ML20149M171

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Ack Receipt of 850726 Response to 850628 Notice of Violation Re Insp Repts 50-369/85-06 & 50-370/85-06.Evaluations & Conclusions Re Notice of Violation Encl.Nrc Concludes That Violation Occurred as Originally Stated
ML20149M171
Person / Time
Site: McGuire, Mcguire  
Issue date: 02/19/1988
From: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Tucker H
DUKE POWER CO.
References
NUDOCS 8802250384
Download: ML20149M171 (4)


See also: IR 05000369/1985006

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FEB 19 USS

Docket Nos. 50-369, 50-370

License Nos. NPF-9, NPF-17

Duke Power Company

ATTN: Mr. H. B. Tucker, Vice President

Nuclear Production Department

422 South Church Street

Charlotte, NC 28242

Gentlemen:

SUBJECT:

NRC INSPECTION REPORT NOS. 50-369/85-06 AND 50-370/85-06

Thank you for your response of July 26, 1985, to our Notice of Violation issued

on June 28, 1985, for

violation 369/85-06-04 and 370/85-06-03.

Due to an

administrative oversight, we did not respond earlier to your rec;uest regarding

the noted violations.

We are hereby documenting our actions relative to your

request.

In your response you deny the violation.

You feel the violation raised two

concerns, lack of notification to plant operations personnel of a potential

backleakage problem past auxiliary feedwater check valves and the failure to

take prompt corrective action for the improper installation of the turbine

driven auxiliary feedwater pump discharge stop check valve, which you

adequately addressed.

After careful consideration of the bases for your denial of the violation, we

have concluded, for the reasons presented in the enclosure to the letter, that

the violation occurred as stated in the Notice of Violation.

As discussed in

your response, we understand the stop check valves have been replaced on both

Units 1 ai 2 and you have stated that you are in full compliance.

We will

examine the implementation of your corrective action during future inspections.

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We appreciate your cooperation in this matter.

Sincerely,

M

J. Nelson Grace

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Regional Administratce

Enclosure:

Evaluations and Conclusions

cc w/ encl:

T. L. McConnell, Station Manager

Senior Resident inspector - Catawba

bec w/ encl:

(See page 2)

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ENCLOSURE

EVALUATION AND CONCLUSIONS

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On June 28, 1985, a Notice of Violation was issued for violation 369/85-06-04,

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370/85-06-03 identified during a routine NRC inspection.

Duke Power Company

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responded to the Notice on July 26, 1985.

Duke denied the violation on the

basis that they promptly identified and corrected the problem associated with

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the auxiliary feedwater pump suction piping overpressurization.

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Restatement of Violation

10 CFR 50, Appendix B, Criterion XVI as implemented by Duke Power Compcny (DPC)

Topical Report, Quality Assurance Program Duke-1-A, Amendment 7. Section

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17.2.16 requires that conditions advorse to quality be promptly identified and

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corrected and that the identification of the significant condition, the cause

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of the condition and the corrective action shall be documented and reported to

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appropriate levels of management.

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Contrary to the above, conditions adverse to quality were not promptly

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identified and corrected, as detailed below:

An occurrence of August ?5,1981, on Unit 1 as reported in Licensee Event

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Report 369/81-136, caused overpret.surization of the suction side of the turbine

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driven auxiliary feedwater pump.

Identified as contributing to this problem

was the stop check valve on the outlet of the pump being mounted in a

horizontal position which prevents the closure of this valve to be aided by

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gravity as designed.

Furthermore, on November 11, 1981, Westinghouse notified

DPC of a potential problem concerning the design of the audliary feedwater

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pump discharge piping valve arrangement such that damage could occur which

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would compromise the safety-related function of the auxiliary feedwater system.

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Westinghouse in this letter, recomrrended system modifications and an operating

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procedures amendment to detect and correct this problem,

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No actions were taken on these items identified above until September 5,1984, when

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NSM 1-1705 for Unit 1 and NSM 2-0550 for Unit 2 were generated to replace the

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existing stop check valves with a different design valve, and NSM's 1-1706 and

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2-0551 were generated to install a temperature monitoring system as reconnended

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by Westinghouse.

As of March 12, 1985, NSM 1-1706 and NSM-20551 were in the

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process of being installed and NSM 1-1705 and NSM 2-0550 were scheduled for

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outages in 1986 due to material delivery,

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Sunwary of Licensee's Response

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The licensee contends that following the August 25, 1981 overpressurization

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appropriate corrective action was taken.

The licensee feels two concerns were

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raised by the violation,

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Enclosure

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The first concern was a lack of notification to plant operations personnel of a

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potential problem with backleakage past auxiliary feedwater check valves.

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backleakage pertains to a waterhammer resulting from check valve leakage.

The

licensee states that plant operations personnel were not notified in 1981 of

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potential waterhanner problems because a Duke Power evaluation found this

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particular situation did not exist at McGuire Nuclear Station.

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The second concern involved a failure to take prompt corrective action for the

improper installation of the tur"ine driven auxiliary feedwater pump (TDAFWP)

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discharge stop check valve.

On August 25, 1981, the suction piping of the

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TDAFWP was overpressurized.

The licensee felt their solution to install a

relief valve in the suction piping and ensure that the mini-flow line to the

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upper surge tank would always be open when the pump was not operating was

appropriate considering the knowledge of the potential problems at the time.

Since the 1981 solution, the licensee states recurrence of the TOAFWP suction

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overpressurization and industry studies have made it more apparent that the

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addition of relief valves may not provide a total solution and that more

insurance against loss of auxiliary feedwater was required.

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As discussed in the licensee's response, as of July 26, 1985, further

corrective steps have been taken.

Temperature indication on discharge piping

was installed and the stop check valves were replaced on both McGuire units.

NRC Evaluation

The NRC has reviewed the licensee's response and does not agree that the

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licensee's corrective action was prompt or adequate.

The licensee's investi-

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gation following the August 25, 1981 overpressurization event discovered the

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stop check valve (ICA-22) in the discharge line of the Unit 1 TDAFWP was

improperly installed.

The identification of the improperly installed valve

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should have been sufficient to initiate replacement of the valves on both

units.

Also following a January 1984 industry report and a review by the

licensee a DPC memorandum dated June 24, 1984, identified the discharge stop

check valves as being improperly installed on both units and should be

corrected.

On August 26 and again on August 30, 1984, the TDAFWP suction

piping was overpressurized due to backleakage.

Contributing to this problem

was the stop check valve on the outlet of the pump being improperly installed.

It was not until September 5,1984, that Nuclear Station Modifications (NSM)

were initiated by the licensee to replace the valves.

NRC Conclusion

From the evaluation given above the NRC concludes that conditions adverse to

quality were not promptly identified and corrected and the violation occurred

as stated.