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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 ML20204H7131999-03-17017 March 1999 Safety Evaluation Concluding That NNECO Provided Adequate Justification for Deviations from RG 1.97,Rev 2, Recommendations,For Instrumentation Monitoring CST Level & Containment Area Radiation at Mnps Unit 2 ML20204C9441999-03-10010 March 1999 Safety Evaluation Denying Licensee Request for License Amend to Revise Frequency of Certain SRs for Electrical Power Sys ML20207L2631999-03-0505 March 1999 Safety Evaluation Supporting Amend 104 to License DPR-21 ML20207L5961999-02-22022 February 1999 Safety Evaluation Concluding That Code Requirements,Which Require 100 Percent Volumetric Exam of RPV flange-to-shell, Impractical to Perform to Extent Required & That Alternative Provide Reasonable Assurance of Structural Integrity ML20203D7601999-02-11011 February 1999 Safety Evaluation Supporting Millstone 1 Certified Fuel Handler Training & Retraining Program ML20196B0501998-11-24024 November 1998 Safety Evaluation Re Licensee 960213 Submittal of 180-day Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant,Unit 2 ML20155K1981998-11-0909 November 1998 Safety Evaluation Re Application of leak-before-break Status to Portions of Safety Injection & Shutdown Cooling Sys ML20195B8711998-11-0909 November 1998 Safety Evaluation Approving Revised Evaluation of Primary Cold Leg Piping leak-before-break Analysis for Plant ML20155C3781998-10-30030 October 1998 SER Denying Amend to Allow Changes to Fsar.Nrc Found That NNECO Had Not Considered Diversity Provided by Switch in Control Room That Removes Power to 1 of 2 MOV in SDC Sys Flow Path in Evaluation of High Low Pressure Design ML20155C8441998-10-29029 October 1998 Safety Evaluation Accepting Licensee Proposal to Withdraw ATWS Test Commitment ML20238F2781998-08-27027 August 1998 SER Related to Proposed Rev 20 to Northeast Utilities Quality Assurance Program Topical Rept for Millstone Nuclear Power Station,Units 1,2 & 3 ML20237D5001998-08-20020 August 1998 SER Approving Code Case N-389-1, Alternative Rules for Repairs,Replacements,Or Mods,Section Xi,Div 1 ML20236U7051998-07-22022 July 1998 Safety Evaluation Granting All Requests for Relief W/Exception of Requests RR-89-17 (Authorized for Class 1 Sys Only) & RR-89-21.Requests RR-13 & RR-14 Will Be Addressed in Separate Evaluation ML20236K6971998-07-0101 July 1998 SER Accepting Third 10-year Interval Inservice Insp Program Plan,Rev 2 & Associated Request for Relief & Proposed Alternatives for Plant,Unit 2 ML20236K3531998-07-0101 July 1998 Safety Evaluation Supporting Amend 218 to License DPR-65 ML20249C2541998-06-24024 June 1998 Safety Evaluation Accepting Proposed Rev 19 to NNECO QAP Topical Rept & Amended Through 980609.Informs That NNECO Exception to Provisions in Paragraph 10.3.5 of Constitutes Temporary & Acceptable Alternative ML20248J0031998-06-0404 June 1998 Safety Evaluation Accepting Millstone Nuclear Power Station Emergency Plan ML20248M2991998-06-0202 June 1998 Safety Evaluation Approving Application Re Restructuring of Central Maine Power Co by Establishment of Holding Company ML20248C4131998-05-26026 May 1998 SER of Individual Plant Exam of External Events Submittal on Millstone Nuclear Power Station,Unit 3 ML20217M4181998-04-30030 April 1998 Suppl Safety Evaluation Accepting Licensee RCS Pressure & Heat Removal by Containment Heat Removal Sys post-accident Monitoring Instrumentation ML20216G7921998-03-13013 March 1998 Safety Evaluation Authorizing Proposed Alternative to Check Valve Obturator Movement Requirements of OM-10 for SIL Accumulator Outlet for Listed Check Valves ML20203E8521998-02-17017 February 1998 SER Accepting Request for Relief from Requirements of 10CFR50.55a(f) for Performing Required Inservice Testing of Certain Class 2 Components IAW ASME Boiler & Pressure Vessel Code Section XI for Plant,Unit 3 ML20203E9341998-02-17017 February 1998 SER Accepting Request for Relief from Requirements of 10CFR50.55a(g) for Performing Required Exams for Certain Class 1 Components IAW ASME Boiler & Pressure Vessel Code Section XI for Plant,Unit 3 ML20203E2441998-02-0909 February 1998 Safety Evaluation Accepting Re Approval of Realistic,Median Centered Spectra Generated for Resolution of USI-A-46 ML20198R9941998-01-13013 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Millstone Nuclear Power Station,Unit 3 ML20202H7461997-12-10010 December 1997 Safety Evaluation Accepting Licensee Position That Correction of AC-11 Single Failure Vulnerability Unncessary ML20202J0911997-12-0202 December 1997 Safety Evaluation Accepting Proposed Exemption,Which Meets Special Circumstance Given in 10CFR50.12(a)(2)(ii) ML20198S2411997-10-31031 October 1997 SE Accepting Licensee Request for Deviations from Recommendations in Reg Guide 1.97,Rev 2 for Temp & Flow Monitoring Instrumentation for Cooling Water to ESF Sys Components & Containment Isolation Valve Position ML20212G5991997-10-27027 October 1997 Safety Evaluation Supporting Amend 103 to License DPR-21 ML20217K8801997-10-27027 October 1997 Correction to Safety Evaluation Supporting Amend 103 to License DPR-21.Phrase or Rod Block Protection Has Been Deleted from Listed Sentence in Staff Associated SE ML20212F1381997-10-22022 October 1997 Safety Evaluation Supporting Amend 102 to License DPR-21 ML20217M9301997-08-19019 August 1997 Safety Evaluation Accepting Continued Operation W/O High Startup Rate Trip by Nene for Millstone,Unit 2 ML20149J2661997-07-23023 July 1997 Safety Evaluation Accepting Changes & Reanalyses in ECCS Evaluation Models & Application of Models for Plant,Unit 2 ML20141L8821997-05-28028 May 1997 Safety Evaluation Supporting Amend 101 to License DPR-21 ML20138A0111997-04-23023 April 1997 Safety Evaluation Accepting Licensee Proposal,Not to Perform Type C Leakage Rate Testing on 14 Subject CIVs ML20137V5931997-04-15015 April 1997 Safety Evaluation Supporting Amend 100 to License DPR-21 ML20137U3121997-04-10010 April 1997 Safety Evaluation Supporting Amends 99,206 & 135 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20134A0331997-01-23023 January 1997 Safety Evaluation Accepting Util Proposed Alternatives to ASME Code Requirements ML20133N3401997-01-14014 January 1997 Safety Evaluation Supporting Amend 98 to License DPR-21 ML20135C4221996-12-0202 December 1996 Safety Evaluation Accepting Proposed Alternative Described in Relief Request R-1 Re Valve Inservice Testing Program at Facility ML20128P4381996-10-0909 October 1996 Safety Evaluation Accepting Review of Cracked Weld Operability Calculations & Staff Response to NRC Task Interference Agreement ML20128L7541996-10-0404 October 1996 Safety Evaluation Supporting Amend 97 to License DPR-21 ML20248C5451995-05-0202 May 1995 SER on Millstone Unit 3 Individual Plant Exam of External Events to Identify plant-specific Vulnerabilities,If Any,To Severe Accidents & Rept Results Together W/Any licensee-determined Improvements & C/A to Commission ML20248C5731994-07-19019 July 1994 SER Step 1 Review of Individual Plant Exam of External Fire Events for Millstone Unit 3 ML20059H4991994-01-24024 January 1994 Safety Evaluation Accepting Revised Responses to IEB-80-04 Re MSLB Reanalysis 1999-08-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
[Table view] |
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/ , ' %, UNITED STATE 8 8 NUCLEAR REGULATORY COMMIS$10N 3 $ - WA.5MNUTON, D. C. 20804
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SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULAl_0N PELATING TO NATURAL CIRCULATION C00LOOWN MILT. STONE UNIT 3 h0RTHEAST UTILITIES
. DOCKET NO. 50-423
1.0 INTRODUCTION
BranchTechnicalPosition(BTP)RSB5-1,"DesignRequirementsoftheResidual Heat Reooval (RHR) System," requiret that test progr6ms for pressurized water I reactors (PWRs) include tests with supporting analysis to (1) confirm that adeauste mixing of borated water added prior to or during cooldown can be achieved under natural circulation cor.ditions and permit estimation of the times required to achieve such mixing, and (2) confirm that the cooldown under 4 natural circulation conditions can be achieved within the limits specified in the emergency operating procedures. In addition, the plant is to be designed so that the reactor can be taken from normal operating conditions to cold shutdown using only safety-grade systems. A comparison of performance to that of previously tested plants of similar design may be substituted for these tests.
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- Hillstone Unit 3 is classified as a Class 2 plant with regard to the implementation of the above BTP.
A natural circulation / boron mixing /cooldown test was performed at Diablo Canyon Unit 1 on March 28-29, 1985. On the basis of the Diablo Canyon tests and l submittals and the Brookhaven National Laboratory (BNL) technical evaluation report (TER) dated December 1986, the staff has concluded that the Diablo Canyen Unit 1 systems meet the intent of BTP RSB 5-1 for a class 2 plant. By letter deed Noverber 6,1987, the licensee for Millstone Unit 3 submitted a 8910260093 091018 PDR ADOCK 05000423 P PDC
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Westinghouse analysis to show the applicability of the Diablo Canyon cooldewn test results to Millstone Unit 3 rather than conduct such a test at the plant.
The licensee provided the analysis en'itled t "Millstone Unit 3, Natural Circulation System Comparison," B-12983, which evaluates the capability of Millstone Unit 3 to successfully achieve cold shutdown conditions under sb reauirements of BTP RSB 5-1. The report includes t:1e following:
- 1) A comparison of the Diablo Canyon plant and Millstone Unit 3 to demonstrate their similarity.
- 2) An evaluation of the applicability of the Diablo Canyon test results to H111 stone Unit 3.
By letter dated August 3, 1988, in response to NRC staff questions, the , ,
licensee provided a revised analysis.
The staff safety evaluation for Diablo Canyon Unit 1, with the attached BNL TET entitled "Technical Evaluation Report for Diablo Canyon Natural Circulation, Boron Mixing, and Cooldown Test," identified the plant parameters that may affect application of the test results to other plants. These parameters are the basis for our evaluation and are discussed in the following sections, f 2.0 EVALUATION Natural Circulation i
Diablo Canyon Unit 1 is rated at 3338 PWt and has four loops in its reactor coolant system (RCS). Millstone Unit 3 is rated at 3411 Mwt and also has a four-loop RCS. The licent2e has stated that the general configuration of the piping and components in each reactor coolant loop is the same in both M111 store Unit 3 and Diiblo Canyon Unit 1. Significant parameters governing natural circulation are hydraulic flow resistance and thermal driving head.
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. . 3 To demonstrafe similarity in design for natural circulation, these two parameters were compared.
Data from the Westinghouse report showed that the Millstone Unit 3 hydraulic resistance coefficients at normal flow conditions was slightly 1cwer than Diablo Canyon's. Thermal driving head, however, because of a difference in steam generator tube lengths, was 5-101 higher for Diablo Canyon. The report showed that the lower natural circulation driving head '
and the lower overali piping flow resistance for Millstone Unit 3 would
> decrease the natural circulation flow ratio to approximately 0.99 times that observed for Diablo Canyon. Therefore, the licensee concluded that the natural circulation loop flow rate for either plant would be nearly the same.
Differences in reactor power and decay heat levels between the two plants are not expected to alter this conclusion.
The staff questioned the applicability of flow resist .ce at normal flow conditions when significantly lower flows would exist during natural circulation. The revised report stated that the hydraulic resistance coefficient would slightly increase at lower flows but the expected flow ratio is expected to be valid for both normal and natural circulation. The staff finds this erplanation acceptable.
RCS Cooldown The plant's ability to cool the RCS at a specified coold in nu vssuming a
,fficient supply of auxiliary feedwater, is determined ty Oh - ..scity of the atmospheric steam dump valves (ADVs). Steam flow through these valves reinoves the sensible heat and decay heat throughout the cooldown period.
The end of the cooldown period, when the ste)m centrator pressure is low, provides the most limiting ccnditions for valve capacity. The energy to be renoved is determined by the water inventory and the amovat of structural l material in the RCS, and the level of decay heat. i l
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. 4 Millstone Unft 1 has four ADVs, one for each steam generator. These ADVs, because of a non-nsfety grade air supply, cannot be given credit for plant shatdown per BTP RSB 5-1. Four motor operated, safety grade main steam pressure relieving bypass valves (MSPitVs), each of ADV capacity, ensure a steam release path in the event any ADY is unavailable. The MSPRVs are powered frem Class 1E buses.
In the event of a single failure, three steam generators would be available for coollown. In response to FSAR Question 440.24, the licensee stated that two steam g.1erators are sufficient to to cool down the RCS to the RHR initiation temperature. Therefore we find that there is reasonable assurance that the MSPRVs have n.fficient capacity to perform an RCS cooldown to the RHR initiation temperature in a reasonable time and the MSPRV capacity is therefore acceptable. In adoition, the ADVs have handwheels for ran el ope'ation and thus are potentially operab'e in the event of an insufficient air supply, i
Bypass Flow and Upper-Head Cooling A potential exists for void formation in the upper-head of the reactor tiessel during the cooldown/depressurization of the RCS under natural circulai. ion I
conditions if the upper head is relatively isolated from the res*, of the kCS and its fluid temperature remains higher than the coolatt temperature in the main flow paths of the RCS. Upper-head cooling under natural circulation conditions is influenced by core bypass flow and mixing in the upper head.
1 Westinghouse plants may be divided into wo groups according to the magnitude of the bypass flow: Thot and Teold plants. For the Tcold plants, such as Millstone Unit 3, iffic.ient bypass flow exists to make the temperature of the upper head fluid . ally e9.sa' to the cold-leg temperature. On the other hand, for the Tho' su , whi- s des Diablo Canyon, the bypass flow is e rcumstance results in upper head
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much smaller. Fs e temperature r.ing' V t w
eg and the hot-leg temperatures and
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- raises a possiteitit -
ion in the upper-heed region.
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5 The licensee stated that the reactor vessel spray nozzle between the downcorer and the upper-head region for Millstone Unit 3 has a significantly larger flow area than that of Diablo Canyon. This circumstance allows better flow comunication and mixing in the upper head during natural circulation. The upper head volume for Millstone Unit 3 is larger than that of Diablo Canyon.
The NRC staff considers the upper head volume effect on cooling of Die upper head to be small compared to the contribution of flow through the spray nozzles. We would therefore expect a shorter cooling time for a Tcold plant compared with that of a Thot plant of the same size.
Boron Mixing The Diablo Canyon boron mixing test evaluation demonstrated adequate boren mixing under natural circulation conditions when highly borated water was injected into the RCS. Contributing to the diffusion of the boron is the mixing effect created as the flow passes through the reactor coolant pumps
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and the steam generator tubes. The plant's ability to achieve the proper shutdown margin, however, depends mainly on the injection rate of boron relative to the total inventory of water in the RCS. The required concentration change of about 300 ppm for the test was achieved in less than 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.
Under normal operation at Millstone Unit 3, the boric acid solution is injected i
) into the RCS vie the charging and reactor coolant pump seal injection lines.
Upon loss of instrument air, charging flow control is possible by use of a f safety-related throttling flow path that bypasses the air operated charging flow control valva. A different thrattling valve, powered from a Class 1E bus can be used to throttle seal injection line flow.
1 In the event that both the nonna* and excess letdown lires are unavailable
! for the RCS inventory control, a safety grade reactor head vent letdown flow l path to the pressurizer relief tank is available.
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. 6 The source of boron for Millstone Unit 3 is the boric acid tanks (BAT 3) which have a boron concentration significantly less than that of Diablo Canyon.
Thus, addition of a larger quantity of borated water over a longer time will be required to reach the desired condntration change. The licensee calcula+ed that for Millstone Unit 3, approximately one hour is needed to achieve the same concentration change demonstrated in the test. On the basis of this calculation the staff finds that there is reasonable assurance that sufficient time exists for boron injection and mixing to achieve the required shutdown margin.
Depressurization -
The Diablo Canyon test demonstreted that the RCS could be depressurized from cooldown conditions to the RHR initiation pressure under natural circulation conditions using the pressurizer auxiliary spray and/or pressurizer power operated relief valves (PORVs).
At Millstone Unit 3 depressurization may be accomplished through the use of the pressurizer PORVs or the pressurizer auxiliary spray.' However, the pressurizer auxiliary sprsy is not safety grade, and thus is not available for the RCS depressurization per BTP RSB 5-1.
The licensee steted that either of the two PORVs is capable of providing the depressurization function, Each PORY has a safety-grade Class IE solenoid operated valve. In the event that a PORV fails open, the PORY block valves,
- which are safety-grade, may be used to block the affected PORY flow path. At i
che end of the depressurization, the RCS is approximately at 400 psig. The RHR system may now be placed in service and the cooldown to cold shutdown condition cont:n'uei. <
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Cooling Water' The primary auxiliary feedwater supply to the steam generators is provided by the condensate storage tank (CST)a ' t Diablo Canyon, while Millstone Unit 3 uses the reismic category I demineralized water storage tank (DWST).
Alternate sources of auxiliary feedwater at Hillstone Unit 3 include the CST, service water system, and the domestic water system. Spoolpieces, maintained on site, must be added to connect the service water and domestic water systems to the auxiliary feedwater system.
The BNL TER estimated a 360,000-gallon auxiliary feed water requirement for Diablo Canyon on the basis of e 43-hour cooling time for the upper head.
This calculation was based on assumptions of no heat loss from the upper head to the containment and a limited amount of bypass fluid mixing with fluid in the Lottom of the uppar head. We would further conclude that had Diablo Canyon been a Tcold plant, and with heat transfer from the upper head to containment considered, the cooling requirement would have been eig,,if t:rtly less than 360,000 gallons.
The Millstone Unit 3 DWST has a capacity of 340,000 gallons with a technical specification (TS) uinimum capacity of 334,000 g:llons. In addition, the alternate or backup supply provides an essentially unlimited auxiliary feedwater supply. Since Millstone Unit 3 is a Tcold plant, we conclede that there is reasonable assurance that sufficient cooling water inventory exists to meet the proposed plant cooldown method . -
3.0 CONCLUSION
The staff assessed the capability of Millstone Unit 3 to meet the requirements of RSB BTP 5-1. We have identified and evaluated the plant paran ters that may affect application of the Diablo Canyon natural circulation test results to Millstone Unit 3. l l
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On the basis'of the licensee's submittals, and our evaluation as previously discussed, we conclude that the licensee has demonstrated that the Diablo Canyon natural circulation tests are applicable to Millstone Unit 3 and that they comply with the requiremerits of BTP RSB 5-1.
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