ML20168A452

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Final ASP Analysis - D.C. Cook 1 (LER 315-79-058)
ML20168A452
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 06/16/2020
From: Christopher Hunter
NRC/RES/DRA/PRB
To:
Littlejohn J (301) 415-0428
References
LER 1979-058-00
Download: ML20168A452 (4)


Text

B-697 PRECURSOR DESCRIPTION AND DATA NSIC Accession Number: 153333 Date: November 15, 1979

Title:

Flowpath from AFW Pump to Two Steam Generators Made Inoperable at Cook 1 The failure sequence was:

With the reactor at 100% power and the turbine driven AEW pump out of service for repair, the motor control center which provides power for valves which direct flow from one motor-driven AFW pump to two of the four steam generators was removed from service for inspection.

Corrective action:

The motor control center was returned to service.

Design purpose of failed system or component:

The motor control center provides power to the two motor operated valves associated with the AFW flow path from the motor-driven AFW pumps to two of the four steam generators.

Unavailability of system per WASH 1400: *AEW (loss of net + 8 hrs): 2.5 x 1-Unavailability of component per WASH 1.400: -

Unavailabilities are in units of per demand UD Failure rates are in units of per hour HR-'

Reactor at 100% Power Supply for Valves Potential Power with Turbine- from Motor-Operated AFW Severe Driven AFW Pump Pump to Two of Four Gore Damage Out of Service Steam Generators Removed from Service for Inspection

.1.

No - Flowpath from one motor-operated AFW pump to two steam generators still available plus no loss of feedwater.

- No 0%

NSIC 153333 - Actual Occurrence for Flowpath from AFW Pump to Two Steam Generators Made Inoperable at Cook 1

Potential Sequence Severe No.

Core Damage No 1 No 2 Yes 3 Yes 4 No 5 No to 6

Yes 7 Yes 8 No 9

-No 10

.Yes 11

.Yes 12 Yes 13 NSIC 153333 - Sequence of Interest for Flowpath from AFW Pump to Two Steam Generators Made Inoperable at Cook 1

B-700 CATEGORIZATION OF ACCIDENT SEQUENCE PRECURSORS NSIC ACCESSION NUMBER: 153333 DATE OF LER: November 29, 1979 DATE OF EVENT: November 15, 1979 SYSTEM INVOLVED: Auxiliary Feedwater COMPONENT INVOLVED: Motor Operated Valves CAUSE: Motor Control Center removed from service for inspection while the turbine-driven AFW pump was out of service for repair, human error SEQUENCE OF INTEREST: loss of of feedwater ACTUAL OCCURRENCE: unavailability of two AFW system valves plus the turbine driven AFW pump REACTOR NAME: Cook 1 DOCKET NUMBER: 50-315 REACTOR TYPE: PWR DESIGN ELECTRICAL RATING: 1054 MWe REACTOR AGE: 4.8 yr VENDOR: Westinghouse ARCHITECT-ENGINEERS: American Electric Power Corp.

OPERATORS: -Indiana and Michigan Electric Co.

LOCATION: 11 miles south Of Benton Harbor, Michigan DURATION: 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> PLANT OPERATING CONDITION: 100% power SAFETY FEATURE TYPE OF FAILURE: (a) inadequate performance; (b) failed to start; 5

lc~ýjmade inoperable; (d)____________

DISCOVERY METHOD: operator observation COMMENT: The Cook 1 FSAR states the LOFW analysis for Cook 1 assumes flow to all four steam generators. The failure reported herein resulted in flow to only two steam generators.