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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P3791999-10-21021 October 1999 Forwards NRC Form 396 & NRC Form 398 for Renewal of Licenses SOP-20607-1 & SOP-20610-1.Without Encls ML20217N2521999-10-20020 October 1999 Provides Supplemental Info Re 990405 Containment Insp Program Requests for Relief RR-L-1 & RR-L-2,in Response to 991013 Telcon with NRC ML20217K7541999-10-15015 October 1999 Forwards Rev 1 to Unit 1,Cycle 9 & Unit 2 Cycle 7 Colrs,Iaw Requirements of TS 5.6.5.Figure 5, Axial Flux Difference Limits as Function of Percent of Rated Thermal Power for RAOC, Was Revised for Both Units ML20217G6751999-10-13013 October 1999 Requests Withholding of Proprietary Info Contained in Application for Amend to OLs to Implement Relaxations Allowed by WCAP-14333-P-A,rev 1 ML20217G1071999-10-0707 October 1999 Informs That on 990930,NRC Staff Completed mid-cycle PPR of Vogtle & Did Not Identify Any Areas in Which Performance Warranted More than Core Insp Program.Nrc Plans to Conduct Core Insps at Facility Over Next Six Months ML20216J9041999-10-0101 October 1999 Forwards Response to RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20216J9161999-10-0101 October 1999 Forwards Response to NRC 990723 RAI Re GL 95-07, Pressure Locking & Thermal Binding of SR Power-Operated Gate Valves ML20217B0141999-10-0101 October 1999 Forwards Insp Repts 50-424/99-06 & 50-425/99-06 on 990725- 0904 at Vogtle Units 1 & 2 Reactor Facilities.Determined That One Violation Occurred & Being Treated as non-cited Violation ML20212E8751999-09-20020 September 1999 Forwards Response to NRC GL 99-02, Lab Testing of Nuclear Grade Activated Charcoal. Description of Methods Used to Comply with Std Along with Most Recent Test Results Encl ML20212E7481999-09-20020 September 1999 Requests Approval Per 10CFR50.55a to Use Alternative Method for Determining Qualified Life of Certain BOP Diaphragm Valves than That Specified in Code Case N-31.Proposed Alternative,Encl ML20212C2191999-09-16016 September 1999 Forwards NRC Form 536, Operator Licensing Exam Data, Which Is Current Need for NRC Operator Licensing Exams for Years 2000 Through 2003 of Plant Vogtle,Per Administrative Ltr 99-03 ML20211Q4801999-09-0101 September 1999 Informs That on 990812-13,Region II Hosted Training Managers Conference on Recent Changes to Operator Licensing Program. List of Attendees,Copy of Slide Presentations & List of Questions Received from Participants Encl ML20211J5291999-08-30030 August 1999 Forwards Snoc Copyright Notice Dtd 990825,re Production of Engineering Drawings Ref in VEGP UFSAR ML20211J5251999-08-30030 August 1999 Forwards Response to NRC 990727 RAI Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20211J7381999-08-27027 August 1999 Informs That Licensee Vessel Data Is Different than NRC Database Based on Listed Info,Per 990722 Request to Review Rvid ML20211E9251999-08-23023 August 1999 Forwards fitness-for-duty Performance Data for Jan-June 1999,as Required by 10CFR26.71(d).Data Reflected in Rept Covers Employees at Vogtle Electric Generating Plant ML20210V0881999-08-16016 August 1999 Forwards Insp Repts 50-424/99-05 & 50-425/99-05 on 990620- 0724.No Violations Noted.Vogtle Facility Generally Characterized by safety-conscious Operations,Sound Engineering & Maintenance Practices ML20210Q4611999-08-0505 August 1999 Informs That NRC Plans to Administer Generic Fundamentals Exam Section of Written Operator Licensing Exam on 991006 for Vogtle.Requests Info Re Individuals Who Will Take Exam. Sample Registration Ltr Encl ML20210L2181999-08-0202 August 1999 Forwards NRC Form 396 & Form 398 for Renewal of Listed Licenses,Iaw 10CFR55.57.Without Encl ML20210N1191999-08-0202 August 1999 Discusses 990727 Telcon Between Rs Baldwin & R Brown Re Administration of Licensing Exam at Facility During Wk of 991213 ML20210G3351999-07-27027 July 1999 Forwards Second Request for Addl Info Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20210E0121999-07-23023 July 1999 Forwards Second Request for Addl Info Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20210D9341999-07-22022 July 1999 Discusses Closure of TACs MA0581 & MA0582,response to Requests for Info in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20210C8011999-07-21021 July 1999 Provides Response to NRC AL 99-02,which Requests That Addressees Submit Info Pertaining to Estimates of Number of Licensing Actions That Will Be Submitted for NRC Review for Upcoming Fy 2000 & 2001 ML20210E0431999-07-15015 July 1999 Forwards Insp Repts 50-424/99-04 & 50-425/99-04 on 990502- 0619.Two Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20209H3881999-07-14014 July 1999 Forwards Revs 1 & 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Unit 1 & 2 ML20209C4041999-07-0101 July 1999 Forwards Rev 29 to VEGP Units 1 & 2 Emergency Plan.Rev 29 Incorporates Design Change Associated with Consolidation of Er Facilities Computer & Protues Computer.Justifications for Changes & Insertion Instructions Are Encl ML20196H8081999-06-28028 June 1999 Discusses 990528 Meeting Re Results of Periodic PPR for Period of Feb 1997 to Jan 1999.List of Attendees Encl ML20212J2521999-06-21021 June 1999 Responds to NRC RAI Re Yr 2000 Readiness at Nuclear Power Plants.Gl 98-01 Requested Response on Status of Facility Y2K Readiness by 990701 ML20196F9171999-06-21021 June 1999 Forwards Owner Rept for ISI for Vogtle Electric Generating Plant,Unit 1 Eighth Maint/Refueling Outage. Separate Submittal Will Not Be Made to NRC on SG Tubes Inspected During Subj Outage ML20195F8031999-06-11011 June 1999 Forwards Changes to VEGP Unit 1 Emergency Response Data Sys (ERDS) Data Point Library.Changes Were Completed on 990308 While Unit 1 Was SD for Refueling Outage ML20207E7421999-06-0303 June 1999 Refers to from NRC Which Issued Personnel Assignment Ltr to Inform of Lm Padovan Assignment as Project Manager for Farley Npp.Reissues Ltr with Effective Date Corrected to 990525 ML20207F6201999-06-0202 June 1999 Sixth Partial Response to FOIA Request for Documents.Records in App J Encl & Will Be Available in Pdr.App K Records Withheld in Part (Ref FOIA Exemptions 7) & App L Records Completely Withheld (Ref FOIA Exemption 7) ML20207D9861999-05-28028 May 1999 Informs That,Effective 990325,LM Padovan Was Assigned as Project Manager for Plant,Units 1 & 2 ML20207D2701999-05-19019 May 1999 Forwards Insp Repts 50-424/99-03 & 50-425/99-03 on 990321- 0501.One Violation of NRC Requirements Identified & Being Treated as non-cited Violation Consistent with App C of Enforcement Policy ML20206M5141999-05-11011 May 1999 Informs That NRC Ofc of Nuclear Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Rl Emch Section Chief for Vogtle. Reorganization Chart Encl ML20206U4061999-05-11011 May 1999 Confirms Telcon with J Bailey Re Mgt Meeting Scheduled for 990528 to Discuss Results of Periodic Plant Performance Review for Plan Nuclear Facility Fo Period of Feb 1997 - Jan 1999 05000424/LER-1998-006, Forwards LER 98-006-03 Re Motor Control Ctr Breaker Buckets Not Being Seismically Qualified.Rev Is Submitted to Document Results of Seismic Testing That Demonstrated That No Condition Outside Design Basis of TS Requirements Exi1999-05-10010 May 1999 Forwards LER 98-006-03 Re Motor Control Ctr Breaker Buckets Not Being Seismically Qualified.Rev Is Submitted to Document Results of Seismic Testing That Demonstrated That No Condition Outside Design Basis of TS Requirements Existed ML20206D6411999-04-29029 April 1999 Forwards Vogtle Electric Generating Plant Radiological Environ Operating Rept for 1998 & Vogtle Electric Generating Plant Units 1 & 2 1998 Annual Rept Annual Radioactive Effluent Release Rept ML20206D5881999-04-29029 April 1999 Forwards Rept Which Summarizes Effects of Changes & Errors in ECCS Evaluation Models on PCT for 1998,per Requirements of 10CFR50.46(a)(3)(ii).Rept Results Will Be Incorporated Into Next FSAR Update ML20206D6951999-04-28028 April 1999 Provides Update of Plans for VEGP MOV Periodic Verification Program Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20206C2241999-04-21021 April 1999 Forwards Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2.Page E2-2 Was Iandvertently Omitted from Previously Submitted Rept on 990413 ML20206A6371999-04-21021 April 1999 Forwards SE Authorizing Licensee Re Rev 9 to First 10-yr ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML20205Q3351999-04-15015 April 1999 Forwards Insp Repts 50-424/99-02 & 50-425/99-02 on 990214-0320.Three Violations Identified & Being Treated as Non-Cited Violations ML20205T2351999-04-0909 April 1999 Informs That on 990317,B Brown & Ho Christensen Confirmed Initial Operator Licensing Exam Scheduled for Y2K.Initial Exam Date Scheduled for Wk of 991213 for Approx 10 Candidates ML20205K7501999-04-0505 April 1999 Informs That Effective 990329,NRC Project Mgt Responsibility for Plant Has Been Transferred from Dh Jaffe to R Assa ML20209A3741999-04-0505 April 1999 Submits Several Requests for Relief for Plant from Code Requirements Pursuant to 10CFR50.55a(a)(3) & (g)(5)(iii).NRC Is Respectfully Requested to Approve Requests Prior to Jan 1,2000 ML20205H3481999-03-31031 March 1999 Forwards Georgia Power Co,Oglethorpe Power Corp,Municipal Electric Authority of Ga & City of Dalton,Ga Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81 ML20205F9091999-03-29029 March 1999 Submits Rept of Number of SG Tubes Plugged During Plant Eighth Maintenance/Refueling Outage (1R8).Inservice Insps Were Completed on SGs 1 & 4 on 990315.No Tubes Were Plugged ML20205G0761999-03-26026 March 1999 Provides Results of Individual Monitoring for 1998.Encl Media Contains All Info Required by Form NRC 5.Without Encl 1999-09-20
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217P3791999-10-21021 October 1999 Forwards NRC Form 396 & NRC Form 398 for Renewal of Licenses SOP-20607-1 & SOP-20610-1.Without Encls ML20217N2521999-10-20020 October 1999 Provides Supplemental Info Re 990405 Containment Insp Program Requests for Relief RR-L-1 & RR-L-2,in Response to 991013 Telcon with NRC ML20217K7541999-10-15015 October 1999 Forwards Rev 1 to Unit 1,Cycle 9 & Unit 2 Cycle 7 Colrs,Iaw Requirements of TS 5.6.5.Figure 5, Axial Flux Difference Limits as Function of Percent of Rated Thermal Power for RAOC, Was Revised for Both Units ML20217G6751999-10-13013 October 1999 Requests Withholding of Proprietary Info Contained in Application for Amend to OLs to Implement Relaxations Allowed by WCAP-14333-P-A,rev 1 ML20216J9161999-10-0101 October 1999 Forwards Response to NRC 990723 RAI Re GL 95-07, Pressure Locking & Thermal Binding of SR Power-Operated Gate Valves ML20216J9041999-10-0101 October 1999 Forwards Response to RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20212E7481999-09-20020 September 1999 Requests Approval Per 10CFR50.55a to Use Alternative Method for Determining Qualified Life of Certain BOP Diaphragm Valves than That Specified in Code Case N-31.Proposed Alternative,Encl ML20212E8751999-09-20020 September 1999 Forwards Response to NRC GL 99-02, Lab Testing of Nuclear Grade Activated Charcoal. Description of Methods Used to Comply with Std Along with Most Recent Test Results Encl ML20212C2191999-09-16016 September 1999 Forwards NRC Form 536, Operator Licensing Exam Data, Which Is Current Need for NRC Operator Licensing Exams for Years 2000 Through 2003 of Plant Vogtle,Per Administrative Ltr 99-03 ML20211J5291999-08-30030 August 1999 Forwards Snoc Copyright Notice Dtd 990825,re Production of Engineering Drawings Ref in VEGP UFSAR ML20211J5251999-08-30030 August 1999 Forwards Response to NRC 990727 RAI Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20211J7381999-08-27027 August 1999 Informs That Licensee Vessel Data Is Different than NRC Database Based on Listed Info,Per 990722 Request to Review Rvid ML20211E9251999-08-23023 August 1999 Forwards fitness-for-duty Performance Data for Jan-June 1999,as Required by 10CFR26.71(d).Data Reflected in Rept Covers Employees at Vogtle Electric Generating Plant ML20210L2181999-08-0202 August 1999 Forwards NRC Form 396 & Form 398 for Renewal of Listed Licenses,Iaw 10CFR55.57.Without Encl ML20210C8011999-07-21021 July 1999 Provides Response to NRC AL 99-02,which Requests That Addressees Submit Info Pertaining to Estimates of Number of Licensing Actions That Will Be Submitted for NRC Review for Upcoming Fy 2000 & 2001 ML20209H3881999-07-14014 July 1999 Forwards Revs 1 & 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Unit 1 & 2 ML20209C4041999-07-0101 July 1999 Forwards Rev 29 to VEGP Units 1 & 2 Emergency Plan.Rev 29 Incorporates Design Change Associated with Consolidation of Er Facilities Computer & Protues Computer.Justifications for Changes & Insertion Instructions Are Encl ML20196F9171999-06-21021 June 1999 Forwards Owner Rept for ISI for Vogtle Electric Generating Plant,Unit 1 Eighth Maint/Refueling Outage. Separate Submittal Will Not Be Made to NRC on SG Tubes Inspected During Subj Outage ML20212J2521999-06-21021 June 1999 Responds to NRC RAI Re Yr 2000 Readiness at Nuclear Power Plants.Gl 98-01 Requested Response on Status of Facility Y2K Readiness by 990701 ML20195F8031999-06-11011 June 1999 Forwards Changes to VEGP Unit 1 Emergency Response Data Sys (ERDS) Data Point Library.Changes Were Completed on 990308 While Unit 1 Was SD for Refueling Outage 05000424/LER-1998-006, Forwards LER 98-006-03 Re Motor Control Ctr Breaker Buckets Not Being Seismically Qualified.Rev Is Submitted to Document Results of Seismic Testing That Demonstrated That No Condition Outside Design Basis of TS Requirements Exi1999-05-10010 May 1999 Forwards LER 98-006-03 Re Motor Control Ctr Breaker Buckets Not Being Seismically Qualified.Rev Is Submitted to Document Results of Seismic Testing That Demonstrated That No Condition Outside Design Basis of TS Requirements Existed ML20206D5881999-04-29029 April 1999 Forwards Rept Which Summarizes Effects of Changes & Errors in ECCS Evaluation Models on PCT for 1998,per Requirements of 10CFR50.46(a)(3)(ii).Rept Results Will Be Incorporated Into Next FSAR Update ML20206D6411999-04-29029 April 1999 Forwards Vogtle Electric Generating Plant Radiological Environ Operating Rept for 1998 & Vogtle Electric Generating Plant Units 1 & 2 1998 Annual Rept Annual Radioactive Effluent Release Rept ML20206D6951999-04-28028 April 1999 Provides Update of Plans for VEGP MOV Periodic Verification Program Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20206C2241999-04-21021 April 1999 Forwards Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2.Page E2-2 Was Iandvertently Omitted from Previously Submitted Rept on 990413 ML20209A3741999-04-0505 April 1999 Submits Several Requests for Relief for Plant from Code Requirements Pursuant to 10CFR50.55a(a)(3) & (g)(5)(iii).NRC Is Respectfully Requested to Approve Requests Prior to Jan 1,2000 ML20205H3481999-03-31031 March 1999 Forwards Georgia Power Co,Oglethorpe Power Corp,Municipal Electric Authority of Ga & City of Dalton,Ga Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81 ML20205F9091999-03-29029 March 1999 Submits Rept of Number of SG Tubes Plugged During Plant Eighth Maintenance/Refueling Outage (1R8).Inservice Insps Were Completed on SGs 1 & 4 on 990315.No Tubes Were Plugged ML20205G0761999-03-26026 March 1999 Provides Results of Individual Monitoring for 1998.Encl Media Contains All Info Required by Form NRC 5.Without Encl ML20205H4051999-03-25025 March 1999 Forwards Info on Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81,as Requested IAW 10CFR50.75(f)(1) ML20205H3891999-03-25025 March 1999 Forwards Info on Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81,as Requested IAW 10CFR50.75(f)(1).Page 2 in Third Amend Power Sales Contract of Incoming Submittal Not Included ML20205A9441999-03-25025 March 1999 Forwards VEGP Unit 1 Cycle 9 Colr,Per TS 5.6.5.d ML20205H3811999-03-24024 March 1999 Forwards Info on Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81,as Requested IAW 10CFR50.75(f)(1) ML20205H3621999-03-22022 March 1999 Forwards Info on Status of Decommissioning Funding for Each Reactor or Part of Reactor Owned for OLs NPF-68 & NPF-81, as Requested IAW 10CFR50.75(f)(1) ML20204G4361999-03-18018 March 1999 Forwards Summary Rept of Present Level & Source of on-site Property Damage Insurance Coverage for Vegp,Iaw Requirements of 10CFR50.54(w)(3) ML20204C0591999-03-17017 March 1999 Forwards Rev 0 to WCAP-15160, Evaluation of Pressurized Thermal Shock for Vegp,Unit 2 & Rev 0 to WCAP-15159, Analysis of Capsule X from Vegp,Unit 2 Reactor Vessel Radiation Surveillance Program ML20207K9551999-03-11011 March 1999 Forwards Response to Rai,Pertaining to Positive Alcohol Test of Licensed Operator.Encl Info Provided for NRC Use in Evaluation of Fitness for Duty Occurrence.Encl Withheld,Per 10CFR2.790(a)(6) ML20207L9721999-03-10010 March 1999 Forwards Rev 15 to EPIP 91104-C of Manual Set 6 of Vogtle Epips.Without Encl ML20207B0191999-02-25025 February 1999 Forwards Fitness for Duty Performance Data for six-month Reporting Period 980701-1231,IAW 10CFR26.71(d) 05000424/LER-1998-009, Forwards LER 98-009-00 Re Event in Which Improper Testing Method Resulted in Inadequate Surveillances on 9812291999-01-27027 January 1999 Forwards LER 98-009-00 Re Event in Which Improper Testing Method Resulted in Inadequate Surveillances on 981229 ML20199F7701999-01-13013 January 1999 Submits Revised Response to RAI Re Licensee 980713 Proposed Amend to Ts,Eliminating Periodic Response Time Testing Requirements on Selected Sensors & Protection Channels. Corrected Copy of Table,Encl ML20199F7981999-01-13013 January 1999 Forwards Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage. Change Bar in Margin of Affected Pages Denotes Changes to Rept ML20199G1381999-01-13013 January 1999 Forwards Copy of Permit Renewal Application Package for NPDES Permit Number GA0026786,per Section 3.2 of VP Environ Protection Plan 05000424/LER-1998-007, Forwards LER 98-007-00,re Inadequate Surveillances Due to Improperly Performed Response Time Testing,On 981215,IAW 10CFR50.731999-01-13013 January 1999 Forwards LER 98-007-00,re Inadequate Surveillances Due to Improperly Performed Response Time Testing,On 981215,IAW 10CFR50.73 ML20198F6131998-12-18018 December 1998 Forwards Revised Certification of Medical Exam Form for License SOP-21147.Licensee Being Treated for Hypertension. Util Requests That Individual License Be Amended to Reflect Change in Status ML20198L6631998-12-18018 December 1998 Forwards Amend 37 to Physical Security & Contingency Plan. Encl 1 Provides Description & Justification for Changes & Encl 2 Contains Actual Amend 37 Pages.Amend Withheld,Per 10CFR73.21 ML20198D9291998-12-16016 December 1998 Forwards Requested Info Re Request to Revise TSs Elimination of Periodic Pressure Sensor Response Time Tests & Elimination of Periodic Protection Channel Response Time Tests ML20198D9991998-12-16016 December 1998 Forwards Responses to 980916 RAI Re Response to GL 97-01, Degradation of Control Rod Drive Mechanism Nozzle & Other Vessel Closure Head Penetrations ML20198D8171998-12-14014 December 1998 Forwards NRC Form 396 & Form 398 for Renewal of License OP-20993.Without Encls ML20206N3051998-12-0808 December 1998 Submits RAI Re Replacement of Nuclear Instrument Sys Source & Intermediate Range Channels & post-accident Neutron Flux Monitoring Sys 1999-09-20
[Table view] Category:UTILITY TO NRC
MONTHYEARELV-02056, Forwards Operator Exam Schedule for Facility,Per Generic Ltr 90-07 Request,Including Number of Candidates to Be Examined During NRC Site Visits,Requalification Schedules & Number of Candidates to Participate in Generic Fundamentals Exam1990-09-0606 September 1990 Forwards Operator Exam Schedule for Facility,Per Generic Ltr 90-07 Request,Including Number of Candidates to Be Examined During NRC Site Visits,Requalification Schedules & Number of Candidates to Participate in Generic Fundamentals Exam ELV-01599, Discusses Mods to HED-1114 Re Plant Dcrdr,Per . Amber Monitor Light Covers Installed for Spare Pumps to Make Status of Pumps Readily Apparent to Operator1990-09-0404 September 1990 Discusses Mods to HED-1114 Re Plant Dcrdr,Per . Amber Monitor Light Covers Installed for Spare Pumps to Make Status of Pumps Readily Apparent to Operator ELV-02059, Clarifies 900409 Response to 900323 Confirmation of Action Ltr.Util Made 31 Successful Start Attempts for Diesel Generator (DG) 1A & 29 Successful Start Attempts for DG 1B1990-08-30030 August 1990 Clarifies 900409 Response to 900323 Confirmation of Action Ltr.Util Made 31 Successful Start Attempts for Diesel Generator (DG) 1A & 29 Successful Start Attempts for DG 1B ELV-01956, Forwards Listed Documents in Response to Request for Addl Info Re Settlement Monitoring Program,Per 900614 Request1990-08-30030 August 1990 Forwards Listed Documents in Response to Request for Addl Info Re Settlement Monitoring Program,Per 900614 Request ELV-02050, Responds to Violations Noted in Insp Repts 50-424/90-08 & 50-425/90-08.Corrective Actions:Administrative Procedures Controlling Verification & Validation of Emergency Operating Procedures Will Be Evaluated & Revised as Required1990-08-30030 August 1990 Responds to Violations Noted in Insp Repts 50-424/90-08 & 50-425/90-08.Corrective Actions:Administrative Procedures Controlling Verification & Validation of Emergency Operating Procedures Will Be Evaluated & Revised as Required ELV-02028, Forwards Fitness for Duty Performance Data for First Six Month Period,Per 10CFR26.71(d)1990-08-22022 August 1990 Forwards Fitness for Duty Performance Data for First Six Month Period,Per 10CFR26.71(d) ELV-02022, Forwards Revised LER Re Apparent Personnel Error Leading to Unsecured Safeguards Info.Ler Withheld1990-08-22022 August 1990 Forwards Revised LER Re Apparent Personnel Error Leading to Unsecured Safeguards Info.Ler Withheld ELV-02027, Forwards Rev 0 to Core Operating Limits Rept, for Cycle 3, Per Amends 32 & 12 to Licenses NPF-68 & NPF-79,respectively1990-08-20020 August 1990 Forwards Rev 0 to Core Operating Limits Rept, for Cycle 3, Per Amends 32 & 12 to Licenses NPF-68 & NPF-79,respectively ELV-01973, Submits Rept Re Results of Leakage Exams Conducted During Spring 1990 Refueling Outage,Per TMI Item III.D.1.1.None of Identified Leakage Considered Excessive.Work Orders Issued in Effort to Reduce Leakage to Level as Low Practical1990-08-14014 August 1990 Submits Rept Re Results of Leakage Exams Conducted During Spring 1990 Refueling Outage,Per TMI Item III.D.1.1.None of Identified Leakage Considered Excessive.Work Orders Issued in Effort to Reduce Leakage to Level as Low Practical ELV-01918, Responds to NRC 900612 Request for Comments & Suggestions on Draft risk-based Insp Guide.Util Conducting Individual Plant Exam & Will Withhold Comment on risk-based Insp Guide Until Completion1990-08-0303 August 1990 Responds to NRC 900612 Request for Comments & Suggestions on Draft risk-based Insp Guide.Util Conducting Individual Plant Exam & Will Withhold Comment on risk-based Insp Guide Until Completion ELV-01943, Responds to Violation & Proposed Imposition of Civil Penalty in Insp Repts 50-424/90-11 & 50-425/90-11.Corrective Action: Complete Audit of Contents of Safeguards Info Container Performed & Unassigned Safeguards Info Dispositioned1990-07-27027 July 1990 Responds to Violation & Proposed Imposition of Civil Penalty in Insp Repts 50-424/90-11 & 50-425/90-11.Corrective Action: Complete Audit of Contents of Safeguards Info Container Performed & Unassigned Safeguards Info Dispositioned ELV-01949, Forwards Info Re Status of Pen Branch Fault Investigation. Investigations Conducted So Far Still Indicate That Pen Branch Fault Not Capable1990-07-26026 July 1990 Forwards Info Re Status of Pen Branch Fault Investigation. Investigations Conducted So Far Still Indicate That Pen Branch Fault Not Capable ELV-01500, Forwards Nuclear Decommissioning Funding Plan for Plant.Info Provides Assurance That NRC Prescribed Min Funding Will Be Available to Decommission Facilities1990-07-25025 July 1990 Forwards Nuclear Decommissioning Funding Plan for Plant.Info Provides Assurance That NRC Prescribed Min Funding Will Be Available to Decommission Facilities ML20055H6441990-07-23023 July 1990 Submits Summary of Snubber Types & Sample Plans for Functional Testing to Be Performed During Sept 1990 Outage ML20044B0311990-07-13013 July 1990 Forwards Vogtle Electric Generating Plant Unit 1 Reactor Containment Bldg 1990 Integrated Leakage Rate Test Final Rept. ML20044B1541990-07-12012 July 1990 Responds to NRC 900612 Ltr Re Violations Noted in Insp Repts 50-424/90-08 & 50-425/90-08.Corrective Actions:Eop Step Deviation Documents to Be Upgraded,Adding More Justification & Temporary Change Issued to Correct EOP Deficiencies ELV-01867, Responds to Violations Noted in Insp Repts 50-424/90-10 & 50-425/90-10.Corrective Action:Level Indication Error Corrected After Discrepancy Discovered1990-07-12012 July 1990 Responds to Violations Noted in Insp Repts 50-424/90-10 & 50-425/90-10.Corrective Action:Level Indication Error Corrected After Discrepancy Discovered ML20055F1651990-07-0909 July 1990 Forwards Comments Re NUREG-1410 ELV-01858, Advises That Full Compliance W/Violation Will Not Be Achieved Until Nov 1990,when Evaluation of VP-2693 Complete1990-07-0606 July 1990 Advises That Full Compliance W/Violation Will Not Be Achieved Until Nov 1990,when Evaluation of VP-2693 Complete ML20044A8851990-07-0606 July 1990 Forwards Response to NRC Question on Steam Generator Level Instrumentation Setpoints,Per Revised Instrument Line Tap Locations.Tap Location Will Be Changed from Above Transition Cone to Below Transition Cone ELV-01834, Forwards Response & Comments to Regulatory Effectiveness Review Rept.Encl Withheld (Ref 10CFR73.21)1990-06-28028 June 1990 Forwards Response & Comments to Regulatory Effectiveness Review Rept.Encl Withheld (Ref 10CFR73.21) ML20044A2791990-06-25025 June 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Licensee Implementation of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions. Table Indicating Status of Each Generic Safety Issue Encl ML20043J0171990-06-22022 June 1990 Discusses Corrective Actions for Plant Site Area Emergency, Per 900514 Ltr.Jacket Water High Temp Switches Calibr for Diesel Generators,Using Revised Calibr Procedure ML20043H3061990-06-15015 June 1990 Forwards Rev 3 to ISI-P-014, Inservice Insp Program, for Review & Approval,Per Tech Spec 4.0.5 Re Surveillance Requirements.Rev Includes Withdrawal of Relief Requests RR-45,47,48 & 54 ML20043G2071990-06-12012 June 1990 Forwards Amend 18 to Physical Security & Contingency Plan. Amend Withheld (Ref 10CFR73.21) ML20043G1021990-06-0606 June 1990 Requests Temporary Waiver of Compliance from Requirements of Action Statement 27 of Tech Spec 3.3.2 for Period of 6 H When Two Operating Control Room Emergency Filtration Sys Trains Shut Down for Required Testing ML20043E6901990-06-0505 June 1990 Forwards Rev 12 to Emergency Plan & Detailed Description & Justification of Changes.W/O Rev ML20043G7651990-06-0505 June 1990 Forwards Rev 13 to Emergency Plan & Description & Justification of Changes ML20043B5991990-05-25025 May 1990 Forwards Scope & Objectives Re 1990 Annual Emergency Preparedness Exercise to Be Conducted on 900801 ML20043B5981990-05-24024 May 1990 Responds to Violations Noted in Insp Rept 50-424/90-05 on 900217-0330.Corrective Actions:Locked Valve Procedure Revised to Eliminate Utilization of Hold Tag on Valves Required by Tech Specs to Be Secured in Position ML20043B6291990-05-22022 May 1990 Forwards Rev 5 to ISI-P-008, Inservice Testing Program, Per Tech Specs 4.0.5 Re Surveillance Requirements & Generic Ltr 89-04 ML20043B6351990-05-22022 May 1990 Forwards Rev 2 to ISI-P-016, Inservice Testing Program, Per Generic Ltr 89-04, Guidance on Developing Acceptable Inservice Testing Programs. ML20042H0601990-05-14014 May 1990 Forwards Summary of Corrective Actions for 900320 Site Area Emergency Due to Loss of Offsite Power Concurrent W/Loss of Onsite Emergency Diesel Generator Capability.Truck Driver Disciplined for Lack of Attention ML20042G7301990-05-11011 May 1990 Forwards Revised Pages for May 1989,Jan & Mar 1990 Monthly Operating Repts for Vogtle Electric Generating Plant,Units 1 & 2.Revs Necessary Due to Errors Discovered in Ref Repts ML20042E2911990-04-18018 April 1990 Forwards Amend 17 to Security Plan.Amend Withheld (Ref 10CFR2.790) ML20042E7481990-04-0909 April 1990 Requests Approval to Return Facility to Mode 2 & Subsequent Power Operation,Per 900320 Event Re Loss of Offsite Power Concurrent W/Loss of Onsite Emergency Diesel Generator Capability ML20012E9001990-03-28028 March 1990 Provides Supplemental Response to Station Blackout Rule,Per NUMARC 900104 Request.Mods & Associated Procedure Changes Identified in Sections B & C W/Exception of Mods to Seals Will Be Completed 1 Yr from Acceptance of Analysis ML20012E8581990-03-28028 March 1990 Suppls Response to NRC Bulletin 88-010,Suppl 1 Re Traceability Reviews on Molded Case Circuit Breakers Installed in safety-related Applications.All Breakers Procured & Installed in Class 1E Equipment Reviewed ML20012E9761990-03-27027 March 1990 Requests Withdrawal of Inservice Insp Relief Requests RR-45, RR-47,RR-48 & Conditional Withdrawal of RR-54 Based on Reasons Discussed in Encl,Per 900206 Conference Call ML20012D8561990-03-22022 March 1990 Submits Special Rept 1-90-02 Re Number of Steam Generator Tubes Plugged During 1R2.One of Four Tubes Exceeded Plugging Limit & Required Plugging.Remaining Three Tubes Plugged as Precautionary Measure.No Defective Tubes Detected ML20012D6641990-03-22022 March 1990 Provides Followup Written Request for Waiver of Compliance to Make Tech Spec 3.04 Inapplicable to Tech Spec 3.8.1.2 to Permit Entry Into Mode 5 W/Operability of Diesel Generator a & Associated Load Sequencer Unverified ML20012D3681990-03-19019 March 1990 Forwards Proprietary & Nonproprietary Suppl 2 to WCAP-12218 & WCAP-12219, Supplementary Assessment of Leak-Before-Break for Pressurizer Surge Lines of Vogtle Units 1 & 2, Per 900226 Request.Proprietary Rept Withheld (Ref 10CFR2.790) ML20012D3401990-03-19019 March 1990 Submits Response to 891121 Request for Addl Info Re Settlement Monitoring Program.Current Surveying Procedures Used by Plant to Monitor Settlement of Major Structures Outlined in Procedure 84301-C.W/41 Oversize Drawings ML20012D6631990-03-15015 March 1990 Responds to Generic Ltr 89-19 Re Resolution of USI A-47 on Safety Implications of Control Sys in Lwrs.Overfill Protection Sys Sufficiently Separate from Control Portion of Main Feedwater Control Sys & Not Powered from Same Source ML20012C4681990-03-0606 March 1990 Provides Summary Rept of Property Damage Insurance Levels, Per 10CFR50.54(w)(1) ML20012B2891990-03-0606 March 1990 Forwards Plant Pipe Break Isometrics,Vols 1 & 2 & Advises That Encl Figures Have Been Revised to Be Consistent W/Pipe Analysis in Effect at Time That Unit 2 Received Ol,Including Revs Through 890930.W/309 Oversize Figures ML20012B2421990-03-0606 March 1990 Forwards Cycle 3 Radial Peaking Factor Limit Rept & Elevation Dependent Peaking Factor Vs Core Height Graph ML20011F5291990-02-26026 February 1990 Withdraws 881107 Proposed Amend to Tech Spec 3.8.1.1, Revising Action Requirements for Inoperable Diesel Generator to Clarify Acceptability of Air Roll Tests on Remaining Operable Diesel Generator ML20011F5261990-02-26026 February 1990 Forwards 1989 Annual Rept - Part 1. Part 2 Will Be Submitted by 900501 ML20011E8911990-02-12012 February 1990 Advises That Hh Butterworth No Longer Employed by Util 1990-09-06
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' Cevg a Fbwer Cc-mpany
.* . 333 P edmort Avenue Afr.f a Georg a 30303 Wetrore 404 5:GL526 0 ce 4545 naca. cm.; a aox2
$?;((ll',4"h, ee wvem N eeat OccutW s Log: VL-101 0069e X7GJ17-V600 October 3,1988 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 PLANT V0GTLE - UNIT 1 NRC DOCKET 50-424 OPERATING LICENSE NPF-68
- REQUEST FOR DISCRETIONARY ENFORCEMENT
- REGARDING TECHNICAL SPECIFICATION 3.5.4 1
l Gentlemen:
Georgia Powoe Company (GPC) in our letter SL-4682 dated May 19, 1988, propored revisions to Plant Vogtle's Technical Specifications related to shutdown margin requirements. Specifically one change was to increase the range of boron concentration for the refueling water storage tank (RWST) to i 2400 ppm to 2600 ppm.
i j During the transition to the new Technical Specification limit for RWST boron concentration (i.e., Technical Specification 3.5.4) associated with the Positive Moderator Temperature Coefficient employed in Cycle 2, there i
will be a period of time during which the RWST boron concentration will be betweer the present upper limit of 2100 ppm and the amended Technical l Specification lower limi t of 2400 ppm.
1 It is our intent to raise the boron concentration of the RWST to its new limit by circulating water between the s fuel pool (current boron
! concentration of approximately 3200 ppm) pent and the RWST (current boron concentration of approximately 2000 ppm) by a portion of procedure l 13719-1 Rev 6T (Enclosure 1). This will be accomplished by utilizing a l gravity feed from the RWST to the spent fuel pool with a return to the RWST via a spent fuel pool cooling pump bypass loop. The end result would be equal boron concentrations in the RWST and the spent fuel pool of approximately 2500 ppm.
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Georgia Power d Nuclear Regulatory Commission October 3,1988 Page 2 The change in boron concentration in the RWST should occur prior to flooding the refueling cavi ty to ensure that adequate mixing occurs.
Adequate mixing is required to meet the specification of uniformity of boron concentration required by Technical Specification 3. 9.1. To delay increasing the RWST boron concentration until Mode 5, the plant condition at which the RWST boron concentration upper limit of 2100 ppm no longer applies, would result in either an unwarranted delay of up to nine days on the outage schedule or a reduced assurance of adequate mixing. In the worst case, the refueling cavity would have a boron concentration on the order of 2100 ppm while the spent fuel pool would have a boron concentration of approximately 3200 ppm.
Additionally, Westinghouse performed a specific evaluation for the change in the boron concentration from 2100 ppm to the proposed lower limit of 2400 ppm. As a result of this evaluation, Georgia Power Company will, prior to boron concentration exceeding 2100 ppm, change E0P-19010. "Loss of Reactor or Secondary Coolant," such that hot leg recirculation switchover will occur at 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />. Also, RWST level will be maintained at approximately 36,000 gal above the existing Technical Specification limit durir.9 this evolution (approximately 90% of level).
As discussed between representatives of the NRC and GPC in telephone conversations on this date, GpC, therefore, requests the NRC to grant discretionary enforcement of Technical Specification 3.5.4 to allow RWST boron concentration to exceed the current Technical Specification upper limit of 2100 ppm while achieving the proposed lower limit of 2400. The period of time this action would be required would be from October 3,1988, until the plant is in Mode 5 following shtttdown for refueling. Plant shutdown is currently scheduled to begin October 7,1988.
Enclosure 2 to this letter is a safety evaluation, prepared by Westinghouse Electric Corporation, which documents the technical acceptability of this requested action. The Plant Vogtle Plant Review Board has reviewed this safety evaluation and concurs in its findings.
Should you have questions regarding this request, please contact this office. Your prompt response to this matter is requested.
Sincerely, ' ?
b, [%
h 4 W. G. Hairston III
/v WEB:llh c: (see next page)
Georgia Powerkn Nuclear Regulatory Commission October 3,1988 Page 3 c: Georgia Power Company Mr. P. D. Rice Mr. G. Bockhold, Jr.
GO-NORMS U. S. Nuclear Regulatory Commission Dr. J. N. Grace, Regional Administrator Mr. J. B. Hopkins, Licensing Project Manager, NRR (2 copies)
Mr. J. F. Rogge, Senior Resident Inspector - Operations, Vogtle
Enclosure:
- 1. Excerpt from Procedure 13719-1 Rev 6T
- 2. Safety Evaluation i
5
)
Enclosure 1 - Excerpt from Procedure 13719-1 Rev. 6T 4.4.13 Recirculation And Interchange Of Water In The SFP And RWST By Gavity Flow From RWST 1 CAUTION During the water interchange operation between the RWST and SFP, the RWST levels shall be maintained within Technical Specification :
3.1.2.6 limits.
NOTE
- a. This Sub-section transfers water from the RWST to the SFP by continuous gravity flow through 1-12094-U4-066, and from the SFP to the RWST via the SFP filter through 1-1213-06-049.
- b. Spent Fuel Cooling Loop B is to be in servica and Loop A shutdown to reduce backpressure on the gravity flow from the RWST.
- c. Maximum flow for interchange of water between the SFP and RWST for mixing is desired. The limiting flow is expected ,
to be the gravity letdown path from the RWST to the SFP, between 75 and 100 gpn.
- d. The SFP level should be maintained between the HI and L0 level alarms,
- e. Chemistry should be notified to verify the SFP and RWST water quality satisfactory for transfer, and to monitor during and after transfer for boron concentration.
4.4.13.1 PLACE SFP Cooling Pump B in service per Sub-subsection 4a141.
NOTE If SFP water quality is satisfactory as determined by Chemistry to go to the RWST, the filtration only path should be used. If required by water quality, use the Spent Fuel Pit Demineralizer p at h.
4.4. 13.2 ENSURE Spent Fuel Pit Filter is aligned for service per 11213-1 "Backflushable Filter System Alignment.
Page Two of Enclosure 1 4.4. 13.3 PLACE the SFP Purification Loop in service from Cooling loop B for filtration per Sub-subsection 4.1.2 and THROTTLE Spent Fuel Pit Demineralizer Bypass 1-1213-U6-032 te achieve 75 to 100 gpm through the SFP Demineralizer as todicated on 1-FI-0631.
4.4. 13.4 KAKEUP to the SFP from the RWST rp
- Sub-subsection 4.2.1 4.4413.5 PLACE Sludge Mixing Pump 1-1204-P4-001 in service per 13105-1 "Safety Injection System."
4.4.13.6 OPEN Safety Injection RWST Purification Pump Discharge to RWST Isolation 1-1204-U4-003, 4.4.13.7 OPEN Purification Loop Datlet to RWST l-1213-06-049, 4.4. 13. 8 CLOSE Purification Loop Return to SFP 1-1213-U6-053, 4.4413.9 OBSERVE the Spent Fuel Pit Filter differential pressure on 1-P01 f-41351. If the differential pressure reaches 20 psid, BACKFLUSH the filter per 13213-1 "Backflushable Filter System."
4.4. 13. 10 OBSERVE the level in the RWST and throttle Spent Fuel Pit Demineralizer Bypass 1-1213-06-032 to equalize the amount of water to and from the RWST and SFP.
4.4.13411 When desired mixing results are obtained between the RWST and SFP, RESTORE system to normal as follows:
- a. OPEN 1-1213-U6-053,
- b. CLOSE 1-1213-U6-049,
- c. CLOSE l-1204-L4-003,
- d. CLOSE 1-1204-U4-066,
- e. RETURN SFP Purification to desired configuration per Sub-subsection 4.1.2.
- f. If desired, SiUT 00WN Sludge Mixing Pump 1-1204-P4-001.
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ECP 30 '?3 13:21 WEC-EAST 405A
- ENCLOSURE 2 INTRODUCTION j As a result of operational problems encountered at the Alvin W. Vogtle Unit 1 Nuclear Power Plant Westinghouse has lean asked to evaluate the impact of continuing recirculation between the Refueling Water Storage Tank (RWST) and the Spent Fini Pool (SFP). Since the SFP water was at a concentration of 3200 ppm boron, the RWST boron concentration will be raised to a value greater than the current Technical Specification upper limit of 2100 ppa.
Should the mixing process between the RWST and the SFP continue indefinitely, the maximum RWST boren concentration that would occur has been calculated to be approximately 2550 ppm. The impact of the increased RWST boron concentration and the continued operation with a recirculation flow of 100 gpm between the RWST and the SFP needs to be I determined to support an emergency Technical Specification change to permit Plant Vogtle Unit 1 to operate to the end of Cycle 1 under these conditions, riON LOCA EVALUATION The inc* ase in the RWST boron concentration due to a leakage between the RWST and the SFP has been evaluated for the impact on the Non LCCA transients. The general conclusion is that an increase in RWST boren concentration over the current initial condition of 2052 ppm will only be beneficial to the Non LOCA transients. The boron concentration could increase to the assumed 2600 r,pm concentration with no adverse impact on the conclusions of the Non LOCA FSAR transients. This is explained in more detail below.
SEP 30 '89 13:22 LEC-CAST 05A P.3 for the Section 15.1 transients, "Increase in Heat Removal by the Secondary System", th6re is no adverse effect of an increased RWST concentration on the results or conclusions of the FSAR. The only transients which rely on Safety Injection from the RWST in this Section are the Steam System Piping Failure and the Inadvardent Opening of a Steam Generator Relief or Safety Valve transients. For these two transients an increased boron concentration in the RWST will result in more negative reactivity being injected sooner into the primary system, which would result in a better DNBR (higher) being calculated.
For the Section 15.2 transients, ' Decrease in Heat Removal by the Secondary System", there is no adverse effect of an increased RWST concentration on the results or conclusions of the FSAR. These transients do not rely on the Safety Injection system and the borated water from the RWST for reactivity control. As a result there is no significant impact i
on the results and no impact on the conclusions in the FSAR for these transients.
i t
For the Section 15.3 transients. "Decrease in Reactor Coolant System
- flowrate', there is no adverse effect of an increased RWST concentration on the results and conclusions of the FSAR. These transients do not rely l on the Safety Injection system and will therefore be unaffected by a change to the RWST boron concentration.
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SEP 20 '99 13:22 LEC-CA5T 405A P.4 For the Section 15.4 transients, "Reactivity and Power Distribution Anomalies", there is no adverse effect of an increased RWST concentration on the results and conclusions of the FSAR. Except for the Boron Dilution accident these transients do not rely on the Safety Injection system and the borated water from the RWST for reactivity control. As a consequence, the results and conclusions reached fo the accidents other than the Baron Dilution event will be unaffected. For the Boron Dilution Events, the increased RWST boron concentration will provide more negative reactivity with which to shutdown the system, and will be a benefit. There are constraints on the Shutdown Margin required as a function of Primary system boron concentration which must continue to be met. The curros for c
this constraint are found in the Technical Specifications and are explained further as follows.
Boron dilution is most limiting at beginning of life when critical boren concentrations are very high and increased shutdown margin is required in the shutdown modes to provide adequate operator action time. At the end of life the transient is much less limiting due to very low critical boron concentrations. In the event that the RCS boron concentration increases above the current RWST limit of 2100 ppm, more shutdown margin via boron will be provided and this will contribute to the amount of time available for operator action. To o;. orate with RCS boren concentrations greater than maximum values for the abscissa (2100 ppm) reported in the current Technical Specifications (Figure 3.1 1 and 3.1-2) for the shutdown margin curves, maintain the shutdown margin at the value related to 2100 ppm.
This will provide adequate tire for operator action to isolate any -
dilution source before the return to criticality.
5EP 20 '98 13:23 LEC-CAST 405A P.5 For the Section 15.5 transients, "Increase in Reactor Coolant Inventory',
there is no significant adverse effect of an increase RWST concentration on the results and conclusions of the FSAR. For the Spurious Safety Injection transient, due to the higher RW$T boron concentration, a greater i
power mismatch will occur early in the transtant. However, this transient is easily controlled by the existing protection systems and it is judged that the DNBR would still be well above the limit value as it is in the case reported for :ninimum feedback in the FSAR. DNBR is the major criterion of concern for this transient and the ONBR continually increases l for the minimum feedback transient presented.
i For the Section 15.6 transients, "Decrease in Reactor Coolant Inventory",
there is no adverse effect of an increased RWST concentration on the results and conclusions of the FSAR for the Non LOCA transients. These transients do not rely on the Safety Injection system for reactivity l control and will therefore be unaffected by a change to the RW$T boron l concentration.
i 1 For the Macs and Energy release calculations for the Steam Line break transients, there is no adverse effect of an increased RWST concentration on the results and conclusions of the FSAR. An increased boron 4
i concentration in the RWST will be of benefit to these transients since the i
increased boron will serve to offset the increase in reactivity due to the l l cooldown. This would result in less energy being available on the primary
, side to be transferred out the break.
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SEP 20 '88 13124 LEC-CAST 4054 P,6 Insunenary, the Non LOCA transients have been reviewed to assess the impact of cn increase in the RWST boron concentration above the current limit valua of 2100 ppm. It is concluded that an increase in RWST concentration to as high as 2600 ppm will have no significant adverse impact on the results of the FSAR, and the conclusions of the FSAR remain valid, c
1 s
SEP 30 '88 13:24 W C-EAST 40!A P.7 LOCA EVALUATION The evaluation that has been performed for the implementation of the PMTC and for an increased RWST boron concentration of 2600 ppa (Reference
- 1) is applicable at this time for the following LOCA related accidents:
1
- 1. Large Break LOCA i
- 2. Small Break LOCA <
- 3. LOCA Hydraulic Forcing Functions i
- 4. Post LOCA l.ong Term Cooling
- 5. Rod Ejection Mass Releases
- 6. Hotleg Switchover to Prevent Boron Precipitation The conclusions outlined in Reference 1 are applicable and valid and envelope the increased boron concentration conditions experienced at this time. It should be noted however, that as a result of the increased RWST boron concentration a change to the hotleg switchover time to 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> ,
should be made to the applicable operating procedures.
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[QK[&!NMENT INTEGAITY LOCA MASS AND ENERGY ANALYSIS !
The containment integrity LOCA mass and energy analyses do not take credit for the soluble boron present in the RWST via safety injection supplied to the RCS. The minimum boron concentration allowed by the i technical specifications is modeled in the mass and energy release analysis for postulated secondary system pipe ruptures inside containment.
An increase in the boron concentration will insert more negative reactivity into the core and result in less limiting mass and energy releases and therfore will lessen the consequences of adverse containment 1
conditions.
'AM GENERATOR TUBE RUPTURE ACCIDENT An evalutaion on the SGTR accident has been performed and it is determined that the ',ow pressurizer pressure SI signal is actuated due to the decrease in the RCS inventory shortly after reactor trip and borated water from the RWST in delivered to the RCS. For the SGTR anlysis, the i
primary to secondary break flow was assumed to be terminated at 30 minutes "
! after the initiation of the svent. However, the operator actions required to terminate the break flow, including the initial RCs cooldown were not modeled in the analysis. Although the RCS cooldown is not modeled, suff tecient shutdown margin is assumed to be available initially due to l
the insertion of the control rods following a reactor trip, and adequate shutdown margin is assumei to be maintained for the long term by borated safety injection. Since the minimum boron concentration is modeled in the SGTR sccident to simulate reactivity insertion the higher RWST boron concentration will have no adverse effect on the FSAR SGTR accident.
.- SEP 30 '89 13:25 LEC-GST 405A P,9 RWST Voll*E REQUIRED L
As stated in Reference 1, raising the RWST boron concentration increases the conservatism of the volumes presently specified as being required in
, the RWST.
L With the line from the RWST to the spent fuel pool open and resulting in a continuing d:'aindown of about 100 gpm, operability of the RWST is a v.
concern.
If a large break loss of coolant accident were to occur as this process is continuing, the volume of RWST water that woule be delivered to the containment sump would be reduced by approximately 3000 gallons. This volume of water is considered insignificant when compared to the total volume of RWST water available. In terms of the volume of water lost and
'herefore unavailable for injection, the small break LOCA is considered to be more limiting because of the longer injection time during which the RWST is drawn down.
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SEP 30 'S913:26 LEc-CAST 45A P.10 If a small break LOCA were to occur as this process is continuing, the emergency response guidelines E1/E2 indicate that the injection phase would only last 185 minutes before all the high head safety injection pumps are off except for one charging pump operating in the normal charging moda. The RWST 1evel would not reach the low low level switchover setpoint and the small LOCA would be terminated before recirculation is required. The presence of an additional 100 gpm outflow from the RWST during this injection period does not change these conclusions.
i If the small break LOCA were to endure for a longer period of time, then l recirculation from the containment sump would be required after approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Due to the 100 gpm outflow from the RWST over this period of time, there would be approximately 36,000 gallons of injection j water lost to the spent fuel pit which would not be available on the containment floor for recirculation. However, the containment sump would still be flooded above the required elevation of 170.6 feet so that there would be no impact on ECCS recirculation. (Note Georgia Power should verify that this is a true statement; alternatively, a comitment can be i made to maintain the RWST level at 36,000 gallons abcVe present Technical Specification minimum limit if this is possible).
REACTOR MAXEUP CONTROL SYSTEM Although the AWST will be operating with an increased baron concentration, c there will be no impact on the reactor makeup control system since there is no need to supply borated water at a concentration to match the increased RWST concentration.
o- SEP 20 '?9 13:26 WCC-EAST .:0!A P.it MINIMUM POST LOCA SUMP SOLUTION pH As discussed in Reference 1, operation of the Vogtle Station with 2600 ppm boron in the RWST will result in a reduction in the minimum post accident sump solution pH from 8.5 to 8.15. Since the equilibrium RWST boron concentration (after mixing with the spent fuel pool) is less than 2600 ppm boren, the evaluations provided in Reference 1 for areas impacted by reduction in the sump solution pH remain bounding for this case. These areas include:
Hydrogen Generation Due to Corrosion of Aluminum and Zine Equipment Qualification Chloride Induced Stress corrosion of Stainless Steel LOCA Thyroid Doses Reference 1 concluded that with the proposed operation with an RWST boron -
concentration as high as 2600 ppm boron there was no significant impact on safety associated with the above concerns.
Mnimum POST LOCA SUMP SOLUTION eH The maximum sump solution pH remains less than the present licensing basis of 10.5 since the increase in RWST baron concentration would decrease the sump pH.
INJECTION SPRAY oH As discussed in Reference 1. the pH of the containment spray flow during the injection phase is conservatively estimated to be less than 10.5 and greater than 8.5 and is thus within the present licensing basis.
.- . SEP ?0 '59 13:27 LEC-EAST 40!A P.12 CONCLUSIONS lit summary, a review of the LOCA, Non LOCA, and fluid system related transients was performed to evaluate the effects of the increased RWST boron concentration. It has been determined that the conclusions of the FSAR or conclusions discussed in Reference 1 remain valid and that the presence of an increased RWST boron concentration up to 2600 ppm do not involve an unreviewed safety quest 19.;,
REFERENCES
- 1. Positive Moderator Temperature Coefficient and RWST/ Accumulator Boron Concentration Increase Licensing Report for Vogtle Electric Generating Plant Units 1 and 2 April 1988.