ML20154D158

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Monthly Operating Rept for Aug 1988 for Cooper Nuclear Station
ML20154D158
Person / Time
Site: Cooper Entergy icon.png
Issue date: 08/31/1988
From: Horn G, Scheuerman J
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
CNSS888204, NUDOCS 8809150171
Download: ML20154D158 (5)


Text

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s OPERATING DATA REPORT DOCKET NO. 050-0298 DATE 09-09-RA COMPLETED BY J. T. Schegorrnan TELEPilONE NO2) 825 4 811 OPERATING STATUS N'

1. Unit Name: CnnDor Nuclear Station
2. Reporting Pniod:

Acoust 1988 2381

3. Licenwd Thermal Pow er (MWt):

AV

4. Namephte Rating (Grom mwd):
5. Design Electrical Rating (Net MWe): 779 787
6. Maximum Dependable Capacity (Grou MWe):

764

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratinp (Items Number 3 Through 7) Since Last Reprt,Gise Reasons:
9. Powee Level To Which Restricted,if Any (Net MWe):
10. Reasons For Restrictions.lf Any:

1 This Month Yr. to' Date Cumularise

11. Iloun in Reporting Period 744.0 5.RM 0 1?4_??4.0
12. Number Of Houn Reactor Was Critical 694.5 3.03R.9 93.n46.3
13. Reactor Rewne Shutdown floun 0.0 0,0 0.0
14. Iloun Genentor On.Line 661.7 2.961.2 91.505.6 l
15. Unit Rewne Shutdown lioun 0.0 0.0 U.0
14. Grou Thermal Energy Genented (MWil) 1.542.312.0 6.?;1.3c?.n 180.R92,059,5
17. Grou Electrical Energy Generated (MWH) 5% 8 5 2_ 0,,,

2,043.818.0 58,102,899.0

18. Net Electrical Energy Genented (Mkil) 485,768.0 1.990.766.0 56.009.390.0
19. Unit Senice Factor 91.6 50.6 73./
20. Unit Aiaihbility Factor 91.6 50.6 73.7 85.5 44.3 59.0
21. Unit Capacity Factor (Using MDC Net)
22. Unit Capacity Factor (Using DER Net) 83.9 43.5 66.0

.23. Urdt Forced Outage Rate 8.4 10.9 4.6 I

24. Shutdowns Scheduled Oser Nest 6 Months (Type. Date.and Duration of Each t:

i

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units la Test Status (Prior io Commercial Operationi:

Forecast Achiesed INITIA L CRITICALITY INITIA L ELECTRICLTY l

COMMERCI AL OPER ATION 8809150171 880831 1

PDR ADOCK 05000298 R

PDC gg,

AVERAGE DAILY UNIT POWER LEVEL l

DOCKET NO. 050-0?99 UNIT CNS l

DATE 09-09-88 COMPLETED BY J. T. Scheuerman TELEPHONE (402) 925-3R11 MONTil _ Aucust 1988 DAY AVER AGE DAll.Y POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (Mhe Net)

(gw,.p,,)

1 740 g7 7p 2

7J5 is 74 0 3

742 19 741 4

740 20 740 8

7#2 21 656 6

744 22 736 7

703 23 755 s

755 24 756 g

9 756 25 21 10 7R1 26 0

33 7#9 27 43 32 7bI 21s 465 13 50 29 608 14 713 30 752 l

15 716 3,

749 1

16 645 INSTRUCTIONS On this format. list the aserage dauy uit power levelin MWe Net for each day in the reperting amth. Compute to the riearest whole rnegawatt.

(9/77) wn =

LA'

. -=._ _ r n _.

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UNI T S!!U rt>0WNS AND POWElt REDUCilONs IMM*KET ND. 060-0298 UNirNAitE CNS DALE 09-09 RR Ntri.ETED liY 7 Y c

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6 88-06 880825 i

62.3 A

3 88-021 NA NA Reactor scranraed due to spurious Main Steam Line High Radiation signals. - A grounding cable was added to the radiation cionitor chassis, and a Directive was issued restricting the use of 2-way radios in the plant.

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3 4

F: Forced steas..n:

nicahod:

Exhibia C. Instruchis 5: Sc!wduled A Isinipmen Failure (Eal. lain) 1412nual f..e Psepasati.wi of D2:

2 fl4tainicnance niTes:

24tanust Scram.

Ensey $hcess f.n I.keence l

C.itefi. cling 3 Aul.msanic Scism.

Evens Itcp.ns (LEltIl'dc tN1Ilt!L l

D.itegulai.ny Itestsic 1.m 4-Other (Explain) 0161)

E41pensos Tsaisiing A Ucense Emainin2 tion F.Adininiseranive 5

G Operational Ensur (Emplain)

Estu% I.Sanx Source P8/77).

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I OPERATIONS NARRATIVE Cooper Nuclear Station August 1988 l

At 0040 on August 25, 1988, the reactor scranmed due to spurious Main Steam 1

Line High Radiation signals.

Corrective actions included adding an extra i

grounding cable between the radiation monitor chassis and the instrument f

ground bus, and restricting the use of 2-way radios in the plant, r

t The plant was returned to service at 1459 on August 27, 1988.

No other scheduled or unscheduled shutdowns, or unscheduled power reductions

[

l were experienced during the month of August.

A capacity factor of 85.5% was achieved for the month.

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COOPCR NUCLE AR ST ATeoN Nebraska Public Power District

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CNSSB88204 September 9, 1988

[

6 i

Document Control Desk U.S. Nuclear Regulatory Commission

[

Washington, D.C.

20555

Subject:

Monthly Operation Status Report for August 1988 Docket No. 50-298 l

Gentlemen.

t i

Enclosed for your information and use is the Cooper Nuclear Station Monthly f

Operating Status Report for August 1988.

The report includes Operating i

Status, Average Daily Unit Power Level, Unit Shutdown Data, and a Narrative l

Sumary of Operating Experience.

l t

Should you have any coments or require additional information regarding this report, please contact me.

Sinc 'rel,

j i

i w

orn i

Di on Manager of Nuclear Operations l

GRH/JTS:nd i

Enclosure cc:

G. D. Watson w/ enc.

l R. D. Martin w/ enc.

rezy

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