ML20141H509

From kanterella
Jump to navigation Jump to search
Insp Repts 50-348/85-43 & 50-364/85-43 on 851119-1218. Violation Noted:Approved Procedures Not Adhered to During New Fuel Receipt & Insp
ML20141H509
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 01/09/1986
From: Brian Bonser, Bradford W, Cantrell F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20141H497 List:
References
50-348-85-43, 50-364-85-43, NUDOCS 8601140155
Download: ML20141H509 (7)


See also: IR 05000348/1985043

Text

'

pa ia

UNITE 3 STATES

.

g

o,

NUCLEAR REGULATORY COMMISSION

g

REGION 11

y'

j

101 MARIETTA STREET.N.W.

t

AT LANTA, GEORGI A 30323

...../

Report Nos.:

50-348/85-43 and 50-364/85-43

Licensee: Alabama Power Company

600 North 18th Street

Birmingham, AL 35291

Docket Nos.:

50-348 and 50-364

License Nos.:

NPF-2 and NPF-8

Facility Name:

Farley 1 and 2

Inspection Conducted:

November 19 - December 18, 1985

Inspectors: bbO

b. 8>-r.

/

b

W.H.BraQford

GG

Qfite ' Signed

MLA &

thhc

B. R. Bor0(er

UU

obte Sign'ed

r

Approved by:

N/$M

/ 9dI,

F. S. Cantrell, Ydo(4on Chief

Date Signed

Division of Reactor Projects

SUMMARY

Scope: This routine, unannounced inspection entailed 105 inspector-hours on site

in the areas of licensee action on previous enforcement matters, monthly

surveillance observation, monthly maintenance observation, operational safety

verification, and new fuel receipt and inspection.

Results:

Within the areas inspected, one violation was identified in that

approved procedures were not adhered to during new fuel receipt and inspection.

This is discussed in paragraph 7.

!

B601140155 860109

~~

PDR

ADOCM 05000348

G

PDR

>

_

_

-

.

,

.

REPORT DETAILS

1.

Licensee Employees Contacted:

J. D. Woodard, General Plant Manager

D. N. Morey, Assistant General Plant Manager

W. D. Shipman, Assistant General Plant Manager

R. D. Hill, Operations Superintendent

C. D. Nesbitt, Technical Superintendent

R. G. Berryhill, Systems Performance and Planning Superintendent

L. A. Ward, Maintenance Superintendent

L. W. Enfinger, Administrative Superintendent

J. E. Odom,. Operations Sector Supervisor

B. W. Vanlandingham, Operations Sector Supervisor

T. H. Esteve, Planning Supervisor

J. B. Hudspeth, Document Control Supervisor

L. K. Jones, Material Supervisor

R. H. Marlow, Technical Supervisor

L. M. Stinson, Plant Modification Supervisor

W. G. Ware, Supervisor, Safety Audit Engineering Review

Other licensee employees contacted included technicians, operations

personnel, maintenance and I&C personnel, security force members, and office

personnel.

2.

Exit Interview

The inspection scope and findings were summarized during management

interviews throughout the report period and on December 18, 1985, with the

general plant manager and selected members of his staff. The inspection

findings were discussed in detail. The licensee acknowledged the violation.

The licensee did not identify as proprietary any material reviewed by the

inspector during this inspection.

3.

Licensee Action on Previous Enforcement Matters (92702)

This area was not inspected during this inspection period.

4.

Monthly Surveillance Observation (61726)

During the inspection period, the inspector verified plant operations were

in compliance with various TS requirements. Typical . of these requirements

were confirmation of compliance with the TS for reactor coolant chemistry,

refueling water storage tank, emergency power systems, safety injection,

emergency safeguards systems, control room ventilation, and direct current

electrical power sources. The inspection verified that surveillance testing

was performed in accordance with the approved written procedure, test

3

L-.

-

-

. - _ .

--

- -

--

-

- - - - - _ _ -

.

.

.

l

2

i.

'

instrumentation was calibrated; limiting conditions for operation were met,

appropriate removal

and restoration of the affected equipment was

accomplished, test result met requirements and were reviewed by personnel

other than the individual directing the test; and that any deficiencies

identified during the testing were properly reviewed and resolved by

i

appropriate management personnel.

Typical of the surveillance items that were witnessed in part or in full

were various calibrations of the nuclear instrumentation radiation

monitoring systems instrumentation, battery testing, auxiliary feedwater

system testing, heat removal system testing, diesel generator testing and

reactor protection system testing.

I

The following surveillance tests are discussed:

i

a.

FNP-2-STPE33.28 - Reactor Trip Breaker Train B Operability Test.

On 12/16/85 during the performance of surveillance test STP-33.2B on

Unit 1 B train reactor trip breaker, the trip breaker was opened and

would not reclose.

The licensee declared a 6 hour6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> LC0 and immediately began trouble-

shooting.

The problem was narrowed down to the breaker cubicle or a

'

spurious trip signal.

The licensee then determined that there was no

problem with the trip breaker itself by placing a Unit 2 reactor trip

bypass breaker in the Unit 1 B train trip breaker cubicle and deter-

rgining that it also would not close. The problem was found in the trip

contact actuated by the Auto Shunt Trip trip button. The contact had

stuck in the closed position when the Auto Shunt Trip trip button had

-

been depressed while performing the STP.

The problem with the contact was corrected and the surveillance test

was performed again to verify operability of the B train reactor trip

-breaker. The problem with the trip breaker did not result in a reactor

trip. The B train bypass breaker was closed throughout the entire

event.

The limiting condition for operation was not exceeded.

b.

FNP-2-STP-80.5 - Diesel Generator Operability With Safety Injection

Test Signal.

On 12/9/85 an 18 month surveillance test STP-80.5 was performed on 28

diesel generator. The surveillance test is designed to verify that on

a Safety Injection test signal the diesel will auto start and all

except specified essential auto diesel trips are automatically

bypassed.

During the performance of the test after the diesel had automatically

started, and in accordance with the test procedure, the Emergency Start

reset pushbutton on the Emergency Power Board was depressed. The 2B

diesel shutdown when the button was depressed.

This was contrary to

the requirements of the surveillance test.

.- _

_

_

_ _ . _ -

. _ - _ _ _ _ .

__._ _.

______

l

!

!...

-

.

.

L

l

3

s

An evaluation by.the licensee determined that the shutdown signal came

from a shutdown relay, with a 140 second timer, which was energized

when the stop pushbutton or NEEP relay pushbutton was depressed earlier

in the procedure.

When the Emergency Start reset pushbutton was

.

depressed before tne 140 second timer had timed out the 2B diesel-

L

shutdown on a non-essential trip signal. This :ondition resulted from

.

I

a circuit modification which the licensee had not

1.

eporated into the

test procedure; however, safety of the emergency diesels was not

'

effected.

l

The inspectors verified that the modification had gone through the

'

licensee's internal review process which requires that an evaluation be

-

made which would determine if a procedure change was required, a

training change notice be issued, and drawing changes be made if

required.

The reviewers determined that there was no safety

>

significance to the diesel generator in regard to the affected

surveillance test, which is performed on a 18 month basis, and

-

therefore, no procedure change would be required. A training change

.

notice is in the issue process and the appropriate drawings are being

'

changed. The operability of the diesel generator was not compromised.

The licensee now recognizes that this subtle change to the diesel 140

second timer requires a procedure change. The licensee recognized this

during the performance of the STP and has changed the procedure.

This is considered to be an isolated event.

Inasmuch as this was

licensee identified, corrected promptly and was not a violation that

.

could reasonably be expected to have been prevented by the licensee's

'

l

corrective action for a previous violation, a Notice of Violation will

not be issued.

p

5.

Monthly Maintenance Observation (62703)

Station maintenance activities of safety-related systems and components were

!

observed / reviewed to ascertain that they were conducted in accordance with

r-

approved procedures, regulatory guides, industry codes and standards, and

j

were in conformance with Technical Specifications.

1

The following items were considered during the review: limiting conditions

L

for operations were met while components or systems were removed - from

service; approvals were obtained prior to initiating the work; activities

were accomplished using approved procedures and were inspected as appli-

cable; functional testing and/or calibrations were performed prior to

'

returning components or systems to service; quality control records were

i

maintained; activities were accomplished by qualified personnel; parts and

!

materials were properly certified; radiological controls were implemented;

!

and fire prevention controls were implemented,

j

l

l

,

I

r

%

.

.

- . .

- - - -

-

- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

-

.

.

.

4

Work requests were reviewed to determine the status of outstanding jobs to

assure that priority was assigned to safety-related equipment maintenance

which may affect system performance.

The following maintenance activities

were observed / reviewed:

Replacement of battery cells in Unit 1 auxiliary building 125 V DC

-

battery.

2 B diesel generator.

-

.

Unit I service water emergency recirculation valve - Header A

-

(pressure switch replacement).

Unit 1 4160 V ACB's puffer tubes replacement.

-

Unit I reactor trip breaker.

-

Within the areas inspected, no violations or deviations were identified.

6.

Operational Safety Verification (71707)

a.

The inspectors observed control room operations, reviewed applicable

logs and conducted discussions with control room operators during the

report period.

The inspectors verified the operability of selected

emergency systems, reviewed tagout records, and verified proper return

to service of affected components. Tours of the auxiliary, diesel, and

turbine buildings were conducted to observe plant equipment conditions,

including fluid leaks and excessive vibrations.

b.

The inspectors verified compliance with selected Limiting Conditions

for Operation (LCO) and results of selected surveillance tests.

The

verifications were accomplished by direct observation of monitoring

instrumentation, valve positions, switch positions and review of

,

completed logs, records, and chemistry results.

The licensee's

compliance with LC0 action statements were reviewed as they happened.

The

following

systems

and components were

observed / verified

operational:

Station electrical boards in the control room and various elec-

-

trical boards throughout the plant for proper electrical

alignment.

Certain accessible hydraulic snubbers.

-

Accessible portions of service water and component cooling water

-

systems.

Units 1 and 2 suction and discharging piping and valves on

-

auxiliary feedwater system.

Diesel generators and support systems.

-

Certain accessible portions of CVCS piping and valves to and from

-

the charging /high head safety injection pumps.

_ _ -

_ _ _ _ _ __

.-

e

.

-

5

,

Cert'ain portions of RHR and cantainment spray systems.

-

,

Portions of various other systems (safety-related and nonsafety-

-

related).

[

c.

The inspectors routinely attended met. tings with certain licensee

'

management and observed various shift tcrnovers between shif t super-

visors, shift foremen, and licensed operators.

These meetings and

,

discussions provided a daily status of plant operating, maintenance,

j

!

and testing activities in progress, as well as discussions of

j

significant problems.

d.

The inspector verified by observation and interviews with security

.

force members that measures taken to assure the physical protection of

the facility met current requirements. Areas inspected included the

organization of the security force; the establishment and maintenance

of gates, doors, and isolation zones; that access control and badging

'

were proper; and procedures were followed.

e.

The inspectors reviewed the licensee's plans and actions for cold

j

-

weather operations.

The inspectors judge the plans and actions to be

adequate,

f.

The inspectors questioned the operability of the emergency air

compressors on Units 1 and 2.

These compressors are not included in

a

1

the Technical Specifications.

Their function is to supply emergency

operating air to certain valves on the auxiliary feedwater system and

the main steam power operated relief valves in case of a complete loss

of the normal instrument air supply.

The surveillance which had been performed consisted of annual

mechanical. preventative maintenance procedure. This procedure required

,

.

that comoressors to be disassembled and checked.

The compressor was

'

!

eassembled and operated for a short period of time.

i

The licensee has prepared and initiated STP-65.0 " Emergency Air

Compressor Operability Test." This procedure is designated " Safety

,

Related" and will be performed by operations personnel.

.

The inspectors had no further questions.

Within the areas inspected, there were no violations or deviations

.

identified,

i

f

7.

Receist, Inspection and Storage of New Fuel (60705)

[

i

On No/ ember 21, 1985, the licensee was unloading, inspecting and storing new

,

fuel assemblies in the Unit 2 new fuel storage building.

The receipt and

{

inspection of the fuel was carried out under FNP-0-FHP-3.0 " Receipt and

'

!

!

[

t

i

i

!-

'

,

.

m

m

.

.

.

.

-

.

.*

.

.

,

6

Storage of New Fuel." The inspectors observed this operation for about 4

hour during the morning of November 21 and verified that the operators were

briefed on each step of the procedure prior to performing the work, each

operator was qualified Senior Reactor Operator who had no other duty

assignments other than the fuel handling.

At 2:35 p.m., during the unloading of the last new fuel cask, a new fuel

assembly fell from the cask during the unloading operation.

The new fuel

assembly cradle was being lifted by crane to the upright position. At the

vertical position one of the new fuel assemblies pushed open the top clamp

and fell out of the cradle.

The fuel assembly come to rest in a slight

twist position on the concrete floor. The damage observed was buckled grid

straps and crushing of the internal spacers between the fuel rods.

There

was no release of contamination; there were no personnel injuries. The fuel

assembly was sent back to Westinghouse corporation to be rebuilt.

The Fuel Handling Procedure, FNP-0-FHP-3.0 requires in step 4.12.4 "to

break, but do not unfasten, each of the clamping frame fastener nuts except

those on the top frame" prior to raising the new fuel carriage to the

vertical position. The incident was caused by the top frame fastener being

loosened while the assembly was in the horizontal position.

When the

assemblies reached the vertical position the assembly pushed open the top

frame fastener and fell out. The top frame fastener was released by a

licensed operator who came into the new fuel area as the last fuel

assemblies were being prepared for unloading.

The operator obtained a

wrench to help the other operators unfasten the clamp frame assemblies. He

had not been brie'ed on the procedure and was unaware that the top fasteners

were not to be loosened. The operator should have been briefed on the fuel

handling procedure prior to performing this work.

This is a violation for failure to follow an approved procedure (364/

85-43-01).

,.

L.