ML20147B095

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Forwards Final Rept on Failure of 2CV-4950(a William Powell Co Valve)As Reported to Tom Westerman,Region Iv,On 780822. the Deficient Valves Are Located in the Chemical & Volume Control Sys & Associated W/The Lo-Lo Level
ML20147B095
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 09/20/1978
From: David Williams
ARKANSAS POWER & LIGHT CO.
To: Seyfrit K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
2-098-13, 2-98-13, NUDOCS 7810030253
Download: ML20147B095 (3)


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A R K A N S A S' ' P O W E R & L I G H T C O M P A N Y l

STH G LOUIStAN A ST AEETG e LITTLE AOCK. AAK ANS AS 72203.(501)37

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September 00, 1978

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2-098-13 Seyfrit l Mr..

Of fice K.. of V./ Inspection & Enforcement Region IV l U. S. Nuclear Regulatory Commission I 611 Ryan Plaza Drive, Suite.1000  ;

Arlington, Texas 76012 l

Subject:

Arkansas N'uclear One-Unit 2 l Docket No. 50-368 License No. NPF-6 10CFR50.55(e) Significant Deficiency William Powell Valves (File: 0520)

Dear Mr. Seyfrit:

On August 22, 1978, we reported to Mr. Tom Westerman, Region IV,

' the failure of 2CV-4950 (a William Powell Co. valve). Attached is )

al final rep' rt on this deficiency.

Very truly yours, *

(L w s- 7e 4t m 4 Daniel H. Williams i Ec Manager, Licensing DHW: CSP:tw s Attachment ./

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- cc: Mr. W. 'D. MacDonald, Director Office of Management Information i

.and Program Control U. S.; Nuclear Regulatory Commission Wa.shington, D. C. 20555

- Dr. : E'... Vol genau,, Di rector Office of Inspection & Enforcement

- Washington, D. C. 20555 -

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A. Description of-the Deficiency The valves in question are in the_ Chemical and Volume Control System ,

(CVCS) and are associated'with the Lo-Lo level of the volume control tank )

(VCT) and in boration of the reactor coolant system and are manufactured by  !

William Powell Company.

The problem was first identified on valve 2CV-4873 which is located at the outlet of the Volume Control Tank. It is equipped with a motor operator manufactured by Limitorque Corporation. The valve was disassembled -

after it became stuck and the stem was found to be distorted. The stem was replaced with the spare stem which also became distorted after about 20 open and close cycles. The motor was found to cycle on and off after the valve was run_ to the closed position, i.e. , the valve operator would run to the closed position, the motor stop on torque and a moment later i During the motor would start again. This cycling continued repeatedly.

this cycing the valve disk did not withdraw from the seat.

l The valve specification calls for a maximum of 10 sec. closing time.

In order to meet this requirement the Limitorque operator was furnished with non self-locking gearing. Without the scif-locking gearing, it is i a characteristic of the mechanical train for the stem compression to i relax slightly through the non self-locking gearing and allow the torque l switch to reclose. This arrangement causes no problem when a momentary, contact control system is utilized and the torque switch reclosure will not re-energize the operator and drive the valve " shut". On ANO-2 the valve l control system utilizes a continuous, not a momentary contact, which allows the motor to restart each time the torque switch closed. 4 The valve specification requires that "The motor will stall upon failure l of the limit or torque switches without causing damage to any valve component or the motor operator." The material of the original and first i replacement stem was 316 stainless steel. It appears that 316 does not l have sufficient strength to meet the specification requirement. l Later, the same trouble occurred with valve 2CV-4950. It became stuck and upon disassembly the stem was found distorted. A replacement 316SS stem also distorted in the same manner. An investigation into all of the valves on this order was made to resolve the two problems: (1) cicctrical control and (2) stem distortion after repeated closures.

All the valves in question are equipped with Limitorque operators.

B. Analysis of the Safety Implications The valves involved are 2CV-4916, 4920, 4921, 4950 and 4873. All of the  !

valves except 2CV-4950 receive an SIAS. Valve 2CV-4873, at the outlet of the i VCT, closes upon SIAS to prevent dilution of the concentrated boric acid which j is coming from valves 2CV-4921 and 2CV-4920 in the gravity drain lines at i the outlet of the boric acid makeup tanks (BAMT), and 2CV-4916 at the outlet of the boric acid pumps. Valves 2CV-4921, 2CV-4920 and 2CV-4916  !

open upon an SIAS. j

.These valves, along with the charging pumps and boric acid pumps starting open to borate upon an SIAS. No credit is taken in the LOCA safety analysis for this boration. Conservative credit for these actions is taken in the main steam line br'eak safety analysis, but a recent review of the calcula-

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. tions reveals that the effect of this credit is negligible. Boration for normal operation and for normal shutdown is unaffected by these valves.

Valves.2CV-4873' closes and 2CV-4950 opens upon Lo-Lo VCT level. If this f should occur, the operator is L informed first by a VCT Lo Level alarm and then by a Lo-Lo level alarm and will be-alerted as to whether makeup is actually taking place by noting whether valve 2CV-4873 has opened and whether boric acid is flowing to the suction of the charging pumps by observing flow recorder 2FR-4926. If flow is not taking place, valve 2CV-4930 can be opened to the suction of the charging pumps. If suction _j to the charging pumps is not maintained and if the pressurizer level con-trol, by terminating letdown, is not able to prevent pressurizer level from falling, ultimately, the reactor will trip on low pressurizer pressure with-out affecting safety.

The conclusion is that the malfunction does not change the conclusions of the plant safety analysis and has no effect on normal plant operations.

C. -Corrective Action The electrical circuitry of all 5 valves has been modified to include an "a" contact from the Limitorque motor controller which prevents torque switch limit cycling, see Figure 3. It opens the circuit when ]

the torque switch opens such that the motor will not re-energize if the '

torque switch recloses due to the mechanical relaxation of the stem.

To correct the valve stem problem, new stems of heat treated 17-4 ph material l have been substituted for the 316 stainless steel stem. Valve 2CV-4920 had been changed during construction to a valve of a different manufacturer and i hence only circuit changes were made to this valve. These two actions will 1 preclude the problem discussed. j 1

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