ML20151X362

From kanterella
Jump to navigation Jump to search
Notice of Violation from Insp on 880301-31.Violation Noted: Licensee Failed to Make 4 H Rept for Automatic ESF Actuation That Is Not Part of Preplanned Sequence During Testing of Emergency Diesel Generator
ML20151X362
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 04/29/1988
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20151X360 List:
References
50-285-88-11, NUDOCS 8805040131
Download: ML20151X362 (1)


Text

B

. 1 APPENDIX A NOTICE OF VIOLATION Omaha Public Power District Docket:

50-285 Fort Calhoun Station Operating License:

DPR-40 During an NRC inspection conducted on March 1-31, 1988, violations of NRC requirements were identified. The violations involved the failure to provide correct and accurate information in response to an NRC-identified violation and failure to make a 4-hour report as required by 10 CFR Part 50.72.

In accordance with the "General Statement of Policy (and Procedure for NRC1988),theviola Enforcement Actions," 10 CFR Part 2, Appendix C listed below:

A.

Section 50.72(b)(2) of 10 CFR Part 50 states, in part, that a 4-hour report shall be made whenever any event or condition that results in automatic actuation of any engineered safety feature (ESF). The actuation of ESF that results from and is part of the preplanned sequence during testing need not be reported.

Contrary to the above, the licensee failed to make a 4-hour report for an automatic ESF actuation that was not part of a preplanned sequence during testing, in that, during the testing of Emergency Diesel Generator 1 on March 23, 1988, operator error caused the unplanned actuation of Emergency Diesel Generator 2, an engineered safety feature.

This is a Severity Level V violation.

(SupplementI)(285/8811-03)

B.

Section 50.9 of 10 CFR Part 50 states, in part, that information provided to the Commission by a licensee shall be complete and accurate in all material aspects.

('

Contrary to the above, the licensee submitted a response to Violation 285/8724-04, dated February 24, 1988, that contained inaccurate information, in that the response stated that no instances of the failure to control gas cylinders had been noted since September 1987.

The NRC inspector had noted and discussed with licensee personnel, an instance of l

the failure to control gas cylinders in December 1987.

This is a Severity Level V violation.

(SupplementVII)(285/8811-04) l Pursuant to the provisions of 10 CFR Part 2.201, Omaha Public Power District is hereby required to submit to this office, within 30 days of the date of the j

letter transmitting this Notice, a written statement or explanation in reply, including for each violation:

(1) the reason for the violation if admitted.

(2) the corrective steps that have been tak'in and the results achieved (3) the corrective steps that will be taken to avoid further violations, and (4) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending the response time.

Dated at Arlington, Texas, this 29th day of April 1988 8805040131 880429

{DR ADOCK 05000285 DCD t

L