| | | Reporting criterion |
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| 05000277/LER-1997-001-03, :on 970318,TS Violation Due to non-conservative Average Power Range Monitor Flow Bias Scram Setpoints for Single Loop Operation.Procedural Enhancements to Ensure That Single Loop Flow Conditions,Accommodated |
- on 970318,TS Violation Due to non-conservative Average Power Range Monitor Flow Bias Scram Setpoints for Single Loop Operation.Procedural Enhancements to Ensure That Single Loop Flow Conditions,Accommodated
| 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000278/LER-1997-001, :on 970122,determined Plant Thermal Power Exceeded 100% Due to Out of Tolerance Test Equipment.Retired Test Apparatus from Future Use & Will Review and Revise Procedures for Feedwater Temp Instruments |
- on 970122,determined Plant Thermal Power Exceeded 100% Due to Out of Tolerance Test Equipment.Retired Test Apparatus from Future Use & Will Review and Revise Procedures for Feedwater Temp Instruments
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000277/LER-1997-002-03, :on 970326,TS Violation Identified as Result of Reactor Operation Slightly in Excess of Licensed Thermal Power.Ctp Calculation Program Was Modified to Compensate for Recirculation Pump Motor Power Factor |
- on 970326,TS Violation Identified as Result of Reactor Operation Slightly in Excess of Licensed Thermal Power.Ctp Calculation Program Was Modified to Compensate for Recirculation Pump Motor Power Factor
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000278/LER-1997-002-02, :on 970309,manual Scram Occurred Due to Loss of Forced Reactor Core Circulation at Power as Result of 13kv Feeder Breaker Auxiliary Switch Failure.Auxiliary Switch Assembly Was Cleaned & Lubricated |
- on 970309,manual Scram Occurred Due to Loss of Forced Reactor Core Circulation at Power as Result of 13kv Feeder Breaker Auxiliary Switch Failure.Auxiliary Switch Assembly Was Cleaned & Lubricated
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000277/LER-1997-003, Forwards LER 97-003-00,concerning Inoperability of Hpcis When Wire Lug Was Lifted in Control Circuit on 970601 | Forwards LER 97-003-00,concerning Inoperability of Hpcis When Wire Lug Was Lifted in Control Circuit on 970601 | 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000277/LER-1997-003-03, :on 970601,HPCI Was Inoperable.Caused by Lifting of Common Power Wire Lug in HPCI Electrical Power Logic as Part of GP-25 Activity.Hpci Sys Was Restored to Operable Condition |
- on 970601,HPCI Was Inoperable.Caused by Lifting of Common Power Wire Lug in HPCI Electrical Power Logic as Part of GP-25 Activity.Hpci Sys Was Restored to Operable Condition
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) |
| 05000278/LER-1997-003-01, :on 970404,TS Noncompliance Due to Loss of 3C RFP High Water Level Trip,Occurred.Caused by Failure to Correlate Turbine/Reset Light Problem to Inoperability. Operating Shift Procedures Revised |
- on 970404,TS Noncompliance Due to Loss of 3C RFP High Water Level Trip,Occurred.Caused by Failure to Correlate Turbine/Reset Light Problem to Inoperability. Operating Shift Procedures Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000277/LER-1997-004-02, :on 970710,discovered non-compliance W/Ts When TS Action Times Were Exceeded.Caused by Procedural Control Not Being Adequate to Ensure Radiation Monitor Would Be Maintained in Trip Condition.Made Rev to GP-25 App 13 & 14 |
- on 970710,discovered non-compliance W/Ts When TS Action Times Were Exceeded.Caused by Procedural Control Not Being Adequate to Ensure Radiation Monitor Would Be Maintained in Trip Condition.Made Rev to GP-25 App 13 & 14
| 10 CFR 50.73(a)(2)(i) |
| 05000277/LER-1997-004, Forwards LER 97-004-00 Re non-compliance of MCR Emergency Ventilation Sys TS Which Occurred on 970710 | Forwards LER 97-004-00 Re non-compliance of MCR Emergency Ventilation Sys TS Which Occurred on 970710 | 10 CFR 50.73(a)(2)(i) |
| 05000277/LER-1997-005-02, :on 970808,discovered TS non-compliance Associated W/Rod Block Contact Testing.Caused by Rev in Oct 1989,attempted to Consolidate Testing of Rod Block Logic from Two Instrument Panels.Procedure Revised |
- on 970808,discovered TS non-compliance Associated W/Rod Block Contact Testing.Caused by Rev in Oct 1989,attempted to Consolidate Testing of Rod Block Logic from Two Instrument Panels.Procedure Revised
| 10 CFR 50.73(a)(2)(i) |
| 05000277/LER-1997-006, Forwards LER-97-006-00,concerning Unplanned ESF Actuation During 4-kV Electrical Bus Relay Testing Activities on 970923 | Forwards LER-97-006-00,concerning Unplanned ESF Actuation During 4-kV Electrical Bus Relay Testing Activities on 970923 | 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000277/LER-1997-006-02, :on 970923,DG Auto Start During 4-kV Relay Testing Occurred.Caused by Personnel Error.Need for Exercising Caution When Removing or Installing Relay Cover Was Discussed W/I&C Technicians |
- on 970923,DG Auto Start During 4-kV Relay Testing Occurred.Caused by Personnel Error.Need for Exercising Caution When Removing or Installing Relay Cover Was Discussed W/I&C Technicians
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000277/LER-1997-007, Forwards LER 97-007-00 Which Documents Event That Occurred at Peach Bottom Atomic Power Station,Units 2 & 3 on 740705 | Forwards LER 97-007-00 Which Documents Event That Occurred at Peach Bottom Atomic Power Station,Units 2 & 3 on 740705 | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000277/LER-1997-007-02, :on 970821,engineering Personnel Identified Potential Suppression Chamber Steam Bypass Leakage Path Between Air Spaces of Drywell & Torus.Caused by Original Design Deficiency.Drywell Purge Supply Valve Disabled |
- on 970821,engineering Personnel Identified Potential Suppression Chamber Steam Bypass Leakage Path Between Air Spaces of Drywell & Torus.Caused by Original Design Deficiency.Drywell Purge Supply Valve Disabled
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000277/LER-1997-008, Forwards LER 97-008-00,reporting Discovery of safety-related Logic Components That Were Not Tested Per TS Surveillance Requirements on 740705 | Forwards LER 97-008-00,reporting Discovery of safety-related Logic Components That Were Not Tested Per TS Surveillance Requirements on 740705 | 10 CFR 50.73(a)(2)(1) |
| 05000277/LER-1997-008-02, :on 740705,logic Sys Functional Testing Did Not Contain All Required Testing Per TS Surveillance Requirements.Caused by Test Procedures Not Containing Required Testing.Untested Contacts Tested & Proved Operable |
- on 740705,logic Sys Functional Testing Did Not Contain All Required Testing Per TS Surveillance Requirements.Caused by Test Procedures Not Containing Required Testing.Untested Contacts Tested & Proved Operable
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000277/LER-1997-009-01, Forwards LER 97-009-01,reporting Reactor Scram on 971109, Resulting from Generator Lockout Condition & Subsequent Turbine Trip.Rev to Original Submittal & Discussion Anomalies Found w/2A Reactor Feedpump Turbine Trip Sys | Forwards LER 97-009-01,reporting Reactor Scram on 971109, Resulting from Generator Lockout Condition & Subsequent Turbine Trip.Rev to Original Submittal & Discussion Anomalies Found w/2A Reactor Feedpump Turbine Trip Sys | 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000277/LER-1997-009, :on 971109,reactor Scram Occurred.Caused by Generator Lockout Condition & Subsequent Turbine Trip Failure of 2A Reactor Feedpump Turbine to Trip on Demand During Recovery Activities.Reset Appropriate Scram Logics |
- on 971109,reactor Scram Occurred.Caused by Generator Lockout Condition & Subsequent Turbine Trip Failure of 2A Reactor Feedpump Turbine to Trip on Demand During Recovery Activities.Reset Appropriate Scram Logics
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) |
| 05000277/LER-1997-009-02, :on 971109,generator Lockout & Subsequent Turbine Trip Occurred.Caused by Turbine Trip Resulting from Generator Lockout Signal.Appropriate PCIS & RPS Scram Logics Were Reset |
- on 971109,generator Lockout & Subsequent Turbine Trip Occurred.Caused by Turbine Trip Resulting from Generator Lockout Signal.Appropriate PCIS & RPS Scram Logics Were Reset
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000277/LER-1997-010-02, :on 971229,2A RFPT Failed to Trip When RO Pushed CR 2A RFPT Trip push-button.Caused by Intermittent Failure Mechanism.Repaired,Reinstalled & Tested Operability of 2A RFPT |
- on 971229,2A RFPT Failed to Trip When RO Pushed CR 2A RFPT Trip push-button.Caused by Intermittent Failure Mechanism.Repaired,Reinstalled & Tested Operability of 2A RFPT
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) |
| 05000277/LER-1997-010, :on 971229,failure of 2A Reactor Feedpump Turbine to Trip,Occurred.Caused by Main Control Room pushbutton.2A RFPT Trip Device Repaired,Reinstalled & Tested to Prove Operability |
- on 971229,failure of 2A Reactor Feedpump Turbine to Trip,Occurred.Caused by Main Control Room pushbutton.2A RFPT Trip Device Repaired,Reinstalled & Tested to Prove Operability
| 10 CFR 50.73(a)(2) |
| 05000277/LER-1997-010-01, Forwards LER 97-010-01,reporting 971229 Failure of 2A Reactor Feedpump Turbine to Trip in Timely Manner | Forwards LER 97-010-01,reporting 971229 Failure of 2A Reactor Feedpump Turbine to Trip in Timely Manner | |