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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20205G4071999-03-25025 March 1999 Security Event Rept:On 990304,failure to Properly Compensate for Loss of Safeguards Equipment That Could Have Resulted in Undetected Intrusion Into Protected or Vital Area,Was Discovered.Caused by Msk 325 Failure.Replaced Msk 325 ML20248M0501998-06-0808 June 1998 Special Rept 98-02:on 980502,Channel 3 of loose-part Detection Sys Was Declared to Be Inoperable.Caused by Failure of Component Inaccessible at Power.Addl Troubleshooting Will Be Performed ML20198S6361998-01-22022 January 1998 Ro:On 980121,determined That Plant Shutdown Would Be Required IAW TS 3.8.1.1,Action D.Caused by 'B' Train EES Charcoal Absorber Being Determined Inoperable.Requested 24 Hour Extension to Allow Restoration of EDG & ESW Train ML20137S6051997-04-10010 April 1997 Special Rept 97-01:on 970227,train a RVLIS Declared Inoperable Due to Failed Circuit Board in Transmitter. Transmitter Will Be Replaced During Next Outage W/Applicable Conditions or No Later than Spring 1998 ML20097D4121996-02-0101 February 1996 Special Rept 96-01:on 960110,invalid Start Failure of DG B Occurred Due to Air Start Distributor Rotor Misalignment. New Shaft & Rotor Installed ULNRC-03108, Special Rept 94-05:on 941111,discovered Unit Vent - High Range Noble Gas Monitor (GTRE0021B) Inoperable for Greater than Seven Days.Caused by Misunderstanding of Channel 216 Failure Characteristics.Monitor Declared Operable on 9411181994-12-0202 December 1994 Special Rept 94-05:on 941111,discovered Unit Vent - High Range Noble Gas Monitor (GTRE0021B) Inoperable for Greater than Seven Days.Caused by Misunderstanding of Channel 216 Failure Characteristics.Monitor Declared Operable on 941118 ULNRC-03066, Special Rept:On 940809,discovered Two Invalid a Failures During Troubleshooting Due to Air Start Solenoid Failures1994-09-0808 September 1994 Special Rept:On 940809,discovered Two Invalid a Failures During Troubleshooting Due to Air Start Solenoid Failures ULNRC-03060, Special Rept 94-03:on 940726,determined Inoperability of One Channel of loose-part Detection Sys.Caused by Intermittent Field Cable Short.Channel Seven on Reactor Head Assembly Remains Inoperable Pending Next Available Outage1994-09-0101 September 1994 Special Rept 94-03:on 940726,determined Inoperability of One Channel of loose-part Detection Sys.Caused by Intermittent Field Cable Short.Channel Seven on Reactor Head Assembly Remains Inoperable Pending Next Available Outage ULNRC-03057, Special Rept 94-02:on 940803,05 & 18,during Tenth Yr Inservice Surveillance Acceptance Criteria of TS 4.6.1.6.1.b.1 Not Met.Observed Tendon Conditions & Voids Do Not Indicate Significant Degradation of post-tensioning Sys1994-08-29029 August 1994 Special Rept 94-02:on 940803,05 & 18,during Tenth Yr Inservice Surveillance Acceptance Criteria of TS 4.6.1.6.1.b.1 Not Met.Observed Tendon Conditions & Voids Do Not Indicate Significant Degradation of post-tensioning Sys ML20072A9341994-08-0505 August 1994 Special Rept:On 940713,valid Failure of DG a Occurred Due to Loose Tachometer Signal Generator Found During Troubleshooting.Tachometer Secured & Verified ULNRC-02925, Special Rept 93-05:on 931020,valid Diesel Generator B Failure Occurred Due to Intermittent Speed Switch Opening Field Flashing Current Limiting Resistor.Surveillance Tests Currently Performed at Least Once Per 31 Days for DG B1993-12-20020 December 1993 Special Rept 93-05:on 931020,valid Diesel Generator B Failure Occurred Due to Intermittent Speed Switch Opening Field Flashing Current Limiting Resistor.Surveillance Tests Currently Performed at Least Once Per 31 Days for DG B ULNRC-02922, Special Rept 93-04:on 931119,channel 7 of loose-part Detection Sys Determined Inoperable for Greater than 30 Days.Charge Converter Replaced.Troubleshooting Revealed Problem W/Sensor Mounting or Associated Sensor Cabling1993-12-20020 December 1993 Special Rept 93-04:on 931119,channel 7 of loose-part Detection Sys Determined Inoperable for Greater than 30 Days.Charge Converter Replaced.Troubleshooting Revealed Problem W/Sensor Mounting or Associated Sensor Cabling ML20095A6951992-04-16016 April 1992 Special Rept 92-01:on 920322,emergency Diesel Generator a Failed to Reach Required Voltage & Frequency within 12 S. Caused by Dust Particles Trapped in Voltage Regulator Relay. Relay Replaced & Generator Successfully Started ML20086D6971991-11-20020 November 1991 Special Rept 91-05:on 911021,gasoline Contaminated Soils Discovered During Removal of Undergound Storage Tank.Site Assessment of Excavated Areas Performed to Define Extent of Gasoline Contamination ML20085D8241991-10-0909 October 1991 Special Rept 91-04:on 910927,red Indication Values Received on Wind Direction Instrumentation Computer Screen.On 911004, Discovered That Wind Direction Recorder Inoperable Since 910923.Wind Direction Transmitter Replaced ML20083D2341991-09-19019 September 1991 Special Rept 91-03:on 910820,determined That loose-part Detection Sys Channel Inoperable for More than 30 Days. Caused by Problems W/Sensor Mounting & Associated Sensor Cabling.Corrective Actions to Be Determined ML20082T1151991-09-12012 September 1991 Special Rept:On 910814,valid Diesel Generator Failure Occurred During 1 H Load Test Due to Component Failure. Failed Governor Sent to Vendor for Evaluation ML20082E2471991-07-25025 July 1991 Special Rept 91-01 Re Loose Part Detection Sys Channel Remaining Inoperable for Greater than 30 Days.Cause Under Investigation.Until Further Troubleshooting Completed, Corrective Actions Cannot Be Determined ML20065K1351990-11-0505 November 1990 Revised Special Rept 90-02-01:on 900924,invalid Diesel Generator Failure Occurred Due to Improper Output Breaker Plunger Clearance.Rev Changes Basis for Invalidity of Diesel Generator Failure Per Reg Guide 1.108 ML20062C3821990-10-24024 October 1990 Special Rept 90-02:on 900924,invalid Diesel Generator Failure Occurred Due to Improper Output Breaker Plunger Clearance.Evaluation of Design & Use of Test Link Will Be Performed ML20058N0871990-08-10010 August 1990 Special Rept 90-01:on 900718,invalid Failure of Diesel Generator a Occurred.Caused by Personnel Error Due to Procedural Inadequacy.Procedure Revised to Reflect Loading Requirements When Paralleling Diesel Generator ML20247R0711989-09-14014 September 1989 Special Rept 89-10:on 890810,fifth-yr Inservice Containment Vessel Tendon Surveillance Failure Identified.Caused by Void Existing within Tendon Duct Boundary.Future Tests Will Monitor Containment to Detect Any Potential Degradation ML20246Q1931989-09-0505 September 1989 Special Rept 89-10:on 890810,discovered That Net Refill Vol of Sheathing Filler Grease Exceeded 5% of Net Duct Vol for Tendons.Caused by Initial Filling Method Inducing Air Entrapment Into Filler Matl.Structural Integrity Unaffected ML20247M3311989-07-26026 July 1989 Special Rept 89-09:on 890619,Channel 3 of Loose Part Detection Sys Inoperable.Caused by Problems W/Sensor,Sensor Mounting or Associated Sensor Cabling.Troubleshooting Will Not Be Performed Until Next Outage of Sufficient Duration ML20247M4481989-07-26026 July 1989 Special Rept 89-06:on 890518,ESF Safety Injection Actuation on Train a Received Due to Low Streamline Pressure Signal During Reactor Trip Breaker Trip Actuating Device Operational Test.Plant Restored to Normal Condition ML20247L0081989-07-24024 July 1989 Rev 1 to Special Rept 89-03:on 890330,emergency Diesel Generator a Declared Inoperable.Caused by Cooling Water Leaking from Exhaust Valve Cooling Jumpers Into Rocker Arm Lube Oil Reservoir.Tests Performed Once Per 31 Days ML20247E1791989-07-19019 July 1989 Special Rept 89-07:on 890401,emergency Diesel Generator a Failed to Start as Required During Performance of Surveillance Test Procedure.Caused by Failure of Relay Driver Card.Card Replaced & Proper Operation Verified ML20247E1581989-07-19019 July 1989 Special Rept 89-08:on 890403,emergency Diesel Generator B Failed to Start Due to Operator Failing to Keep Pushbuttons Depressed Long Enough to Generate Start Signal.Procedures Revised to Caution of 1.2 Time Delay ML20245K7171989-05-0101 May 1989 Special Rept 89-03:on 890330,emergency Diesel Generator a Declared Inoperable Due to Cooling Water Leaking from Exhaust Valve Cooling Water Jumper O-rings on Cylinder 8 Into Rocker Arm Lube Oil Reservoir.Jumpers Replaced ML20245L1891989-04-28028 April 1989 Special Rept 89-02:on 890329,emergency Diesel Generator a Tripped on Overspeed Due to Governor Not Being Set Low Enough.Caused by Procedural Inadequacies.Procedure OT-NE-00001, Standby Diesel Generation Sys to Be Revised ML20235P8921989-02-21021 February 1989 Special Rept 89-01:on 890119,smoke Observed Coming from Diesel Generator Regulator Power Transformer Cabinet.Caused by Open Output Fuses from Exciter Power Potential Transformer.Transformer Meggered ML20150D9781988-07-0808 July 1988 Special Rept 88-02:on 880613,approx 13,000 Gallons of NaOC1, 12.45 Ph Spilled at Cooling Water Chemical Control Sys Bldg. on 880617,second Spill Occurred.Caused by Open Drain Valve. PVC Piping to Be Replaced W/Stronger Piping ML20155C8801988-05-31031 May 1988 Rev 1 to Special Rept 88-01:on 880213,ECCS Actuation Occurred.Caused by Open Main Steam Line Drain Valves & Malfunctioned Main Steam Seal Automatic Pressure Regulator Valve.Eccs Repaired & Plant Restored to Normal ML20154B3901988-05-0909 May 1988 Special Rept 88-01:on 880213,low Steam Line Pressure Signal Received Resulting in Safety Injection.Caused by Personnel Oversight.Msiv Shut ML20236Q3121987-11-16016 November 1987 Special Rept 87-13:on 871106,prior to Fuel Cycle 3,moderator Temp Coefficient Measured to Be Positive 0.372 Pcm/F.Control Rod Withdrawal Limits Established & Control Rods Have Been Maintained within Limits ML20236Q0951987-11-16016 November 1987 Special Rept 87-14:on 871010,free Field Seismic Sensor Made Inoperable.Caused by Voltage Surge in Power Cable to Sensor Due to Lightning Strike.Seismic Monitoring Instrumentation Sys Expected to Be Restored on 871130 ML20236A8931987-10-15015 October 1987 Special Rept 87-11,reporting Number of Tubes Plugged During Third Steam Generator Tube Inservice Insp.Eight Tubes Plugged ML20235W5421987-10-0909 October 1987 Special Rept 87-10:on 870912,three of Six Delivery Valve Cap Screws on Fuel Injection Pump Failed Causing Fuel Oil Leak.Caused by Improper Torquing of Fuel Injector Delivery Valve Flange Capscrews.Flange Removed & Capsrews Replaced ML20235K1821987-09-28028 September 1987 Special Rept 87-09:on 870911,RCS Specific Activity Exceed 1.18 Uci Per G Dose Equivalent I-131.Caused by Release of Radioactive Idodine from Known Fuel Cladding Defects.Fuel Assemblies Will Be Ultrasonically Tested for Defect ML20238C8091987-08-31031 August 1987 Suppl 1 to Special Rept 87-08:on 870706,tendon V18 & Five Addl Tendons Failed to Meet Surveillance Requirement 4.6.1.6.1.e.1.Initially Reported on 870813.Voids in Excess of 5% of Net Duct Vol Did Not Result in Any Degradation ML20237J8661987-08-13013 August 1987 Special Rept 87-08:on 870706,discovered That Net Refill Vol of Sheathing Filler Matl Exceeded 5% Net Duct Vol for Surveillance Tendon V18.Voids Have Not Resulted in Any Degradation of post-tensioning Sys ML20235T5461987-07-13013 July 1987 Special Rept 87-07:on 870601,while Reinserting Scratch Pads for 48 Sensors,Scriber Tip for Sensor 15 Inadvertently Broke.Cause Unknown.Work Request Initiated & Sensor Will Be Replaced ML20235E6131987-07-0606 July 1987 Special Rept 87-06:on 870622,actuation of Seismic Monitoring Instrumentation Occurred.Probably Caused by Equipment Malfunction.Further Investigation Underway to Determine Exact Cause of Malfunction ML20216F8491987-06-22022 June 1987 Special Rept 87-05:on 870608,unusual Event Declared Due to Actuation of Seismic Monitoring Instrumentation.Caused Not Determined.Evaluation Indicated That Industrial Mine Blasts in Area Did Not Cause Actuation ML20209B9921987-04-22022 April 1987 Special Rept 87-02:on 870402,dose Equivalent I-131 of RCS Sampled & Found to Be 1.143 Uci/Gram.Caused by Fuel Cladding Defects.Appropriate Sampling & Analysis Requirements Performed Until RCS Activity Restored within Limits ML20206G1481987-03-0909 March 1987 Special Rept 86-06:on 860303-31,first Eddy Current Inservice Insp Performed on Steam Generators a & D to Meet Tech Spec 3/4.4.5 Surveillance Requirements.Number of Tubes Containing Imperfections Encl ML20212E2681987-02-27027 February 1987 Special Rept 87-01:on 870130,dose Equivalent I-131 of RCS Found to Be 1.53 Uci/G.Caused by Fuel Cladding Defects. Appropriate Sampling & Analysis Performed Until Activity Restored within Limits ML20215N8651986-10-31031 October 1986 Special Rept 86-08:from 860922,loose-part Detection Sys Inoperable.Caused by Ground Condition in Channel 5 Hard Wire/Soft Wire Junction Box.Hand Hole Cover & Junction Box Will Be Repaired During Next Outage ML20214X4051986-09-23023 September 1986 Special Rept 86-07:on 860825,RCS Sampled & Found to Exceed Tech Spec 3.4.8 Limitation.Caused by Defects in Cladding of Fuel.Appropriate Sampling & Analysis Requirements Performed Until RCS Specific Activity Restored within Limits ML20212N5721986-08-15015 August 1986 Special Rept 86-05:on 860808,loose Part Detection Sys Channel 5 Inoperable in Excess of Tech Spec 3.3.3.8 30-day Limit.Caused by Ground Condition Due to Steam Generator Sludge Lance Hand Hole Cover Leak.Cover Resealed 1999-03-25
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E2691999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Callaway Plant,Unit 1.With ML20212D0711999-09-14014 September 1999 Safety Evaluation Re GL 88-20, Individual Plant Exam for Severe Accident Vulnerabilities ML20212A3361999-09-14014 September 1999 1999 Biennial RERP Exercise, for Callaway Plant. Pages 7,8 & 9 (of 9) in Mini Scenario 1 Section of Incoming Submittal Not Included ML20211N0451999-09-0202 September 1999 Safety Evaluation Concluding That Util Has Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves at Plant That Are Susceptible to Pressure Locking & Binding ML20212A0201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Callaway Plant,Unit 1.With ML20210P0441999-08-10010 August 1999 Safety Evaluation Granting Licensee Requests for Relief (ISI-13 - ISI-18) from Requirements of Section XI of 1989 Edition of ASME B&PV Code,For Second 10-year Interval ISI at Plant,Unit 1 ML20210Q8331999-08-0505 August 1999 Rev 4 to Callaway Cycle 10 Colr ML20210T9481999-08-0303 August 1999 Informs Commission Re Status of Issues Related to Risk Informed Decision Making That Were Raised During Staff Review of License Amend Approving Electrosleeve SG Tube Repair Method for Ue Callaway Plant,Unit 1 ML20216D8791999-07-31031 July 1999 Rev 3 to Callaway Cycle 10 Colr ML20210T4451999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Callaway Plant,Unit 1.With ML20210H6531999-07-30030 July 1999 SER Accepting Relief Request to Second Ten Year Inservice Insp Plant for Plant,Unit 1 ML20209H0881999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Callaway Plant,Unit 1.With ML20195H4831999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Callaway Plant,Unit 1.With ML20206R7111999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Callaway Plant Unit 1.With ML20205Q5561999-04-19019 April 1999 Safety Evaluation Accepting Relief for Request from Certain ASME Section Requirements for Containment Insp ML20205S5791999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Callaway Plant Unit 1.With ML20207A7401999-03-30030 March 1999 Draft, Evaluation of Risk of Induced Steam Generator Tube Rupture, for Callaway Plant ML20205G4071999-03-25025 March 1999 Security Event Rept:On 990304,failure to Properly Compensate for Loss of Safeguards Equipment That Could Have Resulted in Undetected Intrusion Into Protected or Vital Area,Was Discovered.Caused by Msk 325 Failure.Replaced Msk 325 ML20204B6741999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Callaway Plant,Unit 1.With ML20199E7011998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Callaway Plant.With ULNRC-03990, 1998 Annual Rept for Ameren Corp/Union Electric Co. with1998-12-31031 December 1998 1998 Annual Rept for Ameren Corp/Union Electric Co. with ML20198D9811998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Callaway Plant,Unit 1.With ML20195C8341998-11-10010 November 1998 Rev 20 to Operating QA Manual ML20195C8181998-11-0909 November 1998 Rev 19 marked-up Changes to Operating QA Manual ML20195D6931998-10-31031 October 1998 Non-proprietary Rev 3 to Electrosleeving Qualification for PWR Recirculating SG Tube Repair ML20195D3581998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Callaway Plant,Unit 1.With ML20154L4931998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Callaway Plant Unit 1.With ML20151Y5151998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Callaway Plant,Unit 1.With ML20155B5871998-08-28028 August 1998 Non-proprietary Rev 1 to 51-5001925-01, Risk Assessment for Installation of Electrosleeves at BVPS & Callaway Plant ML20237B8421998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Callaway Plant,Unit 1 ML20155H7381998-06-30030 June 1998 10CFR50.59 Summary Rept for Jan-June 1998. with ML20236Q9991998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Callaway Plant,Unit 1 ML20249C5851998-06-30030 June 1998 Rev 1 to Callaway Cycle 10,COLR ML20248M0501998-06-0808 June 1998 Special Rept 98-02:on 980502,Channel 3 of loose-part Detection Sys Was Declared to Be Inoperable.Caused by Failure of Component Inaccessible at Power.Addl Troubleshooting Will Be Performed ML20249A7681998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Callaway Plant,Unit 1 ML20249B2451998-05-18018 May 1998 Nonproprietary Version of Revised Chapters 4 & 5 to Rev 4 of HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants for Ue & Wcnoc. Chapters 4 & 5 Reflect Editorial Revs ML20248C3681998-05-18018 May 1998 Non-proprietary Version of Rev 4 to HI-971769, Licensing Rept for Reracking of Callaway & Wolf Creek Nuclear Plants ML20247G0811998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Callaway Plant Unit 1 ML20217R2031998-04-27027 April 1998 Cycle 10 Colr ML20216H0651998-04-15015 April 1998 SER Approving Licensee Proposed Alternative to Use Code Case N-508-1 for Rotation of Serviced Snubbers & Prvs for Purpose of Testing in Lieu of ASME B&PV Code,Section Xi,Article IWA-7000 Requirements ML20216K0531998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Callaway Plant,Unit 1 ML20217F3181998-03-24024 March 1998 SER Accepting Relief Request for Approval for Use of Alternate Exam Requirements for Plant Inservice Insp Program ML20216G3551998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Callaway Plant, Unit 1 ML20203M0101998-02-25025 February 1998 Rev 11 to Callaway Cycle 9 Colr ML20203A7951998-02-0909 February 1998 Rev 10 to Callaway Cycle 9 Colr ML20202D4821998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Callaway Plant ML20198S6361998-01-22022 January 1998 Ro:On 980121,determined That Plant Shutdown Would Be Required IAW TS 3.8.1.1,Action D.Caused by 'B' Train EES Charcoal Absorber Being Determined Inoperable.Requested 24 Hour Extension to Allow Restoration of EDG & ESW Train ULNRC-03775, 1997 Annual Rept for Union Electric1997-12-31031 December 1997 1997 Annual Rept for Union Electric ML20198Q0631997-12-31031 December 1997 Rev 9 to Callaway Cycle 9 Colr ML20198J6791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Callaway Plant,Unit 1 1999-09-30
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Cataway Plant May 5, 1986 PRIORITY RO'JII M Mr. James G. Keppler I GS~~I hL2 Regional Administrator i d5T_ EA -
Office of Inspection & Enforcement 4" -
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t U.S. Nuclear Regulatory Commission FILE g Region III 799 Roosevelt Road Glen Ellyn, IL 60137
[
ULNRC-1305
Dear Mr. Keppler:
DOCKET NUMBER 50-483 CALLAWAY PLANT UNIT 1 FACILITY OPERATING LICENSE NPF-30 SPECIAL REPORT 86-03 CHALLENGE TO OVERPRESSURE PROTECTION SYSTEM The enclosed Special Report is submitted pursuant to Technical Specification 3.4.9.3 and 6.9.2 concerning a challenge to the Overpressure Protection System.
h Yr G. L. Randolph Manager, Callaway Plant (l' Y MET / EA/TPS/ WK/drs Enclosure cc: Distribution attached k
S Do i e i\
m me g 0 MaMg A#ess PO Box 620, Fulton, MO 65251
cc distribution for ULNRC-1305 Mr. Paul O'Connor Manager, Electric Department Office of Nuclear Reactor Regulation Missouri Public Service Commission U.S. Nuclear Regulatory Commission P. O. Box 360 Mail Stop P-316 Jefferson City, MO 65102 7920 Norfolk Avenue Bethesda, MD 20014 Mr. O. Maynard Kansas Gas and Electric Company P. O. Box 208 American Nuclear Insurers Wichita, KS 62701 c/o Dottie Sherman, Library The Exchange Suite 245 Mr. Nicholas A. Petrick 270 Farmington Avenue Executive Director, SNUPPS Farmington, CT 06032 5 Choke Cherry Road Rockville, MD 20850 Mr. J. H. Smith Bechtel Power Corporation Records Center SNUPPS Project Institute of Nuclear Power Operations 15740 Shady Grove Road Suite 1500 Gaithersburg, MD 20877-1454 1100 Circle 75 Parkway Atlanta, GA 30339 NRC Resident Inspector Mr. Merlin Williams D. F. Schnell (400) Supt. of Regulatory Quality &
R. J. Schukai (470) Administrative Services S. E. Miltenberger Kansas Gas and Electric Company J. F. McLaughlin P. O. Box 309 J. E. Davis (Z40LER) Burlington, KS 66839 (Z40LER) (w/c)
D. W. Capone /R. P. Wendling (470)
F. D. Field (470)
A. P. Neuhalfen A. C. Passwater/D. E. Shafer/D. J. Walker (470)
G. A. Hughes Z40.03 (QA Record)
J. M. Price R. D. Affolter W. R. Robinson M. E. Taylor H. Wuertenbaecher, Jr. (100)
S. L. Auston (470)(NSRB)
J. D. Schnack GLR Chrono 3456-0021.6 3456-0260 Z40ULNRC G56.37 N. Date (Sandra Auston) (470)
SPECIAL REPORT 86-03 CHALLENCE TO OVERPRESSURE PROTECTION SYSTEM The Overpressure Protection System was challenged on 4/5/86 at approximately 0121 CST while the plant was in Mode 5 (Cold Shutdown).
Pressurizer power operated relief valve (PORV) BB-PCV-455A and Residual Heat Removal (RHR) suction relief valves EJ-8708A and EJ-8708B lif ted during a Reactor Coolant System (RCS) pressure transient initiated as a result of control problems experienced with control valve BC-HV-8357A (Centrifugal Charging Pump 'A' discharge to Reactor Coolant Pump seals control valve).
Prior to the event, the RCS was in a solid plant condition with RCS pressure being maintained between approximately 380 to 405 p.s.i.g. and RCS temperature at approximately 104 degrees F. Centrifugal Charging Pump ' A' was in service providing RCS charging flow through the Boron Injection Tank and Reactor Coolant Pump seal injection flow through BG-HV-8357A. RHR trains 'A' and 'B' were in service.
At approximately 0120 the reactor operator attempted to close BG-HV-8357A however the valve did not properly respond. Approximately one minute later a 'PORV OPEN' annunciator was momentarily received on the main control board. A pressure spike was recorded on pressure recorder BB-PR-403 (RHR Pump 'A' Suction and PORV Control Wide Range Pressure Recorder) and the Alarm Printer indicated a 'RCS Water Pressure
- Hi' alarm. The reactor operator adjusted control valve BG-HCV-128 (RHR Cleanup to the Letdown Heat Exchanger Flow Hand Control Valve) to stabilize RCS pressure.
The cause of the pressure transient was determined to be excessive flow through BG-HV-8357A. The excess flow entered the RCS through the Reactor Coolant Pump seals and was sufficient to initiate the RCS pressure transient. The inability to reposition BG-HV-8357A was due to a failure of a controller card. The failure was determined to be a random card failure and the controller card was replaced on 4/9/86.
Based on receipt of the 'PORV OPEN' annunciator and available data, an engineering evaluation determined an RCS pressure transient of 97 seconds duration with a maximum RCS pressure of 463 p.s.i.g. did occur.
The overpressure limit of 530 p.s.t.g. required by Technical Specification Figure 3.4-4 was not exceeded. Pressurizer PORV BB-PCV-455A opened 74 seconds into the transient at a pressure very close to its setpoint (453.4 p.s.i.g.) and within its required tolerance. Pressure subsequently decreased to 350 p.s.i.g. within approximately 23 seconds. RCS pressure did not exceed the Ifft setpoint (467.4 p.s.i.g.) of pressurizer PORV BB-PCV-456A.
The duration of the event and previous surveillance testing indicates the RHR suction relief valves contributed minimally to mitigate the transient since RCS pressure was only above 445 p.s.i.g.
(lift setpoints of the RHR suction relief valves are 444 and 445 p.s.i.g.) for approximately eleven seconds.
SPECIAL REPORT 86-03 Page 2 The lift setpoints for BB-PCV-455A, BB-PCV-456A, EJ-8708A, and EJ-8708B were verified within tolerance by surveillance testing on 3/3/86, 3/4/86, 4/12/86, and 4/8/86, respectively. Since the setpoints of BB-PCV-455A and BB-PCV-456A were found within tolerance and EJ-8708A and EJ-8708B were tested satisfactorily after the transient, no additional testing is required.
Plant instrumentation / components functioned per design in accordance with the Technical Specifications to limit the duration and magnitude of the transient. Replacing the failed controller card and including its failure in the plant's instrument trending program is considered sufficient corrective action to prevent recurrence of this incident.
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