ML20154R017

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Insp Repts 50-445/88-54 & 50-446/88-50 on 880803-0908. Violations Noted.Major Areas Inspected:Applicant Action on Previous Insp Findings,Followup on Violations & Deviations, Preoperational Retesting Program & Plant Tours
ML20154R017
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 09/27/1988
From: Bitter S, Burris S, Joel Wiebe
NRC OFFICE OF SPECIAL PROJECTS
To:
Shared Package
ML20154Q985 List:
References
50-445-88-54, 50-446-88-50, NUDOCS 8810040128
Download: ML20154R017 (13)


See also: IR 05000445/1988054

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U. S. NUCLEAR REGULATORY COMMISSION

OFFICE OF SPECIAL PROJECTS

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NRC Inspection Report:

50-445/88-54'

Permits: CPPR-126

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50-446/88-50

CPPR-127

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Dockets: 50-445

Category: A2

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50-446

. Construction Permit

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Expiration Dates

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Unit 1: Extension request

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submitted.

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Unit 2: Extension request

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submitted.

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Applicant:

TU Electric

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Skyway Tower

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400 North Olive Street

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Lock Box 81

Dallas, Texas

75201

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Facility Nam't

Comanche Peak Steam Electric Station (CPSES),

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Units 1 and 2

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Inspection Att

Comanche Peak Site, Gle.n Rose, Texas

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Inspection conducted:

August 3 through September 8, 1988

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9/2

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Inspector

S. D. Bitter, Resident Inspector,

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Operations

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Inspector

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S. P. Burris, Senior Resident Inspector,

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Operations

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Reviewed b :

J. S. Wiebe, Lead Project Inr.,ptsctor

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8910040108 880927

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PDR

ADOCK 05000445

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PDC

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Inspection Summary

Inspection Conducted:

August 3 through September 8,

1988 (Report

50-445/88-54; 50-446/88-50)

Arcas Inspected:

Unannounced resident safety inspection of

applicant's action on previous inspection findings, follow-up on

violations and deviations, preoperational rotesting program, plant

tours, and safety evaluation report follow-up.

Results: During the inspection, one violation was identified in the

area of radiological controls (paragraph 5.b).

The violt. tion,

which includes two instances where an individual did not obtain the

appropriato administrative controls prior to entering a radiation

control area, indicaten a potential weakness in the applicant'r

program.

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DETAILS

1.

Persons Contacted

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  • R. W. Acklcy, Jr., Project Manager, Stone & Webster

Engincoring Corporation (SWEC)

  • M.

Axelrad, Attorney, Newman and Holtzinger,

P. C.

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  • R.

P. Baker, Licensing Compliance Manager, TU Electric

  • J.

L. Barker, Manager, Engineering Assurance, TU Electric

  • H.

D. Bruner, Senior Vice President, TU Electric

  • W.

J. Cahill, Consultant, TU Electric

  • J. T. Conly, APE-Licensing, SWEC
  • W.

G. Counsil, Executive Vice President, TU Electric

  • J.

C. Crnich, Project General Manager, Ebasco

  • G.

G. Davis, Nuclear Operations Inspection Report Item

Coordinator, TU Electric

  • S.

H. Freid, Chief Mechanical / Nuclear Engineer, Bechtel

  • P.

E. Halstead, Manager, Que.lity Control (QC), TU Electric

  • T.

L. Hoatherly, Licensing Complianco Engineer,

TU Electric

  • C.

B. Hog, Engineering hanager, Bechtel

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  • R.

T. Jenkins, Manager, Mechanical Engineering, TU Electric

  • J.

J. Kelley, Manager, I'lant Operations, TU Electric

  • J.

E. Krechting, Director of Technical Interface, TU Electric

  • 0. W. Lowe, Director of Engineering, TU Electric
  • F. W. Madden, Mechanical Engineering Manager, TU Electric

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  • D.

M. McAfco, Manager, QA, TU Electric

  • J.

C. Miller, CPRT, Tenera

  • J. W. Muffett, Manager of Civil Engineering, TU Electric

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  • L.

D. Nace, Vice President, Engineering & Construction,

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TU Electric

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  • E.

Ottncy, Representative, CASE

  • S.

S. Palmer, Project Manager, TU Electric

  • J.

D. Redding, Executive Assistant, TU Electric

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  • D. M. Reynorson, Director of Construction, TU Electric
  • M.

J. Riggs, Plant Evaluation Manager, Operations, TU Electric

  • E.

J. Schmidt, Radiation Protection Manager, TU Electric

  • A.

B. Scott, Vice President, Nuclear Operations, TU Electric

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  • C,

E. Scott, Manager, Startup, TU Electric

  • S.

L. Stamm, Project Engineering Manager, SWEC

  • P.

D. Stevens, Manager, Electrical Engineering, TU Electric

  • J.

F. Streeter, Director, QA, TU Electric

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  • C.

L. Terry, Unit 1 Project Manager, TU Electric

  • T.

G.

Tyler, Director of Projects, TU Electric

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  • R.

D. Walker, Manager of Nuclear Licensing, TU Electric

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  • K.

C. Warapius, Project Director, Impell

  • J.

R. Waters, Licensing Compliance Engineer, TU Electric

The NRC inspector also interviewed other applicant employees

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during this inspection period.

  • Donotes personnel present at the September 8,

1988, exit

interview.

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2.

Follow-up Previous Inspection Findings (92701)

a.

(Closed) Open Item (445/8722-0-09):

Completion of

analysis of circuits related to safe shutdown.

The NRC

inspector that opened this item reviewed the associated

circuit analysis and the CPSES calculation (No. 152,

Revision 4) that resulted in the need for modifications.

The inspector has determined that the applicant has

issued the design change authorizations (DCAs) necessary

to impicment the modifications.

Revision 4 of calculation No. 152 appears to have

adequately addressed this open item.

On the basis of the

NRC review and the modifications initiated by the

applicant, Item 445/8722-0-09 is closed,

b.

(closed) Open Item (445/8822-0-01):

Nonconforming lock

washer.

This item originated during observation of

electrical maintenance activitics on the Unit 1, Train B

residual heat removal (RHR) pump motor.

The pump motor

lower bearing had just boon modified and while attempting

to install a nut and locking tab washer on the rotor of

the motor, electrical maintenance discovered that the

lock washer provided would not fit without being

machined.

Because no documentation concerning the

machining had boon provided to electrical maintenance,

the reinstallations of the RHR pump motor was deferred

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until the applicant could determine the circumstances

surrounding this nonconformance.

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subsequently, the applicant determined that the locking

tab washer was procured properly using the correct stock

numbers furthermore, the correct part was roccived and

issued.

Apparently, the vendor failed to provide

sufficient documentation to indicate that the washer

needed to be modified slightly to fit the rotor shaft.

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In order to document this nonconformance, the applicant

initiated nonconformance report (NCR) 88-05961.

The

disposition of this NCR was to machine the washer (por

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the instructions of Westinghouse Field Deficiency

Report TBXM-10339) and to incorporate the machining

instructions in Maintenance Prnceduro MSE-Cl-4312, "RHR

Pump Motor Rowork."

NRC inspectors have verified the completion of these

actions; the pump motor has been reinstalled

satiafactorily.

Overall review of this item resulted in

no discrepancies; therefore, this item is closed.

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c.

(Closed) Open Item (445/8852-o-03):

Applicant's actions

concerning postulated oil spill as described in

NUREG-0797, "Safety Evaluation Report (SER) for CPSES

Unit 1 and Unit

2."

This item was open pending roccipt

of additional informaticn from the applicant.

In the

SER, Section 2.2.2, the staff states that the applicant

has indicated that station personnel will patrol the area

west of the safe-shutdown impoundment once a day to check

for oil pipeline breaks.

The inspectors reviewed

Security Post Order for Post 213 dated February 29, 1988.

The order requires, in part, a random mobile patrol of

the oil scopage ponds to check for oil spills or seeps.

The times of these patrols are designated by the security

shift sergeant at least once a shift.

The inspectors,

therefore, determined that there is reasonable assurance

that patrols will be conducted at least once por day as

specified by the SER.

The SER also states that the applicant has analyzed

several pipeline breaks and will install three retaining

ponds betwoon the pipeline and safe shutdown impoundment.

The inspector reviewed the applicant's analyses of

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pipeline breaks, reviewed the design drawings of the

three retaining ponds, and inspected the retaining ponds.

The inspectors have determined that there is reasonable

assurance that the retaining ponds will prevent an oil

line break from spilling oil into the safe shutdown

impoundment (SSI).

The inspectors had no further

questions in this area.

This item is considered closed.

d.

(closed) open Item (445/8852-0-04):

Higher than design

ground water level.

This item was open pending receipt

of additional information concerning the ground water

field monitoritig program.

The inspectors reviewed

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specification CPES-S-1035, Revision 1, "Borcholes and

Installation of Piezometers," dated January 13, 1988;

"Groundwater Monitoring Piezometer Installation Report

(Final)," dated May 9, 1988; and "Groundwater Monitoring

Six Month Evaluation Report" (January-June 1988).

The

inspectors determined that there is reasonable assurance

that the Groundwater Monitoring Program will fulfill the

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commitment made in the Safety Evaluation Report (SER).

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The preliminary revision of tha Groundwater Monitoring

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Six Month Evaluation Report (January-June 1988) indicates

that there is no evidence of a continuous static

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groundwater table or piezometric surface within the Glen

Rose formation to the depth investigated.

However, the

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report also indicates that groundwater occurs in isolated

zones (perched water) at various levels from elevation

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734 up to the rock surface.

As a result, the original

design water level (elevation 775) is no longer

justifiable.

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The inspectors reviewed design basis document

(DBD-CS-091), Revision 1, "Foundation Material

Properties," dated December 31, 1987, and determined that

although the original design basis water level was at

elevation 775, the plant design was checke.d for an

assumed groundwater level at elevation 810 (plant grade).

At the service water structure, groundwater was assumed

at elevation 780, 5 feet above the normal safe shutdown

impoundment water level.

All seismic Category I

structures were found to be stable.

The inspector

determined that there is reasonable assurance that the

assumed groundwater level at grade (elevation 810) will

not be exceeded.

However, it is not clear to the

inspectors that the assumed groundwater level

(elevation 780) for the service water intake structure is

adequate.

The preliminary version of the Ground Water

Monitoring Six Month Evaluation Report (January - June

1988) indicates that the groundwater level near the

service water intake structure is relatively constant at

elevation 783.

In addition, the SER states that during a

probable maximum flood (PMF), the maximum stillwater

level reached in the safe shutdown impoundment is at

elevation 790.5.

Significant Deficiency Analysis Report (SDAR) CP-88-23

dated February 4,

1988, was issued concerning the same

subject matter.

Open Item 445/8852-0-04 is closed and

the concern over the design basis groundwater icvel at

the service water intake structure will be followed by

SDAR-CP-88-23.

c.

(Open) Open Item (445/8852-0-05):

program for monitoring

sediment buildup in the SSI.

This item was open pending

rece.pt of information relating to the applicant's

commitment to a program for monitoring sediment buildup

in the SSI.

The inspectors reviewed Procedure EGT-758,

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Revision 1, "Safe Shutdown Impoundment Dam Inspection,"

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dated January 22, 1988, and the draft Revision 2 to this

procedure.

The procedure requires annual testing for

sediment buildup in the intake channel and if the

sediment depth exceeds 1.5 feet, the procedure refers to

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Technical Specification 4.7.5 which requires the sediment

to be removed wi. thin 30 days.

The inspector determined

that there is reasonable assurance that excess sediment

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will be detected.

The procedure states that when

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sediment removal is necessary, procedures will be

developed and approved to remove sediment from the intake

channel.

The inspectors are concerned that if excess sediment is

identified while the plant is in operation and must be

removed within 30 days, adequate forethought and

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preparation may not be utilized to develop the procedure.

Disturbing sediment and debris in the intake channel has

the potential for clogging pump suctions or discharge

filters thereby causing a common made failure of all

service water trains for the two units.

The failure of

the service water system would not only cause a plant

transient, but would cause a failure of the safety

systems required to mitigate the transient.

An activity

with this potential should be carefully analyzed and

reviewed without a 30-day time limit.

The applicant is considering a procedure change to

identify the approach of the silt icvel to the 1.5-foot

limit.

This would allow the applicant time to determine

the optimum time to conduit the silt removal activities,

time to develop procedures, and time to let a contract to

conduct the silt removal operation prior to reaching the

1.5-foot limit.

This item remains open pending the

applicant's action to change the procedure and NRC's

review of the procedure,

f.

(closed) Open Item (445/8852-0-06):

Annual riprap

inspection of the SSI.

The inspectors reviewed applicant

Procedure EGT-758, "Safe Shutdown Impoundment Dam

Inspection," Revision 1, dated January 22, 1988, and

draft Revision 2 to this procedure and determined that

the procedure requires the dam slopes to be visually

inspected to ensure there are no erosion-formed gullies

or wave-formed notches or benches that reduce the

embankment cross section or expose less wave-resistant

materials.

The inspectors found the procedure to be

adequate and this item is considered closed.

c.

(Closed) Open Item (445/8852-0-07):

Annual inspection of

SSI dam in accordance with Regulatory Guide 1.127,

Revision 1.

The inspectors reviewed applicant's

Procedure EGT-758, "Safe Shutdown Impoundment Dam

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Inspection," Revision 1 dated January 22, 1988, and draft

Revision 2 to this procedurc and determined that annual

measurements of piezometric levels and annual surveys of

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the surface alignment monument locators are required.

In

addition, the inspectors reviewed several of the annual

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dam safety inspection reports and determined that they

have the applicable information required by Regulatory

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Guide 1.127, Revision 1.

This item is considered closed.

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3.

Follow-up on Violations / Deviations (92702)

a.

(Closed) Deviation (445/8716-D-01):

Retest requirements

for previously accepted systems.

This deviation dealt

with the applicant's Operations Administration Procedure

STA-623, "Post Work Testing," Revision 1 dated June 26,

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1987, not containing administrative controls to ensure

adequate retesting of systams or design features which

have been maintained or modified following preoperational

testing.

Since the completion of the original

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preoperational testing program, there has been an

extended amount of time has elapsed and the applicant has

committed to several measures to ensure that systems are

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adequately tested and maintained in an acceptable

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condition.

First, the applicant is currently

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implementing the Unit 1 preoperational retest program

which will retest Regulatory Guide 1.68 requirements

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unless acceptable justification is provided on an

individual test basis.

Secondly, Procedure STA-623,

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"Post Work Testing," has been revised to include

administrative controls which:

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Outlines in more detail the types of post-work tests

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to be conducted;

i.e.,

equipment test, surveillance

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test, design modification acceptance test,

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preoperational test, acceptance test, and system

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test,

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Identifies specific organizational responsibilities;

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i.e.,

responsible work organization, responsible

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test organization, post-work test report review,

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system test matrix review, etc.

Identifies amount of detail for specific job

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responsibilities; such as, start up manager, I&C

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manager, etc.

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Adds a post-work test list which is used as a cross

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reference between required surveillance procedures,

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technical specification requirement, and the

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specific component tag number.

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In addition to the above change, the applicant reviewed

and revised the following procedures to include

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clarification of the impact of Regulatory Guide 1.68

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(Revision 2, August 1978) for testing prior to the

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issuance of an operating license.

STA-623, "Post Work Testing," Section 6.4.1.3 was

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revised to provide for a sign-off block verifying

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review for port-test review.

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STA-606, Revision 8, "Work Requests and Work

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orders," Section 6.8.1 was changed to provide

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Startup review of work orders for impact on

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preoperational test program.

Section 2.0 ensures

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that testing performed by Startup or

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components / systems in the custody of operations

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shall be performed in accordance with an' authorized

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work order.

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STA-808A, Revision 1, "Unit 1 Prestart Test

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Program," Section 2.0, states that the program is

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applicable to all Unit 1 and common systems required

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for safe power operation of Unit 1.

Figure 7.2,

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Unit 1 Prestart Test Program Flow Chart, references

Regulatory Guide 1.68.

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STA-809A, Revision 0,

"Development of System Test

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Matrices," Section "5.3 assigns responsibility for

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implementing the Unit 1 Prestart Test Program to the

Unit 1 test managar.

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Based on these changes to the Operation /Preoperation Test

Program, the inspectors consider this item closed.

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4.

Preoperational Retest Program Activities (70301, 70302)

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NRC staff obtained and reviewed the most recent information

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regarding Unit 1 Preoperational Retest Program.

This review

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included discussions with preoperational supervision and

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personnel, procedure status review, projected schedule

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(overall and individual test performance) and status of

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preoperational test procedure review and acceptance.

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applicant's published preoperational test procedure list shows

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that there are 146 total procedures for Unit 1 review, with

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106 procedures issued for comment.

Of these 106 procedures, 7

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have been approved for use.

The inspectors have requested

copies of the approved procedures for review during a future

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inspection period.

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There were no violations or deviations identified in the areas

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inspected.

5.

Plant Tours (71302)

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The NRC inspectors conducted planc tours during this

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inspection period.

These tours provided coverage during

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nornial, off-normal, and backshif t working hours.

During the

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tours, inspection activities included reviewing work

documentation, witnessing ongoing work activities, observing

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and interviewing shift operations personnel, reviewing the

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status of control room construction work, reviewing the status

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of system and component completion, observing the status of

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Units 1 and 2 equipment lay up, observing housekeeping

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activities, and inspecting for general safety compliance.

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To support these activities, NRC inspectors attended

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plan-of-the-day meetings, discussed plant status with

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operations personnel, reviewed plant lay up logs, and

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performed a walkdown inspection of all major Unit 1 systems in

lay up.

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a.

During the course of the tours and inspections, the NRC

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inspectors noted the following:

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(1)

The Unit 1 lay up status walkdown covered the main

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turbine generator, the diesel generator, the primary

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.and secondary systems, and electrical penetrations.

During the walkdown, the on-shift auxiliary

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operators accompanied the inspector; the operators

demonstrated to the inspector's satisfaction that

they were knowledgeable as to valve and component

locations, methods of verifying valve positions, and

methods of verifying lay up status.

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ancies were noted in this inspection of lay up

status.

(2)

Housekeeping measures appear to be adequately

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implemented.

(3)

observations of the component cooling water system

flush procedure and discussions with control room

personnel indicated that they are cognizant of the

flush lineup and status of the component cooling

water system.

b.

The radiation protection manager informed the resident

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insrectors of two separate instances where radiological

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barrier violations had occurred on two separate

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occasions, August 14 and 15, 1988.

The incidents

resulted when a contract employee, working in the fuel

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building, twice crossed a barrier into a radiation

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controlled area (RCA) in order to gain access to the fuel

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building bridge crano lower platform,

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In the second instance, as the employee crossed onto the

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erane's lower platform (thus crossing the boundary of the

radiation controlled area), a radiation protection

technician stopped him and informed him that he had

crossed a radiation controlled area boundary without

proper authorization in the form of a radiatjon work

permit (RWP).

The employee explained that he had crossed

the barrier in a similar fashion on the previous day.

Furthermore, he explained that he belic'.ed that he had

received permission from the responsible envincering and

security departments prior to crossing the boundary to

reach the crane's lower platform.

He based this belief

on a discussion he had with the fuel building

coordinator.

In this discussion, the fuel building

coordinator told the employee that he could enter green

badge security areas (areas above the 860 foot level in

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the fuel building).

Because the fuel building

coordinator thought that the employee did not want access

to the crane's lower platform, the fuel building

coordinator did not perceive that the employee was

actually asking for permission to enter a radiation

controlled area.

The preliminary cause of this violation appears to be

that neither the contract employee nor the security

personnel recognized that the crane's lower platform was

in a radiation controlled area. Contributing causes

appear to be that security personnel were under the

impression that. blue badge security areas (areas where

nuclear fuel is being stored or handled) were equivalent

to radiation controlled areas, that the barrier signs

posted did not include instructions to notify radiation

protection prior to entry, and that the work package did

not identify any of the contract employee's work as being

in an radiation controlled area and therefore, the work

permit did not call for radiation protection

participation.

The radiation protection department responded to these

incidents by issuing radiological incident / problem report

(88-0002) and a deficiency report (DR) P88-04086

documenting the occurrences.

Corrective actions include

improving the postings and barricades on the 860 foot

level, changing the security post order to include a

radiation protection escort for all blue badge area

entries, instructing the security personnel that blue and

green badges are for security purposes only, and that

personnel should contact radiation protection prior to

entry into radiation controlled areas.

The above constitutes a violation of the applicant's

special nuclear material license, and is identified as a

violation (445/8854-V-01): Unauthorized Entry into

Radiological Controlled Area.

6.

Safety Evaluation Report (SER) Review and Follow-up (92719)

Comanche Peak SER (NUR.EG 0797) includes various commitments

and requirements that the applicant must meet prior to the

NRC's decision on issuance of an operating license.

The

following items were reviewed by the inspector.

Section 9.3.2.

The applicant committed to install provisions

to sample containment sump water.

The inspector has

ascertained that the applicant has the capability to sample

the containment recirculation sumps via the Train A residual

heat removal pump.

The sampling procedure is covered in

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Chemistry Procedure CHM-512A, "Operation of the Reactor

Coolant Post Accident Sampling System."

7.

Exit Meeting (30703)

An exit meeting was conducted on September 8, 1988, with the

applicant's representatives identified in paragraph 1 of this

report.

No written meterial was provided to the applicant by

the inspectors during this reporting period.

The applicant

did not identify as proprietary any of the materials provided

to or reviewed by the inspectors during this inspection.

During this mocting, the NRC inspectors summarized the scope

and findings of the inspection.

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50-445/83-66 50-446/88-5 0

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DISTRIBUTION:

Docket Files'(50-445/446))

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NRC PDR~

LPDR

CPPD-LA

CPPD Reading (HQ)

OSP Reading

  • Site Reading File

R. Warnick

  • J. Wiebe
  • H. Livermore
  • MIS System, RIV
  • RSTS Operator, RIV

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DRP, RIV

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RIV Docket File

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  • L.

Shea, ARM /LFMB

J. Taylor

J.

Partlow

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C. Grimes

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P. McKee

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J. Lyons

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J. Wilson

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M. Malloy

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D. Terao

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J. Moore, OGC-WF

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J. Gilliland, RIV

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F. Miraglia

E. Jordan

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B. Grimes

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B. Hayes

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  • w/766

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