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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20153B0531998-09-16016 September 1998 Special Rept:On 980817,errors in Implementation of Selected Licensee Commitment Testing Requirements on Fire Protection Sys Instruments,Was Discovered.Caused by Error in Interpretation of SLC Requirement.Will Revise Procedures ML20236M9151998-07-0707 July 1998 Special Rept:On 980611,determined That Required Firewatch Patrol Had Been Missed.Caused by Firewatch Being Performed on Wrong Unit Due to Human Error.Employee Was Verbally Counseled on Firewatches & Documentation Was Corrected ML20236G4451998-07-0101 July 1998 Special Rept:On 980618,declared Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Inoperable.Caused by Failure to Meet TS Definition of Channel Calibr.Will Revise Selected Licensee Commitment ML20248K1431998-06-0202 June 1998 Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Shrinkage of Foam & Improper Installation During Construction of Plant.Posted Fire Watches & Repaired Firestop F-AX-348-W-134 ML20247H5351998-04-12012 April 1998 Special Rept:On 980415,missed Insp of Fire Hose Caskets Was Discovered.Caused by Error in Transferring Info from One Procedure to Another.Planned Rev of Applicable Procedure to Include Gasket Insp at Appropriate Frequency ML20216B0211998-04-0606 April 1998 Special Rept:On 980325,determined That Loose Parts Monitoring Sys Being Inoperable for Greater than Thirty Days.Caused by Incorrect Testing.All Channels of Loose Parts Monitoring Sys Tested Utilizing Revised Test Method ML20217K9271998-03-26026 March 1998 Special Rept:On 971229,procedure Step for Closing Safety Injection Pump Cold Leg Injection Isolation Valve Was Inadvertently Skipped.Caused by Injection of Water Into RCS from Rwst.Simplified Procedures & Discussed Event ML20216D5641998-03-0505 March 1998 Special Rept:On 980204,discovered That Fire Detection Panel Was Apparently Not Communicating W/Several Local Fire Detectors.Caused by Faulty Computer Sys Cards.Replaced Four Computer Cards in Sys ML20202C4701998-02-0505 February 1998 Ro:On 971228:Unit 1 Loose Parts Monitoring Sys Channel 6 Was Declared Inoperable Due to Excessive Static on Channel. Caused by Loose Connection.Work Order Has Been Written to Pursue Repairs ML20138E6851997-04-24024 April 1997 Special Rept:On 970318,Unit 1 Loose Parts Monitoring Sys Channel 13 Was Declared Inoperable Due to Sporadic Electical Static.Channel Was Removed from Svc & Entered Into TS Action Item Logbook as Inoperable ML20149M7251997-01-20020 January 1997 Special Rept:On 961209,Unit 1 Loose Parts Monitoring (Lpm) Sys Channel 20 Declared Inoperable Due to No Signal Being Received from Field.Lpm Channel 20 & 22 Operable & Providing Monitoring Coverage for Primary Side of 1D S/G ML20134K4901996-11-0606 November 1996 Special Rept:On 961009,selective Licensee Commitment for Operability of Fire Protection Sprinkler Sys Not Maintained. Continuous Fire Watch Established within One H Following Identification of Incorrect Remedial Action ML20134H1331996-11-0404 November 1996 Special Rept:On 961004,Unit 1B DG Failed Due to Failure of Motor Operated Pot,Electronic & Mechanical Governor,Governor Droop Relay & Mechanical Binding of Fuel Rack Control Linkage.Dg Procedures Will Be Revised ML20113A1801996-06-17017 June 1996 Special Rept:On 960521,declared Detectors A01 for Zone 69 & A04 for Zone 60 Inoperable Because Detectors Effectively Isolated from Area in Intended Protection.Detectors Relocated,Tested & Declared Operable on 960524 ML20100H9801996-02-20020 February 1996 Special Rept:On 960111,Unit 1 Loose Parts Monitoring Channel 21 Declared Inoperable,Due to Spurious,Unexplainable Electronic Bursts.Work Request Initiated to Pursue Corrective Action ML20100H9751996-02-20020 February 1996 Special Rept:On 960111,Unit 2 Loose Parts Monitoring Sys Channel 7 Declared Inoperable,Due to pre-amp Bias Voltage Indicating Zero Volts Twice During Previous Seven Days.Work Request Written to Pursue Corrective Action ML20097F5011996-02-11011 February 1996 Special Rept:On 960102,Unit 2 Loose Parts Monitoring Sys Channel 17 Was Declared Inoperable.Two Other Channels Operable & Providing Coverage Against Loose Parts ML20096E7731996-01-12012 January 1996 Special Rept:On 951214,unit 2 DG Valid Failure Occurred. Caused by Fuel Line Fitting Backing Off from Cylinder Head Connection,Which Resulted in Fuel Oil Leakage.Dg Successfully Started,Run & Declared Operable on 951215 ML20096A8761995-12-18018 December 1995 Special Rept:On 951120,during Periodic Surveillance Testing, Lpms Channel 5 Declared Inoperable.Caused by Erratic Preamp Bias Voltage Indications.Work Request 95048483 Initiated to Perform Corrective Maint During Unit 1 Cycle 9 ML20094Q5811995-11-13013 November 1995 Special Rept:On 951014,auxiliary Bldg Filtered Exhaust Sys Pump Room Heater Declared Inoperable Due to Blown Fuse & Not Restored to Operable Status within 7 Days Per Ts. Technical Investigation Will Be Performed ML20094B8291995-10-25025 October 1995 Special Rept:On 950919,loose Parts Monitoring Sys Channel 1 Declared Inoperable Due to Erratic Preamp Bias Indication. Work Request Written to Investigate & Repair Channel ML20098A4641995-09-19019 September 1995 Special Rept:On 950817,Unit 2 Lpms Channel 12 Was Declared Inoperable Due to Channel Sensor Failing Acceptance Criteria During Performance of PT/O/A4600/03 ML20092G6041995-09-14014 September 1995 Special Rept:On 950815,CNS Unit 1 DG 1A Invalid Failure Occurred Due to Main Bearing High Temp Trip Signal.Caused by Failed Splice Installed in Circuit for RTD 1LDRD5630.New RTD Installed in Main Bearing 5 ML20086H1401995-07-12012 July 1995 Special Rept:On 950615,Channel 4 Was Declared Inoperable Due to Noise Uncharacteristic of Healthy Channel Detected Via Vibration & Loose Parts Monitoring Sys.Corrective Maint Will Be Performed During 1EOC9 Outage ML20086H1431995-07-11011 July 1995 Special Rept:On 950608,Channel 13 Was Declared Inoperable. Trending of Bias Voltage & Background Rms Evaluated to Conclude Channel Was Experiencing Periodic Failures. Corrective Maint Will Be Performed During 1EOC9 Outage ML20086C6441995-06-29029 June 1995 Special Rept:On 950523,Unit 1 Train a Fuel Handling Ventilation Filter Heaters Declared Inoperable.Evaluation Done to Determine Fault ML20085M4061995-06-20020 June 1995 Special Rept:On 950501,lower Rv Tube 4 Was Declared Inoperable ML20084N7271995-05-25025 May 1995 Special Rept:On 950425,valid Failure of DG 1A Occurred. Caused by Jacket Water Thermostatic Control Valve Sticking in Position Which Reduced Engine Cw Flow Through Heat Exchanger.Thermostatic Cv Internals Removed & Replaced ML20082L2711995-04-17017 April 1995 Special Rept:On 950308,Unit 2 Cathodic Protection Sys Was Declared Inoperable & Remained Inoperable Greater than 10 Days ML20081D4851995-03-13013 March 1995 Special Rept:On 950211,actuation of PORV 1NC32B Occurred. Procedure OP/1(2)/A/6100/02 Revised to Require More Emphasis on Monitoring Pressure Indication During Sensitive Evolutions ML20080Q8701995-03-0202 March 1995 Special Rept:On 950202,Unit 1 DG 1B Invalid Failure Due to Overcurrent Breaker Trip During Governor Troubleshooting ML20149H7821994-12-20020 December 1994 Special Rept:On 941129,discovered That Selective Licensee Commitment (SLC) for Visual Insp of Fire Rated Assemblies Exceeded Due to Misinterpretation of Requirements of SLC 16.9-5.Fire Barriers Visually Inspected ML20078R0021994-12-12012 December 1994 Special Rept:On 941103,Channel 3 (Upper Rv a) Declared Inoperable.Caused by Channel Sensor Failure of Acceptance Criteria During Performance of PT/0/A/4600/03.Repair Planned for End of 2EOC7 Outage Due to Containment Entry Required ML20078K7361994-11-17017 November 1994 Special Rept on 941021,DG 1A Invalid Failure Occurred Due to Main Bearing High Temp Trip.Operability Performance Test Successfully Completed & Engine Declared Operable on 941022 ML20149G8041994-11-0101 November 1994 Special Rept:On 940922,CNS,Unit 2 Cathodic Protection Sys Declared Inoperable & Remained Inoperable for Greater than 10 Days.Wo 94080948-01 Initiated to Replace Prepackaged Anode Well 1.WO Scheduled for 941114 ML20076F3191994-10-0404 October 1994 Special Rept:On 940908,valid Failure of D/G 1A Occurred Due to Air Start Valve Sticking Open.Maint Procedure MP/0/A/7650/99 Revised,New Air Roll Criteria Developed & Sixteen Starting Air Valves Replaced ML20072P4251994-08-23023 August 1994 Ro:On 940719,channel 9 (S/G a Channel 2) Declared Inoperable.Work Request Was Generated to Repair Channel During Future Outage of Sufficient Length Since Containment Entry Required for Work ML20072E5961994-08-15015 August 1994 Special Rept:On 940715,inoperability of Unit 2 Vibration & Loose Parts Monitoring System Channel 4 & 6 Occurred.Caused by Leds Not Lighting During Performance of PT/0/B/4600/03. Work Orders 94051250-01 & 94051251-01 Initiated ML20071N7441994-07-28028 July 1994 Special Rept:On 940711,delta-t Channel on Chart Recorder Found to Be out-of-tolerance Due to Drifting of Analog to Digital (A/D) Converter Card.A/D Card Replaced & delta-t Channel Chart Recorder Declared Operable ML20071N8511994-07-28028 July 1994 Special Rept:On 940711,main Steam Relief Valve Exhaust Monitors Declared Inoperable Due to Engineering Calculation Concerns.Engineering Calculation CNC-1229.00-00-0047 re-performed Using EPA-400 Methodology ML20070K0191994-07-18018 July 1994 Special Rept:On 940630,re Inoperability of Main Steam Line Radiation Monitor 2EMF12.Work Request 94026262 Generated to Reattach 2EMF12 to Main Steamline.Work Request Completed on 940701 ML20069H0861994-05-31031 May 1994 Special Rept:On 940501,Unit 2 DG 2A Invalid Failure Occurred Due to Right Bank Turbocharger Vibration Trip.Based on Cooper-Enterprise Recommendations,Procedure Changes Made to Calibr Procedures for All Four DGs ML20065K5011994-04-13013 April 1994 Special Rept:On 940314,invalid Failure of Diesel Generator 1B Occurred Due to Output Tripping During Calibration of Electronic Governor.Dg 1B Started Successfully on 940315 & Declared Operable ML20064G2911994-03-15015 March 1994 Special Rept:On 940203,SG Channels 9 & 11 Declared Inoperable.Channels Failed to Meet Band Limited Rms Acceptance Criteria During Performance of 18 Month Channel Calibr Test.Work Request Written to Repair Channels ML20064G2771994-03-0707 March 1994 Special Rept:On 940125,Channels 6,7 & 10 Were Declared Inoperable.Channels Failed to Meet Acceptance Criteria During Performance of 18 Month Channel Calibr Test.Work Request Written to Repair Channels 1999-09-07
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9561999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20203A2581999-02-0505 February 1999 Safety Evaluation of TR DPC-NE-3002-A,Rev 2, UFSAR Chapter 15 Sys Transient Analysis Methodology. Rept Acceptable. Staff Requests Duke Energy Corp to Publish Accepted Version of TR within 3 Months of Receipt of SE ML20204C9161999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Catawba Nuclear Station,Units 1 & 2 ML20199K8711999-01-13013 January 1999 Inservice Insp Rept for Unit 2 Catawba 1998 Refueling Outage 9 ML20199E3071998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20205E9441998-12-31031 December 1998 1998 10CFR50.59 Rept for Catawba Nuclear Station,Units 1 & 2, Containing Brief Description of Changes,Tests & Experiments,Including Summary of Ses.With ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20203A4101998-12-22022 December 1998 Rev 16 to CNEI-0400-25, Catawba Unit 2 Cycle 10 Colr ML20203A4041998-12-22022 December 1998 Rev 14 to CNEI-0400-24, Catawba Unit 1 Cycle 11 Colr ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196J8351998-12-0808 December 1998 Safety Evaluation Granting Relief Request Re Relief Valves in Diesel Generator Fuel Oil Sys ML20199E3221998-11-30030 November 1998 Revised MOR for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198E3151998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 ML20196C0251998-11-27027 November 1998 SER Accepting Clarification on Calibration Tolerances on Trip Setpoints for Catawba Nuclear Station ML20196A6881998-11-25025 November 1998 Safety Evaluation Granting Relief Request 98-02 Re Limited Exam for Three Welds ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20195E5521998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3261998-10-31031 October 1998 Revised Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154M7661998-10-12012 October 1998 LER 98-S01-00:on 980913,terminated Vendor Employee Entered Protected Area.Caused by Computer Interface Malfunction. Security Retained Vendor Employee Badge to Prevent Further Access & Computer Malfunction Was Repaired.With 1999-09-07
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DUKE POWER COMPANY P.O. Itox 33180 CHAMLOTTE. N.O. 28949 TE LE P,,0NE HAL H. Tt'CKER
..m m (ro4) ara-4aan mm. mm April 21, 1988 f
U. S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, D. C. 20555
Subject:
Catawba Nuclear Station, Unit 1 Docket No. 50-413 Special Report Gentlemen:
Pursuant to Technical Specification 3/4.8.1.1.3, please find attached a Special Report concerning a Diesel Generator 1A valid failure to start on March 22, 1988.
Very truly yours, l2 -
afs.e e.
llal B. Tucker JGT/7/sbn Attachment xc Dr. J. Nelson Grace, Regional Administrator U. S. Nuclear Regulatory Comission Region II 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323 Mr. P. K. Van Doorn NRC Resident Inspector Catawba Nuclear Station
%[ p IUh1 s 6.s
SPECIAL REPORT CATAWBA NUCLEAR STATION, UNIT 1 DIESEL GENERATOR 1 A FAILURE TO START ON MARCH 22, 1988 DUE TO FAULTY PNEUMATIC LOGIC COMPONENTS A Valid Failure of Diesel Generator (D/G) 1A occurred on March 22, 1988, while the Unit was in Mode 1, Power Operation, at 98% power. This was the third Valid Failure within the last 100 Valid Starts of D/G 1A and the second within the last 20 starts. Consequently, the current testing interval is seven days, which is in accordance with Technical Specification Surveillance 4.8.1.1.2.
At 0243 hours0.00281 days <br />0.0675 hours <br />4.017857e-4 weeks <br />9.24615e-5 months <br />, while performing a D/G 1A Operability Periodic Test (PT), D/G 1A was started locally at the D/G 1A control panel (start no. 631). The D/G accelerated to rated speed in the proper time and all enc'ne parameters were normal. After approximately 45 seconds, alarms for low lube oil pressure, low low lube oil pressure, low turbocharger lube oil pressure, high crankcase pressure, high Jacket water temperature, and high vibration were activated. Each alarm, except the low and low low lube oil pressure alarms, c1 cared before the D/G tripped approximately one minute into the run. Because the low low lube oil pressure trip is not bypassed in the emergency mode of operation, the trip was classified as a Valid Failure and the D/G was declared inoperable.
At 0327 hours0.00378 days <br />0.0908 hours <br />5.406746e-4 weeks <br />1.244235e-4 months <br />, a second start attempt (start no. 632) was conducted. This attempt was successful and the D/G 1A PT completed. The D/G was declared operable at 0443 hours0.00513 days <br />0.123 hours <br />7.324735e-4 weeks <br />1.685615e-4 months <br />. The D/G was inoperable for 44 minutes.
At approximately 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br />, and again at 0945 hours0.0109 days <br />0.263 hours <br />0.00156 weeks <br />3.595725e-4 months <br />. Operations personnel started D/G 1A to determine if the problem would recurs it did not. Work Request 227352 OPS was written by Operations personnel for Instrumentation and Electrical (IAE) personnel to troubleshoot the D/G. The D/G was again declared inoperable at 1540 hours0.0178 days <br />0.428 hours <br />0.00255 weeks <br />5.8597e-4 months <br />, while IAE technicians inspected several pneumatic logic control elements. The inspection revealed a slight cut in the diaphragm of the OR 5 logic element. The element was replaced.
Twelve subsequent start attempts were all successful, including a simulated emergency start. The D/G 1A PT was again completed and the D/G declared operable at 0330 hours0.00382 days <br />0.0917 hours <br />5.456349e-4 weeks <br />1.25565e-4 months <br />, on March 23, 1938. The D/G was inoperable for 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, 20 minutes.
On March 29, 1988, Work Request 27412 OPS was written by Operations personnel to i investigate the cause of further spurious alarms on D/G 1A. IAE personnel discovered that a timer which inhibits the actuation of alarms until a 60 second time delay has passed was faulty and allowed alarms to prematurely activate. The timer was replaced. The D/G was inoperable for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, 15 minutes.
On April 12, 1988, while performing D/G 1A Operability Periodic Test, D/G 1A tripped during a start attempt (start no. 652) at 0352 hours0.00407 days <br />0.0978 hours <br />5.820106e-4 weeks <br />1.33936e-4 months <br /> (a Special Report concerning this event will be submitted'on May 12, 1988). Work Request 27513 OPS was written by Operations for IAE to troubleshoot D/G 1A and the D/G was declared inoperable at 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br />. Investigation by IAE revealed that one of the three low low lube oil pressure pneumatic trip valves was faulty. It would periodically fail to close as oil pressure was applied to the valve. This caused
' the D/G to trip, and apparently caused the previous trip on March 23, (as the
, symptoms were identical). The other two trip valves were disassembled and showed signs of corrosion. All three of these trip valves were replaced.
i Three subsequent D/G 1A start attempts were successful and the D/G was declared operable at 0025 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br /> on April 13, 1988. The D/G was inoperable for 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />, 25 minutes. The total time of D/G 1A inoperability during these repairs was 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> and 44 minutes.
In order to minimize the potential for recurrence, Operations personnel have increased the blowdown frequency of the D/G Starting Air System (VG) air compressor aftercoolers from once te twice per shift. This is intended to reduce the amount of carryover moisture entering the air dryers, which is the suspected cause of the valve corrosion problem. Operations personnel have requested the Maintenance group to doubic the frequency of performing Preventive Maintenance (PM) on the VG air dryers, from semi-annually to quarterly.
Operations personnel will initiate work requests to inspect the internals of all pneumatic trip valves on all remaining Unit 1 and Unit 2 D/Gs during scheduled maintenance periods over the next six months.
Performance personnel are planning to increase their frequency of testing Dew Point of the air in the VG receivers from semi-annually to monthly.
Long term solutions to the D/G pneumatic trip problems are currently being investigated by Operations, Projects, and IAE personnel.
Operatiens personnel are pursuing modifications to install additional desiccant filters in each main instrument air line to the D/Gs. They are also pursuing the installation of automatic drains on the D/G Air Compressor aftercoolers.
IAE and Operations personnel are continuing the investigating of the cauce of the corrosion of the low low lube oil pressure trip valves.
Projects and General Office personnel are evaluating alternative electric D/G trip systems for the Emergency Mode trips.
Operations personnel are to submit a Station Problem Report which will further evaluate the replacement of the non-emergency mode trips with an electronic system.
Offsite power and the alternate train D/G were verified to be operable during this period of D/G 1A inoperability, as required by Technical Specifications.
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