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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217C1051999-10-0808 October 1999 Forwards Amend 153 to License DPR-3 & Safety Evaluation. Amend Revises TS Section 6.0,Administrative Controls,By Deleting TS Sections 6.2.2.f Which Contains Limits on Working Hours of Plant Staff ML20212J2231999-10-0101 October 1999 Forwards Copy of Environ Assessment & Fonsi Re 990317 Application for Amend to Revise TS Section 6.0 by Deleting TS Section 6.2.2.f Which Contains Limits on Working Hours of Plant Staff ML20211J5001999-08-31031 August 1999 Forwards Proposed Rev 29 to Yankee Decomissioning QA Program, for NRC Info & Approval.Yaec Requests That Rev 29, Dtd May 1999 & Originally Transmitted in Be Withdrawn from Further Consideration by NRC Staff ML20211J2711999-08-27027 August 1999 Forwards Amend 152 to License DPR-3 & Safety Evaluation. Amend in Response to Application Dated 990324,deletes License Condition 2.C (10) Which States: Licensee Shall Maintain FFD Program IAW Requirements of 10CFR26 ML20216F1891999-08-26026 August 1999 Forwards Copies of Maine Yankee & Yankee Rowe Refs Listed, Supporting Industry Position That Branch Technical Position Asb 9-2 Methodology over-estimates Spent Fuel Decay Heat ML20210S0621999-08-10010 August 1999 Forwards semi-annual fitness-for-duty Program Performance Data for six-month Period of 990101-990630,IAW 10CFR26.71(d) ML20210R1421999-08-0404 August 1999 Forwards Insp Rept 50-029/99-02 on 990411-0714.One Severity Level 4 Violation Occurred,Being Treated as NCV ML20210F3691999-07-21021 July 1999 Submits Response to NRC Request for Clarification of Certain Details of Yaec Proposed Mods to Yankee Nuclear Power Station Defueled TS ML20209D4881999-07-0909 July 1999 Forwards Rev 29 to Decommissioning QA Program, for Info & NRC Approval,Iaw 10CFR50.54(a)(3).Attachment a Provides Listing of Changes,But Does Not Discuss All Refomatting, Grammatical,Editorial or Typographical Changes ML20209C3271999-07-0101 July 1999 Forwards Rev 2 to Security Training & Qualification Plan.Rev Withheld ML20209C3151999-07-0101 July 1999 Forwards Rev 9 to Security Plan,Reflecting Plant Decommissioning Activities & Continues to Provide Protection Against Radiological Sabotage.Rev Withheld ML20209D1611999-06-28028 June 1999 Forwards UFSAR for Ynps.Updated Ynps FSAR Is Being Submitted Biennially,Iaw Commitment in Ltr Dtd 950614.Document Reflects Changes Made to Ynps as of 981231,unless Otherwise Noted ML20195H1741999-06-15015 June 1999 Forwards Original & Copy of Request for Approval of Certain Indirect & Direct Transfer of License & Ownership Interests of Montaup Electric Co (Montaup) with Respect to Nuclear Facilities Described as Listed ML20195D6781999-06-0707 June 1999 Forwards Original & Two Copies of New England Coalition on Nuclear Pollution & Consolidated Intervenor Opposition to Yankee Atomic Electric Co Motion to Terminate,As Required by Rule for Filing ML20207E6301999-06-0101 June 1999 Informs of Relocation of Yaec Corporate Ofcs,Effective 990501.New Address Submitted.All Formal NRC Correspondence to Util Should Be Directed to Duke Engineering & Svcs, Marlborough,Ma ML20207D7991999-05-29029 May 1999 Forwards Original & Two Copies of Ltr to ASLB Chairman in Matter of Yankee Nuclear Power Station Proceeding.With Certificate of Svc ML20207D8181999-05-29029 May 1999 Requests That Board Convey to Panel That within Period of Time Authorized by NRC Regulations Author Intends to File, on Behalf of Intervenors,Responsive Pleading to Yaec Pending Motion to Withdraw in Ref Matter.With Certificate of Svc ML20207D8131999-05-27027 May 1999 Discusses Reorganization of Nrr,Effective 990328.Forwards Organizational Chart ML20195B3491999-05-25025 May 1999 Submits Withdrawal of Proposed License Amend to Approve Plant Termination Plan.New Application Will Be Submitted in Future ML20206Q1881999-05-17017 May 1999 Forwards for Filing,Necnp Request for Permission to File Contentions & Contentions on Inadequacy of NRC Staff 990412 Environ Assessment & Finding of No Significant Impact of Approval of Util Termination Plan.With Certificate of Svc ML20206H8701999-05-0505 May 1999 Informs That DB Katz Unable to Locate Copy of Attachments to Which Zobler Referred to in Response to Block Ltr.Requests Info on How Panel Will View Receipt of Ea.With Certificate of Svc ML20206R3221999-05-0505 May 1999 Forwards Insp Rept 50-029/99-01 on 990101-0411.No Violations Noted.Activities at Rowe Facility Generally Characterized by safety-conscious Operations to Maintain Spent Nuclear Fuel & Careful Radiological Controls to Workers ML20206D1801999-04-30030 April 1999 Forwards Citizens Awareness Network First Set of Interrogatories,Requests to Produce & Certificate of Svc. Requests Any Objections Be Submitted Withing Five Days of Filing Receipt.Without Encls.Related Correspondence BVY-99-031, Forwards Ynps Annual Radiological Environ Operating Rept for Jan-Dec 1998, IAW Plant Defueled TS 6.8.2.a1999-04-26026 April 1999 Forwards Ynps Annual Radiological Environ Operating Rept for Jan-Dec 1998, IAW Plant Defueled TS 6.8.2.a ML20206B6641999-04-24024 April 1999 Requests Board Take Action to Remedy NRC Failure to Comply with Board Request & NRC Counsel Representation to Board in Relation to That Request Re Serving EA Upon Petitioners Per Request of Board.With Certificate of Svc ML20206C0801999-04-23023 April 1999 Requests That Change Proposed in Request for Transfer of Administrative Requirements for Ynps Defueled TS to Plant Decommissioning QA Program Be Withdrawn ML20206A6871999-04-22022 April 1999 Informs of Completion of Review of Re Nepco in Capacity as Minority Shareholder in Vermont Yankee Nuclear Power Corp,Yaec,Myap & Connecticut Yankee Atomic Power Co ML20205S0131999-04-17017 April 1999 Forwards Original & Two Conformed Copies of Necnp First Set of Interrogatories & Requests to Produce for Filing in Matter Re Yaec License Termination Plan.Related Correspondence ML20205L0701999-04-13013 April 1999 Grants Voluntary Extension to Allow CAN to Effectively Participate in Hearing Process (ASLBP 98-736-01-LA-R).With Certificate of Svc.Served on 990413 ML20205P9091999-04-13013 April 1999 Informs That Item Intended to Be Attached to 990412 Filing (Motion for Leave to Reply(Reconsideration of Portion of of Prehearing Conference Order)) Inadvertently Overlooked. Section 4, Final Radiation Survey Plan Encl ML20205P2191999-04-12012 April 1999 Informs That Mj Watkins Has Been Appointed to Position as Yankee Rowe Decommissioning Licensing Manager,Effective 990412.Individual Will Serve as Primary Point of Contact for All Info Flow Between NRC & Yaec ML20205K9361999-04-0808 April 1999 Informs That J Block,T Dignan & D Katz Came to Agreement to Extend Discovery in Yankee Rowe License Termination Plan Hearing Process (ASLBP 98-736-01-LA-R) by 1 Wk from 990611 Until 990618 ML20205G7791999-03-31031 March 1999 Provides Info Re Status of Decommissioning Funding for Yankee Power Station,Per 10CFR50.75(f) ML20206A6951999-03-29029 March 1999 Request Confirmation That No NRC Action or Approval,Required Relative to Proposed Change in Upstream Economic Ownership of New England Power Co,Minority Shareholder in Vermont Yankee Nuclear Power Corp,Yaec,Myap & Connecticut Yankee ML20205F6331999-03-29029 March 1999 Forwards Effluent & Waste Disposal Semi-Annual Rept, for Third & Fourth Quarters of 1998.Rept Summarizes Quantities & Estimated Dose Commitments of Radioactive Liquid & Gaseous Effluents Released During 1998 ML20205N1531999-03-24024 March 1999 Submits Request to Elminate fitness-for-duty Requirement from Plant.Proposed Change Has Been Reviewed by PORC & Nuclear Safety Audit & Review Committee ML20204E5051999-03-17017 March 1999 Requests NRC Review & Approval of Listed Mods to App a of Plant Possession Only License DPR-3 ML20207F8791999-03-0505 March 1999 Forwards Amend 151 to License DPR-3 & Safety Evaluation. Amend Revises Pol by Changing Submittal Interval for Radioactive Effluent Repts from Semiannual to Annual ML20207H8981999-03-0303 March 1999 Responds to Concerns Raised in Petitions to Intervene Filed with NRC by Necnp on 980224 & Citizens Awareness Network on 980226.Petitioners Requested Hearing on NRC Staff Consideration of License Termination Plan for Yankee Plant ML20203G2391999-02-12012 February 1999 Forwards Corrected Index Page for Amend 150 Issued to License DPR-3 on 990203 ML20202H5741999-02-0303 February 1999 Forwards Amend 150 to License DPR-3 & Safety Evaluation. Amend Revises Possession Only License Through Three Changes to TS ML20202F1921999-01-28028 January 1999 Forwards Copy of EA & Fonsi Re Application for Amend to Yaec Pol for Ynps Dtd 980820.Proposed Amend Would Revise Pol Through Listed Changes to TS ML20202E9401999-01-25025 January 1999 Submits Correction to Encl Request for Leave to Make Oral Appearance Statement, .Date of Conference & Desire to Make Oral Appearance Were Inadvertently & Incorrectly Entered on 990127 Instead of 990126 ML20199L1811999-01-22022 January 1999 Requests Opportunity for Representative of EPA to Make Oral Limited Appearance Statement & Submit Written Comments During 990126 Prehearing Conference Re Licensee Termination Plan ML20199K9151999-01-21021 January 1999 Requests Leave to Make Oral Limited Appearance Statement at 990127 Prehearing Conference Re License Termination Plan,Per 981130 Order Concerning Change in Filing Schedules & Date of Prehearing Conference ML20198N1691998-12-30030 December 1998 Forwards Motion for Leave to Participate in Matter of Yankee Atomic Electric Co License Termination Plan ML20198S1661998-12-17017 December 1998 Final Response to FOIA Request for Documents.Records Encl & Identified in App C & D.App E Records Withheld in Part & App F Records Withheld in Entirety (Ref FOIA Exemption 5) & App G Records Withheld in Entirety (Ref FOIA Exemptions 4 & 5) ML20154P9431998-10-16016 October 1998 Forwards Rev 28 to Yankee Atomic Electric Co Decommissioning QA Program. Program Name Changed Due to Status of Plant.Plant in Final Stages of Decommissioning ML20154F0861998-10-0101 October 1998 Forwards Insp Rept 50-029/98-03 on 980601-0731.No Violations Noted ML20153D7271998-09-23023 September 1998 Informs of Changes Made in Personnel Staff at Yankee Nuclear Power Station 1999-08-04
[Table view] Category:NRC TO UTILITY
MONTHYEARML20058G4961990-11-0808 November 1990 Advises That Maint Activity for Control Rod Relatch Witnessed by NRC on 901104.Activity Successful ML20197H6971990-11-0606 November 1990 Forwards Resident Safety Insp Rept 50-029/90-16 on 900821- 1001 & Notice of Violation ML20058F2151990-11-0202 November 1990 Forwards Safety Evaluation Accepting Util Responses to Generic Ltr 83-28,Item 1.2, Post-Trip Review - Data & Info Capability ML20058D3501990-10-30030 October 1990 Forwards Safety Insp Rept 50-029/90-17 on 900730-0803. Unresolved Items Noted ML20058D2411990-10-26026 October 1990 Requests Written Policies & Procedures Required by 10CFR26.20 Providing Background for fitness-for-duty Insp ML20058C3901990-10-22022 October 1990 Forwards Amend 137 to License DPR-3 & Safety Evaluation. Amend Modifies Surveillance Requirement 4.1.3.4 ML20062B8901990-10-19019 October 1990 Forwards one-time Exemption from 10CFR55.59(c)(3)(i)(A)-(L) Re Annual Operator Simulator Training ML20058D2811990-10-19019 October 1990 Discusses Violations Noted in Insp Rept 50-029/90-14 & Forwards Notice of Violation ML20062B8671990-10-12012 October 1990 Extends Invitation to Attend 910220-21 Util Symposium/ Workshop in King of Prussia,Pa Re Engineering Role in Plant. Interest to Participate,Intent to Attend & Approx Number of Representatives to Attend Requested by 901115 ML20059P0161990-10-12012 October 1990 Advises That 900920 Response to Generic Ltr 90-03, Relaxation of Staff Position in Generic Ltr 83-28,Item 2.2 Part 2, 'Vendor Interface for Safety-Related Components,' Acceptable ML20059N4801990-10-0303 October 1990 Forwards Maint Team Insp Rept 50-029/90-81 on 900709-20 & 0806-10.Weaknesses & Unresolved Item Noted ML20059M0511990-09-26026 September 1990 Forwards Corrected Pages to Amend 136 to License DPR-3 ML20059M5301990-09-25025 September 1990 Forwards Safety Insp Rept 50-029/90-12 on 900619-0820. Violations Noted But Not Cited ML20059J2411990-09-12012 September 1990 Advises That 900828 Revised Diesel Generator Test Plan for Qualification & Preoperational Testing Acceptable.Tech Spec Changes to Enable Util Achieve Credit for Increased Generator Capacity Will Be Considered When Proposed ML20059H5671990-09-12012 September 1990 Advises That NRC Terminated Review of YAEC-1710, Yankee Nuclear Power Station Pilot Evaluation Rept for Plant License Renewal, Per Util 900716 Request.Resolution of Issues Will Occur as Part of Review of Application ML20059K7111990-09-10010 September 1990 Forwards Insp Rept 50-029/90-14 on 900802-27.Enforcement Conference Scheduled for 900921 ML20059H0601990-09-0707 September 1990 Discusses Unescorted Access to Licensee Facilities & fitness-for-duty Program,Per .Nrc Regulations Do Not Prohibit Licensee from Accepting Access Authorization Program of Another Licensee,Contractor or Vendor ML20059G2231990-09-0606 September 1990 Forwards Amend 135 to License DPR-3 & Safety Evaluation. Amend Modifies Tech Spec Surveillance Requirement 4.5.2a to Change ECCS Pump Surveillance Frequency from Monthly to Quarterly ML20059E3011990-08-31031 August 1990 Forwards Safety Assessment of Yae 1735, Reactor Pressure... Evaluation Rept for Yankee Nuclear Power Station, Submitted w/900705 Ltr.Nrc Calculations Recognizing Uncertainties Conclude That Plant May Operate Until Feb 1992 ML20058P0701990-08-0909 August 1990 Forwards Insp Rept 50-029/90-11 on 900619-22.No Violations Noted ML20058N0681990-08-0606 August 1990 Discusses Licensee Engineering Initiatives.Cooperative Effort Would Promote Efficiency & Enhance Effectiveness of Nuclear Power Plant Activities ML20056A9341990-08-0303 August 1990 Forwards Radiological Safety Insp Rept 50-029/90-13 on 900709-13.One Noncited Violation Noted ML20058L5981990-08-0202 August 1990 Forwards Amend 134 to License DPR-3 & Safety Evaluation. Amend Incorporates NRC Guidance in Generic Ltr 88-17 to Facility Tech Specs.Three New Tech Specs Added & Change Also Addresses Low Temp Overpressurization ML20058L5331990-08-0202 August 1990 Forwards Rept from NRC Consultant Gr Odette Re Yankee Rowe Reactor Vessel Integrity.Response Requested by 900806 ML20058L0241990-08-0202 August 1990 Forwards Amend 133 to License DPR-3 & Safety Evaluation. Amend Incorporates Wording from Std Westinghouse Tech Specs Into Util Limiting Condition for Operation Specs 3.10.3 & 3.10.4 ML20055J4861990-07-31031 July 1990 Requests Performance of PTS Probablistic Analysis Using Broad Range of Matl Properties Re Reactor Pressure Vessel Evaluation Rept ML20055J2651990-07-27027 July 1990 Forwards Request for Addl Info Re Yankee Rowe Severe Accident Closure Submittal.Questions Concern Individual Plant Exam,Containment Performance Improvement Program & Accident Mgt.Response Requested within 1 Month ML20058L4761990-07-25025 July 1990 Forwards Exam Rept 50-029/90-06OL on 900619-21 IR 05000029/19890801990-07-25025 July 1990 Ack Receipt of Re Violations Noted in Insp Rept 50-029/89-80 ML20055G7991990-07-16016 July 1990 Forwards Safety Insp Rept 50-029/90-09 on 900515-0618.No Violations Noted ML20055C8531990-06-18018 June 1990 Forwards Amend 132 to License DPR-3 & Safety Evaluation. Amend Changes Title of Technical Svc Supervisor & Establishes New Positions Entitled Maint Support Supervisor & Operations Support Supervisor ML20059M9131990-06-13013 June 1990 Forwards NRC Performance Indicators for First Quarter 1990. W/O Encl ML20055C2961990-02-19019 February 1990 Forwards Safeguards Insp Rept 50-029/90-05 on 900207-09.No Violations Noted ML20248H7331989-10-0303 October 1989 Forwards Safety Evaluation Re Procedures Generation Program for Plant.Program Incomplete in Some of Its Content & Should Be Revised.Revision Need Not Be Submitted to NRC But Retained for Subsequent Review ML20247H4021989-09-0909 September 1989 Formalizes Requests Made in Conversation Between M St Lauren,R Clark & G Maret Re Planned Insp of Plant Emergency Operating Procedures During 891106-17 ML20247F0841989-09-0707 September 1989 Forwards Amend 124 to License DPR-3 & Safety Evaluation. Amend Moves Onsite & Facility Organizational Charts from Section 6.0 of Tech Specs to Section 401 of FSAR ML20246P6861989-09-0101 September 1989 Forwards Notice of Withdrawal of 890321 & 0414 Applications for Amend to License DPR-3,revising Tech Specs Re Snubber Listing,Per Generic Ltr 88-12.List of Snubbers Should Be Included in FSAR or Other Document IR 05000029/19890141989-08-31031 August 1989 Forwards Insp Repts 50-029/89-14 & 50-271/89-10 on 890717-21.No Violations Noted ML20246Q0121989-08-31031 August 1989 Forwards Insp Repts 50-029/89-14 & 50-271/89-10 on 890717-21.No Violations Noted ML20246L6361989-08-31031 August 1989 Forwards Safety Insp Rept 50-029/89-11 on 890626-0731.No Violations Noted.Tmi Action Plan Commitments Re Main Steam Line Radiation Monitor Should Have Received More Attention. Addl Info Re Four Unresolved Items Requested ML20247E6531989-08-31031 August 1989 Forwards Amend 123 to License DPR-3 & Safety Evaluation. Amend Removes Description of High Pressurizer Water Level in Section 2 Re Bases on Page B2-4 of Tech Specs ML20246L0551989-08-25025 August 1989 Forwards Safeguards Insp Rept 50-029/89-13 on 890724-28.No Violations Noted ML20246G1741989-08-23023 August 1989 Forwards Requalification Exam Rept 50-029/89-03OL.Licensee Requalification Program Assigned Overall Program Rating of Satisfactory ML20246H7301989-08-18018 August 1989 Clarifies NRC Position Re Definition of Extremity for Purposes of Setting Occupational Exposure Limits.Request That Util Ensure Procedures Incorporate Applicable Dose Limits of 10CFR20 ML20246C7181989-08-15015 August 1989 Forwards Safety Insp Rept 50-029/89-15 on 890731-0803.No Violations Noted ML20245H4521989-08-11011 August 1989 Responds to 890712 Application for Amend to License DPR-3, Revising Tech Specs Re Main Steam Line Monitors & Primary Vent Stack Noble Gas Monitor.Verification Requested That Util Withdraw 890712 Application,Per 890810 Meeting 1990-09-07
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217C1051999-10-0808 October 1999 Forwards Amend 153 to License DPR-3 & Safety Evaluation. Amend Revises TS Section 6.0,Administrative Controls,By Deleting TS Sections 6.2.2.f Which Contains Limits on Working Hours of Plant Staff ML20212J2231999-10-0101 October 1999 Forwards Copy of Environ Assessment & Fonsi Re 990317 Application for Amend to Revise TS Section 6.0 by Deleting TS Section 6.2.2.f Which Contains Limits on Working Hours of Plant Staff ML20211J2711999-08-27027 August 1999 Forwards Amend 152 to License DPR-3 & Safety Evaluation. Amend in Response to Application Dated 990324,deletes License Condition 2.C (10) Which States: Licensee Shall Maintain FFD Program IAW Requirements of 10CFR26 ML20210R1421999-08-0404 August 1999 Forwards Insp Rept 50-029/99-02 on 990411-0714.One Severity Level 4 Violation Occurred,Being Treated as NCV ML20207D8131999-05-27027 May 1999 Discusses Reorganization of Nrr,Effective 990328.Forwards Organizational Chart ML20206R3221999-05-0505 May 1999 Forwards Insp Rept 50-029/99-01 on 990101-0411.No Violations Noted.Activities at Rowe Facility Generally Characterized by safety-conscious Operations to Maintain Spent Nuclear Fuel & Careful Radiological Controls to Workers ML20206A6871999-04-22022 April 1999 Informs of Completion of Review of Re Nepco in Capacity as Minority Shareholder in Vermont Yankee Nuclear Power Corp,Yaec,Myap & Connecticut Yankee Atomic Power Co ML20205L0701999-04-13013 April 1999 Grants Voluntary Extension to Allow CAN to Effectively Participate in Hearing Process (ASLBP 98-736-01-LA-R).With Certificate of Svc.Served on 990413 ML20207F8791999-03-0505 March 1999 Forwards Amend 151 to License DPR-3 & Safety Evaluation. Amend Revises Pol by Changing Submittal Interval for Radioactive Effluent Repts from Semiannual to Annual ML20207H8981999-03-0303 March 1999 Responds to Concerns Raised in Petitions to Intervene Filed with NRC by Necnp on 980224 & Citizens Awareness Network on 980226.Petitioners Requested Hearing on NRC Staff Consideration of License Termination Plan for Yankee Plant ML20203G2391999-02-12012 February 1999 Forwards Corrected Index Page for Amend 150 Issued to License DPR-3 on 990203 ML20202H5741999-02-0303 February 1999 Forwards Amend 150 to License DPR-3 & Safety Evaluation. Amend Revises Possession Only License Through Three Changes to TS ML20202F1921999-01-28028 January 1999 Forwards Copy of EA & Fonsi Re Application for Amend to Yaec Pol for Ynps Dtd 980820.Proposed Amend Would Revise Pol Through Listed Changes to TS ML20198S1661998-12-17017 December 1998 Final Response to FOIA Request for Documents.Records Encl & Identified in App C & D.App E Records Withheld in Part & App F Records Withheld in Entirety (Ref FOIA Exemption 5) & App G Records Withheld in Entirety (Ref FOIA Exemptions 4 & 5) ML20154F0861998-10-0101 October 1998 Forwards Insp Rept 50-029/98-03 on 980601-0731.No Violations Noted ML20237F1281998-08-27027 August 1998 First Partial Response to FOIA Request for Documents. Forwards App a Records Already Available in Pdr.App B Records Being Made Available in PDR ML20236F3391998-06-24024 June 1998 Forwards Combined Insp Repts 50-029/98-01 & 50-029/98-02 on 980101-0331.No Violations Noted ML20249A7841998-06-17017 June 1998 Forwards Amend 149 to License DPR-3 & Safety Evaluation. Amend Revises TS Sections Pertaining to Minimum Water Cover Over Sf,Crane Travel Over Sf & Related Bases ML20248M0111998-06-0909 June 1998 Informs That Review of QA Program (YOQAP-1-A),rev 28,has Been Terminated & TAC M99265 Closed,Per 980414 Withdrawal ML20217C2501998-03-18018 March 1998 Requests Info to Provide NRC W/Adequate Assurance That Ynps Operated IAW Provisions of Yaec QAP Description Following Sale of Yankee Nuclear Svcs Div to Duke Engineering & Svcs ML20216G1311998-03-17017 March 1998 Forwards NRC Staff Response to Requests for Hearing, Filed on 980316 Re Yankee Atomic Electric Co Proceeding Per 980317 Telcon.Name Inadvertently Omitted from Service List. Related Correspondence ML20217Q4251998-03-11011 March 1998 Responds to Addressed to Chairman SA Jackson Forwarding Hearing Request of Franklin Regional Planning Board (Frpb).Aslb Established to Consider Hearing Requests Including That of Frpb.Served on 980311 IA-98-175, Submits Request for Addl Info Re Spent Fuel Pit License Amend Request Concerning Defueled TSs of Plant1998-03-0202 March 1998 Submits Request for Addl Info Re Spent Fuel Pit License Amend Request Concerning Defueled TSs of Plant ML20237F2221998-03-0202 March 1998 Submits Request for Addl Info Re Spent Fuel Pit License Amend Request Concerning Defueled TSs of Plant ML20216F8551998-02-0505 February 1998 Forwards Copy of Transcript of 980113 Public Meeting in Shelburne,Ma.Meeting Sponsored by NRC in Order to Inform Public About Regulations Re License Termination Process for Permanently Shutdown Nuclear Power Plant ML20202E5031997-11-28028 November 1997 Ack Receipt of License Termination Plan,Dtd 970515.NRC Placed Notice of Receipt in Fr 62FR43559.Application for Amend That Complies W/Appropriate Sections of Commission Regulations Should Be Filed by Licensee ML20202F4041997-11-26026 November 1997 Responds to ,Supplemented by Facsimile Addressed to J Callan,Executive Director for Operations, Requesting Hearing on Proposed Action by NRC Licensee. Informs That Request Denied by NRC for Listed Reasons ML20217C4401997-09-23023 September 1997 Forwards Insp Rept 50-029/97-02 on 970401-0814.No Violations Noted ML20217B0511997-09-0909 September 1997 Requests Addl Info to Complete Review of Licensee License Termination Plan ML20217K7561997-08-0808 August 1997 Ack Receipt of License Termination Plan & Forwards Notice of Receipt of Availability for Comment ML20148P5161997-06-30030 June 1997 Second Partial Response to FOIA Request for Documents.App B Records Being Made Available in PDR ML20141J4461997-05-16016 May 1997 Forwards Insp Rept 50-029/97-01 on 970301-31.No Violations Noted ML20138H2951997-05-0202 May 1997 Responds to Offering NRC Staff Opportunity to Participate in 970620 Meeting.Informs That NRC Staff Will Not Participate in Meeting ML20148B2201997-05-0101 May 1997 Discusses Expressing Concerns Re Security Program at Facility Being Maintained Under License from Nrc. NRC Will Conduct Evaluation of Program Including Security Risks Involved W/Configuration If License Requests Change ML20134B5141997-01-24024 January 1997 Forwards Insp Rept 50-029/96-04 on 961121.No Violations Noted ML20129G9121996-10-28028 October 1996 Forwards Notice of Completion of Hearing Process Re Approval of Decommissioning Plan.Commission Denied Petition for Review by Hearing Re Approval of Decommissioning Plan. Plan Is Considered PSDAR ML20129C9211996-10-16016 October 1996 Forwards Insp Rept 50-029/96-03 on 960829.No Violations Noted ML20237F1771995-08-10010 August 1995 Informs That NRC Would Like to Conduct Site Release Research at Yankee Rowe Reactor Site ML20149H0801994-11-0404 November 1994 Ack Receipt of Providing Comments on Plant Decommissioning Plan.Nrc Currently Reviewing Plan & Comments Will Be Addressed During Review CLI-94-03, Forwards Decision CLI-94-03 in Response to Formal Petition Re Decommissioning Activities at Plant.Commission Ruled That Component Removal Program Does Not Involve Any Activities Requiring Adjudicatory Hearing & Denies Request1994-03-31031 March 1994 Forwards Decision CLI-94-03 in Response to Formal Petition Re Decommissioning Activities at Plant.Commission Ruled That Component Removal Program Does Not Involve Any Activities Requiring Adjudicatory Hearing & Denies Request ML20059K1851994-01-26026 January 1994 Discusses 930804 Telcon & Subsequent Correspondence Phone Calls Re NRC Commitment to Respond to Concerns Raised by Citizens Awareness Network.Nrc Response Will Be Delayed Beyond Early January & Response Provided within Two Months ML20059C7701993-12-29029 December 1993 Discusses to J Taylor of Allegations Against NRC Re Early Component Removal Project.Informs Licensee of No Objection Re Removal of Four Sg,Pressurizer & Portions of Intervals from Plant & Site.W/Encl ML20059D6291993-12-29029 December 1993 Forwards Insp Rept 50-029/93-07 on 930826-27,0923 & 1115-18 & Notice of Violation ML20059A6911993-12-22022 December 1993 Forwards Which Requested Info Re Potential Radiation Doses from Plant Reactor Vessel Internals Proposed for Removal Under Util Component Removal Program ML20059J7591993-12-20020 December 1993 Responds to to Chairman Selin Re Component Removal Project at Plant & NRC Provisions to Obtain Public Comments on Project ML20058P2741993-12-0808 December 1993 Advises That Rev 2 to Defueled Security Plan Consistent W/ Provisions of 10CFR50.54(p) & Acceptable for Inclusion Into Plan ML20058E3461993-11-19019 November 1993 Forwards Granted Exemption from Requirements of 10CFR50.54 to Util in Response to Licensee Request of 930924 ML20058D6241993-11-19019 November 1993 Forwards Approved Partial Exemption Request from Training rule,10CFR50.120,in Response to Util ML20059C8101993-11-18018 November 1993 Responds to Re Request for Hearing on Early Removal Project at Plant.Requests Specific Info Re Early Component Removal Project ML20058B6331993-11-15015 November 1993 Forwards Physical Security Insp Rept 50-029/93-08 on 931018-19.No Safety Concerns or Violations Noted 1999-08-04
[Table view] |
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1 Gentlemen , 1
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- The enclosed Directorate of Regulatory Operations Bulletin No. 73-6, l d " Inadvertent Criticality in a Boiling Water Reactor" has been sent for completion of the requested action to utilities that are presently licensed
- (or that will be licensed in the near future) to operate boiling water reactors.
This bulletin is being sent to you to provide you with information f j that was reported
- to the AEC by the Vermont Yankee Nuclear Power Corporation, concerning an inadvertent criticality incident that was experienced at their Vermont Yankee facility. This bulletin is provided only for your h@ ,
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RO Bulletin No. 73-6 3 November 26, 1973 2
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INADVERTENT CRITICALITY IN A BOILING WATER REACTOR
$ We recently received an abnormal occurrence report from the Vermont
! Yankee Nuclear Power Corporation relating to an iriadvertent criticality
'j incident that was experienced at their Vermont Yankee facility. A copy e of the abnormal occurrence report is attached to this Bulletin to provide j , you with pertinent details of this event.
a i At the time of the inadvertent criticality incident, the reactor vessel i and primary containment heads were removed, the refueling cavity above 4 the reactor vessel was flooded, control rod friction tests were in 3 progress, the rod worth minimizer was bypassed, and core verification j- had been in progress. As a result of the incident, no measurable '
radioactivity was released, no fuel damage resulted and no personnel
. , exposures were experienced. The incident is currently under review and evaluation by the Regulatory Staff.
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- Action requested by this bulletin is contained in Section A.
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3 A. Action Requested by Licensees In light of this occurrence.you are requested to take the following actions. Upon completion of these actions you are requested to inform this office in writing, within 45 days of the date of this letter, of the status of each item identified in each paragraph and subparagraph listed below: ,
- 1. Procedural Review
- a. Control Rod Drive Operating and Testing Procedures (1) Conduct a review of your control rod drive t.cerating '
and testing procedures to determine that approved procedures
. exist for all operations and tests.
t (2) Verify that appropriate prerequisites are included in the procedures to require testing of associated interlock and protective features before control rod testing is ,
.f permitted. :
(3) Assure that prerequisites and detailed instructions are !
provided that demonstrate compliance with technical spe- !
cification requirements and design bases. ;
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- b. Bypass Installation Procedures (Jumpers or Lifting of Leads)
Assure that existing bypass installation procedures have been ,
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conservatively reviewed for technical adequacy and for adminis-strative controls.
- c. Radiation Protection Procedures Assure that procedures for access control and personnel accountability in areas subject to accidents are current.
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- d. Shif t Transition Procedure (Turnover) l l
Assure that complete and detailed procedures are in effect l
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- that provide instructions for a proper and conservative turnover of shift responsibilities. Such procedures must include requirements for commun,1cating the status of all safety related equipment and conditions.
p l 2. Management Controls Assure that your management controls that are in effect provide E
for qualified technical and administrative reviews and approvals of temporary circuitry changes and temporary off-normal plant conditions. This review should assure that the responsibilities and requirements associated with the review and' approval, installation, verification, removal, and subsequent testing.of temporary circuitry changes and temporary off-normal plant conditions are clearly delineated in station procedures, are understood by the station staff, and are being properly implemented.
- 3. Licensed Operator Performance Assure that management provides the necessary opporturities and time so that operators are adequately trained to carry out
- their assigned responsibilities. In particular, confirm that shift crew me=hers are provided special training for safety related activities that are infrequent, complex, or have unusual safety significance.
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If you have any questions concerning this request, please contact this oL'fice. ,
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Attachment:
Vermont Yankee A0 No. 73 Letter dated November 14, 1973'to the Directorate of Licensing, USAEC, Washington, D.C.
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- i RUTLAND, URMUNT 03701 REPLY TOs VYV-3071 p, o, oox is7 VERNON. VERMONT OS354 November 14, 1973 f t
1 Director -
Directorate of Licensing a.__..
United States Atomic Energy Commission .
j h ashington, D.C. 20545 '
REFERENCE:
Operating License DPR-28 Docket No. 50-1:1 Abnormal Occurrence No. A0-73-31 Gentlemen:
As defined in Section 6.7.B.1 of the Technical Specificaties for the Vermont Yankee Nuclear Power Station, we are reporting the following l Abnormal Occurrence as A0-73-31.
On November 7, 1973, at 2101, while the plant was in a shutdown
- condition and while the reo,uired Control Rod Friction testing was being perforned on control, rod 26-23, a reactor scram occurred initiated by a high-high flux signal from the Intermediate Range Neutron Monitoring j System.
An immediate investigation revealed that rod 30-23 was in the fully withdrawn position while rod 26-23 was being withdrawn' for its friction test., This situation was a result of inadequate impicmentation of
.,dministrative or procedural controls and constituted a violation of Cection 1. A.S of the Technical Specifications.
l Section 14.5.3.2 of the Ver.aont Yankee FSAR deals with control rod withdrawal crrors when the reactor is at poh'cr levels below the pcwcr L
range. The most severo case occurs when the reactor is just critical ~
at room temperature and. an out-of-sequence rod is continuously withdrawn.
The resultt of these analyses indicate that no fuel damage will occur due to the .od withdrawal. ,
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'Ihc station h'ad been in a planned shutdown condition since September 28, 1973, in order to perform core reconstitution and .
interconnection of the Advanced Off-Gas System. On November 7, 1973, work had progressed to the point where final core loading ,
had been completed.- At that point, it became desirable to perform ;
- final' core verification concurrent with control rod timing and. '
{. friction tests. In order to accomodato both requirements, it was .
p necessary to install jumpers to the refuel interlock portion of the p Reactor Manual Contro1' System in. order to allow traversing of the
[ television camera mounted on the fuel grapple while performing control rod friction and timing tests. Although the intent of installing 5 .
the jumpers was reasonabic and proper, the ensuing impicmontation of this program went beyond the scope of original intent, 'Ihe reasons for this were the, inadequacy of interdepartmen,tal communications; in <
addition, certain procedures demonstrated inadequacies, specifically AP 504, Lifted Leads Log, OP 408, Control Itod Drive' System, Further, .
the control rod friction testing was being performed in accordance with ,
a Startup Test Procedure; an approved operating procedure did not exist.
The result of the jumper installation _.was a condition of interlocks which did not prevent withdrawal of nore than one contrp1 rod at a time. ,
, The operating personnel were not adequately informed of the jumpored interlock status; control rod testing was resumed concurrent with core verification. As control rod testing progressed, rod 30-23 was inadvertantly Icft in the fully withdrawn position. After core verification ;
was c,onipleted, and since the reactor operator was not cognizant that control ~
rod 30-23 was still withdrawn, an adjacent lateral control rod 26-23 was solccted and its continuous withdrawal begun in preparation for the ' friction ,
test. Detween notch position 20 and 26, the operator noticed rapid source range monitor response, lic immediately initiated control rod insertion. ,
At thp timo n. full rod scrau was initiated by the intermediate range '
monitor high-high flux signals. It was later demonstrated that control rod 30-23 digital position display was functioning properly. The reactor ,
operator could not explain his failure to observe the indication of control rod 30-23 being fully withdrawn. -
The immediate action of the. Shift Supervisor on duty was to notify higher' plant management and to determine if personnel were on the refuchng floor during the incident and to request dosincter readings of all personnel at that location on the conservativo assumption that a criticality may have i occurred. Five personnel'wcre on the refueling floor at the tiac in areas not adjacent to.the open vessel. The maximum dosimeter rending of the !
' personnel involved was 25 mr; however, this total was accumplated over a '
five hour work period and not attributabic to this -incident alone. It was ,
also verified that the local area nonitors, the continuous air monitor on ;
the refueling floor, as well a . thc. I:cactor Cuilding Ventilation lixhaust ;
monitors: showed no inercased level of radiation. -
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. Directorate of Licensing 3y November 14, 1973 -
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Following the arrival on site of the . Assistant Pla'nt Superintendent and the Reactor Engineer, further evaluation determined that the scope
- of installed jumpers was beyond'the original intent. 'lhe jumpers werc l
removed and it was decided to perform a subcriticality test on each of the two involved control rods which verified their proper effectiveness.
Based upon the above evaluations, it was determined that no fuel failurc had occurred and no radiation prob 1cm existed. 'lho installed interlock l -
jumpers were removed and a verification test conducted to determine that
) the rod block interlock was restored.
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On Novenber 8,1973, consultation with off-site higher management and engineering personnel resulted in the removal of the involved fuel
- assemblics .from the core for sipping and visual inspection. No evidence b of Icakage or visual degradation was observed. The following is a listing
(. 'of. the assemblics examined and their location:
Assembly Number Core Location -
\T 164* 27-22
\T 171* 29-22
\T 167 27-24 Vr 175 ~
29-24 17 049 31-32
- In addition, a two rod critical test was conducted utilizing control rods 30-23 and 26-23. As a result of this test, it was detornined that with control rod 30-23 in the fully withdrawn position, criticality was achieved when control rod 26-23 was withdrawn to notch 16.
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- The filn had;;cs assigned to parsonnel on the refueling floor at the timo M the incident ucre sent out for processing. The results of the-badge bearing neutron sensing indicated a total of 50 mr beta-gamma and zero neutron exposure. This total badge exposure was accuwilated over a p
j two day work period. The results of the remaining four badges indicated L that two badges measured 20 nr beta-gamma and two badges measured 0 mr beta-gamma. ,
Subsequent calculations by General Electric Co. verified criticality n
at not ch 16 on rod 26-23 with rod 30-23 fully withdrawn. l'orther calculation
' by Cencral F.lectric Co., determined that with rod 30-23 fully withdrawn and rod 26-23 at notch 26, the excess reactivity was 0.67% AK, and had rod 26-23 been fully withdraun, the exccr.s reactivity would have been 0.970 AK.
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- These assemblics were visually inspected. .
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.y VERMONT YANKEC NUCLEAR POWCR CORPORAT!b
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Hovember 14, 1973 Page 4 .
General Electric personnel with recognized competency in the area'of core hinctics, and in particular control rod drop accidents, uncontrolled withdrawal incidents, etc., did a qualitative evaluation of what transpired based on the above statistical information. An estimate based upon many previous calculations of a similar nature, was that' the bounding results were as follows. The peak fuel center line temperature would have increased no more than 500*F and the peak clad tenperature would have
. increased no more than 50*F from the starting conditions. Therefore, the fuel center line temperature was no higher than 585 F an.d the peak clad temperature was no higher than 135*F.
Plant management has discussed at length with all involved personnel the significance of this incident and stressed the areas of inadequate personnel performance. Further, a review has been ma'de of the past and present performance of the employees directly involved in this incident.
,This assessment has determined that these employees are capabic, sincere, and conscientous and that every reasonabic assurance exists that they are adequately qualificd in all respects to continue in their present assigned job responsibilities.
Upon completion of an indepth evaluation of the total inci. dent and the varicas now apparent inadequacies, it is concludcnl that no singular outstanding area was predominant.-
The Plant Operations Review Committee (PORC), uct to review the
, incident and made the following recommendations and/or conclusions:
- 1. The original intent of the jumpers was reasonabic; however, the final condition obtained was improper and the applied jumpers should have been removed immediately following the
, completion of core verification. ,
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- 2. The results obtained from the fuel assemblics sipped and inspected on November 8,1973, showed no observed indications which would preclude plant startup.
The Plant Operations Review Committee. questioned whether adequate sensitivity to sipping still existed considering the clapsed shutdown time and recomucnded taking two known Icahers previous]y removed during this shutdown and sipping to deteruine if adequate sensitivi ty still existed. On November 11, 1973, two fue) assemblics were sipped in-an attempt to prove 1 131 and 1 132 sensitivity. The positive results obtained verify the adequacy of sipping sensitivitics observed on November 8,1973.
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L 3. Suberitical testing results of the two involved control rods g: and the management evaluation of the plant condition on L
" Noveber 7, '1973, were deemed sufficient to permit further gn control rod friction testing following the incident.
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- 4. Administrative Procedure AP 504 " Lifted Lead Log"' was not g4l adhered to. Jumpor installation was not recorded in the di
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g All plant procedures re'lating to control rod movement shall be fp modified to reficct interlock requirements imposed by the reactor modo switch position. .
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g; 6. Specific operating procedures addressing control rod friction and M
+ ' settling test s shall. be developed.
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The present AP 504, Lifted Leads Log procedure, is inadequate NN and a PORC sub-committee has been appointed to review and/or revisc the current procedure.
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e Until the above appointed P. ORC sub-committe.e performs its . task, W no installation of jumpers or lifted Icads shall be performed on the circuitry associated with the Reactor Protection System, the Primary Containment Isolation System, any ECC System, the Reacter Manual Control System and any refuci ' interlock until approved by PORC. .
, 9. No further two (2) rod critical . testing shall.be performed on side by side rods. .
- 10. The following ' items contributed to the incident; er
- a. A lack of definition on the interfacing of responsibilitics on an interdepartmental leycl.
- b. Failure by plant supervision to exercise rigorous skepticism l
relative to abnormal or inadequate plant conditions that are' encoMntered.
- c. Operator crror.
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NUCLEAR POWER CORPORATI Directorate of Licensing- ,.
November'14, 1973 * '
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At the request of the Manager of Operations, the nuclear Safety 7 ,
.Aud t and Review Conunittec met in. a special meeting on November 14, i
1973, to review the -incident. The NSAR returned the following
- - conclusions: -
- y. 1. No unreviewed safety question was involved. .
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- 2. The health and safety of the public and plant personnel '
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.t not impaired. -
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[ 3. Thero' is no -undue risk to tho' health and safety of the public y' if the plant'is started up and operated in accord with the 1 proposed schedule.
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?- . Sincerely; A -
p YERMONT YANKEE NUCLEAR P0h'ER CORPORATION ,
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. B.tl. Riley Plant Superintendent Bh'R/h'FC/kbd .
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