ML20149M260

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Forwards Insp Rept 50-298/87-33 on 871222-880131.No Violations or Deviations Noted
ML20149M260
Person / Time
Site: Cooper Entergy icon.png
Issue date: 02/22/1988
From: Callan L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Trevors G
NEBRASKA PUBLIC POWER DISTRICT
Shared Package
ML20149M263 List:
References
IEB-87-002, IEB-87-2, NUDOCS 8802250443
Download: ML20149M260 (2)


See also: IR 05000298/1987033

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FEB 2 21988

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In Reply Refer To:

Docket:

50-298/87-33

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Nebraska Public Power District

ATTN:

George A. Trevors

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Division Manager - Nuclear Support

P.O. Box 499

Columbus, NE

68601

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Gentlemen:

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This-refers to the inspection conducted by Messrs. W. R. tiennett and

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E. A. Plettner of this office during the period December 22, 1987, through

January 31, 1988, of activities authorized by NRC Operating License DPR-46 for

Cooper Nuclear Station and to the discussion of our findings with Mr. G. R. Horn

and other members of your staff at the conclusion of the inspection.

Areas examined during the inspection included operational safety verification,

engineered safety feature walkdown, preparation for refueling, monthly

surveillance and maintenance observations, NRC Bulletin 87-02, radiological

protection, and security. Within these areas, the inspection consisted of

selective examination of procedures and representative records, interviews with

personnel, and observations by the NRC inspectors.

The inspection findings are

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documented in the enclosed inspection report.

We have also identified actions you have taken with regard to previously

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identified inspection findings.

The status of these items is identified in

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paragraph 2 of the enclosed report.

Within the scope of the inspection, no violations or deviations were

identified.

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Should you have any questions concerning this inspection, we will be pleased to

discuss them with you.

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Sincerely,

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Orls!=1 ff;ned By

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L. J. Callan, Director

Reactor Projects Division

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Enclosure:

(see next page)

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Nebraska Public Power District

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Enclosure:

Appendix - NRC Inspection Report

50-298/87-33

cc/w enclosure:

Cooper Nuclear Station

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ATTN:

Guy R. Horn, Division Manager

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of Nuclear Operations

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P.O. Box 98

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Brownville, Nebraska

68321

Kansas Radiation Control Program Director

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Nebraska Radiation Control Program Director

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bcc to DMB (IE01)

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R. D. Martin, RA

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  • Section Chief (ORP/C)
  • Lisa Shea, RM/ALF

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Nebraska Public Power District

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Enclosure:

Appendix - NRC Inspection Report

50-298/87-33

cc/w enclosure:

Cooper Nuclear Station

ATTN: Guy R. Horn, Division Manager

of Nuclear Operations

P.O. Box 98

Brownvi?ie, Nebraska

68321

Kansas R.tdiation Control Program Director

Nebraska Radiation Control Program Director

bcc to DMB (IE01)

bec distrib. by RIV:

  • RRI

R. D. Martin, RA

  • Section Chief (DRP/C)
  • Lisa Shea, RM/ALF

RPSB-DRSS

  • MIS System
  • RIV File
  • Project Engineer, DRP/C
  • RSTS Operator
  • W. Long, NRR Project Manager
  • R. Hall
  • DRS
  • TSS
  • DRP
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Inspection Sunnary

Inspection Conducted December 22, 1987, through January

{ Report 50-298/87-33)

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31, 1988

Areas Inspected:

Routine, unannounced inspection of licensee actions on

previous inspection findings, operational safety verification, engineered

safety feature walkdown, preparation for refueling, monthly surveillance and

maintenance observations, NRC Bulletin 87-02, radiological protection, and

security.

Results: Within the areas inspected, no violations or deviations were

identified.

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OETAILS

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Persons Contacted

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Principal Lictnsee Employeel

  • G. R. Horn, Division Manager of Nuclear Operations
  • D. M. Norvell, Maintenance Manager
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  • G. E. Smith, Quality Assurance Manager

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  • R. Brungardt, Operations Manager
  • L. E. Bray, Regulatory Compliance Specialist

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The NRC inspectors also interviewed additional. licensee employees during

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the inspection pe~iod.

  • Denotes those present during exit interview conducted on' February 1,1988.

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2.

Licensee Action on Previous Inspection Findings

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The following open item was reviewed by the NRC resident inspector.

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(Closed) Open Item 298/8626-01: Deficient As-built Instrument Drawings -

This item discussed deficiencies between 50P 2.2.33. Revision 27

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Appendix A, and Drawings NPPD 1.D.15,1550406, and GE 11506011. Drawing

Change Notice 87620 was completed on October 26, 1987, to correct the

deficiencies. The NRC' resident inspector compared 50P 2.2.33. Revision 31,

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Appendix A, to the above drawings and found no deficiencies.

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This item is closed.

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3.

Operational Safety Verification

The NRC inspectors observed operational activities throughout the

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inspection period. Control room activities and conduct were observed to be

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well controlled.

Proper control room staffing was maintained. Discussions

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with operators determined that they were cognizant of plant status and

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understood the importance of, and reason for, each lit annunciator. The

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NRC inspectors observed selected shift turnover meetings and noted that

information concerning plant status was communicated to the oncoming

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operators.

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On January 11, 1988, a railroad car carrying an empty spent fuel cask

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derailed on Nebraska Public Power District controlled property without

damage to the fuel cask. The NRC inspectors monitored licensee actions to

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return the car to the track and ensure no damage was incurreri by the fuel

cask.

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On January 22, 1988, both steam header pressure transmitters to the Digital

Electro-Hydraulic Control System (DEH) failed causing reactor pressure

control to shift to manual.

Licensed operators in the control room

controlled the evolution utilizing System Operating Procedure (SOP) 2.2.77,

"Turbine Generator," Revision 29, dated December 17, 1987, Abnormal

Operating Procedure (A0P) 2.4.5.2, "Reactor Pressure Control System

Malfunction," Revision 9, dated August 1,1985, and A0P 2.4.9.1.11, "DEH

Pressure Cont oller Output Fails Low," Revision 6, dated July 16, 1987.

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addition, discussions were held among the licensed operators about what

their actions would be in case of further problems with the system.

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blown fuse was discovered to be the cause of the loss of bot 5 pressure

transmitters possibly due to surveillance testing being performed on the

main turbine first stage pressure indicator.

The surveillance was secured,

the fuse replaced, and the DEH system restored to Mode 4 (automatic

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pressure control) after approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> in manual pressure control.

The licensee is still investigating the cause for the blown fuse.

Tours of accessible areas at the facility were conducted to confirm

operability of plant equipment including the fire suppression systems and

other emergency equipment.

The NRC inspectors performed a walkdown of the

High Pressure Coolant Injection (HPCI) System.

Results of this walkdown

are documented in paragraph 4 of this report.

Facility operations were

performed in accordance with the requirements established in the CNS

Operating License and TS.

During a tour on J6nuary 13,1988, the NRC inspectors noted that light was

passing through the seal between the rail and outer airlock door in the

reactor building railroad air lock.

This is a similar condition to that

documented as NRC Violation 50-298/8728-03.

Further investigation revealed

that sealant had been applied between the rail and outer airlock door but

had apparently been insufficient to completely seal thi opening.

Discussion with the licensee identified that corrective action is ongoing

to solve this sealing probitm.

This occurrence will be reviewed during a

subsequent inspection to verify corrective actions for

Violation 50-298/8728-03.

On January 28, 1988, a reactor scram occurred when attempting to restore

"B" recirculation pump to service.

Reactor Recirculation Pump "B" had

earlier been secured due to problems with the reactor recirculation motor

generator (MG). When restoring the recirculation pump to service, the MG

failed to maintain 20 percent speed as designed.

The control room

operators placed the MG set in lockout at approximately 50 percent speed

and were attempting to reduce speed when the recirculation pump discharge

valve started to open as designed.

When the discharge valve opened, a high

flux scram occurred.

All systems appeared to operate normally during the

scram.

Subsequent to the reactor scram, and separate from the scram, a

short to ground on the motor for Residual Heat Removal (RHR) Pump "B" was

discovered after the breaker to the motor tripped.

The SRI monitored

licensee actions subsequent to the scram and RHR pump problems.

No violations or deviations were identified in this area.

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4.

Engineered Safety Feature (ESF) Walkdown

The NRC inspectors performed an independent walkdown of the HPCI System.

The inspection was performed to verify operability, to confirm that

licensee system lineup procedures match plant drawings and the as-built

configuration, and to identify equipment conditions or items that might

degrade system performance.

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In preparation for performing the walkdown of the HPCI System, th. n C

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inspectors conducted a review of, and a comparison between, the following

licensee system checklist and applicable as-built drawings:

System Operating Procedure (SOP) 2.2.33 "High Pressure Coolant

Injection System," Revision 31, dated November 5, 1987; Appendix A,

"Valve Checklist."

As-Built Drawing - Burns & Roe 2041_for HPCI system

As-Built Orawing - Burns & Roe 2044 for HPCI system

As-Built Drawing - HPPD 1550-406 for HPCI system

As-Built Drawing - NPPD I.D.-15 for HPCI system

As-Built Drawing - GE 11506011 for HPCI system

During the inspection minor discrepancies involving missing or broken valve

labels and valve handwheels were noted.

None of the discrepancies

identified affected system operability.

When these discrepancies were

brought to the licensee's attention, the licensee initiated actions to

correct them.

The discrepancies were corrected during this inspection

period.

No violations or deviations were identified in this area.

5.

Preparation For Refueling

The NRC inspectors observed fuel movement from the new fuel boxes to the

spent fuel pool.

The NRC inspectors also reviewed the following t,uclear

performance procedures concerning new fuel movement:

Procedure

Title

Revision

Date

10.21

Special Nuclear Materials

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May 14, 1987

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Control and Accountability

Instructions

10.22

Receiving and Handling

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October 16, 1986

Unirradiated Fuel

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Unirradiated Fuel Inspection

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and Channeling and Control

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Blade Inspection

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The NRC inspectors observed that all personnel performing the fuel movement-

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were aware of procedure requirements and precautions and that the evolution

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was performed in accordance with the applicable procedures.

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inspectors verified new fuel pool fuel assembly locations, accountability

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records, and status board updates.

All personmi engaged in the fuel

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movement were qualified to perform the evolution.

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No violations or deviations were identified in this area.

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Monthly Surveillance Observations-

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The NRC inspectors observed and reviewed the performance of Surveillance

Procedure (SP) 6.3.12.1, "Diesel Generator Operability Test," SP 6.4.8.4.2,

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"Reactor Feed Pump Turbine (RFPT) Backup Oil Pumps and Filter / Cooler

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Differential Pressure Alarm Tests," and Nuclear Performance Evaluation

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Procedure (PEP) 10.9, "Control' Rod Scram Time Evaluation."

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SP 6.3.12.1, "Diesel Generator Operability Test," Revision 22, dated

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November 19, 1987: This surveillance was performed on January 8,

1988, to ensure operability of DG IB prior to performing maintenance

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on DG 1A.

Testing was performed properly and operators were cognizant

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of surveillance requirements.

1.imiting conditions for operation were

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properly entered for the surveillance and subsequent maintenance.

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DG 1A was declared inoperable while inspections for water leakage were

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performed. When maintenance was completed, the operability test for

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DG 1A was completed satisfactorily and DG 1A was declared operable,

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SP 6.4.8.4.2, "RFPT Backup Oil Pumps and Filter / Cooler Differential

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Pressure Alarm Tests," Revision 7, dated October 22, 1987:

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surveillance was performed on January 24, 1988, to ensure proper

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operation of the RFPT backup oil pumps.

The NRC inspectors observed

that the operator performing the test was aware of all precautions

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associated with the test and performed the test in accordance with the

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procedure,

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PEP 10.9, "Control Rod Scram Time Evaluation," Revision 14, dated

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November 6, 1986:

This procedure was performed on January 24, 1988,

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to meet Technical Specification (TS) requirements to insure the

reactor can be made subcritical at a rate fast enough to prevent fuel

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damage during power transients.

This is accomplished by measuring the

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time it takes individual rods to go from the fully withdrawn condition

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to the fully inserted condition when a scram signal is introduced.

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The NRC senior resident inspector observed that the test was performed

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by qualified personnel and performed in accordance with the procedura.

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When the primary means of timing the rod insertion (the Plant

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Management Information System computer) did not function properly, a

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strip chart recorder, as authorized in the procedure, was utilized.

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The NRC senior resident' inspector verified that the strip chart

recorder was in calibration ~and'that operators were familiar with its

usage.

The NRC senior resident inspector verified that a.second

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qualified person observed all rod withdrawals as required by TS and

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the procedure.

All data was properly verified to be acceptable per

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the procedure and TS.

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No violations or deviations were identified in this area.

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Monthly Maintenance Observation

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The NRC inspactors verified that the maintenance activities were conducted

in accordance with approved procedures, regulatory guides, and industry

codes or standards and in conformance with TS.

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The following station' maintenance activities of safety-related systems and

components were observed and reviewed by the NRC inspectors on the

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indicated dates:

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January 6, 1988:

Preventative Maintenance 03910 "Check Coupling and Oil

Levels of Standby Liquid Control Pump"

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January 8, 1988:

Inspection of 1A Diesel for water leaks

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No violations or deviations were identified in this area.

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NRC Bulletin 87-02

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The purpose of this bulletin was to request that licensees review their

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receipt inspection programs for fasteners and to' independently determine,

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through testing, whether fasteners in stores at the licensee facilities met

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required mechanical and chemical specifications.

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On December 4,1987, the NRC senior resident inspector assisted the

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licensee in selecting 20 fasteners and 20 corresponding nuts.

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samples were then sent to Metals Engineering and Testing Laboratories of

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Phoenix, Arizona, where chemical, mechanical, and hardness testing as

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required by the bulletin was performed.

The satisfactory results of this

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tetting, as well as other information required by the bulletin, were

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transmitted by NPPD to the NRC via letter NLS 8800014 on January 11, 1988.

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The NRC senior resident inspector reviewed the response to the bulletin and

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found no discrepancies.

In addition, the NRC senior resident inspector's

review of Plant Services Procedures 1.5, "Warehouse Receiving," Revision 7,

dated October 15, 1987; and 1.8, "Warehouse Issue and Return," Revision 3,

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dated August 13, 1987; as well as discussions with licensee personnel,

confirmed the licensee's response to the bulletin.

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This bulletin and associated Temporary Instruction 2500/26 are closed.

(SIMS issue number BL-87-02)

No violations or deviations were identified in this area.

9.

Radiological Protection Observations

The NRC inspectors verified that selected activities of the licensee's

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radiological protection program were implemented in conformance with

facility policies, procedures, and regulatory requirements.

Radiation work

permits contained appropriate information to ensure that work could be

performed in a safe and controlled manner.

Personnel in radiation

controlled areas were wearing the required personnel monitoring equipment

and protective clothing.

Radiation and/or contaminated areas were properly

posted and controlled based on the activity levels within the area.

Radiation monitors were utilized to check for contamination.

No violations or deviations were identified in this area.

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Security

The NRC inspectors observed security personnel perform their duties of

vehicle, personnel, and package search.

Vehicles were properly authorized

and escorted or controlled within the protected area (PA).

The PA barrier

had adequate illumination and the isolation zones were free of transient

material.

Compensatory measures were implemented in a timely manner when

equipment failed.

These observations verified that the physical security

plan was being implemented in accordance with the requirements established

in the CNS Operating License.

The licensee implemented a cipher pad system for personnel entry into the

PA.

The NRC senior resident inspector monitored the implementation of

these new procedures.

No violations or deviations were identified in this area.

11.

Exit Interviews

An exit interview was conducted on February 1, 1988, with licensee

representatives (identified in paragraph 1).

During this interview, the

NRC senior resident inspector reviewed the scope and findings of the

inspection.