LER-1978-006, Forwards LER 78-006/03L-0 |
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esuun SACRAMENTO MUNICIPAL UTILITY DISTRICT O 6201 S Street, Box 15830, Sacramento, California 95813; (916) 45b3211 July 5, 1978
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in Nuclear Regulatory Commission pg C
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ATTN:
Mr. R.11. Engelken
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NRC Operations Offlee, Region V gj w
Q 1990 N. Califernia Boulevard
. Walnut Creek Plaza, Suite 202 xrw U1' Da kSi5 Diij Walnut Creek, California 94596
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Re: Operating License DPR-54 j
g Docket No. 50-312 g
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Reportable Occurrence 78-6
Dear Mr. Engelken:
In accordance with Technical Specifications for Rancho Seco Nuclear Generating Station, Section 6.9.4.2 h, the Sacramento Municipal Utility District is hereby submitting a thirty day report of Reportable Occurrence 78-6.
During the latter part of May, 1978, leak rate calculations performed per SP 200.02, the Daily Instrument Surveillance and SP 207.04, Evaluating RCS Leakage, although within the 1 gpm unidentified leak rate per Technical Specifications Section 3.1.6, showed an increase. This was attributed to known Icakaga from the pressurizer c1cetromatic relief, PV-21511, its assoc-lated block valve HV-21505, and one of the pressurizer code safety valves, PV-21506.
On Sunday, May 21, 1978, a thorough Reactor Building inspection was made looking for leaks. This reinforced previous findings that the major source of leakage was from the above mentioned valves.
PV-21506 was deter-mined to have a ruptured bellows, HV-21505 was determined to be Icaking past its seat, and PV-21511 appeared to be leaking past its pilot valve. A rep-resentative from the Dresser Valve and Instrument Division of Dresser Indust-ries was present to observe the leaking valves.
Based on the inspection and discussion'with the Dresser Industries representative, it was determined that there was no safety problem relating to the leaking valves.
Since the leakage was identifie.d, the majority of the leakage was to the pressurizer relief tank, and the valve leakage was determined not to pre-1 sent a safety problem, Technical Specifications Section 3.1.6.2 was not con-sidered applicable.
An engineering evaluation of the leakage from the valves, which was not j
going to the pressurizer relief tcnk but rather to the building atmosphere, i
and then showing up in the Reactor Building Drain accumulation tank was done.
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$00k;6 g llO fl AN ILlCTRtC SYSTEf4 S E RVIN G MDRE THAN 600,000 IN THE HLART C A l l f 0 F: h I A
b' R.11. Engelken July 5, 1978 Utilizing this evaluation and review by the Plant Review Committee, Meeting No. 502, a conservatively low 0.56 gpm value was assigned to this now considered identified leakage.
This value was used in subsequent leak rate calculations per SP 207.04.
Basically this allowed reindexing the leak rate procedure to show any new leak from the RCS.
It was also decided that if the leak rate calculation exceeded the 1 gpm unidentified leak rate w511e utilizing the 0.56 gpm value as identified, another inspection and engineering evaluation would be necessary.
On June 11, 1978, the calculated leak rate per SP 207.04 exceeded the 1 gpm unidentified.
Follow-up calculations utilizing the same procedure indicated leak rates varying from 1.1 gpm to 1.7 gpm.
On June 12, 1978, within twenty-four hours of the first unacceptable leak rate, the reactor was shut down per Technical Specifications Section 3.1.6.2.
Rather than conduct another engineering evaluation and determine a new value for the identified leakage f rom the volves, it was decided that repair and replace-ment of the problem valves was a more logical course of action. The known leaking code safety valve PV-21506 and the electromatic relief valve PV-21511 were replaced. The electromatic relief block valve HV-21505 was reworked (disc / seat lapped) and the other code safety valve PV-21507 was completely rebuilt and all new internal parts installed. The replacement valves were identical to the originals.
The three relief valves were bench-tested prior to installation and hydro-assist tested with the system pressure at 1500 PSI.
The three relief valves were all manufactured by Dresser Valve and Instrument Division of Dresser Industries (PV-21506 and PV-21507 being Consolidated Closed Bonnet Maxiflow Safety Valves, 3 inch, and PV-21511 being a Consolidated Elec tromatic Relief Valve, 2-1/2 inches). The block valve HV-21505 is a 2-1/2 inch gate valve manufactured by Velan Valve Corporation.
Respectfully submitted, A
Y. J. Sbttimoe J
Assistant General Manager and Chief Engineer JJM:Hil:jlk Attachment es: Director, MIPC (3)
Director, IE (30)
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| 05000312/LER-1978-001-04, /04T-0:on 780109,plant Liquid Effluent Ph Levels Exceeded Tech Spec 8.5 Limit.Ph Sensor Setpoint Raised in Summer to Folson South Canal Ph Level & Not Reset When Ph Level Dropped,Eliminating Automatic Diversion Feature | /04T-0:on 780109,plant Liquid Effluent Ph Levels Exceeded Tech Spec 8.5 Limit.Ph Sensor Setpoint Raised in Summer to Folson South Canal Ph Level & Not Reset When Ph Level Dropped,Eliminating Automatic Diversion Feature | | | 05000312/LER-1978-001, Responds to NRC Expressing Concern That 780320 Transient,Reported as LER 78-1,could Have Led to Results as Serious as Tmi.Operator Recognized That once-through Steam Generators Were Dry & Therefore Admitted Main Feedwater | Responds to NRC Expressing Concern That 780320 Transient,Reported as LER 78-1,could Have Led to Results as Serious as Tmi.Operator Recognized That once-through Steam Generators Were Dry & Therefore Admitted Main Feedwater | | | 05000312/LER-1978-001-01, /01T-0:on 780320,non-nuclear Instrumentation Dc Power Short Resulted in Reactor Trip & RCS Cooldown in Excess of Tech Spec Figure 3.1.2-2 Limits.Caused by Operator Changing Lightbulb.Conditions Imposed for Return to Power | /01T-0:on 780320,non-nuclear Instrumentation Dc Power Short Resulted in Reactor Trip & RCS Cooldown in Excess of Tech Spec Figure 3.1.2-2 Limits.Caused by Operator Changing Lightbulb.Conditions Imposed for Return to Power | | | 05000312/LER-1978-002-03, /03L-0:on 780228,safety Sys Hydraulic Snubbers 25 & 26 Found Low on Fluid During Visual Insp.No Leakage Found. Cause Not Determined.Snubbers Refilled & Surveillance Interval Reduced to Six Months | /03L-0:on 780228,safety Sys Hydraulic Snubbers 25 & 26 Found Low on Fluid During Visual Insp.No Leakage Found. Cause Not Determined.Snubbers Refilled & Surveillance Interval Reduced to Six Months | | | 05000312/LER-1978-002-04, /04T-0:on 780414,hypochlorite Spilled & Flushed Into Drain Sys During Hypochlorite Chemical Tank Filling, Causing Chlorine Levels to Exceed Limits.Fill Line Will Be Capped Prior to Removal & Spills Will Not Be Flushed | /04T-0:on 780414,hypochlorite Spilled & Flushed Into Drain Sys During Hypochlorite Chemical Tank Filling, Causing Chlorine Levels to Exceed Limits.Fill Line Will Be Capped Prior to Removal & Spills Will Not Be Flushed | | | 05000312/LER-1978-002, Forwards LER 78-002/03L-0 | Forwards LER 78-002/03L-0 | | | 05000312/LER-1978-003-03, /03L-1 on 780710:Maintenance on Safety Sys Hydraulic Snubber Previously Found to Have Low Fluid Accumulator Level Revealed 2 Deteriorated o-rings Made W Polyurethene Seals Instead of ethylene-propylene Seals | /03L-1 on 780710:Maintenance on Safety Sys Hydraulic Snubber Previously Found to Have Low Fluid Accumulator Level Revealed 2 Deteriorated o-rings Made W Polyurethene Seals Instead of ethylene-propylene Seals | | | 05000312/LER-1978-003-04, /04T-0:on 780913,during Steady State Operation, Dissolved Oxygen Concentration Downstream of Confluence of Hadselville & Clay Creek Was Less than Minimum of 5mg/liter Typical of Stagnant Water.Location Is Beyond Util Propert | /04T-0:on 780913,during Steady State Operation, Dissolved Oxygen Concentration Downstream of Confluence of Hadselville & Clay Creek Was Less than Minimum of 5mg/liter Typical of Stagnant Water.Location Is Beyond Util Property | | | 05000312/LER-1978-003, Forwards LER 78-003/04T-0 | Forwards LER 78-003/04T-0 | | | 05000312/LER-1978-004, Forwards LER 78-004/01T | Forwards LER 78-004/01T | | | 05000312/LER-1978-004-01, /01T-1:on 780414,small Break Analysis Determined to Be at Rc Pump Discharge.Analysis Identified & Evaluated Solutions.Facility Has Incorporated Procedural Changes & Initiated Design Changes | /01T-1:on 780414,small Break Analysis Determined to Be at Rc Pump Discharge.Analysis Identified & Evaluated Solutions.Facility Has Incorporated Procedural Changes & Initiated Design Changes | | | 05000312/LER-1978-005-01, /01T-0:on 780509,four Main Steam Code Safety Valves Found Improperly Set in Nonconservative Direction. Caused by Procedural Inadequacy.Maint Procedure Included Hydroset Curve for One Type Orifice.Procedure Revised | /01T-0:on 780509,four Main Steam Code Safety Valves Found Improperly Set in Nonconservative Direction. Caused by Procedural Inadequacy.Maint Procedure Included Hydroset Curve for One Type Orifice.Procedure Revised | | | 05000312/LER-1978-006, Forwards LER 78-006/03L-0 | Forwards LER 78-006/03L-0 | | | 05000312/LER-1978-006-03, /03L-0:on 780611,during Normal Operation,Increased Leakage Noticed,Between 1.1-1.7 Gallons/Min.Caused by Leaking Pressure Safety Valves & Block Valve on Electromatic Relief Valve.Valves Replaced or Reworked | /03L-0:on 780611,during Normal Operation,Increased Leakage Noticed,Between 1.1-1.7 Gallons/Min.Caused by Leaking Pressure Safety Valves & Block Valve on Electromatic Relief Valve.Valves Replaced or Reworked | | | 05000312/LER-1978-007-03, /03L-0:on 780622,frequent Makeup Tank Level Changes Observed.Caused by Excessive Leakage from B Decay Heat Removal Sys Pump Seal.Pump Valved Out & Sys a Continued Operation.Leaking Seal Replaced | /03L-0:on 780622,frequent Makeup Tank Level Changes Observed.Caused by Excessive Leakage from B Decay Heat Removal Sys Pump Seal.Pump Valved Out & Sys a Continued Operation.Leaking Seal Replaced | | | 05000312/LER-1978-008, Forwards LER 78-008/02T-0 | Forwards LER 78-008/02T-0 | | | 05000312/LER-1978-008-02, /02T-0:on 780804,analysis Showed Atypical Weld Filler Wire W/High Silicon & Low Nickel Contents in Archive Weldments.Wire Mixed by Supplier W/Shipment of Mn-Mo-Ni Filler Wire.Caused by Inadequate QA | /02T-0:on 780804,analysis Showed Atypical Weld Filler Wire W/High Silicon & Low Nickel Contents in Archive Weldments.Wire Mixed by Supplier W/Shipment of Mn-Mo-Ni Filler Wire.Caused by Inadequate QA | | | 05000312/LER-1978-009-03, /03L-0:on 780913,diesel Driven Fire Pump P-996 Tripped on Overspeed During test.Engine-to-pump Coupling Bolts Were Discovered to Be Sheared,Probably Due to Overtorquing.Bolts Were Replaced,Torque Values Verified | /03L-0:on 780913,diesel Driven Fire Pump P-996 Tripped on Overspeed During test.Engine-to-pump Coupling Bolts Were Discovered to Be Sheared,Probably Due to Overtorquing.Bolts Were Replaced,Torque Values Verified | | | 05000312/LER-1978-009, Forwards LER 78-009/03L-0 | Forwards LER 78-009/03L-0 | | | 05000312/LER-1978-010, Forwards LER 78-010/01T-0 | Forwards LER 78-010/01T-0 | | | 05000312/LER-1978-010-01, /01T-0 on 780914:During Normal Oper It Was Found That Fire Hydrant 3 Hose Cabinet Had Not Been Relocated W/Hydrant.Upon Discovery of Discrepancy Hose Cabinet Was Relocated | /01T-0 on 780914:During Normal Oper It Was Found That Fire Hydrant 3 Hose Cabinet Had Not Been Relocated W/Hydrant.Upon Discovery of Discrepancy Hose Cabinet Was Relocated | | | 05000312/LER-1978-011-01, /01T-0:on 780914,required Continual Fire Watch Erroneously Terminated.Caused by Shift Personnel Misunderstanding.Personnel Instructed | /01T-0:on 780914,required Continual Fire Watch Erroneously Terminated.Caused by Shift Personnel Misunderstanding.Personnel Instructed | | | 05000312/LER-1978-011, Forwards LER 78-011/01T-0 | Forwards LER 78-011/01T-0 | | | 05000312/LER-1978-012-03, /03L-0:on 780927,header Failed to Discharge During Routine Testing of CO2 Sys.Caused by Defective Microswitch on Solenoid Which Operates Pilot Valve Integral W/Main Isolation Valve Controller | /03L-0:on 780927,header Failed to Discharge During Routine Testing of CO2 Sys.Caused by Defective Microswitch on Solenoid Which Operates Pilot Valve Integral W/Main Isolation Valve Controller | | | 05000312/LER-1978-012, Forwards LER 78-012/03L-0 | Forwards LER 78-012/03L-0 | | | 05000312/LER-1978-013, Forwards LER 78-013/03L-0 | Forwards LER 78-013/03L-0 | | | 05000312/LER-1978-013-03, /03L-0:on 780925,HPI Loop a Flow Transmitter FT-23807 Found Inoperable During Surveillance Procedure 200.14.Caused by Broken Bellows in Flow Transmitter.Failed Bellows Replaced | /03L-0:on 780925,HPI Loop a Flow Transmitter FT-23807 Found Inoperable During Surveillance Procedure 200.14.Caused by Broken Bellows in Flow Transmitter.Failed Bellows Replaced | | | 05000312/LER-1978-015-01, /01T-0:on 781120,failure of 9 Bergen-Patterson Snubbers.Seven of 9 Failures Caused by Abusive Handling During Reinstallation Following 1977 Testing.Other Two Failures Isolated Cases.Failed Units Repaired | /01T-0:on 781120,failure of 9 Bergen-Patterson Snubbers.Seven of 9 Failures Caused by Abusive Handling During Reinstallation Following 1977 Testing.Other Two Failures Isolated Cases.Failed Units Repaired | | | 05000312/LER-1978-015, Forwrds LER 78-015/01T-0 | Forwrds LER 78-015/01T-0 | | | 05000312/LER-1978-016, Forwards LER 78-016/01T-0 | Forwards LER 78-016/01T-0 | | | 05000312/LER-1978-016-01, /01T-0:on 781024,operability of a Diesel Generator Lost Due to Failure of Primary Fuses on the Voltage Regulators Control Power Circuit.Fuses Replaced,A Generator Tested Then Returned to Svc | /01T-0:on 781024,operability of a Diesel Generator Lost Due to Failure of Primary Fuses on the Voltage Regulators Control Power Circuit.Fuses Replaced,A Generator Tested Then Returned to Svc | | | 05000312/LER-1978-017, Forwards LER 78-017/03L-0 | Forwards LER 78-017/03L-0 | | | 05000312/LER-1978-017-03, /03L-0:on 781215,during Refueling Shutdown, Blowdown Heat Transfer Pump Started & Sys Subjected to Sizable Water Hammer.Caused by Incomplete Valve Lineup. Hangers & Failed Snubber Repaired, & Personnel Notified | /03L-0:on 781215,during Refueling Shutdown, Blowdown Heat Transfer Pump Started & Sys Subjected to Sizable Water Hammer.Caused by Incomplete Valve Lineup. Hangers & Failed Snubber Repaired, & Personnel Notified | | | 05000312/LER-1978-018-03, /03L-0:on 781221,while Increasing Power After Second Refueling Outage,Rcs Flow Indicator a Unusually Steady & Spurious Alarms Received.Caused by Operator Error. Transmitter Returned to Svc & Operator Instructed | /03L-0:on 781221,while Increasing Power After Second Refueling Outage,Rcs Flow Indicator a Unusually Steady & Spurious Alarms Received.Caused by Operator Error. Transmitter Returned to Svc & Operator Instructed | | | 05000312/LER-1978-018, Forwards LER 78-018/03L-0 | Forwards LER 78-018/03L-0 | |
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