:on 851011 & 13,RWCU Sys Spilled Process Water & Resin Resulting in Isolation.Caused by Erosion of Valve Seat FV-14566A & Inadequate Single Valve Isolation.Valve Seat Replaced.Valve Control Circuitry Modified| ML20137Z251 |
| Person / Time |
|---|
| Site: |
Susquehanna  |
|---|
| Issue date: |
12/02/1985 |
|---|
| From: |
Sadvary D PENNSYLVANIA POWER & LIGHT CO. |
|---|
| To: |
|
|---|
| Shared Package |
|---|
| ML20137Z226 |
List: |
|---|
| References |
|---|
| LER-85-032, LER-85-32, NUDOCS 8512110259 |
| Download: ML20137Z251 (5) |
|
text
i e
seRC Form aos U.S. NUCLEA A 6.EGULATORY COtmetNIO88
'N APNIOvf 3 OMS seO.3150 4 104
'*""'*8"
LICENSEE EVENT REPORT (LER) i FACILITV psaast (U DOCKET fouteGR (2)
PAGE (3 Susquehanna Steam Electric Station - Unit 1 o l5 l 0 l 0 I o 13 I 817 1 lOFl 0 l 4 TITLE del Reactor Water Clean-up System Spills and Isolations.
EVENT DATE 153 LER NURISER ($1 REPOft? DATE (7)
OTHER F ACILITIES INVOLVED (BI II$U MONTH DAY YEAR PACILITY NAMES DOCKET NUMSER(3)
L MONTH DAY YEAR YEAR 4
u 015l01010 1 l I 1l0 1l1 85 8l5 0l 3l2 0l 1 1l2 0l2 8l5 0 1 5 1 0 1 00 1 l l
]
Tuis REeORT is suenairTED puReuANT TO TwE REOuiREMENT O, se C,R t icw
.r m
., n.e w
,s nu I
a ** **
m4 w x
esmaHi.i 73.7 mi
]
]
]
73.71 si es.734eH2iw 30.4eswH1Ho so.3skuu not Il010 ao.amaHum O m gs7,e'r7d"N7/ I.-.
umwH2i es.73mH Hwi 20.405(eH1Hilli 80.73IeH2HG 98.734sH3HvillHA Js5AJ 30.40SleH1Hivt 00.734eH2Hal OS.73delt3HvesHS) 20.406(sH1Hvi 30.73teH2Hiill 30.73teH3Hal LICENSEE CONTACT FOR TMBS LER Hal NAME TELEPHONE NUMSER AREA CODE Duane D. Sadvary 7l1l7 5 l 4121-13181516 COMPLETE ONE LINE FOR EACH COesPONENT FAILURE DGSCRIBED IN TMBS REPORT (13)
'f flyy MA RTA MA hC.
R A A
CAUSE
SYSTEM COMPONENT hC.
CAUSE
SYSTEM COMPONENT pq 5
~
I l I I I I I I
I I I I I I s
l I I I I I I I
I I I I I I SUPPLEMENTAL REPORT EXPECTED (14)
MONTH DAY YEAR SUOMIS$10N YES (19 yes, s.meten EXPECTEO sus 4015$10N DA TE)
NO l
l l
ASSTR ACT lllawt to f 400 mascas. i.e., aperomerery rdines wande4pece typewreren maest 043 On October 11 and 13, 1985, the Unit 1 Reactor Water Clean Up (RWCU) System (CE)~ isolated when placing the 1A Filter Dmineralizer (F/D) in service. The RWCU isolation valves are Primary Containtmnt Isolation Valves (Engineered Safety Feature (ESF)) and these unplanned actuations are reportable in accordance with 10CFR72. Both events occurred due to abnormal leakage through the EV-14566A Flow Control Valve (EU/) which pressurized the system's low pressure piping and caused. pressure relief valve PSV-14561 to lift and discharge. The first event resulted in spillage of both process water and resin in areas inmediate and adjacent to the affected system. Autmatic system isolation on HI-FIOW occurred approximately one minute after event initiation and terminated the spillage. Spill counter measures included the activation of a support team. One instance of personnel contamination occurred in that an operator's shoe contacted spillage and was contaminated.
An estimated twenty gallons of resin spilled. Approximately five gallons of water spilled through the same relief valve on October 13, 1985 during systm restoration. The system isolated autmatically on "RWCU HI IFAKAGE".
Subsequent review and investigation determined that the EV-14566A valve seat was eroded and that the as-designed single-valve isolation between the high and low pressure systems was inadequate.
The FV-14566A valve seat was replaced and a modification to the valve control circuitry installed to provide double valve isolation between the high and low pressure systems.
0512110259 851202 PDR ADOCK 05000387
""Es,'"
,/ /
- RC Form 3644 U S. NUCLEAR KEGULATOAY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPRovEo cua No. siso-clo4 EhPIRES S/3115 PAC 8LITY NAME tu DOCKET NUMBER (2)
LER NUMBER (6)
PAGE(3)
Susquehanna Steam Electric Station
"=
%*,7; vena Unit 1 015 I010 lo 131817 815 0,13 l2 011 Ol2 OF 0 14 TEXT #f more spece a regured, use adseones enc form JiiECsf 117)
This report describes two isolations of the Reactor Water Clean Up System (RWCU) (CE) which occurred on 10/11/85 and 10/13/85. The RWCU System isolation valves are containment isolation valves (Engineered Safety Feature (ESF)), and unplanned actuations are reportable per 10CFR72 (B) (2) (ii).
Refer to Attachment 1 for a simplified drawing of the system discussed in this License Event Report.
On 10/11/85, with the Unit 1 Reactor at 100% power and the RWCU 1B Filter Demineralizer (F/D) in service, the lA F/D was isolated for Maintenance to investigate / work on the Flow Control Valve, EV-14566A. Operations, including supervision, Maintenance, and Health Physics personnel were assembled to support the maintenance activity which was initiated by 3 report that the FV-14566A valve appeared to be bound in the open positica.
Operations personnel assumed manual control of the F/D Program Sequencer and manually stepped through the RWCU "A" F/D program to establish a system configuration within which the FV-14566A problem could be investigated.
Having successfully sequenced through the backwa.sh and precoat cycles, the operator positioned the " Vessel Isolation Control Switch" to the "Deisolate" position. Personnel in the area heard flow and observed the RWCU 1B F/D flow indication to go offscale high. Water and resin were observed emanating frm the floor drains. No water hanmer noises wete haux1.
The operator quickly returned the " Vessel Isolation Control Switch" to the
" Isolate" position, and placed the IB F/D in " Hold". While performing these operations, the operator's shoe became contaminated as the radioactive water spread across the floor. During th,is sequence the "RWCU Hi Flow" alarm in the Control Rom annunciated followed by the RWCU System isolating appronmately one minute after receipt of the alarm.
Health physics, maintenance, and engineering support personnel, under the direction of plant managment, were assembled to both initiate the appropriate clean-uo activities and to determine the cause of the event. Post-event investigation / follow-up consisted of: operator and health physics personnel interviews, two Plant Operations Peview Ccnmittee (PORC) meetings to review the recovery / restoration; syst s inspection and corrective maintenance on identified deficiencies, and the generation of technical procedure TP-161-007, Reactor Water Clean-up System Restoration Following System Isolation and Blow-down. No personnel errors or procedure violations were identified, and the deficiencies identified during system inspection were determined to be non-contributory to the event. No problems with program sequence logic or valve operation were identified.
1B F/D was precoated and returned to service approximately 0630 on 10/13/85.
'Ihe progranmer utilized during this sequence of operating activities is ccumon to both the lA and 1B F/D's.
1B F/D activities, e.g., backwash, precoat, deisolate, etc., were ccmpleted without incident.
The cause of this spill was initially attributed to manual cycling of the program sequencer allowing the F/D inlet isolation valve to open while the gaw 3.
1.
NRCF.em354A U S NUCLEAR KEGULATOav COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Areaovso ove No. siso-oio4 EXPlRES S/3125 FACILITY NAME l1)
DOCKET NUM8ER Qi (ER NUMBER (6)
PAGE (3)
Susquehanna Steam Electric Station ngp gy,p vE..
Unit 1 o l5 lo jo jo l3 l8 l7 8l5 0l3[2 0l1 0 l3 OF 0 l4 rEn n m,u
, we,.,,, mmm HV-14510A and llB valves (backwash and precoat cycle isolation valves) were open thus allowing high pressure water to enter the low pressure piping. 'Ihis caused the relief valves on the low pressure piping to lift and discharge into the liquid radwaste drains. The drains backed up and overflowed on the floor.
Based on the above findings and conclusion, the decision was made to put the lA F/D back in service. At approximately 1130, on October 13, 1985, with the Unit 1 Reactor at 100% power, and the IMCU IB F/D in service, lA F/D was being returned to service using operating procedure OP-161-001. After precoating this F/D, the operator proceeded per the procedure to place the " Vessel Isolation Control Switch" in the "Deisolate" position. The influent and effluent isolation valves (HV-14531A and 32A) opened and the flow control valves (HV-14506A and W-14566A) remained closed per indication at the local panel. The operator heard a loud " bang" and saw the Pressure Relief Valve PSV-14561 on the low pressure piping discharge into the floor drain.
In the Control Rom, the alarm for "RWCU System Hi Leakage" annunciated. The systs flow indicator pegged high and after the designed time delay, the system isolated.
No personnel contamination occurred during this incident and the spillage was estimated at approximately five gallons of water and no resin.
Additional atts pts to restore the system to service were terminated pending empletion of an expanded review / evaluation of the circumstances leading to both incidents. Personnel interviews were conducted including in situ reviews of operator actions and observations made during the event; plausible scenarios with and without operator error were developed; filter demineralizer logic sequences were reviewed; and leak tests were performed on various valves within the systs.
During the leak tests, flow control valve W-14566A failed to provide adequate tightness such that a test pressure could be established for leakage measurement. Engineering review of the 1A F/D logic sequence determined that the normal program sequence allows deisolation of the system with the precoat cycle still in operation. In this configuration, isolation between the high pressure and low pressure piping is dependent upon ' single valve isolation'.
The single valve for isolation was the leaky W-14566A valve. With the RWCU 1A F/D System filled with water (i.e., " solid") and the system "deisolated",
leakage through the FV-14566A valve allowed the entire system to becme pressurized frm the high pressure to the low pressure piping. This caused the PSV-14561 relief valve to lift.
The HV-14531A Effluent Isolation Valve was disasserrbled and inspected. No wear or damage was found. However, the ball and seats were replaced. The FV-14566A Flow Control Valve was disassetrbled and inspected. It was found that the soft seat had been empletely eroded. The seat was replaced.
Post-maintenance leak testing per test procedure TP-161-008 established that the repairs were satisfactory and leakage was reduced to acceptable levels.
gC,oaM =..
J
2Rcem= meo u.s NuctE Ao cEautcroov commission LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AreaovEo OMS No siso-oto4
)
EXPIRES S/3115 F ACALITY NAME (1)
DOCKET NUM8ER (2)
LER NUMBER 16)
PAGE 131 Susquehanna Steam Electric Station 5'typ,
- "'383:
vtAa Unit 1 o l5 lo lo lo l3 l8 l7 8l5
- - 0l3l2
- - 0l1 O j4 OF 0 l4 W W MWE 800C0 *F mouwed. une endeonef NRC Fem 366Kel(1h A modification (PMR 85-9054, RWCU F/D Valve Control Sequence) was implemented to provide double valve isolation between the high and low pressure piping.
The valve control sequence change was ccmpleted on 10/23/85. Test procedure TP-161-010 was ccmpleted to prove the operability of the emplete backwash and precoat cycles with the double valve isolation protection.
'Ihe system was subsequently filled, vented and restored per test procedure TP-161-009 to prepare to put one of the F/D's back in service. The IB F/D was precoated and successfully placed in service at approximately 1930 on October 23, 1985. The lA F/D was precoated and successfully placed in service at approximately 0030 on October 24, 1985. A similar modification for the Unit 2 RWCU F/D Valves' Control Sequence is being initiated.
r b) f l-l /6TO M
J, 1*
A " sas-s v.s 7ans CLEAN-UP
] [/2A FIL1ER DMIN.
TD RECENERAM VF 3 r IA REAT EXQIAN 55 E
J L 1F 203A
/
I
~
j i i I HV-14532A~
HV-14506A 41A FV-14566A HV-14531A j g FROM NON-RECEN
]
M' W
O O
M HEAT I b EXQlANGERS j t W
M 35A O
CLEAN-UP j p DRAIN 38A
][
,g(
34A HOLDING PUNP y
,A IP223A I f I l LRW HICH PRESSURE SIDE A l b l PSV-14561 PSV-14563 CLEAN-UP p,
HV-14519 FROM F/D TO F/D j l PREC0AT PUMP n
1
'r^C CLEAN-UP LRW I.RW IP222 PRECOAT
- gyj4gg, 3
TANK I P
=
HV-14520 g
IT209
-^-
l m
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000387/LER-1985-001-01, :on 850213,while Removing Jumpers from Refuel Floor Wall Duct Trip Units,Zone III Isolated on High Radiation Signal.Caused by Reactor Bldg Recirculation Fans Not Starting.Investigation Continuing |
- on 850213,while Removing Jumpers from Refuel Floor Wall Duct Trip Units,Zone III Isolated on High Radiation Signal.Caused by Reactor Bldg Recirculation Fans Not Starting.Investigation Continuing
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-001, :on 850112,HPCI Turbine Failed to Trip During Hot Functional Test HF-252-011.Caused by Broken Stop Valve Actuator Shaft.Actuator Shaft Replaced |
- on 850112,HPCI Turbine Failed to Trip During Hot Functional Test HF-252-011.Caused by Broken Stop Valve Actuator Shaft.Actuator Shaft Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000387/LER-1985-002-01, :on 850121,diesel Generators a & D Failed to Start in Violation of Tech Spec Requirements.Caused by Cold Temp Problems.Diesel Generator Outside Air Supply Dampers Repaired |
- on 850121,diesel Generators a & D Failed to Start in Violation of Tech Spec Requirements.Caused by Cold Temp Problems.Diesel Generator Outside Air Supply Dampers Repaired
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000388/LER-1985-002, :on 850112,nonlicensed,nonutility Electrician Caused Reactor Protection Sys Motor Generator M-G Set to Trip When Wrench Came in Contact W/Energized Conductor. Caused by Failure to Isolate Equipment |
- on 850112,nonlicensed,nonutility Electrician Caused Reactor Protection Sys Motor Generator M-G Set to Trip When Wrench Came in Contact W/Energized Conductor. Caused by Failure to Isolate Equipment
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-003-01, :on 850124,unit Scrammed on Main Turbine Control Valve Fast Closure Signal Resulting from Main Generator Lockout.Caused by Ice Formations in Main Generator a & C Isophase Bus Ducts at Low Point in Ducts |
- on 850124,unit Scrammed on Main Turbine Control Valve Fast Closure Signal Resulting from Main Generator Lockout.Caused by Ice Formations in Main Generator a & C Isophase Bus Ducts at Low Point in Ducts
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-003, :on 850119,reactor Scrammed on Turbine Control Valve Fast Closure.Caused by Main Turbine Trip on High Vibration During Turbine Control Valve Testing.Vibration Reduced After Rebalancing |
- on 850119,reactor Scrammed on Turbine Control Valve Fast Closure.Caused by Main Turbine Trip on High Vibration During Turbine Control Valve Testing.Vibration Reduced After Rebalancing
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-004-01, :on 850129,diesel Generator B Tripped After 8 Minutes of Operation.Caused by Actuation of Connecting Rod Bearing High Temp Detector Vent Valve.Maint Personnel Will Perform Addl Insp |
- on 850129,diesel Generator B Tripped After 8 Minutes of Operation.Caused by Actuation of Connecting Rod Bearing High Temp Detector Vent Valve.Maint Personnel Will Perform Addl Insp
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000388/LER-1985-005, :on 850119,following Reactor Scram Due to Turbine High Vibration,Suppression Chamber Vacuum Breaker Surveillance Test Completed After Tech Spec Time Limit. Caused by Cognitive Error |
- on 850119,following Reactor Scram Due to Turbine High Vibration,Suppression Chamber Vacuum Breaker Surveillance Test Completed After Tech Spec Time Limit. Caused by Cognitive Error
| 10 CFR 50.73(a)(2)(i) | | 05000387/LER-1985-005-01, :on 850213,verification of 6 Plus or Minus 1 Simulated Thermal Power Time Constant Inadvertently Omitted from Routine Surveillance Testing for Aprms.Time Constant Since Verified |
- on 850213,verification of 6 Plus or Minus 1 Simulated Thermal Power Time Constant Inadvertently Omitted from Routine Surveillance Testing for Aprms.Time Constant Since Verified
| 10 CFR 50.73(a)(2)(i) | | 05000388/LER-1985-006, :on 850129,w/unit in Hot Shutdown,Rhr Sys Shutdown Cooling Suction Inboard Isolation Valve Closed Unexpectedly.Possibly Caused by Faulty Pressure Switch. Switch May Be Replaced Pending Evaluation |
- on 850129,w/unit in Hot Shutdown,Rhr Sys Shutdown Cooling Suction Inboard Isolation Valve Closed Unexpectedly.Possibly Caused by Faulty Pressure Switch. Switch May Be Replaced Pending Evaluation
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-006-01, :on 850213,monthly Composite Sample Analyses Not Completed.Caused by Dec Aliquots Added to Wrong Monthly Composite Container.Procedure Changes Made to Prevent Recurrence |
- on 850213,monthly Composite Sample Analyses Not Completed.Caused by Dec Aliquots Added to Wrong Monthly Composite Container.Procedure Changes Made to Prevent Recurrence
| 10 CFR 50.73(a)(2)(i) | | 05000387/LER-1985-007-02, :on 850216,breaker Supplying Instrument Bus Opened,Causing Isolation of Reactor Water Cleanup Sys on False Signal.Caused by Loss of Power to Temp Sensor Trip Circuitry.Addl Training for Operators Provided |
- on 850216,breaker Supplying Instrument Bus Opened,Causing Isolation of Reactor Water Cleanup Sys on False Signal.Caused by Loss of Power to Temp Sensor Trip Circuitry.Addl Training for Operators Provided
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-007, :on 850129,RHR Sys Shutdown Cooling Suction Valve Closed Unexpectedly.Cause Not Stated.Pressure Switch Checked & Shutdown Cooling Established.Switch May Be Replaced Pending Evaluation |
- on 850129,RHR Sys Shutdown Cooling Suction Valve Closed Unexpectedly.Cause Not Stated.Pressure Switch Checked & Shutdown Cooling Established.Switch May Be Replaced Pending Evaluation
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-007-01, :on 850130,during Purge of Containment,One Train of Standby Gas Treatment Sys Became Inoperable.Caused by Annunciation of Standby Gas Treatment Sys B Heater Failure Alarm.Event Reviewed W/Operators |
- on 850130,during Purge of Containment,One Train of Standby Gas Treatment Sys Became Inoperable.Caused by Annunciation of Standby Gas Treatment Sys B Heater Failure Alarm.Event Reviewed W/Operators
| | | 05000388/LER-1985-008, :on 850216,logic Power Lost to HPCI & Loop B of Core Spray.Caused by Broken Lug on Negative Terminal.Lug Replaced.Power Restored |
- on 850216,logic Power Lost to HPCI & Loop B of Core Spray.Caused by Broken Lug on Negative Terminal.Lug Replaced.Power Restored
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) | | 05000387/LER-1985-008-01, :on 850302,standby Gas Treatment Sys & Control Room Emergency Outside Air Supply Sys Actuated.Caused by Electricians Working on Mod to Reactor Protection Sys B Alternate Power Source Transformer |
- on 850302,standby Gas Treatment Sys & Control Room Emergency Outside Air Supply Sys Actuated.Caused by Electricians Working on Mod to Reactor Protection Sys B Alternate Power Source Transformer
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-009, :on 850212,setpoints for Three Reactor Water Level Switches Found to Be Outside Acceptance Criteria During Performance of Scheduled Surveillance.Caused by Instrument Drift.Instruments Recalibr |
- on 850212,setpoints for Three Reactor Water Level Switches Found to Be Outside Acceptance Criteria During Performance of Scheduled Surveillance.Caused by Instrument Drift.Instruments Recalibr
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000387/LER-1985-009-01, :on 850310,11 & 28,inadvertent ESF Actuations Occurred.Caused by Welding in Vicinity of Detectors,Inducing Noise in Instrumentation.Radiation Loop Reset & Tested |
- on 850310,11 & 28,inadvertent ESF Actuations Occurred.Caused by Welding in Vicinity of Detectors,Inducing Noise in Instrumentation.Radiation Loop Reset & Tested
| | | 05000387/LER-1985-010-01, :on 850313,during Cavity Draining Process, Refuel Floor High Exhaust Radiation Monitor Channel a Tripped.Caused by Shine Associated W/Lowering Reactor Cavity Water Level.Caution Added to Procedures |
- on 850313,during Cavity Draining Process, Refuel Floor High Exhaust Radiation Monitor Channel a Tripped.Caused by Shine Associated W/Lowering Reactor Cavity Water Level.Caution Added to Procedures
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-010, :on 850223,ESF Actuation Occurred.Caused by Tripped Reactor Protection Sys Power Supply Breaker.Breaker Reset & Affected Sys Restored |
- on 850223,ESF Actuation Occurred.Caused by Tripped Reactor Protection Sys Power Supply Breaker.Breaker Reset & Affected Sys Restored
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-011-01, :on 850323 & 0402,refuel Floor Radiation Monitors Tripped & Started ESF Sys.Caused by Radiographic Testing.Esf Starts Unavoidable Due to Detector Location Near Testing.Testing Suspended & HVAC Sys Restored |
- on 850323 & 0402,refuel Floor Radiation Monitors Tripped & Started ESF Sys.Caused by Radiographic Testing.Esf Starts Unavoidable Due to Detector Location Near Testing.Testing Suspended & HVAC Sys Restored
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-011, :on 850310,damper in Standby Gas Treatment Sys Train a Malfunctioned.Caused by Damaged Damper Actuator. Actuator Replaced & Damper Operation Verified to Be Correct on 850312 |
- on 850310,damper in Standby Gas Treatment Sys Train a Malfunctioned.Caused by Damaged Damper Actuator. Actuator Replaced & Damper Operation Verified to Be Correct on 850312
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) | | 05000387/LER-1985-012, :on 850404,determined That Four Fire Dampers in Standby Gas Treatment Sys Ductwork Not Included in Surveillance Procedures & Fire Watch Not Verified.Fire Watch Implemented |
- on 850404,determined That Four Fire Dampers in Standby Gas Treatment Sys Ductwork Not Included in Surveillance Procedures & Fire Watch Not Verified.Fire Watch Implemented
| 10 CFR 50.73(a)(2)(1) | | 05000388/LER-1985-012, :on 850316,power Supply to Standby Gas Treatment Sys Exhaust Vent Process Radiation Monitor Momentarily Shortened When Component Removed During Calibr. Caused by Malfunctioning Dampers |
- on 850316,power Supply to Standby Gas Treatment Sys Exhaust Vent Process Radiation Monitor Momentarily Shortened When Component Removed During Calibr. Caused by Malfunctioning Dampers
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-013-01, :on 850416,alternate Sampling for Turbine Bldg Lost Once & for Reactor Bldg Lost Twice.Caused by Circuit Overload,Resulting in Tripped Circuit Powering Sample Pumps. Alternate Power Supplies Being Investigated |
- on 850416,alternate Sampling for Turbine Bldg Lost Once & for Reactor Bldg Lost Twice.Caused by Circuit Overload,Resulting in Tripped Circuit Powering Sample Pumps. Alternate Power Supplies Being Investigated
| 10 CFR 50.73(a)(2)(1) | | 05000388/LER-1985-013, :on 850327,standby Liquid Control Pump a Failed 92-day Flow Verification Surveillance Test.Caused by Faulty Suction & Discharge Valves Internal to Positive Displacement Pump.Repairs Completed |
- on 850327,standby Liquid Control Pump a Failed 92-day Flow Verification Surveillance Test.Caused by Faulty Suction & Discharge Valves Internal to Positive Displacement Pump.Repairs Completed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000388/LER-1985-014, :on 850417,RCIC Sys Inboard Steam Supply Valve Isolated on Equipment Area High Temp.Caused by Malfunction of Temp Indicating Switch E51-N600B.Switch Replaced on 850418 & Isolation Signal Cleared |
- on 850417,RCIC Sys Inboard Steam Supply Valve Isolated on Equipment Area High Temp.Caused by Malfunction of Temp Indicating Switch E51-N600B.Switch Replaced on 850418 & Isolation Signal Cleared
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-014-01, :on 850413,loss of Power Initiated Isolation of HVAC Zone III & Started Standby Gas Treatment Sys & Control Room Emergency Outside Air Supply Sys Train A.Caused by Open Circuit Breaker.Breaker Closed |
- on 850413,loss of Power Initiated Isolation of HVAC Zone III & Started Standby Gas Treatment Sys & Control Room Emergency Outside Air Supply Sys Train A.Caused by Open Circuit Breaker.Breaker Closed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-015-01, :on 850421,spray Pond Bypass Valve HV-01222A Did Not Automatically Open When Emergency Svc Water Pump a Started.Caused by Two Open Sliding States Link Terminal Blocks in Relay Panel.Links Evaluated |
- on 850421,spray Pond Bypass Valve HV-01222A Did Not Automatically Open When Emergency Svc Water Pump a Started.Caused by Two Open Sliding States Link Terminal Blocks in Relay Panel.Links Evaluated
| 10 CFR 50.73(a)(2)(i) | | 05000387/LER-1985-015, :on 841213,portions of Upper Cable Spreading Room Structural Steel Found W/O Requisite 3 H Fire Proofing. Caused by Intentional Cutouts to Facilitate Installation. Fire Watch Established on 850409 |
- on 841213,portions of Upper Cable Spreading Room Structural Steel Found W/O Requisite 3 H Fire Proofing. Caused by Intentional Cutouts to Facilitate Installation. Fire Watch Established on 850409
| 10 CFR 50.73(a)(2)(i) | | 05000387/LER-1985-016, :on 850425,five Emergency Svc Water & Control Structure Chilled Water Sys Suveillances Completed Late. Caused by Mods to Sys & Problems W/Weekly Surveillance Schedule.Schedule Revised |
- on 850425,five Emergency Svc Water & Control Structure Chilled Water Sys Suveillances Completed Late. Caused by Mods to Sys & Problems W/Weekly Surveillance Schedule.Schedule Revised
| 10 CFR 50.73(a)(2)(i) | | 05000388/LER-1985-016-01, :on 850427,water Hammer Caused Reactor Water Level Transient.Caused by Rapid Filling of Partially Drained RHR Piping from Reactor Vessel.Operating Procedure for RHR Being Revised |
- on 850427,water Hammer Caused Reactor Water Level Transient.Caused by Rapid Filling of Partially Drained RHR Piping from Reactor Vessel.Operating Procedure for RHR Being Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-017, :on 850505,reactor Water Cleanup Sys Containment Outboard Isolation Valve Closed on High Flow Signal Causing Unanticipated ESF Actuation.Caused by Higher Differential Pressure When Sys Runs Cold |
- on 850505,reactor Water Cleanup Sys Containment Outboard Isolation Valve Closed on High Flow Signal Causing Unanticipated ESF Actuation.Caused by Higher Differential Pressure When Sys Runs Cold
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-017-01, :on 850530,drywell Sump Inleakage of About 10 Gpm Caused Reactor Shutdown.Shutdown Completed on 850531. Caused by Severe Packing Leak in Reactor Recirculation Pump Discharge Bypass Valve A.Valve Repaired |
- on 850530,drywell Sump Inleakage of About 10 Gpm Caused Reactor Shutdown.Shutdown Completed on 850531. Caused by Severe Packing Leak in Reactor Recirculation Pump Discharge Bypass Valve A.Valve Repaired
| 10 CFR 50.73(a)(2)(i) | | 05000388/LER-1985-018, :on 850529,circuit Breaker 8B in Reactor Protection Sys Distribution Panel 2Y201B Tripped.Caused by Loose Load Side Connection Leading to Overheating of Terminal Lug.Breaker Replaced |
- on 850529,circuit Breaker 8B in Reactor Protection Sys Distribution Panel 2Y201B Tripped.Caused by Loose Load Side Connection Leading to Overheating of Terminal Lug.Breaker Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-018, :on 850513 & 14,unanticipated Actuation of Reactor Protection Sys Ocurred When Intermediate Range Monitor Spuriously Tripped Upscale.Caused by Shorting Links Being Removed from Reactor Protection Sys |
- on 850513 & 14,unanticipated Actuation of Reactor Protection Sys Ocurred When Intermediate Range Monitor Spuriously Tripped Upscale.Caused by Shorting Links Being Removed from Reactor Protection Sys
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-018-01, :on 850529,three ESF Actuations Occurred Due to Tripping of Reactor Protection Sys Power Supply Breaker W/Unit at 100% Power.First Two Events Caused by Loose Connection.New Breaker Installed |
- on 850529,three ESF Actuations Occurred Due to Tripping of Reactor Protection Sys Power Supply Breaker W/Unit at 100% Power.First Two Events Caused by Loose Connection.New Breaker Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-019, :on 850516,reactor Protection Sys Actuation Occurred When Intermediate Range Monitor C Mistakenly Taken Out of Bypass.Caused by Telcon Misunderstanding.Personnel Counseled |
- on 850516,reactor Protection Sys Actuation Occurred When Intermediate Range Monitor C Mistakenly Taken Out of Bypass.Caused by Telcon Misunderstanding.Personnel Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-019-01, :on 850524,Limiting Condition for Operation 3.0.3, Motherhood Clause, Declared & Standby Gas Treatment Sys Suction Ductwork Access Doors Opened.Entry Required to Perform Fire Damper Surveillance |
- on 850524,Limiting Condition for Operation 3.0.3, Motherhood Clause, Declared & Standby Gas Treatment Sys Suction Ductwork Access Doors Opened.Entry Required to Perform Fire Damper Surveillance
| 10 CFR 50.73(a)(2)(i) | | 05000388/LER-1985-020-01, :on 850531,lightning Strike Caused Voltage Transient.Caused by Loss of Motive or Control Power. Malfunctioning Damper Actuator Replaced |
- on 850531,lightning Strike Caused Voltage Transient.Caused by Loss of Motive or Control Power. Malfunctioning Damper Actuator Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-021-01, :on 850630,neutral Overvoltage Occurred in Main Generator,Causing Primary Lockout.Caused by Failure of Phase C Main Transformer Low Voltage Bushing.Bushing Replaced W/Spare Component |
- on 850630,neutral Overvoltage Occurred in Main Generator,Causing Primary Lockout.Caused by Failure of Phase C Main Transformer Low Voltage Bushing.Bushing Replaced W/Spare Component
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-022, :on 850528,loss of Zone I & Zone III Reactor Bldg Ventilation Occurred,Causing Automatic ESF Actuation. Caused by Communication Error Between Personnel Conducting 18-month Logic Sys Test.Personnel Counseled |
- on 850528,loss of Zone I & Zone III Reactor Bldg Ventilation Occurred,Causing Automatic ESF Actuation. Caused by Communication Error Between Personnel Conducting 18-month Logic Sys Test.Personnel Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-022-01, :on 850703,instrumentation & Controls Technician Inadvertently Connected Test Equipment to Electronics Module for Reactor Water Cleanup Sys.Technician Counseled.Rear Input Wires Labeled |
- on 850703,instrumentation & Controls Technician Inadvertently Connected Test Equipment to Electronics Module for Reactor Water Cleanup Sys.Technician Counseled.Rear Input Wires Labeled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-023-01, :on 850805,unit Scrammed Due to Turbine Control Valve Fast Closure Trip.Caused by Technician Error.Rcic Manually Initiated to Maintain Vessel Level.Special Rept to Be Filed Per Tech Spec 4.7.3d |
- on 850805,unit Scrammed Due to Turbine Control Valve Fast Closure Trip.Caused by Technician Error.Rcic Manually Initiated to Maintain Vessel Level.Special Rept to Be Filed Per Tech Spec 4.7.3d
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-023, :on 850611,manual Isolation Valve 141005 Found Open.Caused by Inability to Perform Required Surveillance Testing on Excess Flow Check Valve XV-141F009.Procedures Revised |
- on 850611,manual Isolation Valve 141005 Found Open.Caused by Inability to Perform Required Surveillance Testing on Excess Flow Check Valve XV-141F009.Procedures Revised
| 10 CFR 50.73(a)(2)(i) | | 05000387/LER-1985-024, :on 850609,HPCI Declared Inoperable Due to Inability to Meet Flow & Discharge Pressure Requirements. Caused by Incorrect High Speed Setting of Turbine Control Sys.High Level Signal cut-off Raised |
- on 850609,HPCI Declared Inoperable Due to Inability to Meet Flow & Discharge Pressure Requirements. Caused by Incorrect High Speed Setting of Turbine Control Sys.High Level Signal cut-off Raised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000388/LER-1985-024-01, :on 850807,reactor Water Cleanup Containment (RWCU) Inboard Isolation Valve Closed on High Sys Flow Signal.Caused by Fast Opening of Filter/Demineralizer Inlet Valve.Rwcu Operating Procedure Revised |
- on 850807,reactor Water Cleanup Containment (RWCU) Inboard Isolation Valve Closed on High Sys Flow Signal.Caused by Fast Opening of Filter/Demineralizer Inlet Valve.Rwcu Operating Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-025, :on 850619,B Trains of Standby Gas Treatment & Control Room Emergency Outside Air Supply Sys Actuated Due to Trip of Exhaust Duct Radiation Detector B.Caused by Buildup of Contaminated Particles |
- on 850619,B Trains of Standby Gas Treatment & Control Room Emergency Outside Air Supply Sys Actuated Due to Trip of Exhaust Duct Radiation Detector B.Caused by Buildup of Contaminated Particles
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000388/LER-1985-025-01, :on 851005,phase-to-ground Fault Occurred on 500 Kv Transmission Lines Due to Lightning Strike.Failure of Auxiliary Relay Resulted in Isolation of Generator.Caused by Stuck Relay.Relay Repaired |
- on 851005,phase-to-ground Fault Occurred on 500 Kv Transmission Lines Due to Lightning Strike.Failure of Auxiliary Relay Resulted in Isolation of Generator.Caused by Stuck Relay.Relay Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000387/LER-1985-026, :on 850624,during Testing of HPCI Sys,Oil Leak Discovered on HPCI Steam Stop Valve Oil Supply Flange. Caused by Loose Nuts Securing Stop Valve Oil Supply Flange. Nuts Torqued & Leak Test Performed |
- on 850624,during Testing of HPCI Sys,Oil Leak Discovered on HPCI Steam Stop Valve Oil Supply Flange. Caused by Loose Nuts Securing Stop Valve Oil Supply Flange. Nuts Torqued & Leak Test Performed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
|