|
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M3371999-10-20020 October 1999 Forwards Notice of Docketing of License SNM-2506 Amend Application.Notice Has Been Forwarded to Ofc of Fr for Publication ML20217M1111999-10-19019 October 1999 Forwards Insp Repts 50-282/99-14 & 50-306/99-14 on 990920- 22.One Violation Noted & Being Treated as Ncv.Insp Focused on Testing & Maint of Heat Exchangers in High Risk Sys ML20217F4331999-10-15015 October 1999 Forwards Rev 39 to Security Plan.Changes Do Not Decrease Effectiveness of Security Plan.Rev Withheld,Per 10CFR73.21 ML20217C2351999-10-0606 October 1999 Forwards Insp Repts 50-282/99-12 & 50-306/99-12 on 990823-0917.No Violations Noted.Insp Consisted of Selected Exam of Procedures & Representative Records,Observation of Activities & Interviews with Personnel ML20212J8811999-09-28028 September 1999 Forwards Preliminary Accident Sequence Precurson Analysis of Operational Event That Occurred at Plant,Unit 1 on 990105, for Review & Comment.Comment Requested within 30 Days of Receipt of Ltr IR 05000272/19990071999-09-28028 September 1999 Forwards Insp Repts 50-272/99-07 & 50-306/99-07 on 990721- 0831.One Potentially Safety Significant Issue Identified Dealing with Control Room Special Ventilation System.Four Addl Issues of Low Safety Significance Identified ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20212G9801999-09-23023 September 1999 Refers to Resolution of Unresolved Items Identified Re Security Alarm Station Operations at Both Monitcello & Prairie Island ML20212F5121999-09-20020 September 1999 Forwards Response to NRC , Preparation & Scheduling of Operator Licensing Examinations ML20212D8401999-09-16016 September 1999 Discusses 990902 Telcon Between D Wesphal & R Bailey Re Administeration of Retake Exam at Prairie Island During Wk of 991206.NRC May Make Exam Validation Visit to Facility During Wk of 991116 ML20217H2331999-09-10010 September 1999 Forwards Security Insp Repts 50-282/99-10 & 50-306/99-10 on 990809-12.Two Findings,Each of Low Risk Significance Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217H5661999-09-0909 September 1999 Discusses 990907 Pilot Plan Mgt Meeting Re Results to-date of Pilot Implementation of NRC Revised Reactor Oversight Process at Prairie Island & Quad Cities.Agenda & Handouts Provided by Utils Encl ML20212A9241999-09-0909 September 1999 Discusses Plans Made During 990902 Telephone Conversation to Inspect Licensed Operator Requalification Program at Prairie Island During Weeks of 991101 & 991108.Requests That Written Exams & Operating Tests Be Submitted by 991022 ML20212B0511999-09-0909 September 1999 Forwards Insp Repts 50-282/99-11 & 50-306/99-11 on 990816-20.One Issue of Low Safety Significance Was Identified & Being Treated as Ncb ML20211Q7641999-09-0808 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Plant Operator License Applicants During Wk of 000515,in Response to D Westphal ML20211N8631999-09-0707 September 1999 Withdraws 970814 Request for Exemption from 10CFR50,App R, Section III.G.2, Fire Protection of Safe Shutdown Capabilities ML20211K5911999-09-0101 September 1999 Informs That Util Reviewed Rvid Data Base,As Requested in NRC .Summary of Proposed Changes & Observed Differences Are Included in Encl Tables ML20211L0211999-09-0101 September 1999 Provides Notification That License Amends 141 & 132 & Associated License Conditions 6 & 7 Have Been Fully Implemented ML20211K5931999-08-31031 August 1999 Forwards License Amend Request for License SNM-2506, Proposing Change to License Conditions 6,7 & 8 & TSs App a of License by Permitting Inclusion of Bpras & Thimble Plug Devices in Sf Assemblies Stored in TN-40 Casks ML20211Q6041999-08-31031 August 1999 Forwards Rev 19 to USAR for Pingp,Per 10CFR50.71(e).Rev Brings USAR up-to-date as of 990228,though Some Info Is More Recent.Attachment 1 Contains Descriptions & Summaries of SE for Changes,Tests & Experiments,Per 10CFR50.59 ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211D3541999-08-24024 August 1999 Discusses GL 95-07 Re Pressure Locking & Thermal Binding of safety-related Power Operated Gate Valves.Forwards SE Re Response to GL 95-07 ML20211C7601999-08-19019 August 1999 Confirms NRC Intent to Meet with NSP & Ceco on 990807 in Lisle,Il to Discuss with Region III Pilot Plants,Any Observations,Feedback,Lessons Learned & Recommendations Relative to Implementation of Pilot Program ML20211B8311999-08-19019 August 1999 Forwards Request for Relief 8 Re Limited Exams Associated with Unit 1 Third ten-year Interval Inservice Insp Program. Licensee Requests Relief Due to Impractibility of Obtaining 100% Exam Coverage for Affected Items ML20211B5711999-08-19019 August 1999 Forwards Second 90-day Rept for Implementation of Voltage Based Repair Criteria at Prairie Island Unit 1.Rept Fulfills Requirements of Section 6.b of Attachment 1 to GL 95-05 ML20211C2311999-08-19019 August 1999 Forwards Unit 1 ISI Summary Rept,Interval 3,Period 2 Refueling Outage Dates 990425-0526,Cycle 19 971212-990526. Rept Identifies Components Examined,Exam Methods Used,Exam Number & Summarizes Results ML20211B0561999-08-18018 August 1999 Provides Addl Info on Proposed Rev to Main Steam Line Break Methodology ,in Response to NRC Staff Request Made in 990416 Telcon.Nuclear Svcs Corp Rept PIO-01-06, Analysis Rept Structural Analyses of Main Steam Check... Encl ML20211B2621999-08-17017 August 1999 Forwards Insp Repts 50-282/99-09 & 50-306/99-09 on 990719-22.No Violations Noted.Insp Included Review & Evaluation of Current Emergency Preparedness Performance Indicators ML20211C7371999-08-17017 August 1999 Discusses Closure of Staff Review Re Generic Implication of Part Length Control Rod Drive Mechanism Housing Leak on 980123.Enclosed NRC 980811 & 1223 Ltrs Responded to WOG Positions Re Corrective Actions ML20210T5661999-08-12012 August 1999 Forwards RAI Re & Suppl ,which Requested Exemptions from TSs of Section III.G.2 of 10CFR50 App R,To Extent That Specifies Separation of Certain Redundant Safe Shutdown Circuits with fire-related Barriers ML20210R7021999-08-12012 August 1999 Forwards Insp Repts 50-282/99-06 & 50-306/99-06 on 990601- 0720.One NCV Occurred,Consistent with App C of Enforcement Policy ML20210P5191999-08-11011 August 1999 Discusses GL 92-01,Rev 1,Supp 1, Rv Integrity, Issued by NRC on 950519 & NSP Responses for PINGP & 951117. Staff Reviewed Info in Rvid & Released Info as Rvid Version 2.Requests Submittal of Comments Re Revised Rvid by 990901 ML20210G5061999-07-30030 July 1999 Responds to Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates 05000282/LER-1999-007, Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics1999-07-23023 July 1999 Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics ML20210J4991999-07-22022 July 1999 Forwards Rev 18 to USAR for Pingp,Bringing USAR up-to-date as of 990228,though Some Info More Recent.Safety Evaluation Summaries Also Encl ML20209J0941999-07-15015 July 1999 Forwards SER Finding Rev 7 to Topical Rept NSPNAD-8102, Reload Safety Evaluation Methods for Application to PI Units, Acceptable for Ref in Plant Licensing Actions ML20209H8051999-07-14014 July 1999 Forwards Summary of non-modification Safety Evaluation Number 515 Re Storage of Fuel Inserts,Per Insp Rept 72-0010/99-201 ML20209D4181999-07-0707 July 1999 Informs That Util Has Changed Listed TS Bases Pages Attached for NRC Use.Util Made No New Commitments in Ltr ML20209H8361999-07-0202 July 1999 Forwards Operator Licensing Exam Repts 50-282/99-301(OL) & 50-306/99-301(OL) for Tests Administered During Week of 990517-21.Two Applicants Passed All Sections of Exam & Issued Reactor Operator Licenses to Operate Pings ML20196J9681999-07-0101 July 1999 Informs That in Sept 1998,Region III Received Rev 20 to Portions of Util Emergency Plan Under 10CFR50.54(q).Based on Determination That Changes Do Not Decrease Effectiveness of Licensee Emergency Plan,No NRC Approval Required ML20209C3951999-07-0101 July 1999 Forwards Supplemental Response to GL 95-07, Pressure Locking & Thermal Binding of SR Power-Operated Gate Valves ML20209B7541999-07-0101 July 1999 Final Response to GL 98-01,Suppl 1 Re Y2K Readiness of Computer Sys.Sys Remediated as Required for Plant Operation. Contingency Plans Developed to Mitigate Impact of Y2K-induced Events at Key Rollover Dates ML20196J8941999-06-30030 June 1999 Transmits Util Comments on Draft Regulatory Guide DG-1074, Steam Generator Tube Integrity. Licensee Recommends That NRC Focus on Several Important Listed Areas Considered Principal Concerns & Contentions ML20209F0391999-06-30030 June 1999 Forwards Insp Repts 50-282/99-04 & 50-306/99-04 on 990407-0531.Violation Noted.Notice of Violation or Civil Penalty Will Not Be Issued,Based on NRC Listed Decision to Exercise Discretion ML20209C3011999-06-29029 June 1999 Forwards Annual Rept of Corrections to NSP ECCS Evaluation Models,Iaw 10CFR50.46.Since All Analyses Remain in Compliance,No Reanalysis Is Required or Planned ML20209B5751999-06-24024 June 1999 Submits Revised Relief Request for Limited Examinations Associated with Third 10-yr ISI Examination Plan.Attached Is Unit 1 Relief Request 7,rev 1 Which Addresses Limited Examinations ML20196F3871999-06-23023 June 1999 Forwards Revised Pages 71,72 & 298 of Rev 7 to NSPNAD-8102, Prairie Island Nuclear Power Plant Reload Safety Evaluation Methods for Application to PI Units, Per Discussions with Nrc.Approved Version of Rept Will Be Issued 05000282/LER-1999-006, Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics1999-06-18018 June 1999 Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics ML20196D5501999-06-18018 June 1999 Forwards Individual Exam Results for Licensee Applicants Who Took May 1999 Initial License Exam.In Accordance with 10CFR2.790,info Considered, Proprietary. Without Encls ML20196A6741999-06-17017 June 1999 Refers to 990517-20 Meeting with Util in Welch,Minnesota Re Licensee Initiatives in Risk Area & to Establish Dialog Between SRAs & Licensee PRA Staff 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217F4331999-10-15015 October 1999 Forwards Rev 39 to Security Plan.Changes Do Not Decrease Effectiveness of Security Plan.Rev Withheld,Per 10CFR73.21 ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20212F5121999-09-20020 September 1999 Forwards Response to NRC , Preparation & Scheduling of Operator Licensing Examinations ML20211N8631999-09-0707 September 1999 Withdraws 970814 Request for Exemption from 10CFR50,App R, Section III.G.2, Fire Protection of Safe Shutdown Capabilities ML20211K5911999-09-0101 September 1999 Informs That Util Reviewed Rvid Data Base,As Requested in NRC .Summary of Proposed Changes & Observed Differences Are Included in Encl Tables ML20211L0211999-09-0101 September 1999 Provides Notification That License Amends 141 & 132 & Associated License Conditions 6 & 7 Have Been Fully Implemented ML20211Q6041999-08-31031 August 1999 Forwards Rev 19 to USAR for Pingp,Per 10CFR50.71(e).Rev Brings USAR up-to-date as of 990228,though Some Info Is More Recent.Attachment 1 Contains Descriptions & Summaries of SE for Changes,Tests & Experiments,Per 10CFR50.59 ML20211K5931999-08-31031 August 1999 Forwards License Amend Request for License SNM-2506, Proposing Change to License Conditions 6,7 & 8 & TSs App a of License by Permitting Inclusion of Bpras & Thimble Plug Devices in Sf Assemblies Stored in TN-40 Casks ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211C2311999-08-19019 August 1999 Forwards Unit 1 ISI Summary Rept,Interval 3,Period 2 Refueling Outage Dates 990425-0526,Cycle 19 971212-990526. Rept Identifies Components Examined,Exam Methods Used,Exam Number & Summarizes Results ML20211B8311999-08-19019 August 1999 Forwards Request for Relief 8 Re Limited Exams Associated with Unit 1 Third ten-year Interval Inservice Insp Program. Licensee Requests Relief Due to Impractibility of Obtaining 100% Exam Coverage for Affected Items ML20211B5711999-08-19019 August 1999 Forwards Second 90-day Rept for Implementation of Voltage Based Repair Criteria at Prairie Island Unit 1.Rept Fulfills Requirements of Section 6.b of Attachment 1 to GL 95-05 ML20211B0561999-08-18018 August 1999 Provides Addl Info on Proposed Rev to Main Steam Line Break Methodology ,in Response to NRC Staff Request Made in 990416 Telcon.Nuclear Svcs Corp Rept PIO-01-06, Analysis Rept Structural Analyses of Main Steam Check... Encl ML20210G5061999-07-30030 July 1999 Responds to Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates 05000282/LER-1999-007, Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics1999-07-23023 July 1999 Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics ML20210J4991999-07-22022 July 1999 Forwards Rev 18 to USAR for Pingp,Bringing USAR up-to-date as of 990228,though Some Info More Recent.Safety Evaluation Summaries Also Encl ML20209H8051999-07-14014 July 1999 Forwards Summary of non-modification Safety Evaluation Number 515 Re Storage of Fuel Inserts,Per Insp Rept 72-0010/99-201 ML20209D4181999-07-0707 July 1999 Informs That Util Has Changed Listed TS Bases Pages Attached for NRC Use.Util Made No New Commitments in Ltr ML20209C3951999-07-0101 July 1999 Forwards Supplemental Response to GL 95-07, Pressure Locking & Thermal Binding of SR Power-Operated Gate Valves ML20209B7541999-07-0101 July 1999 Final Response to GL 98-01,Suppl 1 Re Y2K Readiness of Computer Sys.Sys Remediated as Required for Plant Operation. Contingency Plans Developed to Mitigate Impact of Y2K-induced Events at Key Rollover Dates ML20196J8941999-06-30030 June 1999 Transmits Util Comments on Draft Regulatory Guide DG-1074, Steam Generator Tube Integrity. Licensee Recommends That NRC Focus on Several Important Listed Areas Considered Principal Concerns & Contentions ML20209C3011999-06-29029 June 1999 Forwards Annual Rept of Corrections to NSP ECCS Evaluation Models,Iaw 10CFR50.46.Since All Analyses Remain in Compliance,No Reanalysis Is Required or Planned ML20209B5751999-06-24024 June 1999 Submits Revised Relief Request for Limited Examinations Associated with Third 10-yr ISI Examination Plan.Attached Is Unit 1 Relief Request 7,rev 1 Which Addresses Limited Examinations ML20196F3871999-06-23023 June 1999 Forwards Revised Pages 71,72 & 298 of Rev 7 to NSPNAD-8102, Prairie Island Nuclear Power Plant Reload Safety Evaluation Methods for Application to PI Units, Per Discussions with Nrc.Approved Version of Rept Will Be Issued 05000282/LER-1999-006, Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics1999-06-18018 June 1999 Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics ML20195G4281999-06-0909 June 1999 Notifies That Amsac/Dss Mods Completed & TS 138/129 Has Been Fully Implemented 05000282/LER-1999-005, Forwards LER 99-005-00 Re Containment Inservice Purge Sys Not Isolated During Heavy Load Movement Over Fuel.Event Has Indicated That Level of Performance Expected by Mgt Has Not Yet Been Achieved1999-06-0707 June 1999 Forwards LER 99-005-00 Re Containment Inservice Purge Sys Not Isolated During Heavy Load Movement Over Fuel.Event Has Indicated That Level of Performance Expected by Mgt Has Not Yet Been Achieved ML20207F4301999-06-0101 June 1999 Forwards 1999 Unit 1 SG Insp Results,Per TS 4.12.E.1. Following Insp 84 Tubes Were Plugged for First Time ML20196L2461999-05-21021 May 1999 Forwards Rev 0 to COLR for Pingp,Unit 1 Cycle 20, IAW TS Section 6.7.A.6 ML20195C6861999-05-21021 May 1999 Forwards Rev 17 to USAR for Prairie Island Nuclear Generating Plant.Attachment 1 Contains Descriptions & Summaries of SEs for Changes,Tests & Experiments Made Under Provisions of 10CFR50.59 During Period Since Last Update ML20206U6781999-05-17017 May 1999 Forwards Revised Emergency Response Plan Implementing Procedures,Including Rev 15 to F3-3,rev 15 to F3-16,rev 14 to F3-22 & Table of Contents ML20206U7131999-05-17017 May 1999 Forwards Revised EOF Emergency Plan Implementing Procedures, Including Table of Contents & Rev 2 to F8-10, Record Keeping in Eof. with Updating Instructions ML20206T2461999-05-17017 May 1999 Forwards Off-Site Radiation Dose Assessment for Jan-Dec 1998, Rev 0 to Annual Radiactive Effluent Rept for 980105- 990103 & Effluent & Waste Disposal Annual Rept Solid Waste & Irradiated Fuel Shipments,Jan-Dec 1998 ML20206R0401999-05-13013 May 1999 Forwards Application for Amends to Licenses DPR-42 & DPR-60, Removing Plant Organization Requirement,Imposed in Amend 141/132 That Plant Manager,Who Has Responsibility for Overall Safe Operation of Plant,Report to Corporate Officer ML20206Q0871999-05-13013 May 1999 Forwards Result of Evaluation Re Ultrasonic Exams of SG Number 22 Performed in Accordance with ASME Boiler & Pressure Vessel Code Section Xi.Procedure Used for Evaluation Contained in WCAP-14166,submitted for Review ML20206F9381999-05-0303 May 1999 Forwards Response to NRC 990304 RAI Re GL 96-05 Program at Pingp.Licensee Commitments Are Identified in Encl as Statements in Italics ML20206J3851999-05-0303 May 1999 Forwards 1998 Annual Radiological Environmental Monitoring Rept 05000282/LER-1999-004, Forwards LER 99-004-00 Re Discovery of Inadequate Sp That Demonstrates Operability of SFP Special Ventilation Sys.Two New NRC Commitments Are Contained in Corrective Action Section of Rept in Bold Italics1999-05-0303 May 1999 Forwards LER 99-004-00 Re Discovery of Inadequate Sp That Demonstrates Operability of SFP Special Ventilation Sys.Two New NRC Commitments Are Contained in Corrective Action Section of Rept in Bold Italics ML20206E1761999-04-28028 April 1999 Forwards Revised TS Pages for Amends 144 & 135 to Licenses DPR-42 & DPR-60,respectively,to Update Controlled Manual or File ML20205S3221999-04-20020 April 1999 Forwards Application for Amends to Licenses DPR-42 & DPR-60, Changing Implementation Date for Relocation from TS to UFSAR of Requirements in TS 3.1.E & Flooding Shutdown Requirements of TS 5.1 ML20205P9891999-04-12012 April 1999 Requests Approval for Proposed Alternatives to Liquid Penetrant Requirements of N-518.4 of 1968 ASME Boiler & Pressure Vessel Code.Results of Analysis & Summary of Tests Performed & Tests Results Are Encl ML20205Q0191999-04-12012 April 1999 Forwards Application for Amend to License DPR-42 & DPR-60, Relocating Shutdown Margin Requirements from TS to COLR 05000282/LER-1998-010, Forwards LER 98-010-01 Re Discovery That 32 App R Related MOVs Are Susceptible to Physical Damage by Fire Induced Hot Shorts.Rept Provides Addl Details on Current Plans for Completing C/As Committed to in Original LER1999-04-0808 April 1999 Forwards LER 98-010-01 Re Discovery That 32 App R Related MOVs Are Susceptible to Physical Damage by Fire Induced Hot Shorts.Rept Provides Addl Details on Current Plans for Completing C/As Committed to in Original LER ML20205P9221999-04-0101 April 1999 Submits Relief Request 8,rev 0 Which Addresses Limited Exams Associated with Unit 2 Third ten-year Interval Inservice Insp Program.Util Requests Relief Per 10CFR50.55a(q)(5)(iii) Due to Impracticality of Obtaining 100% Exam Coverage ML20205E8371999-03-31031 March 1999 Submits Four Copies of Rev 38 to Prairie Island Security Plan,Per 10CFR50.54(p).Changes Do Not Decrease Effectiveness of Security Plan.Encl Withheld,Per 10CFR73.21 ML20196K7831999-03-31031 March 1999 Forwards Decommissioning Funding Status Rept for Monticello & Prairie Island Nuclear Generating Plants,Per Requirements of 10CFR50.75(f)(1) ML20205Q5051999-03-30030 March 1999 Forwards Inservice Insp Summary Rept Interval 3,Period 1 & 2 Refueling Outage Dates 981109-1229 Cycle 19,970327- 981229. Rept Identifies Components Examined,Exam Methods Used,Exam Number & Summarized Results ML20205H5731999-03-29029 March 1999 Submits Required 1998 Actual & 1999 Projected Cash Flow Statements for Monticello Nuclear Generating Plant & PINGP, Units 1 & 2.Encl Contains Proprietary Info.Proprietary Info Withheld,Per 10CFR2.790(b)(1) ML20205C6561999-03-26026 March 1999 Submits Semiannual Update on Project Plans for USAR Review Project & Conversion to ITS ML20204H3371999-03-19019 March 1999 Forwards Application for Amend to Licenses DPR-42 & DPR-60, Removing Dates of Two NRC SERs & Correcting Date of One SER Listed in Section 2.C.4, Fire Protection 1999-09-07
[Table view] |
Text
.,
y Northern States Power Company Prairie Island Nuclear Generating Plant 1717 Wakonade Dr. East Welch, Minnesote $50e9 November 14,1997 10 CFR Part 2 U S Nuclear Regulatory Commission Aitq: Document Control Desk Wasnington, DC 20555 PRAIRIE ISLAND NUCLEAR GENERATING PLANT Docket Nos. 50-282 License Nos. DPR-42 50-306 DPR-60 Raply to Notice of Violation (Inspection Report 97008),
Deficiencies in the Test Control, USAR Update and Corrective Action Programs l
Your letter of October 16,1997, which transmitted additional violations from inspection Report No. 97008, required a response to a Notice of Violation. Our response to the notice is contained in the attachment to this letter. Refer to our August 15,1997 response to Notice of Violation for commitments already made in regard to this inspection.
In addition, your July 16,1997 letter had requested that we inform you of "any planned actions, including timo frames, for re-performing the control room habitability dose l
calculations and any plans to test the control room isolation dampers for verification of the inleakage assumptions..." We plan to perform the control room envelope testing in January 1998. The testing is expected to take about a week. Following evaluation of the test results, we will determine the need to perform a control room habitability dose re-analysis.
The $50,000 civil penalty associated with the Severity Level 111 problem was paid by electronic transfer November 7,1997.
We have made new Nuclear Regulatory Commission commitments, indicated as the italicized statements above and in the attachment. Other comrnitments associated with these violations were made in our August 15,1997 letter. [
.xl 9711200014 971114 i bl PDR ADOCK 05000282 G PDR
- ( '
USNQC November 14,1997 Page:
P! casa cor.tsci Jack !.sysille (S12 389-1121 Ex!. 4662) if you have any questions related to this letter.
Joel P Sorensen Plant Manager Prairie Island Nuclear Generating Plant c: Regional Administrator - Region 111, NRC Senior Resident inspector, NRC NRR Project Manager, NRC J E Silberg
Attachment:
RESPONSE TO NOTICE OF VIOLATION 4
,1 RESPONSE TO NOTICE OF VIOLATION VIOLATION 1 10 CFR Part 50, Appendix B, Criterion XI, " Test Control," requires, in part, that a test program shall be established to assure that all testing required to demonstrate that systems will perform satisfactority in service is idantified and performed in accordance with written test procedures which incorporate the raquirements and acceptance limits contained in applicable design documents.
Updated Safety Analysis Report (USAR) at Section 11.9.3.a, " Loss of Main Feedwater Transients" documented that during a loss of offsite power transient a single Auxiliary Feedwater ( AFW) pump will provide sufficient flow to prevent water relief from the pressurizer relief valves. USAR Table 11,9-2, " Summary of Assumptions used in the AFW System Design Verificat;on Analysis," stated that the minimum required AFW flow during a loss of offsite power transient was 200 gallons per minute to a steam generator.
Contrary to the above, since at least May 31,1991, and continuing until April 24, 1997, the test program failed to assure that written test procedures incorporated the 200 gallons per minute acceptance limits contained in Sectin n 11.9.3.a of the '
USAR; the applicable design documents. Specifically, the acceptance criteria i for the Unit 1 and Unit 2 monthly and refueling outage AFW eurveillance tests listed below would have permitted the AFW pumps to degrade below (and remain operable) the minimum flow - 200 gallons per minute - to a steam generator during a loss of offsite power transient. (01013)
SP 1103, "11 Turbine-Driven Auxiliary Feedwater Pump Once Ever; i Refueling Outage Test;
SP 1101, "12 Motor. Driven Auxiliary Feedwater Pump Once Every Refueling Outage Test;"
SP 2101, "21 Motor-Driven Auxiliary Feedwater Pump Once Every l Retueling Outage Test;"
SP 2103, "22 Turbine-Driven Auxiliary Feedwater Pump Once Every Refueling Outage Test,"
SP 1102, "11 Turbine-Driven Auxiliary Feedwater Pump Monthly Test,"
SP 1100, "12 Motor-Driven Auxiliary Feedwater Pump Monthly Test,"
l SP 2100, "21 Motor-Driven Auxiliary Feedwater Pump Monthly Test,"
SP 2102, "22 Turbine-Driven Auxiliary Feedwater Pump Monthly Test."
Response to Violation 1 Reason for the Violation The Prairie Island Nuclear Generating Plant had implemented pump performance I testing acceptance criteria in accordance with ASME B&PV Code Section XI criteria.
Attachment
. November 14,1997
- Page 2 The ASME acceptance criteria were not conservative for AFW pump design basis flow
, requirements considering instrument inaccuracies, pump recirculation flow, and allowances for steam generator safety valve setpoliM variance.
Corrective Actions Taken end Results Achievad All monthly and refueling outage AFW surveillance tests (SP1103, SP1101, SP2103, SP2101, SP1102, SP1100, SP2102 and SP2100) have been updated with appropriate acceptance criteria.
The revised acceptance criteria have always been met by the AFW pumps, except previously when one pump was declared out of service for not meeting its ASME Section XI acceptance criteria. Three of the AFW pumps installed in 1973 are stillin service and operable with the revised acceptance criteria. The AFW pumps are operable with some margin to the new acceptance criteria. Prairie Island is investigating several options to improve the AFW pump performance margin.
Benchmark data has been gathered during the current Unit 1 refueling outage.
Verification calculations to confirm hydraulic model results are in progress.
Corrective Steos That Have Been or Will Be Taken to Avoid Further Violations Completion of previous Prairie Island initiatives, coupled with a review of all ASME Section XI pumps, has yielded a comprehensive review of the Prairie Island ASME Section XI testing program. ASME Section XI valve limiting stroke time design basis review was started in 1996. The review was completed in July 1997, with all valves determined to be operable. A smell number of surveillance test procedures required revision. These procedure changes have been completed.
ASME Section XI check valve testing full flow values were reviewed and documented during the Prairie Island third ten year program development.
ASME Section XI pump performance limits have also been reviewed. The AFW pump surveillance test acceptance criteria were reviewed and revised during the SSOPl.
Cooling Water pump criteria were previously reviewed. The review determined the ASME Section XI limits were conservative to the USAR stated design requirement, for one Cooling Water pump supplying one train of safeguards equipment. Safety injection pump criteria were previously revised as noted in the Notice of Violation. However, an NSP Quality Assurance department audit conducted at the same time as tne SSOPl ,
found that the Safety injection pump USAR design criteria were not conservative to the ACME Section XI110% criteria in one small area. The Safety injection pumps' performance was verified to meet the more restrictive ASME criteria. Unit 1 Safety injection pump performance test procedures were revised before use during the Oc'ober 1997 refueling outage. Residual Heat Removal pump and Containment Spray
y B
e Attachment
,_ ._* November 14.1997
-- Page 3 pump criteria were reviewed and found to be acceptablo. Margin exists on Residual Heat Removal and Containment Spray pumps between the ASME Section XI criteria and the USAR design requirements, considering instrument inaccuracies. Component Cooling and Control Room Chilled Water pump capacities exceed the DBA loads listed in the USAR or applicable design documents. The extra capacities available from these closed loop system pumps ensure test acceptance criteria exceeds USAR
- requirements.
The design criteria gathered during the valve limiting stroke time reviews and the pump performance criteria reviews is being incorporated into Prairie Islands ASME Section XI program coritrol document H10.1. Any future cornponent test procedure changes will have easy reference to the design criteria. Engineering support personnel have received training on these changes to H10.1.
Date When Full Comollance Will Be Achieved Pump and valve test procedures described above have been revised. Full compliance has been achieved.
.1
?
Attachment
. Ncvember 14,1997 Pege 4 VIOLATION 2 10 CFR 50.71(o),' Maintenance of Records, Making of Reports," requires, in part, that each license periodically update the final safety analysis report (FSAR)
(now know as the USAR at Prairie Island) to assure that the information included in the FSAR contains the latest mater;al developed.
10CFR50.71(e)(4) requires, in part, that revisions be filed such that the intervals between successive updates to the USAR do not exceed 24 months. It further states that the revisions must reflect all changes up to a maximum of 6 months prior to the date of filing.
The applicable section of the FSAR, now titled the Updated Safety Analysis Report (USAR), is Section 11.9.3," Performance Analysis Condensate, Feedwater, and Auxiliary Feedwater Systems" Contrary to the above, as of May 16,1997, the licensee had not assured that the information included in the FSAR contained the latest material developed and had not updated the FSAR periodically, as required in 10 CFR 50.71.
Specifically, in October 1992 the licensee identified that the 400 gpm Auxiliary Feedwater Pump (AFW) flow rue specified in USAR Section 11.9.3 Ur Jer the Main Feedwater Line Rupture accident scunario disagreed with actual Auxiliary Feedwater pump performance capabilities of approximately 200 gpm with only one pump available. Since October 1992, three opportunities to update this section of the USAR were available, yet the revisions of September 1993, June 1994 and December 1995, did not contain the latest material developed or reflect all changes prior to the date of the filing. (01023)
Re nonse to Violation 2 Reason for the Violation The Prairie Island design basis analysis of record for Main Feedwater Line Rupture is stated in the October 1969 Westinghouse letter PlW-P-540, indicating a 200 gpm requirement for Prairie Island specific analysis. As noted in the Notice of Violation, Prairie Island initiated a Design Basis Document Follow On Item A0781 in October 1992 describing the inconsistency with the USAR text on Main Feedwater Line Ruptuie analysis. Operability and reportability were assessed. The Nuclear Analysis Depcrtment was requested to verify the Main Feedwater Line Rupture analysis with an alternate calculation. This item was inappropriately given a low priority and not completed until 1997.
Attachment November 14,1997
- Page5 Corrective Actions Taken and Results Achieved The Nuclear Analysis Department's verification of the Main Feedwater Line Ruptuie analysis by alternate calculation was completed May 1997. The safety evaluation to incorporate the USAR change was approved July 1997. The USAR revision was submitted to the NRC in September 1997.
Corrective Steps That Will Be Taken to Avoid Further Violations:
Prairie Island's configuration management efforts over the past few years has resulted in the development and verification of 34 Design Basis Documents. This effort resulted in 910 Follow-On items (FOls) with 1311 recommended action items. All 910 FOls were assessed (100%) which included operability and reportability determinations,851 FOls are closed (94%) ,1200 actions are completed (92%).
Efforts to close the remaining action items are in progress.
Ninety-five action items pertained to updating the USAR, with 70 items complete as of August 8,1997. The September 1997 USAR submittal incorporated eleven rnore items for a total of 85% complete at this update. Plans are to complete the remaining fou.4een items over the interval before the USAR submittal oflate 1998.
Date When Full Compliance Will Be Achieved The USAR update of Main Feedwater Line Rupture was submitted in September 1997.
Full compliance has been achieved.
A
o Attachmer.t
> November 14,1997
A. Contrary to the above, as of May 16,1997, the ticensee had not resolved a significant condition adverse to quality that was identified on March 6,1991, and
- documented on the assessment of Operating Experience Document NSD-TB 11, "High Head Safety injection". Specifically, the assessment documented that design requirements -- such as flow - had not been adequately considered when the safety injection pump surveillance procedures acceptance criteria were determined and there was a need to ensure that design requirements were correctly incorporated for other pumps' surveillance test acceptance criteria.
Corrective action was not taken for the Auxiliary Feedwater, Residual Heat Removal, and Containment Sprsy Pumps. This was demonstrated when the NRC inspectors determined that the Auxiliary Feedwater Pump Surveillance tests' acceptance criteria would have allowed an AFW pump to be cunsidered operable even if the pump parameters were below the minimum design requirements. (01033)
B. Contrary to the above, as of May 16,1997, the licensee had not resolved a condition adverse to quality that was identified on November 18,1992, and documented on Configuration Management Follow-On item FOI [A]O781, " Basis For AFWP Requiremente After Line Break". Specifically, FOI[A]O781 documented a deviation from the updated final safety analyCs (USAR) in that the AFW pumps were not in conformance with the 400 gpm flow rate for a main feedwater pipe rupture accident scenario as specified in section 11.9.3 of the USAR with only one pump available. The licensee failed to promptly correct the deviation by demonstrating that the AFW pump capacity of approximately 200 gpm with on!v one pump available would be sufficient during a main feedwater pipe rupture. (01043) 3 Response to Violation 3 Reason for the Violation The Prairie Island staff has been proactive in identifying problems, and maintaining equipment operability and reliability. Numerous problems of generic significance have been identified by Prairie Island staff (e.g., Loss of Feedwater ATWS AFW l
l
Attachment
, November 14,1997
' Page 7 performance, Containment pressure response to Cont. Spray versus Fan Coll Units, dilution events at cold shutdown, ATWS power setpoint). However, Prairie Island has not always bcon timely in resolving issues. In response to untimely corrective action program concerns noted in the 1997 Aux Feedwater System SSOPl , NSP assessed its corrective action program. This assessment identified the following concerns:
. Corrective action items locked management involvemen, in prioritizatir>n.
. Many separate corrective action vehicles lead to a poor understanding of the wnole program.
. Resources were not allocated to promptly resolve issues.
- The status of some corrective action programs was not reported to upper management for prioritization and resource loading.
Corrective Actions Taken and Results Achieved Actions to review the operability and reportability determinations made in previous FOI assessments were committed to in LER 1-96-13 on cable tray separation issues. A review of a sample of previous assessments was completed in October 1996.
Management review of old OEA recommendations was completed in July 1997. The items were reviewed for regulatory significance, priority and schedule. Management expectations for timely closure were communicated to the staff.
An NSP Quality Assurance Department Finding on ORA recommendations led to process revision in April 1997. This process change provides more management involvement in OEA prioritization, by requiring management concurrence on the due dates and any scheduled completion dato chenges.
A corrective action process ov;ner was named in September 1997. The Employee Observation Reporting system was revised in September 1997. A new condition reporting system which consolidates mariy correctiva action vehicles was introduced in mid October 1997. These changes should improvs understanding and prioritization of corrective action items. Better tracking of these items shouid assist in proper resource loading to resolve the actions.
Additional personnel resource authorizatioris were approved in February 1997 and these vacancies are being filled.
Corrective Steos That Will De faken to Avoid Further Violations in response to untimely corrective action concerns roted in the July 15,1997 SSOPl Notice of Violation, NSP committed to the following additional program changes. Refer
- . _ . . - - . - . ~ . _ . _ _ . - . - . ... .-. - - _ . . . - ~ _ . - -. . - - ~ -... -
e Attachment l
.. November 14,1997 ;
to the August 15,1997 response to Notice of Violation.
e Institute a management oversi0ht committee by December 1997 ,
, e improve corrective action status reporting functions by December 1997 e Perform industry review of effective corrective actions programs by December 1997
. Institute additional corrective action program improvements in 1998 Date When Full Comoliance Will Be Achieved Design requirements have been proper!y incorporated into the AFW pump surveillance test acceptance criteria. Additionally, AFW pump flow rate specified in the USAR, section 11.9.3 for Main Feedwater Line Rupture has been corrected. Some corrective '
action program enhancements have been completed to date. Other corrective actions listed in the August 15,1997 response that address untimely corrective action will be
-completed in 1997 and 1998. Full compliance has been achieved.
i k
I
(
w - - -
,-sw.,w-,- . .2ny- m,._.._.-w... . w.r. ,..,..w.,, , ._m,w.--,m.ww--,r,.m,_-