ML20154D100

From kanterella
Jump to navigation Jump to search
Insp Rept 50-298/88-07 on 880301-0415.Violation Noted.Major Areas Inspected:Operational Safety Verification,Containment Local Leak Rate Test,Monthly Surveillance & Maint Observations,Esf Walkdown,Outage,Refueling & Security
ML20154D100
Person / Time
Site: Cooper Entergy icon.png
Issue date: 05/10/1988
From: Bennett W, Holler E, Plettner E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20154D093 List:
References
50-298-88-07, 50-298-88-7, NUDOCS 8805190046
Download: ML20154D100 (11)


See also: IR 05000298/1988007

Text

.

-

.

.

I

APPENDIX B

U. S. NUCLEAR REGULATORY COMMISSION

REGION IV

NRC Inspection Report:

50-298/ 88-07

License:

DPR-46

Docket:

50-298

Licensee: Nebraska Public Power District (NPPD)

P. O. Box 499

Columbus, NE

68601

Facility Nanie: Cooper Nuclear Station (CNS)

Inspection At: Cooper Nuclear Statiori, tiemaha County, Nebraska

Inspection Conducted:

itarch 1-April 15, 1988

Inspectors:

. N. / d /suo

I//TI /

C A. Plettner, Resident Inspector, (RI)

Date'

~

fdkt'

Y b>l//

II.~R. Dennett, Senior Resirient inspector, (SRI)

Date

  • '

'

( fo 9[

Approved:

E. J.

. oiler, Chief, Project Section C,

Date '

Reactor Projects Division

8805190046 880511

PDR

ADOCK 05000298

O

DCD

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

.

.

.

%

0

2

Inspection Summary

Inspection Conducted March 1 through April 15, 1988 (Report 50-298/88-07)

Areas Inspected:

Routine, unannounced inspection of operational safety

verification, containment local leak rate-test, monthly surveillance and

maintenance observationt, ESF walkdown, outage, refueling, shutdown,

radiological protection, and security.

Results:

Within the areas inspected, one violation was identified (failure to

follow a health physics procedure, paragraph 11).

-

l

3

r

i

._

- _--___

.-. _

-. -

__

n

-

..

.

.

.

..

t

3

DETAILS

'

1.

Persons Contacted

Principal'L'icensee Employees

  • G. R. Horn, Olvision Manager of Nuclear Operations
  • R. D. Black, Operations Supervisor
  • 0. M. Norvell, Maintenance Manager
  • J. V. Sayer, Radiological Manager
  • G.

E. Smith, Quality Assurance _ Manager

  • L. E. Bray, Regulatory Compliance Specialist
  • G. R. Smith, Licensing Supervisor

The NRC inspectors also interviewed other licensee employees during the

inspection period.-

  • Denotes those present during the exit interview conducted on April 15,

1988.

2.

Licensee Action on Previous Inspection Findings

(Closed) Open Item 298/8709-01:

Deficient As-Built Instrument Drawing -

This item involved discrepancies between System Operating

Procedure (50P) 2.2.20, Revision 23, Appendix A "Valve Checklist

Number 2" and Cooper-Bessemer as-built drawing KSV-46-5; and between

S0P 2.2.12, Revision 8, Appendix A, "Valve Checklist" and Burns & Roe

as-built drawing Nos. 2077 and 2011, Sheet 1.

Drawing Change

Notice (DCN) 87-1682 was issued to correct labeling deficiencies on

KSV-46-5.

DCN 88-29 was issued to correct labeling deficiencies on

Drawing No. 2011, Sheet 1.

DCNs87-154 and 88-174 were issued to correct

labeling defit:iencies on Drawing No. 2077.

The RI compared 50P 2.2.20, Revision 27, Appendix A, to Drawing KSV-46-5;

and S0P 2.2.12, Revision 10, dated October 22, 1987, Appendix A, to

Drawings 2011 and 2077, and found no discrepancies.

This item is closed.

(Closed) Open Item 298/8712-01:

10 CFR 50.59 Conflict with USAR - This

item involved conflict between the CNS Updated Safety Analysis

Report (USAR) Section 13, paragraph 9.5, and the Safety Review and Audit

Board (SRAB) Instructions and Guidelines, Section 1.2.

The conflict

involved the academic requirements of board members.

The USAR required

that all members have degrees.

The SRAB Instructions and Guidelines

stated that they shall have a B.S. degree, or equivalent experience.

The

. __

_ _ _ _

.

.

.

.

.

4

licensee submitted to the NRC a change to the USAR which was approved on

July 22, 1987, to resolve the conflict.

The RI verified agreement between

the USAR and the SRAB Instructions and Guidelines.

This item is closed.

(Closed) Violation 298/8728-03:

Failure to Maintain Secondary Containment

Integrity - This item involved the reactor building railroad airlock

doors. With the inner door open while the outer door was closed, air gaps

existed between the outer door and the ground.

Corrective actions taken

by the licensee were to generate two new procedures, which provide

detailed instructions to verify integrity of secondary containment

penetrations, and to fabricate and mount signs on the airlock doors

stating "Prior to shutting either railroad airlock door, insure that the

associated railseal plates are installed." The RI reviewed Surveillance

Procedure 6.3.10.17, "Secondary Containment Penetration Inspection,"

Revision 0, dated March 1, 1988, and Maintenance Procedure 7.0.10,

"Railroad Airlock Door Operations," Revision 0, dated March 1, 1988, to

verify that corrective actions were complete and adequate.

The RI

verified that signs were mounted on the railroad airlock doors.

This item is closed.

3.

Operational Safety Verification

The NRC inspectors observed operational activities throughout the

inspection period.

Control room activities and conduct were observed to

be well controlled.

Proper control room staffing was maintained.

The NRC

inspectors observed selected shift turnover meetings and noted that

information concerning plant status was communicated to the oncoming

operators.

Tours of accessible areas at the facility were conducted to confirm

operability of plant equipment including the fire suppression systems and

other emergency equipment.

The NRC inspectors performed a walkdown of the

Residual Heat Removal (RHR) System.

Results of this walkdown are

documented in paragraph 7 of this report.

Operators were cognizant of maintenance being performed during the outage

and how it affected operation of the plant.

Limiting conditions for

operation (LCOs) were properly entered when safety equipment was

inoperable for maintenance.

Required surveillance testing was properly

performed when LCOs were in effect.

A tagout desk was setup outside the control room (CR) during the outage.

This allowed qualified personnel to review work packages and initiate

tagouts for work performance without having extra personnel in the CR

area.

This greatly reduced the congestion in the CR and aided the

on-watch operators in maintaining plant status.

No violations or deviations were identified in this area.

-

- - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

. _ _ _ _ _ _ _

_ _ _ _ - _ _ _ _ _ _ _

. _ _ _ _ _ _

.

.

.

.

.

5

4.

Containment Local Leak Rate Test

The R1 performed direct observation, record review, and independent

calculations associated with the Containment Local Leak Rate Test (LLRT)

program conducted by CNS.

The purpose of this inspection was to verify

that primary containment local leak rate tests, as required by CNS TS were

performed to ensure that leakage through testable containment penetrations

and isolation valves would not exceed the allowable leakage specified.

The RI observed the performance of Surveillance Procedure (SP) 6.3.1.1,

"Primary Containment Local Leak Rate Test," Revision 22, dated

February 25, 1988, Attachment 3, for RHR MOV-M021A, M026A, M031A, M0166A,

and M0167A.

Personnel performing the test were cognizant of all

precautions associated with the test and performed the test in accordance

with applicable procedures.

The RI performed independent calculations of

LLRT data for the above listed valves and for other valves tested by the

procedure.

These calculations were in agreement with those performed by

licensee personnel during performance of the test.

The sum of as-found leakages determined during LLRTs exceeds the

requirement of TS.

The licensee will evaluate valves for repair and

perform applicable LLRTs subsequent to any repairs.

The licensee will

issue a Licensee Event Report (LER) to document exceeding requirements for

allowable leakage.

No violations or deviations were identified in this area.

5.

Monthly Surveillance Observations

The NRC inspectors observed and reviewed the performance of Nuclear

Performance Procedure (NPP) 10.5, "LPRM Calibration," Surveillance

Procedure (SP) 6.3.12.1, "Diesel Generator Operability Test," SP 6.3.5.1,

"RHR Test Mode Surveillance Operation," SP 6.2.3.3., "Drywell Air Sampling

System Calibration and Functional / Functional Test," and SP 6.3.8.2, "SLC

Pump Operability Test."

NPP 10.5, "LPRM Calibration," Revision 19, dated February 1,1988,

At'=chment 1, "Tip System Operation": This test was performed on

Marci,1, 1988, to verify that Local Power Range Monitors were within

calibrotion.

The RI observed that the test was performed by

qualified personnel who were cognizant of all precautions associated

with the test.

The test was performed in accordance with all

applicable procedures.

SP 6.3.12.1, "Diesel Generator Operability Test," Revision 22, dated

November 19, 1987:

This test was performed on March 29, 1988, to

verify operability of No. 2 Diesel Generator (DG) after performance

of the annual inspection. The SRI observed that the test was

performed by qualified operators who were cognizant of all

surveillance requirements.

Maintenance identified a potential

problem with one cylinder during the test.

A broken ring and scored

9

.

.

6

liner were discovered on one cylinder, and the ring and liner were

replaced.

SP 6.3.12.1 was repeated on April 5, 1988, and

subsequently, DG No. 2 was declared operable.

'

SP 6.3.5.1, "RHR Test Mode Surveillance Operation," Revision 27,

dated February 25, 1988:

This test was performed on April 6, 1988,

to verify RHR Loop B (Pumps B and D) operability subsequent to

maintenance performed on loop B.

The SRI reviewed the surveillance

and determined that all data was properly verified to be acceptable

per the procedure and TS.

The test was properly reviewed by all

required personnel.

SP 6.2.3.3, "Drywell Air Sampling System and Functional / Functional

Test," Revision 21, dated August 7,1986.

This test was performed on

April 7, 1988, as acceptance testing for maintenance performed on the

drywell particulate monitor per Work Item (WI) 88-1618.

This test

was performed by a qualified technician in accordance with approved

procedures.

The SRI noted that the procedure was written in such a

manner that, at times, it was difficult to follow.

Discussions with

licensee personnel determined that the procedure was being rewritten

and the revision was in the review and approval process.

SP 6.3.8.2, "SLC Pump Operability Test," Revision 27, dated March 3,

1988:

This test was performed on April 11, 1988, to verify

operability per TS 3/4.4 and to meet requirements for inservice

testing.

The test was performed by qualified personnel who were

cognizant of procedure requirements.

The SRI verified that all test

equipment used during the procedure was in calibration. The SRI

observed that independent verification was properly performed and

that seals were properly reinstalled on appropriate valves.

No violations or deviations were identified in this area.

6.

Monthly Maintenance Observation

The NRC inspectors verified that the maintenance activities were conducted

in accordance with approved procedures, regulatory guides, and industry

codes or standards, and in conformance with TS.

On March 16, 1988, the RI observed the performance of Preventive

Maintenance (PM) No. 03728, "Inlet and Outlet Cooler Tubes Inspection,"

and associated Equipment Clearance and Release Order 88-378, RRLO-HX A

and -HX B, dated March 15, 1988.

The RI observed maintenance personnel

performing the PM and noted that it was performed in a professional manner

and that the personnel were cognizant of all procedural requirements.

All

clearance order tags were appropriately identified and hung in accordance

with the equipment clearance and release order.

The NRC inspectors observed maintenance personnel perform Surveillance

Procedure (SP) 6.3.12.6, "Diesel Generator Annual Inspection,"

Revision 20, dated June 12, 1986, and associated Maintenance Work

._____________- __ __ ____

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .

__ _____________________

.

.

.

.

.

.

7

Request (MWR) 88-0866 for DG No. 2.

This procedure was performed to meet

TS requirements that the diesel generator be inspected in accordance with

instructions based on the manufacturer's recommendations.

The NRC

inspectors observed that maintenance personnel were aware of the

requirements of the inspection, and performed the inspection in accordance

with the procedure.

DG No. 2 was declared operable on April 5, 1988,

af ter appropriate acceptance testing was performed.

On March 31, 1988, the SRI observed the performance of hydrostatic testing

on "B" RHR heat exchangers per WI 88-1009.

The hydro was performed as

acceptance testing following maintenance.

The SRI observed that the test

was properly performed in accordance with Maintenance

Procedure (MP) 7.0.8, "Pressure Testing," Revision 4, dated November 5,

1987.

The SRI noted that quality control hold points were properly

observed and that the proper test pressure was maintained throughout the

test.

No violations or deviations were identified in this area.

7.

Engineered Safety (ESF) Feature Walkdown

The NRC inspectors performed an independent walkdown of Loop B of the RHR

system.

The inspection was performed to verify operability, to confirm

that licensee system lineup procedures match plant drawings and the

as-built configuration, and to identify equipment conditions or items that

might degrade system performance.

This system was chosen because Loop B

had just been declared operable following maintenance performed during the

outage.

)

In preparation for performing the walkdown of the RHR system, the NRC

inspectors conducted a review and comparison of the following licensee

system checklist and applicable as-built drawings:

50P 2.2.69A, "Residual Heat Removal Valve Checklist," Revision 1,

dated March 3, 1988

As-Built Drawing - Burns & Roe 2040

"RHR System"

i

General Electric Diagram 729E211BB

"RHR System"

During the walkdown minor discrepancies involving missing labels were

noted which did not affect system operability.

The licensee was notified

of these discrepancies and initiated actions to correct them.

.

'

During the inspection, the NRC inspectors verified proper positioning and

tagging of valves associated with the A Loop of the RHR system which was

I

inoperable due to maintenance being performed on the system.

No violations or deviations were identified in this area.

l

-

I

!

!

'

. _ . _ . _ _ _ _

_

. _ _ _ _ _ _ _

_ __

_

__ ._ _ _ _

. _ .

_ _ _ _ _ _ _ _ _ _ _ _ _

.

.

.

.

.

. .

8

8.

Outage

The licensee commenced a refueling outage on March 5, 1988.

In addition

to refueling, numerous maintenance items and modifications are being

performed including diesel generation inspection, replacement of 125V

batteries, detailed control room design review human factors

modifications, motor control center upgrades, and Standby Liquid Control

System modifications.

The licensee performed maintenance on all "Loop B" safety systems

simultaneously while maintaining all "Loop A" systems operable.

Upon

completion of "Loop B" maintenance, the NRC inspectors monitored and

reviewed acceptance testing of "Loop B" safety systems as they were

declared operable.

The switchover from "Loop A to "Loop B" was performed

in a controlled, conservative manner.

The NRC inspectors observed that

acceptance testing and system lineups were properly performed.

Limiting

conditions for operations were properly observed at all times, and TS were

properly reviewed whenever a system or systems was inoperable.

The NRC inspectors observed the implementation of Design Change 87-029B

"MCC Qualification Upgrade," approved on February 25, 1988, and associated

Maintenance Work Request, MWR 88-1081.

The purpose of the upgrade was to

refurbish breakers located within the Motor Control Centers (MCC) to meet

environmental qualification standards.

The NRC inspectors observed the

electrical craft personnel performing their duties in a professional

manner, and in accordance with procedures.

Quality control hold points

were observed.

Quality control personnel performed their duties in a

professional manner.

The assigned system engineers were also observed

during the implementation of the design change and during performance of

acceptance testing.

On March 16, 1988, the RI observed the performance of Design

Change 87-043, "Replacement of NBI Pressure Switches," approved on

March 4, 1988, and associated MWR 88-1057.

The purpose of the design

change was to upgrade current pressure switches with environmentally

qualified pressure switches.

The RI observed the instrumentation and

control personnel perform their duties in a professional manner and in

accordance with the design change procedure.

The assigned system engineer

was also present at various times to observe the performance of the work.

The NRC inspectors observed the replacement of 125V battery 1B in

accordance with Design Change 87-073.

The design change was implemented

Procedure (SP)6.3.15.7,glicableprocedures.

in accordance with the ap

Surveillance

125V Batteries 1A and 18 Service Test,"

Revision 0, was approved on March 31, 1988, to perform the acceptance test

for the new battery.

The procedure was based on manufacturer's

recommendations and was performed in addition to testing previously

observed by licensee personnel at the battery manufacturers.

SP 6.3.15.7

4

was completed on April 4, 1988.

No violations or deviations were identified in this area.

1

, _ _ _ _ _

. - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ - _ _ _

_ _ _ _ .

-

,

.

.

, . , .

9

9.

Refueling

The NRC inspectors held discussions with fuel handling and control room

personnel, observed fuel movement, verified fuel assemblies locations in

the spent fuel pool and the reactor, accountability records, and status

board updates during this inspection period.

The NRC inspectors also

.

reviewed the licensee's procedures and records concerning the movement of

fuel and storage of fuel assemblies.

Included as part of those reviews

were SP 6.1.2.7, "Refueling Platform Interlocks and System Functional

Tests," Revision 23, dated November 12, 1997, with attachments to the

procedure, NPP 10.21, "Special Nuclear Materials Control and

Accountability Instructions," Revision 1, dated May 14, 1987, NPP 10.25,

"Fueling," Revision 8, dated February 12, 1987, and NPP 10.26, "Working

Over or In Reactor Vessel Requirements," Revision 1, dated March 10, 1988.

Three different operating shifts were observed during this inspection

period.

Each operating shift was cognizant of the requirements of the

various procedures, and performed their duties in a controlled and

professional manner.

All required surveillances were performed including

daily surveillances of "A" Standby Gas Treatment and "A" Standby Liquid

Control when the "B" trains of those systems were inoperative for

maintenance.

On March 7, 1988, the SRI questioned the licensee's intent to lift the

reactor vessel head prior to demonstrating the ability of secondary

containment to maintain 1/4-inch of water vacuum under calm wind

conditions, as stated in TS 4.7 C.1.c.

Paragraph 4.7.C of TS Bases

implies that this test should be done prior to the time that primary

containment is opened for refueling.

Discussions were held among the

licensee, SRI, NRR project manager, and NRC Region IV management.

It was

agreed that the test to demonstrate secondary containment need only be

performed prior to fuel movement.

The licensee committed to reviewing TS

to determine if a change to TS 4.7.C Bases was required.

The test

(SP 6.3.10.8, "Secondary Containment Leak Test, Revision 9, dated

December 17, 1987) was completed satisfactorily on March 9, 1988, prior to

commencing fuel handling operations.

No violations or deviations were identified in this area.

10.

Shutdown

The NRC inspectors held discussions with operations shift personnel and

reviewed control room records including log entries, record traces, and

computer printouts associated with the scheduled shutdown.

The shutdown

started at 4:30 a.m., on March 6, 1988.

The shutdown was required in

order to perform the refueling of the reactor, preventive maintenance

activity on selected equipment, and install approved plant design changes.

The RI reviewed General Operating Procedure (GOP) 2.1.4, "Normal Shutdown

from Power," Revision 27, dated December 10, 1987.

Other procedures which

were revcewed in whole or in part were GOP 2.1.10, "Station Power

- _ - _ . _ _

_ _-__ _

__.

--

_

-. .

. - _ _

-

_ _ _ _ _

.

.

.

.

...o

10

Changes," Revision 15, dated December 10, 1987, and GOP 2.1.20, "RPB

Refueling Preparation," Revision 12, dated February 18, 1988.

During the

shutdown, two safety system challenges occurred:

A Group II, III, and VI Isolation was received at 4:31 a.m. on

March 5, 1988, because of a reactor vessel low-water setpoint

(+12.5 inches) being reached.

The event was attributed to a reactor

vessel water level "shrink" which occurs on a reactor scram. The

manual scram was initiated at 25 percent power as part of the normal

shutdown procedure.

A Group III Isolation was received at 2:40 p.m. on March 5, 1988,

because of an indicated reactor water cleanup (RWCU) system high-flow

condition.

The incorrect indication was the result of pump

cavitation due to the loss of net positive suction head to the pump.

Notification of each event was made to the NRC headquarters operation

central duty officer as required.

In addition, the SRI was notified when

the events occurred.

No violations or deviations were identified in this area.

11.

Radiological Protection Observations

The NRC inspectors verified that selected activities of the licensee's

radiological protection program were implemented in conformance with

facility policies, procedures, and regulatory requirements.

Radiation

work permits contained appropriate information to ensure that work could

be performed in a safe and controlled manner.

Radiation and/or

contaminated areas were properly posted and controlled.

Radiation

monitors were utilized to check for contamination.

During a routine plant tour on March 28, 1988, the RI observed an

individual inside a posted radiation area in the heater bay room with shoe

covers and gloves, which is normal attire for a tour and inspection of the

area.

However, in this case, Special Work Permit (SWP) 88-3-46, issued on

March 21, 1988, for the area, did not allow for tour and inspection, and

required additional protective clothing.

No other SWP was assigned to the

area.

The RI questioned the individual to ascertain whether permission

had been received from health physics personnel to be in the area with

only shoe covers and gloves.

The individual responded that no permission

had been received.

Failure to comply with Health Physics

Procedure (HPP) 9.1.1.4, "Special Work Permit," Revision 16, dated

April 15, 1987, and SWP 88-3-46, titled, "Bypass Valves," is an apparent

violation.

(298/8807-01)

The licensee took immediate corrective actions when notified of the

problem.

No other violations or deviations were identified in this area.

.- -

U

. _ _ _ _ _

.

.

.

.

....

11

12.

Security

The NRC inspectors observed security personnel perform their duties of

vehicle, personnel, and package search.

Vehicles were properly authorized

and escorted or controlled within the protected area (PA).

The PA barrier

had adequate illumination and the isolation zones were free of transient

material.

Compensatory measures were implemented in a timely manner when

equipment failed or when security doors were required to be open for work

being performed during the outage.

These observations verified that the

physical security plan was being implemented in accordance with the

requirements established in the CNS Operating License.

No violations or deviations were identified in this area.

13.

Exit Interview

An exit interview was conducted on April 15, 1988, with licensee

representatives (identified in paragraph 1).

During this interview, the

SRI reviewed the scope and findings of the inspection.

- . - _ .