF Building:
- 1. On isometric drawing Cl-SWP-210 Sht 3 Rev 10 piping support PSR-135 should be labeled PSR 165.
Review 1 Val 6d invol6d Needed Date b initi. tor: Rosa. J. W. Q O Q 1/1s/98 VT Leed: Neri, Anthony A B O O 1'15'S8 VT Mgr: Schopfer, Don K Q O O t/2a/9e IRC Chrm: singh, Anand K G O O ir22/98 3
Date:
INVALir9 D6.e: 2/17/98 RESOLL' TION: Disposit;on:
NU has conciuded that Discrepancy Report, DR4'23-( " has identified a condition not previously discovered by N- ich requires correction. This discrepancy meets the critens specified in NRC letter bib 901 and.17010 It has been screened per U3 Pi-20 criteria and found to have no operability or reportability 8
concems and meets the Unit 3 deferral criteria. CR M3-98 0648 nas been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0975 has identified a condition not previously discovered by NU which requires correction. This L%crepancy meets tho criteria specified in NRC letter B16901 and.17010 It has been screened per U3 PI-20 criteria and found to have no operability or reportability I
concerns and mesis the Unit 3 deferral criteria. CR M3-98-0648 has been writtwl to develop and track resolution ci ltils item per RP-4,
~ Prev 6ously identifled by NUr Q vos @ No Non Discrepent r ww26onrO Yes (*) No Resolution Pending70 ve. (*D No Resoiuiion unre.oived70 ve. (*) No Review inmotor: Reed, J. W.
VT Leed: Nori, Anthony A
, VT Mgt: schopfer, Don K IRC Chrnn: Singh, Anand F.
Date:
' Printed 2/23/9811:44:21 AM Page 1 of 2
ICAVP DR No. DR-MP3 0975 6, Ntrtheast Utilities Millstone unn 3 Discrepancy Report SL Commerits:
\
K r
/
7 s
L E
. 'jI '
Printed 2/23S611. 74:24 AM Page 2 of 2 l
^
1
i DR N2, DR.MP3-0072 Northeast Utilities ICAVP Millstone unM 3 Discrepancy Report Review Group: System DR MSOLUllo6 "* EJECTED ,
"* N'* Potential operability issue Discipione: Mechermi Design Discrepancy Type: Licensks Docust Om
@ ho SysterrvProcess: RSS NRC $6cedficemlavel: 4 Date faxed to NU:
Dete Published: 12m97 D4screpancy: Discrepancies on P&lD EM 112C Revision 16 are as follows:
Du.viption: l tem i h
P&lD EM-112C shows miniflow reckculation lines for containmen'. recirculation pumps,3RSS*P1 A and 3RSS*P1B.
Each mlniflow recirculation line is shown to contain a normally open motor operated valve and a flow restricting orifice. Each s
motor operated valve in the miniflow recirculation lines is
} provided with an interiock to a flow transmitter on the respective
_)
pump discharge. According to the Design Euls Summary Document,3DBS-NSSS-033, Revision 0, Section 12.5.3.2, the a interlock shall function to close the miniflow recirculation valves on RSS pump high discharge flow rate and open them on low flow rate.
The ,lerlocks are shcwn on the P&lD EM 112C as follows:
Miniflow Recirculation Flow Interlock Line MOV Transmitter Function r
3RSS*P1B 3RSS*MOV38B 3RSS*FT38B hv Flow, Close 3RSS*P1A 3RSS*MOV38A 3RSS*FT36A High Flow, Close The intertock function to open the miniflow recirculation line r motor operated valves on low RSS flow rate is net annotated such that it is consistent with the annotation fcr the close interlock function on high flow rate, item 2 FSAR Sectica 6.3.5.1 identifies that the temperature is recorderd for the outlet of the containment recirculatica coolers. P&lD EM.
112C does not show containment recirculation cooler outlet r temperature recorders, p item 3 FSAR Section 6.3.5.2 states that there is localindication of containment recirculation pump discharge pressure. However,
" PalD EM 112C only shows the local pressure transmitters, 3R."9'PT25A,B,C,0 and 3RSS*PT43A,B,C,D, and the control 700... p' : cure Indiccio:0, P!25A,9,C,D :Or the recircu!:tigr d2 P umM
ICAVP DR Ns. DR-MP3 0372 N::rthe:st Utilities '
Millstone Unit 3 Discrepancy Report pump discharge pressures. Thl: Item is duplicated in I&C Discrepancy Report DR MP3-445 which details the discrepant ,
conditions in the wiring diagrams.
Review Volki Involki Needed Date initiator: Felet Ad D.J. g g O 11/2497 11/24s7 VT t ned: Nort, Anthony A G O O VT Mgr: Schopfer, Don K @ Q ] 12/1/97 O i2/i/97 IRC Chmn: singh, Anand K G O D.ie:
- 9 INVALID:
Date: 2/20/98 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR-MP3-0072, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letters B16901 and 17010. It has been screened per U3 PI 20 criteria and found to havo no operability or reportability ccncems and meets the Ur:t 3 deferral criteria, CR M3-98-0167 has been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0072, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letters B16901 and 17010, it has been screened per U3 PI-20 criterta and found to have no operability or reportability concerns and meets the Unit 3 deferral criteria. CR M3-98-0167 >
has been written to develop and track resolution of this item per RP-4.
Provimsty idenEfted by NU7 Q Yes (#) No NonD;ecrepentCondRion?Q Yes @ No ResolutionPending70 Yes @ No ResolutionUnresolved?O Yes @ No Review
- Y
- InMietor: Feingold, D. J.
O O O =
VT Lead: Nert, Anthony A VT Mgr: schopter, Don K IRC Chmn: Singh, Anand K Date: 2/20/98 SL comments: The intended corrective action is not apparent from the Northeast Utilities disposition or frcm condition report CR M3-98-0167.
Printed 2/2356 t i:45:27 AM Page 2 of 2
Nt +m ast Utilities ICAVP DR N:. DR-MP3 0122 j Millstene Unit 3 Discrepancy Report Review Group: sptern DR RESOLUTION REJECTED Potonttal Operability lasue Discipi6ne: Electrical Design O vee Discrepancy Type: DravAng (9) No SystenWrocess: N/A NRC $6gnifncance level: 4 Date faxed to NU: ,,
Date Published: 10/18,97 Discrepancy: SchemallC and wiring drawing discrepancies at motor control centers.
Dascripuon: Various discrepancies were identified between common figures (details), as shown on the wiring diagrams, and the corresponding schematic diagrams as listed below:
- 1) Motor Control Cen.T (MCC) intemal wiring diagram (EE-9JF), figure SA indicates point 5 of contact 42 0 is connected to terminal point 4. The schematic diar em ESK 6AAA (3SWP*MOV57A) indicates point 5 os contact 42-0 is connected to point 6 of device 49X. In addition, wiring diagram EE-9Jt i indicates po;:.; 3 of contact 42-C is connected to terminal point 2 in figure 5A, Schematic diagram ESK-6AAA indicates point 3 of contact 42-C is connected to point 4 of device 49X. Similar situation for 3SWP*MOV57B (ESK-6AAB),3SWP*MOV57C (ESK-6AAC), 3SWP*MOV57D (ESK-6AAt)), 3SWP*MOV1028 (ESK-6AAV),3SWP*MOV102D (ESK 6AAX),3SWP*MOV11EA (ESK-6AGF), 3SWP'MOV115B (ESK-6AGG), 3RSS*MOV20A (ESK-6LD), 3RSS*MOV20B (ESK-6LE), 3RSS*MOV200 (ESK-6LF), 3RSS*MOV200 (ESK-6LG), 3RSS*MV8837A (ESK-6LM),
3RSS*MV8838A (ESK-6LN), 3RSS*MV88378 (ESK-BLP),
3RSS*MV88388 (ESK-6LQ), and 30! *MOV34A (ESK-6LS).
- 2) Schematic diagram (ESK-6AAX) fo, service water motor operated valve (3SWP*MOV102D) indicates terminal point 2 is in-t etwer' contact 57 58 L 52S-3SWP*P1D and contact 5-6 of 49X. Wiring diagram EE 9GB Indicates terminal point 2 is wired in the circuit between contact 57 58 of 52S-3SWP*P1D and the close torque switch (TOS17).
7; Schematic diagram ESK-6AAG (3SWP*MOV54B) indicates a connection between points 4 and 12 in the
- seal-in' portion of the open circuit. The corresponding MCC Intemal wiring diagram (TEE-9JM, figure SE) does not indicate this connection. In addition, the wiring diagram (EE-9JM, figure SE) indicates a connection between terminal points 2 and 7, the schematic (ESK-6AAG) does not indicate this ccanection. Similar for 3SWP'MOV54D (ESK-6AAJ), 3SWP*MOV50A (ESK-6AAh),
3SWP*MOV50B (ESK-BAAL), 3RSS*MOV38A (ESK-6AFL), and 3RSS*MOV388 (ESK 6AFM).
- 4) Schematic diagram ESK-6AAW (3SWP*MOV102C) indicates the use of a transfer switch (43 3SWP*MOV102C) in the control circuit. The schematic and wiring diagram (2424.100-245 sht 689) do not match in various cases. As an example, the schematic indicates point 26 of the switch is connected to terminal point TBC-8, only. The iviring dit. gram indicates and ntiriitinnnt ennnectinn in nnInt ')7 nf the enma ewitch~ Almilmr Printed 2/23/9811:46:08 AM Page 1 of 4
ICAVP DR N3. DR-MP3 0122 Northeast Utilities
- Millstone Unit 3 Discrepancy Report situation for 3SWP*MOV102A (ESK-6AAU & 2424.100-245 sht.
689).
- 5) The wiring diagrams for 3SWP*MOV102A (EE 9JM, figure SD
& EE.9FX) indicates fuse FU1 point 2 (3SWP*MOV102A) is connected in the close circuit, between the torque switch (TOS17) and TBB-47. The schematic diagram (ESK-6AAU) indicates the fuse FU1 point 2 is connected to TBB-48. '
Review Valid invalid Nooded Date initletor: Morton. R- 0 0 O st2e/97 VT Lead: Nort, Anthony A g Q Q 10/1/97 to'SS7 VT Mgt: schopfer, Don K R O O 10/1497 IRC Chmn: singh, Anand K @ Q Q Date:
INVAUo:
Date: 2/20/98 RESOLUTION: Disposition:
NU has concluded tisat issues # 1,2 and 3 in Discrepancy Report, DR-MP3-0122, have identified conditions not previously discovered oy NU which requires correction.
Issue # 1) discusses a confilet between Figure SA on EE 9JF and a number of RSS, QSS & SWP motor operated valve ESKs for the intemal wiring of the 42-0 & 42-C seal in contacts to TB1.
The present configuratiori in this figure shows the 42-0 contact wired to TB1-4 & SA and the 42 C contact wired to TB1-2 & 3A.
Atter a review of each elementary with their corresponding intemal and extemal MCC wiring drawings, it has been determined that Figure SA on EE 9JF is in error for the referenced schematics. This figure and it's assochted table should be revised for the referenced schematics to show the 42-O contact wired to TB15 & SA in lieu of TB1-4 & SA and the 42 -
C contact wired to TB13 & 3A in lieu of TB1-2 & 3A. This is drawing change caly, and will bring all the documents into agreement with this revision.
Issue # 2) A review was performed of ESK-6AAX, EE 9GB &
Figure SA on EE 9JF for the location of terminal point 2 in the closed circuit of 3SWP*MOV102D. Both intemal and extemal wiring drawings depict the locaticn of terminal point TB1-2 to be between the valve's limit / torque switch and the 57-58 contact of 52S-3SWP*P1D.
This agrees with the SWEC termination tickets "or conductor SC2 in cable's 3SWPDPC045 and 3SWPDPCOC as well.
Therefore, ESK-6AAX needs to be revised to show terminal point 2 in the same location as it's corresponding intemal and extemal ning drawings. This is a drawing change only, no field work required.
issue # 3) The referenced SWP & RSS motor operated valve Printed 2/23/9811:46:11 AM Page 2of 4
DR No. D8t-MP3 0122 I Northeact Utilities ICAVP i Miiistone unit 3 Discrepancy Report schematics were verified against Figure SE on EE 9JM to validate the discrepancy. The Figure depicts an unneeded jumper between TB12 & 7 and tiimination of a required jumper between TB1-4 & 12, by means of a deviation symbol (i.e. a darkened triangle). The darkened triangle means that an internal wire needs to be added to the Figare and is correlated with the applicable starter by the addition of this symbol to the deviation column of the corresponding table. Since the darkened triangle is not in deviation column for the referenceo schematics, the impression given is that the needed jumper appears not to be installed and unneeded jumper appears to be insialled in these starters. However, it has been determined that this symbol is misplaced in the Figure and should be moved to be to the left of the jumper between TB12 & 7. This will eliminate the unneeded jumper batween TB12 & 7 and insert the lequired jumper between '!31-4 & 12. This change has already been documented by DCN DM3-00-079197 which was approved on 7/25/97. Since this is after the 27 of May, credit could not be taken for pre-discovery. There is no additional change needed by this issue.
Conditior Report (CR) M197 3711 was written to provide the necessary corrective actions to resolve these issues. Approved Correc'ivo Action Plan (CAP) (attached) and DCN DM3-00-1765-97 were issued to correct the design drawing discrepancies. No work is required in the field.
NU also has concluded that issues # 4 and 5 in Disccepancy Report, DR MP3-0122, do not repregnt discrepant conditions.
t Issue # 4) Both schematics ESK-6AAU rev.13 and 6AAW rev.15 were reviewed against wiring drawings 2424.100-245-689 rev.E, 690 rev.E,691 rev.F & EE 3BA rev.4 for the wiring at polms 25-26-27 on the transfer switches for both motor operated valves and a discrepant condition could not be found on any of these drawings. There are no changes required by this issue.
Issue # 5) This issue implies there is a discrepant condition between Figure SD on EE 9JM rev.5,9FX rev.12,3BA rev.4 &
ESK 6AAU rev.13 for the wiring from fuse FU-F2A through TB1-2 in the MCC to TBB-48 in the FTSP. However , a discrepancy could not be Wnd during this verification process it appears Figure SD on EE 9JM was misinterpreted, because ustr.g the rieviation symbol (l. e, darkened circle) all the documents are in agreement. There are no changes required by this issue.
Conclusion:
NU has concluded that issues # 1,2 and 3 in Discrepancy Report, DR-MP3-0122, have identified conditions not previously discovered by NU which requires correction. Condition Report (CR) M3-97 3711 was written to provide the necessary corroctive actions to resolve these issues. Approved Corrective Action Plan (CAP) (attached) and DCN DM3-00-1765-97 were issued to correct the desian drawino discrepancies. No work is reautred in Page 3 of 4 Printed 2r23/9611:4e:13 AM
ICAVP DR N3. DR-MP3-0122 t
N:rthe:st Utilities Millstone unit 3 Discrepancy Report the field.
NU also has concluded that issues # 4 ard 5 in Discrepan:y Report, DR MP3 0122, do not represent discrepant conditions.
NU has reviewed the referenced drawings and concluded that they are ' onsistent and correct.
Previously kA.tufbed by NU? O Yes @ No Non Discrepent Condation?U Yes @ No Resolution PendingsO Yo. @ 9o Re.osuiionunreceived?O Yee @ No ,
Review Acceptable Not Acceptable Needed Date VT Lead: Neri, Anthony A VT Mgr: schopfer. Don K IRc Chmn: singh. Anand K Date: 2/20/98 sL comments: In general, S&L agrees with NU's respolise wit 61 the following a
comments:
item 1) NU Indicated that for these MOV circuits, the standard detail (Figure SA on EE-9JF) will be revised to coincide with the schematics (reference CR M3 97 3711 & DCN DM3-00-1765-97). S&L agrees, since it appears that this change does not impact other circuits. NU should confirm and provide a positive statement that there is no impact to the other circuits, listed in the corresponding table, as a result of this change, item 2) S&L agrees.
Item 3) NU indicated that for these MOV circuits, revision to the standard detail (Figure SE on EE 9JM) has been documented by DCN DM3-00-079197 and no additional changes ese needed.
S&L agrees, since it appears that this change does not impact other circuits. NU should confirm and provide a poshive statement that there is no impact to the other circuits, listed in the corresponding table, as a result of this change.
Item 4) Based on the drawings provided by NU, with this response S&L agrees with the tollowing exception: Terminal block TBC point 19 on drawing 25212 39245 sht. 691 Rev. F indicates the wire address as 2AM.39, it should be 2AM.35.
Note, the original set of Aperture cards supplied to S&L for the Fire Transfer Switch Panel (FTSP) were filed under the vendor drawing number, such as 12179-2424.100-245-689 Rev. 2, these are the original" Reliance Custom Control Drawings". The drawing provided by NU for this response it 25212 39245 sht. 689 Rev. E, dated 5/9/94 fS&W Dwg 12179-2424.100-245-689) and indicates it is " Redrawn" from the original vendor drawing.
Item 5) S&L agrees.
Printed 2/23/9811:46:14 AM Page 4 of 4 ,
ICAVP DR No. DRAk 3 0483 Nsrtheast Utilities Mi!! stone Unit 3 Discrepancy Report Revlew Group: Configuration DR RESOLUTION REJECTED Potential Operability issue Discipline: Electrical Doongn Discrepancy Type: DrW Om (9)No SysterrvProcess: sWP f4RC Significance level: 4 Date faxed to NU:
Date Pu541shed: 11/13/97 k
Diecropency: Upper Tier versus Lower Tier Design Document Differences Ducription: The following differences in design documents have been noted:
- 1. The Cable and Raceway Program (TSO2) Indicates that tray 3TC1140 is supported by support "A30',-026." Tray Support locations drawing EE 34DT, Rev 7 (C-5) shows this support to be "A306-26." The support installed is marked "A306."
- 2. Tray 3TK210P was observed in the field to be 24 inches wide The Tray Location drawing EE 34Y, Rev. 9, Indicates the tray is 24 inches wide. Contrary to this, the Cable and Raceway Program (TSO2) shows this tray to be 30 linches wide.
- 3. Tray 3TK203P is shown on the Tray Location drawing EE 34Y, Rev. 9, as 24 inches wide. Contrary to this, the Cable and Raceway Program (TSO2) thows this tray to be 30 inches wide.
- 4. The Cable and Raceway Program (TSO2) indicates tray 3TK100P is to have covers top and bottom. Tray Cover identification and Location drawing EE 34TP, Rev.1 Indicates that the tray has no covers and no covers are installed in the field.
- 5. The Cable and Raceway Program (TSO2) indicates tray 3TC140P is to have covers top and bottom. Tray Cover Identification and Location drawing EE-34TQ, Rev. 2 indicates that the tray has no covers and no covers are installed in the field.
- 6. The Cable and Raceway Program (TSO2) indicates tray STC119P is to have covers top and bottom. Tri.y Location drawing EE 34T Rev.11, Indicates tray cover commodity types for this tray. Tray Cover identification and Location drawing EE-34TQ, Rev. 2 indicates that the tray has no covers. No covers are installed in the field.
- 7. The Cable and Raceway Program (TSO2) indicates tray 3TC2010 is to have covers top and bottom. Tray Cover identification and Location drawing EE-34TQ Rev. 2 indicates that the tray has only a top cover. A top cover is installed in the field,
- 8. The Cable and Raceway Program (TSO2) indicates tras 3TK404P is to have covers top and bottom. Tray Cover identification and Location drawing EE-34TL, Rev.1 Indicates that the tray has no covers and no ccvers are installed in the field.
Printed 2/23/9811:43:46 AM Page 1 of 3
1 ICAVP DR No. C't-MP3-0483 NSrtheast Utilities Millstone unit 3 Discrepancy Report
- 9. The Cable and Raceway Program (TSO2) indicates tray 3TX200N has no covers. Tray Cover Identification and Location drawing EE 34TO, Rev.1 Indicates that the tray has a top cover.
- 10. The Cable and Raceway Program (TSO2) lists support C116-74 as a support for tray 3TC4410. Per tray identification drawing EE 34 BM Rev. 8, this tray section ends prior to the location of the support.
Review Vel 6d invalid Needed Date Q 107897 initiator: server, T. L. @ Q VT Leed: Nerl, Anthony A @ O O 10/26/97 o/30S7 VT Mgr: schopfer, Don K 8 0 0 IRC Chmn: singh, Anand K Q Q Q 11/7/97 Deie:
INVALID:
Date: 2/18R8 RESOLUTION: Disposition:
NU has concluded that Discrepancy Report, DR-MP3-0483, has identified a condition not previo'Isly discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screeried per U3 Pl.
20 criteria and found to have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0514 has been writlen to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR-MP3-0483, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets tue criteria sycified in NRC letter B16901 and 17010. It has been scr'.sened per U3 PI-20 criteria and found to have no operabiP r.,r reportability concems and meets the Unit 3 deferral , teria. CR M3-98-0514 has been written to develop and trra resolution of this item per RP-4.
Previously identified by NU? U Yes (G) No Non Discrepent Condition?U Yes (8) No M Resolution Pending?O ve. @ No ResolutionUnresolved?O v.e @ No Review inillator: Werner,l.
VT Lead: Nerl, Anthony A b VT Mge: schopfer, Don K 1RC Chmn: singh, Anand K note: 2/18/98 SLComm nts: The corrective action is not apparent from the response, nor cen we determine if deferral is appropriate. For example, tray 3TK210P is narrower than the database indicates. We could not verift that this descrecancv does not imoact tray fill or amnacitv.
Prwed 2/23/98 iu.6J,id.M Page 2 of 3
l l
ICAVP DR No. DR MP3-0483 l Nertheast Utilities l Millstone Unit 3 Discrepancy Report PrWed 2/23F,811:46:52 AM Page 3 of 3
ICAVP DR N:. DR-MP3 0509 l No;Useast Utilities l Milistone Unit 3 Discrepancy Report Rev6ew Group: Sptem nR RESOLUTION REJECTED Pat etial Operabilsty lasue Disc 6pkie: Mecharucal Design O vee Discrepancy Type: Componert Data p f SysterWProcess: HVX NRC Signifncance level: 4 Date faxed to NU:
Date Published: if22/97 Discrepancy: Areas maintainod at a negative pressure by SLCRS and ABVS Descript6on: During review of the Supplementary Leak Collection and Release System (ELCRS) and the Auxiliary Building Ventilation System (ABVS) discrepancies regarding 1) which buildings and areas are multf air.ed at a negative pressure dring a LOCA and
- 2) which systems are required to maintain the negative pressure were identified.
FSAR Section 1.1.10 states that following a postulated accident, particulate and gaseous railloactive material is ducted from the containment enclosure and de buildings contiguous to the containment structure to the suppiementary leak collection and re! ease system (SLCRS), where it is filtered and discharged to the atmosphere thruogh an c!evated stack rather than through a ground-level vent.
FSAR Section 3.1.2A1 states that the supplementary leak collection and release system (SLCRS) collects radioactive leakage fiom the containment to the containment enclosure and contiguous areas following a LOCA or releasc of radioactivity due to a fuel handling accident.
FSAR Section 6.2.3 states that the seconda9/ containment is comprised of the contal- 9nt enclosure building, engineered safety features building (partial), auxiliary building, main steam building (partial), and hydrogen recombiner building (partial). The secondary containment is kept under a negative pressure relative to atmoshperic pressure. The negative pressure is maintained with the SLCRS operating together with the charging pump, reactor plant component cooling water pump and heat exchanger area ventilation system and auxillary building filtration portions of the auxiliary building ventilation system (ABVS). The SLCRS operating together with the charging pump, reactor plant component cooling water pump and heat exchanger area ventih, tion system and auxiliary building filtrction portions of the auxiliary building ventilation system (ABVS) also maintains all contiguous buildings (main steam valve building, engineered safety features building (pertially), hydrogen recombiner oul ding (partially), and auxiliary building) under a negative presSJre following a DBA by exhausting air from these areas.
FSAR Section 6.2.3.1 states that the SLCRS is designed to maintain a regative pressure in areas contiguous to the containment.
FSAR Section 6.5.1 states that the SLCRS system operated in conjunction with the charging pump, component cooling pump, Ond h00t 0xch0 ger exh0c0' ventilation cycten, ncluding ,4 p g
ICAVP DR No. DR-MP3-0509 Northear.t Utilitle3 Millstone Unit 3 Discrepancy Report auxillary building filters, is designed to maintain a negative pressure in the containment enclosure bu'Iding and associated contiguous structures (auxiliary building, ESF building, main steam valve building, and hydrogen recombiner building) during aLOCA.
FSAR Section 6.5.3.2 states that the secorv'sry containment at Millstone 3 consists of a containment enclosure structura and the contiguous buildings.
P&lD EM-148E-12 and ductwork drawings EB-72A-8 and EB-728-6 shows that the SLCRS does not directly er.haust air from the hydrogen recombinor building as blankoff plates have been installed on the exhaust openings.
P&lD EM 148A-24 does not show the ABVS exhausting air from the main steam valve building.
P&lD EM-148E 12 does not show the SLCR exhausting air from the main steam valve building. P&lD EM 1528-10 shows 1,350 cfm transfer air to the SLCRS in the auxiliary building thru containment enclosure via MSV/ Cont shake space.
Review Valid invalid Needed Date initiator: Stout, M. D. G O O 11/5/S7
'/7/S7 VT Lead: Nort, Anthony A G O O VT Mgr: schopfer, De1 K g Q Q 11/1o/97 O 518'S7 IRC Chmn: Singh, Anand K G O_
Ct.e:
INVfilD:
w Date: 2/6/98 RESOLUTION: NU has concluded that the issues reported in Discrepancy Report, DR MP3-0509, do not represent discrepant conditions.
DR MP3-0509 identifies that P&lDs EM-148E, EM-148A, and EM 152B do not provide the general area exhaust flow paths required to maintain the Secondary Containment under a negative pressure following a LOCA. The format and content of the MP3 P&lDs are established in procedure EDI 30255,'MP3 Piping and Instrumentation Diagrams Detailed Instructions for Format and Content." 90! 30255 does not require MP3 P&lDs to reflect the actual bunaing arrangement. The P&lDs provide the systems configuration required to maintain the Secondary Containment under a negative pressure following a LOCA. The PGlDs are not required to provide general area exhaust flow rates, therefore, changes to P&lDs EM-148E, EM-148A, EM1528 are not required.
The Secondary Containment is comprised of the containment enclosure building, the auxiliary build'ng, and sections of the engineered safety features building, the main steam valve building, and the hydrogen recombiner building. The interior walls of the engineered safety features building, the main steam
~
Printed 2/23/9811:47:24 AM Page 2 of 4 l
l
+
DR N2. DR-MP3 0609 Northe:st Utilities ICAVP Millstone Unit 3 Discrepancy Report j
valve building. and the hydrogen recombiner building which separate the areas contiguous to the containment from the remainder of the buildings serve as the secondary containment boundary. The areas that are not directly exhausted by ar, exhaust duct and registers located within the area are interconnected with adjacent areas that contain exhaust ducts and registers. The Secondary Containment B)undaries are ideMified on S&W EM-60 series drawings, " Plant Fire Radiation and Pressure Boundaries." The areas of the hydrogen recombiner buliding that contain the capped off ducts are not .,,
part of the Secondary Containment Boundary The areas of the main steam building and hydrogen recombiner building that are within the Secondary Containment boundary are $
drawn down through the enclosure building by the SLCRS.,
Calcu!ation P(B)-1089," Establish Acceptance Criteria for Air Leakage Through Pipe and Electrical Penetration Seals,"
provides a summary table for the exhaust flow rates for the applicable areas. The summary table shows the exhaust flow rate for the containment enclosure building as 4950 cim, the hydrogen recombiner building as 130 cfm and the main steam valve building as 1350 cfm. P&lD EM-148E indicates the total exhaust fiow from these areas through the 36" X 18" screened opening as 6430 cfm As an enhancement, FSARCR 97 MP3-569 was initiated, on 7/28/97 to revloe FSAR Section 6.2.3 to clarify the Secondary Containment Boundary. FSARCR 97 MP3-369 was initiated as a result of the CMP FSAR annotation process. Clarification of FSAR Sections 1.2.10,3.1.2.41, and 6.5 is not required with respect to the Secondary Containment Boundary.
As an enhancement, CR M3-07-4557 was initiated to clarify the air flow rates on all of the MP3 P&lDs. CR M3-97-4557 correct:c action requires a review of all air flows and notes on HVAC P& ids, related Technical Specifications, and FSAR Sections. Based on the evaluation results, the P&lDs will be revised to include clarifying notes or remove sir flow information and revise EDI 30225,if required.
Significance Level criteria do not apply here as this is not a discrepant conditlua. g
/
Attachments:
CR M3-97-4557 FSARCR 97-MP3-369 (preliminary)
Prviously identtAed by Nu? O Yes @ No Non clacrypent Condition?O Yet @ No ResolutionPending?O vee (6) No Re.oiution unre.oived?O vee
- No Review
- ## Y *
- Iritiator: Stout, M. D. =
VT Leed: Neri, Anthony A O
VT Mgt: schor*r, Don K b b IRC Chmn: stry unend K
- n. ,-
^~~
Printed 2/23/9611:47:20 AM Page 3 of 4
N:rtheast (11116 ties ICAVP DR N2. DR WIP3 0509 Millstone Unit 3 Discrepancy Report st cormwnts: FSAR Section 6.5.1.2 should be revised to agree with FSAR Section 6.2.3 regarding what portions of the ESF building, main steam valve building, and hydrogen reombiner building are maintained at a negative pre.sure by SLCRS and ABVS.
Agree that EDI 30255, Rev.1 section 4.2.2.1.a does not require the P&lDs to reflect the actual building arrangements. However, section 4.1 states that the P&lD indicates the order and type of
- Interconnecting piping, the direction of flow, and cross connect.sn with other systems. Tt s implies that P&lD EM 148E and EM-152B should be consist. : in how air leakage into the main steam valve building is exhausted from 'he containment enclosure by SLCRS is shown on the two P&lDs. The unducted airflow paths from the main steam valve building and hydrogen recombiner bulling should be shown on the P&lDs but do not necessarily need to show the specific airflow quantitles.
P&lD EM-148E 12 indicates an exhaust flow of 6,430 cfm at the 36' x 18' screened oper'ing in the containment enclosure, it does not identify that a portion of the air exhausted is drawn into the containment enclosure from the main steam valve building and hydrogen recombiner building as indicated in NU's response.
As the ltrams identified are documentation related and do not represent a technical discrepancy the DR is reclassified as Significance Lesel 4.
Printed 2/23/9e 11:4727 AM Page 4 of 4
1 DR N2. DR-MP3-0556 l Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report Review Group: Conrguretton DR REsottfilON REJECTED Raylew Element: systern Design PotentialOperabiliti ssue i Discipline: Ele:trical Design Q y,,
Discrepenty Type: Instatiaten implerrentauon (5) No System / Precess; Oss NRC signifbconce level: 4 Date FAKod to NU:
Da:e Published: 11/2/97 Discrepancy: Inadequate Spacing Descripton: The valve operator for 30SS*MOV200 is located within % of an inch of the ESF building building steel. This valve is attached to piping anchored at a Containment penekation. Given the established 4 inch seismic gap between ouildings, it appears that a potential seismic interaction condition exists.
Review Valid involki Needed Date initialor: sarver, T. L. 8 O O 10/1S'S7 VT Lead: Neri, Anthony A g Q Q 1o/27/97 VT Mgr: schopfer, Don K O O O 1o/2e/97 1o/30/07 IRC Chmn: singh, Anand K Q Q Q Date:
INVALIO:
Date: 2/12/98 RESOLUTION: Response ID M3-IRF 01464 s
Disposition:
NU has concluded that the issue reported in Discrepancy Report, DR-MP3-0506, does not represent a discrepant condition. Since 30SS*MOV20D does not exist, it is assumed that the valve in question is 3RSS*MOV20D. A walkdown determined that valve 3RSS*MOV20D was located near ESF Building Steel. A review of the Accelerations end Displacements Table B-2 (attacheQ for the Containment Structure and Table B-11 (attached) for the Engineered Safety Features Building concluded that the sum of the North-South displacements for SSE at the nearest elevation of the valve is 0.134'. Due to the configuration of the piping the valve will move away from the ESF Building Steel as the system grows thermally or during a DBA so these displacements are not of concem, accordingly no interaction condition exists.
Significance Level criteria do not apply here as this is not a discrepant condition.
Conclusion:
NU has concluded that the issue reported in Discrepancy Report, DR-MP3-0556, does not represent a discrepant condition. A review of the Accelerations and Displacements Table B-2 (attacheu) for the Containment Structure and Table B-11 (attached) for the Engineered Safety Features Building concluded that the sum of the North-South displacements for SSE at the nearest elovation of the valve is 0.134". Since this valve will thermally move away from the interference during Page 1 of 2 Printed 2/23/9611:48:o3 AM
ICAVP DR NS. DR-MP3-0556 Northeast Utilitico Millstone Unit 3 Discrepancy Report system operation or dunng a Design Basis Accident, no interaction condhion exists.
Significance Level criteria do not apply here as this is not a discrepant condition.
Previously identined by Nu? O Yes (*) No Non Discrepent condition?U Yes (9) No Resolution Pending?O ve. 5) No Resolut6on Unresolved?O ve. @ No Review AcceptaW M Accer,dable Needed Date initiatoi: Prakash, A.
VT Leed: Neri. Anthony A O O O wi2m O O O 22im VT Mgr: schopfer, Don g IRC Chmn: sWgh, Anand K O O x2im O O O onte: 2/12/98 st comments: Response ID MS-iRF-01464 NU's disposition, while considering the SSE movements of the ESF Building and the Containment structure, rieglects the SSE movements of the valve operator itself. The disposition that, since the valve will thermally move away from the Interference during system operation or during a Design Basis Accident, no interaction condition exists, is not acceptable. During an SSE event, if the system is not operating, the valve will not thermally move away from the Interference. For the RSS system, this is the more credible DBA case.
The subject valve operator for 3RSS*MOV20D is shown on Piping Location isometric Cl-RSS-7 Sheet 3, and the associated piping is analyzed in pipe stress analysis calet,lation NP(B)-X7919 Rev.2.
According to the commodity c!carance evaluation performed in the stress analysis calculation, ' locations with a clearance less than 1" are identified on the piping location isometrics'. However, PLI Cl-RSS 7 Sh. 3 does not show the 3/4" clearance identified in this DR.
Also, according to the commodity clearance eveluation, locations where piping displacements exceeo 1* are evaluated in Attachment F of the stress analysis calculation. The valve o,corator is modeled in the stress analysis as !!P618. According to Attachment F, SRSS of the total movement at NP618 exceeds 1". Yet, the 3/4" clearance between the valve operator and the ESF building steel has not been identified or evaluated.
l Pnnted 2/2M811:48.07 AM Page 2 of 2 l
ICAVP OR N:. DR MP3 0638 Northeast Utilities Mittstone Unit 3 Discrepancy Report Review Group: Operations & Mehtenance end Testing DR Resol.UTioN REJECTED
'E ' Potential Oposetnitty issue DiscW Operm O vos Discrepam:y Type: Test implemenirN g)
SystervVProcess; sW")
NRC Significance level: 4 Date Faxed to PR)*
Date Published: 11/2497 D6*crarancy: St'rveillance program does not assure that all SWPs are tested for all operating requirements.
Description:
Technical Sper.lfication 4.7 4.a.2 requires that *Esch Service Water System pump starts automatically on en SIS test signal."
It could not be determined that the existing surveillance tests asst're that this requirement is met. SP 3646A.15, SP 3646A.17.
OPS Forms 3646A.151 and 3646A.17-1 are used in conjunction to verify that both serWee water pumps in Train A are started eutomatically with an SIS signal, ideally OPS Form 3646A.15-1 tests pump A and OPS Form 3646A.17-1 tests pump C.
At the bottom of OPS Form 5646.t151, page 2, note 2 states that *3SWP*P1 A should be the lead pump. If 3SWP*P1 A is not availab'e, select 3SWP*PtC as the lead pump and ensure 3SWP*P1 A is the lead for t P3646A.17 or is documented on 3646A17 2 as requiring a .etest when it is available." It is not apparent how this requirement is followed through since there is no requirement on OPS Form 3646A171 to test the opposite pump. The only notation is "If possible, the SW pump not tested in lead during SP3646A.15 should be lead pump." This doesn't reflect a requirement to verify and document. Neither SP3646A.15 or SP3646A.17 list the completion of the other hs a prerequisite so the order of perfo mance isn't required to assure that equipment isn't missed.
OPS Form 3646A.151 (16-i,171,16-1) footnotes suggest that a specift pump be made the lead pump for the test but the form does not provide a place to document that this requirement is y
met. f-ootnote 2 on OPS Form 3646.171 states that "If possible the SW pump not tested in lead during SP3646A.15 should be lead pump." The same footnote on the corresponding procedure for B train states "The SW pump not tested in lead during SP3046.16 must be Isad pump." These two requimments are not equivalent.
A review of the test resuks of SP 3646A.15,16,17 and 18 and their associated OPS Forms 3646A.151,16-1,171 and 18-1 for the pt.rlod 5/96 through 7/96 reveal the following:
No requirement exists that all equipment associated with a specific test is to be available prior to performing the test.
Testing prerequisites are not specific regarding system alignment. The SPs are mute on prerequisites for SWP status and leaves the decision on which pump should be running to the test director based on footnotes on the OPS Fonas.
Annene nn inrme that nra lebelod alMlTIAl
- huun hamn chneknd _
Page 1 of 3 Printed 2/23.Se 11#.04 AM
ICAVP DR No. DR-MP3-0638 Northen:t Utilities Millstone unit 3 Discrepancy Report in some instances and initialed in others. However, the test was accepted and approved as satisfactory.
SP 3646A.15,16,17 and 18 are also used to satisfy the sequencing of equipment following a loss of off site power (TS 4.8.1.1.2.G.4 (6)). The testing does not require that any pump is in
- follow" and therefore the testing does nJt derr.onstrate that the " follow" pump will start if the " lead" pump fails to start.
Review Vand invei6d Needed Date initiator: Tandyn, Tom B O O $ 55'S7
$1/SS7 VT Lead: Bass, Km G O O O /10/87 VT Mgr: Schopfer. Don K G O O " '18'87 IRC Chmn. Singh. Anand K G O D.ie:
LW AUD:
Date: 2/18/98 RESOLUTION: NU has concluded that Discrepancy Report, DR-MP3-0638, has identified a condition not previously discover tt/ NU which requires correction. This dir<repancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 Pl-20 criteria and found to have no operab*llty or reportability concems and meets the Unit 3 deferral criteria. CR M3 98-0169 has been written to develop and track resolution of this item per RP-4.
Conclusion:
NU has concluded that Discrepancy Report, DR MP3-0038, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and 17010. It has been screened per U3 PI-20 criteria and found in have no operability or reportability concems and meets the Unit 3 deferral criteria CR M3 96-0169 has been written to develop and track resolutlen of this item per RP-4.
Prev 6ously identi**d by FM Q Yes (*) No Non Discrepent Condition?O Yes (I) No Resolution Pending?O va @ ao Rasuuonunruoived70 Ye. @ No Review Acceptable Not Acceptable Needed Date Imor: S R.
O O O mm VT Lead: Bass, Ken VT Mge: Schopter, Don K IRC Clwr.n: Singh. Anand K O O O Date: 2/18/98 st comments: It is not apparent from the corres,.ive action description h7n the inconsistent requirements identified in the [,R wil; be resolved.
The DR Identifies tnat footnote 2 on OPS Form 3646.17-1 and the corresponding 0 train OPS Form footnote are not equivalent.
Further, S&L does not concur with NU's determination that this discrecancy mesh the Unit 3 deferral criteria. The DR identifies Page 2 or 3 Printed 2/23/9e 11 Ae:00 AM
ICAVP DR N3. DR MP3-0638 Northeast Utilities ~
Miiistone unit 3 Discrepancy Report a discrepancy between the FSAR and plant procedures which have a direct imract on p! ant sa' 4v and operation.
Printed 2/239811:49:11 AM Page 3 of 3
hhst Utilitie3 ICAVP DR N2. DR-MP3 3915 Millstone Unit 3 Discrepancy Report Rev6ew Group: Programmate DR RESOLUTION REJECTED Potential Operabiltty issue Discipl6ne: Mechanical Design Discrepancy Tyce: CorrectNe Action O Ya
@ No SystemProce :SWP N9C Signis ence les 4: 4 Date faxed to NU:
Date Published: tr25Se Discr*Pency: No Corrective Action Plan included in ACR
Description:
ACR M3-96-0721 does not conform to the requirements of the Corrective Action procedure, i.e., no corrective action plan is included which describes the actions being taken to correct the identified deficiency and close the ACR. Additionally on Form RP 4-4, there is a statement saying 'Close Per MRT Comments.' There are no MRT comments included in the ACR.
Review Valid invenid Needed Date initiator: Wrona, S. P.
O O O tr2ise VT Lsad: Ryan, Thomme J B O O ir2ise VT Mgr: schopfer, Don K 8 O O ir22se IRC Chmn: Singh, Anand K 8 O O tr22se Date:
INVALID:
,,a m.- .
rec: '"t 7/98 RESOLU%Ds Doposition NU has concluded that Discrepancy Report, DR MP3-0915, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 It has been scened per U3 PI-20 crioria and found io have no operability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0552 has been written to develop and track resolution of this item per RP-4.
Conclusion NU has conc;uded that Discrepancy Report, DR-MP3-0915, has identified a condition not previously discovered by NU which requires correction. This discrepancy meets the criteria specified in NRC letter B16901 and.17010 It has beeri screened per U3 PI-20 criteria and found to have no cperability or reportability concems and meets the Unit 3 deferral criteria. CR M3-98-0652 has been written to develop and track resolution of this item per RP-4.
Previously ident: tied by NU? O Yes (#) No NonDiscrepentCondition?O Yes @ No Resolution Pending?O Yes @ No Resolution Unresolved?O Yes @ No Review g g Acceptable Not Acceptable Needed Date VT Lead: Ryan, Thomas J VT Mgr: Schopfer, Don K Printed 2/23Se 11:49:41 AM Page 1 of 2
ICAVP DR N3. DR-MP3 0915 N:rthaast Utilitle3 Millstone unit 3 Discrepancy Report
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IRc Chmn: Singh. Arend K O e O -
Dele: 2/17/98 st.conenents: The CR which was Generated does not contain a corrective action plan. Attematively, the DR Review Screen by the expert panel and BPM dots not contain any statement that the initial technical issue which was documented in ACR M3-96-0721 has indeed S
been resolved which would support the Review Screen conclusion that the issue is only " Administrative'.
Since we have no indication that the technical issue was ever addressed, the response is not acceptable, w
PrWed 2/23/9811:49:45 AM Page 2 of 2
i DR N . DR MP31069 I Northeast Utilities ICAVP MilistOne Unit 3 Discrepancy Report l -
Revle v Oroup; system DR INVALD Review ElemeM: Modtrcatkm Design PdeMW Opersbuny issue Disc 6pline: Mechen6 cal Design O Yes Discrepancy Type: Licensing Documert @ No 9 System / Process: NEW NRC Significance level: 4 Date F.*Xed to NU:
Date Pubushed:
Diecrnancy: Modification M3 9709410CFR50.59 Safety Evaluation Screening Checklist Descripoon: Modification M3 97094, 'RSS Loop Seal Detection," establishes a new serveillance requirement for tha RSS system. The new monthly surveillance requires verificatirAL that the thermal expansion legs of lines 3-RSS-006 40 52 54, and 55 are full of water. This surveillance assures that the RSS system will not deliver trapped air bubbles to the HHSI ECCS pumps upon completion of manual ECCS suction switchover during a postulated LOCA.
This surveillance requires that a change be made to TS surveillance requirement 4.5.2.b.1 as outlined in DR-MP31031.
This constitutes a change to a procedure described in the SAR.
However, the 10CFR50.59 safety evaluation screening checklist for M3 97094 was answered, "no" to the question, "Does the activity make changes to procedures as described in the SAR?"
The technical issue of what surveillance procedu;e changes were omitted from the mod is already addressed DR MP3-1031. This DR addresses only the issue of the error in the 10CFR50.59 screening checklist.
Review Vaud invalid Needed Date 2/2ose initiator: Wakelend, J. F. O O O VT Lead: Nort, Anthony A O @ Q 2/21/98 VT Mgr: schopfer. Don K O O O IRC Chmn: s6ngh, Anand K O O O Dete: 2/20/98 INVALsD: The condition identified in this DR is already addressed by DR-MP3-1031. If TS Surveillance 4.5.2.b.1 did not nced to be changed as described in DR MP3-1031, the 10CFR50.59 screening checklist for modification M3 97094 would have been completed correctly.
Date:
RESOLUTION:
Previously iderdified by NU7 Q Yes @ No NonDiscrepentCondition?U Yes (G) No ResolutionPending70 vos @ No Resoiuiionunresoived70 vos @ No Review Acceptable Not Acceptable Needed Date g
VT Lead: Nort. Anthorry A O O VT Mgr: schopfer, Don K IRC Chmn: singh, Anand K Page 1 of 2 Printed 2/23/9611:5o 45 AM
DR N3. DR-MP31069 Northeast Utilities ICAVP Millstone Unit 3 Discrepancy Report .
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