ML20137M936

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Insp Repts 50-321/85-33 & 50-366/85-33 on 851028-29,1118-22 & 1216.No Violation or Deviation Noted.Major Areas Inspected:Allegation Involving post-accident Sampling Sys & Plant Liquid & Gaseous Radioactive Effluents
ML20137M936
Person / Time
Site: Hatch  
Issue date: 01/06/1986
From: Cline W, Stoddart P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20137M906 List:
References
50-321-85-33, 50-366-85-33, NUDOCS 8601290104
Download: ML20137M936 (13)


See also: IR 05000321/1985033

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION 11

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101 MARIETTA STREET, N.W.

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ATLANTA, GEORGI A 30323

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Report Nos.:

50-321/85-33 and 50-366/85-33

Licensee:

Georgia Power Company

P. O. Box 4545

Atlanta, GA 30302

Docket Nos.:

50-321 and 50-366

License Nos.:

DPR-57 and NPF-5

Facility Name:

Hatch 1 and 2

Inspection Conducted:

October 28-29, November 18-22, December 10, and

D

ber 16, 1985

Inspector:

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P. St

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Approved by:

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  1. W.'E.'ClineP Seection Chief

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Radiological Effluents and Chemistry Section

Division of Radiation Safety and Safeguards

SUMMARY

Scope:

This special, unannounced inspection entailed 41 inspector-hours onsite

in the areas of investigation of an allegation involving the Post Accident

Sampling System (PASS) and plant liquid and gaseous radioactive effluents.

Results:

No violations or deviations were identified.

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REPORT DETAILS

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1.

Persons Contacted

Licensee Employees

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    • H. Nix, General Manager

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P. E. Fornel, Site QA Manager

      • G. Goode, Plant Engineering Superintendent
      • T. Greene, Deputy General Manager
      • Z. Wahab, Balance of Plant Engineering Supervisor
  • A. Fraser, QA Engineer
  • F. Tsakeres, Senior Health Physicist - C,orporate Office
      • R. Zavadoski, Manager, Health Physics and Chemistry
      • R. Rogers, Health Physics Superintendent

N. Dyar, Security Supervisor

    • V. McGowan, Chemistry Supervisor

D. Vaughan, QA Engineer

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S. Ewald, Corporate Health Physicist

R. Ott, Training Supervisor

J. Richardson, PASS Engineer

T. Wells, Acting Balance of Plant Supervisor

C. James, Shift Technical Advisor

C..Stancil, Instrument Shop Supervisor

    • M. Bray, Quality Assurance Engineer

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D. Elder, Quality Assurance Engineer

M. Carter, Quality Assurance Engineer

M. Kehoe, Quality Assurance Engineer

    • C. Goodman, Acting Regulatory Compliance Supervisor

E. Burkett, Senior Plant Enginear

B. Arnold, Chemistry Lab Supervisor

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NRC Resident Inspectors

    • P. Holmes-Ray, Senior Resident Inspector
  • Attended exit interview on October 29, 1985.
    • Attended exit interview on November 22, 1985.
      • Attended both exit interviews on October 29 and November 22, 1985

2.

Exit Interview

The inspection scope and findings were summarized on October 29, and

November 22, 1985, with those persons indicated in Paragraph 1 above.

The

licensee did not identify as proprietary any of the materials provided to or

reviewed by the inspector during this inspection.

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3.

Allegation, Discussion and Findings

On October 18, 1985, Region II received, by mail, an anonymous allegation

concerning operations at the Georgia Power Company's Plant Hatch, located

near Baxley, Georgia.

As of December 16, 1985, no followup letters or

additional allegations had been received and no further contact had been

made by the alleger.

The allegation consisted of a number of statements concerning plant systems

and inferred certain plant system interactions or related effects.

Each of

the several technical aspects of the allegation was investigated in depth

and possible correlations or links were sought between the statements of the

allegation and plant conditions and plant operating records.

The allegation first stated that a " situation" (an apparent shortcoming)

currently existed (approximately October 15, 1985) at Plant Hatch involving

the Post Accident Sampling System (PASS).

It was alleged that the PASS and

three additional, plant systems were involved or in some unspecified way

were related to the " situation" and that the licensee had violated Federal

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Codes and Regulations by failing to file a report.

No specific federal code

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or regulation was cited in the allegation.

On October 28-29, 1985, and again on November 18-22, 1985, a Region II

inspector went to the Plant Hatch site for the purpose of determining the

validity or circumstances of the allegation.

On December 10, 1985, the

inspector went to the Georgia Power Company corporate offices in Atlanta,

Georgia, to review a report of an investigation made by Georgia Power

Company staff of the same allegation, based on a copy of the allegation

received from an unidentified source.

During the November 18-22, 1985 portion of the inspection, the inspector

requested the licensee to supply documentation on the qualifications of

persons known to have installed certain items of safety grade equipment in

the PASS liquid sample lines; this information was received December 16,

1985.

The results of the inspector's findings are described below.

a.

Allegation

"I need to advise you of a situation that presently is existing at the

E. I. Hatch Nuclear plant in Baxley, Ga.

It involves the Post Accident

Sampling System now in use at the plant.

From July 1st thru July 21st,

the plants Radiological waste tanks have been discharged into the

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Altamaha river.

The computer print out showed no variation in the

spectrum of all of those tanks."

Discussion

Processed radioactive liquid wastes containing low level concentr.ations

of radioactive material are routinely discharged from Plant Hatch' to

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the Altamaha River.

Such releases have been routine procedure at Plant

Hatch since plant startLp and are considered as routine practice at

most nuclear power plants.

Radioactive discharges are permitted by the

NRC when they are within the limits in plant Technical Specifications

and conform to the limits of 10 CFR Part 20.

The inspector reviewed plant records for the period of July 1-21, 1985

(the period specified in the allegation), and found no evidence of

increased or unusual liquid discharges and that all releases were in

conformance with Technical Specification requirements.

Gamma radiation spectrum analyses of pre release samples from all

processed liquid radwaste holdup tanks for the period of July 1-21,

1985, were reviewed by the inspector.

The spectra were contained in

119 release procedure packages prepared for the administrative control

of releases and were made prior to release.

Many of the spectra were

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similar in certain respects, as in the recurrence of certain identified

nuclides but in no case were any two spectra identical.

Spectra were

examined for similarity as to (1) identity of radionuclides, (2) energy

value, in MeV, for each peak, (3) height or intensity of each peak, (4)

full width half maximum (FWHM) of each peak, (5) source of input

stream, and (6) age of sample.

Similaritie: in gamma radiation spectra

are to be expected when a reactor is operating normally and has been at

power for an extended period of time.

Differences attributable to

statistical variances, age of sample, and source of material, should be

expected to provide sufficient variation in spectra printouts to assure

that each printout differs in several respects.

Such differences were

observed in the examined spectra and no two spectra were identified as

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being identical.

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The inspector was able to identify a situation which may have been

misunderstood or mistaken by the writer of the allegation.

It was

noted that in the training program which preceded the implementation of

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the Radiological Effluent Technical Specifications (RETS) on July 1,

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1985, the training Lesson Outline required the operator of the RETS

computer program (used to calculate the effects of releases of

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radioactive liquids from the processed radioactive liquid waste tanks)

to " call up" a ore existing radionuclide spectrum from the computer

memory files.

the stored spectrum, which was used to simulate the

analysis of a liquid waste sample containing several typical nuclides,

was employed to shorten the sample counting time to allow more people

to be trained in a given class period.

If a typical routine reactor

coolant sample had been employed, a counting time of one hour or more

could have been required for each sample in order to accumulate

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sufficient data.

Since the identical spectrum would have been printed

out from computer memory each time during training, this may have been

the source of the part of the allegation that the spectra for all

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analyses of liquid radwaste tanks for the period July 1-21, 1985 were

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identical.

As discussed in the preceding paragraph, no basis was found

to substantiate the allegation so far as the record packages for each

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actual release of processed liquid radwaste were concerned.

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The allegation infers that operation of the PASS with the reactor

operating normally would result in release of radioactive material to

the environment or, in this case, to the Altamaha River.

Liquid

drainage resulting from the occasional use of the PASS in training

exercises or periodic checkout is collected in the coolant grade or

high purity waste collection system for cleanup and recycle back to the

reactor water makeup tank or to the reactor coolant system.

Depending

on water inventory, it is occasionally necessary to reduce the reactor

coolant system water inventory by transferring water from the high

purity system to the low purity system, where it is mixed with other

radioactive plant water, treated, and periodically released to the

Altamaha River.

Waste water from the low purity system is filtered,

treated with ion exchange resin beds, or demineralizers for possible

discharge.

When a processed liquid waste holdup tank is filled, it is

mixed thoroughly and then sampled.

The sample is then analyzed for

radioactivity content.

If the analysis shows that the sample meets

administrative criteria for radioactivity content and if a dose

projection based on calculations of the release of the tank contents

shows that Technical Specification guidelines will not be exceeded,

then approval can be made to release the material to the Altamaha

River.

It was noted that the normal sampling point for reactor coolant samples

generates a larger volume of liquid waste than the PASS and is

typically used three times daily, while the PASS is used only

occasionally during required tests and in the training and qualifi-

cation of PASS operators.

Since the same fluid is being sampled in

each case, the normal sampling system would be expected to generate

substantially a larger volume of waste than the PASS.

Records of

analyses of reactor coolant samples for the period July 1-21, 1985

indicated low levels of radioactive materials consistent with a low

incidence of fuel leakage and did not indicate any radioactive release

which could be attributed to operation of the PASS.

Finding

The allegation was not substantiated.

" Radiological" (radioactive)

waste tanks containing processed and analyzed radioactive liquids were

routinely discharged in accordance with NRC regulations and the plant

Technical Specifications.

Nothing was found to be abnormal in the

releases occurring between July 1 and July 21, 1985.

One-hundred and

nineteen (119) waste tank sample analysis gamma spectra were examined,

covering all releases during the specified period, and substantial

variations in the spectra were observed in each instance.

b.

Allegation

"A technician accidentally discovered this was taking place and he

immediately notified his foreman.

An investigation took place and it

was discovered that the PASS System was improperly set up."

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Discussion

The lack of specific detail in the allegation severely limited the

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inspector's investigation.

Names, dates or plant locations which might

have aided in identifying this matter were absent.

The inspector

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discussed the allegation with members of the plant staff and reviewed

plant records and logs but was unable to obtain additional information

as to the existence of either a natification of a foreman by a

technician or the occurrence of an investigation which concluded that

the PASS was improperly set-up.

A NRC contractor performed an operational evaluation of the PASS in

December 1984.

In that evaluation, three items unrelated to the

allegation were identified.

These were: (1) the gas flow rate meter

in the dissolved hydrogen analytical section of the PASS was oversized

and inaccurate for the expected flow and should be replaced with a

smaller capacity flowmeter; (2) the undiluted reactor coolant grab

sample gamma spectroscopy analysis did not meet the required accuracy

guidelines, indicating that a representative sample had not been

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obtained; and (3) an attempt to take an iodine sample using the PASS

grab sample port fittings was unsuccessful.

These items were concerned

with specific components of the PASS system and could not be related to

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the allegation as presented.

To ensure that the PASS was fully operable, the inspector reviewed the

licensee's actions taken to resolve the evaluation items.

Item (1) was

determined to have been the result of an erroneous assumption on the

part of the evaluator in that the flowmeter provided for the dissolved

hydrogen measurement was correctly sized for the value of dissolved ,

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hydrogen specified by the existing criteria.

The nuclear steam supply

system vendor had proposed a smaller value for dissolved hydrogen; the

evaluator was under the impression that the smaller value had been

accepted by NRC.

This was not the case and the larger value remains

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the applicable criterion.

(Closed) Inspector Followup Item (IFI) 321, 366/84-50-01 - Licensee

does not meet accuracy Guidelines for Dissolved Hydrogen Measurements.

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Item based on erroneous assumption.

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Item (2) was concerned with a discrepancy between the analytical

results of a reactor coolant sample taken frca the PASS through a

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manually operated " grab" sample fitting and the results of a routine

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reactor coolant sample taken at the sample station used for reactor

coolant samplS 1 during normal operations.

A licensee representative

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stated that t'a cause of the discrepancy between the samples had been

resolved and that subsequent tests had shown close correlation.

The

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inspector observed as a licensee employee obtained a sample from the

PASS grab sample port, witnessed the preparation of the sample for

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analysis, and reviewed the analysis.

The multiple channel analyzer

printout of the gamma spectrum and the associated computer radionuclide

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identification for the PASS grab sample were compared to the results of

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a normal reactor coolant sample analysis made at approximately the same

time.

Close correlation was seen for the characteristic fission

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product nuclides.

The differences varied from 11.1% for Iodine-133 to

117% for Iodine-134.

Values for the activation product Sodium-24

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varied by 120%.

Since the NUREG-0737 criterion for these measurements

is 1200% (a factor of two), the values obtained were within the

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acceptable range.

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(Closed) IFI 321, 366/84-50-02 - Licensee does not neet all criteria

for backup Liquid Grab Sample.

Re-evaluation showed acceptable

accuracy.

Finding

The allegation was not substantiated.

In the absence of adequate

specific information as to the identity of person or persons involved,

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dates, or plant locations, the inspector was unable to confirm that the

alleged circumstances either occurred or did not occur.

Discussions

with plant staff did not result in additional information.

c.

Allegation

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" ... Rather than bringing in qualified people to install the system

(deletion)

two plant employees who were ... not qualified

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(were used) to implement the system and it was done completely wrong.

Both employees went to work elsewhere knowing that what they did was

wrong and they didn't want to be around when their mistakes were

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discovered ... "

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Discussion

Since no names were given for the two plant employees alleged to be

involved, and since the inspector was unable to otherwise identify the

two plant employees, the inspector was unable to discuss the allegation

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with the persons concerned.

Plant staff members informed the inspector

that ten or more corporate engineers and 30 or more plant and

contractor employees participated in various aspects of the

installation and checkout of the post accident sampling system (PASS).

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The additional number of architect-engineer, vendor and contractor

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engineers, technicians and craftsmen associated with installation and

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implementation is not known with any certainty.

Seventy-two (72)

Georgia Power Company employees and vendor or contractor employees were

specifically identified from plant records as having participated in

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PASS installation, implementation and operation up to and including

November 1, 1985.

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The principal components of the PASS, specifically all of the PASS

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downstream of the second outboard isolation valves on each RCS sampling

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line, were not required to be designed, constructed or installed to

" safety related" criteria since they are not essential to the safe

operation of the reactor, do not affect the safe shutdown of the

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reactor, and are not required to mitigate the consequences of an

accident.

The licensee requires that persons " qualified" to install or repair

" safety related" equipment must be trained and tested to criteria

established by the licensee to meet the requirements of General Design

Criteria (GDC) 1 of 10 CFR Part 50 and of Appendix 8 to 10 CFR Part 50.

Persons installing or repairing "non-safety grade" equipment must also

be trained and tested to licensee criteria; however, the applicable

criteria are less stringent than those applied to " safety grade"

equipment.

Additionally, craft workers must also meet the minimum

union training and experience requirements to hold union status.

As the allegation was written, the inspector could not ascertain

whether

the alleger was

referring

to

safety-related or

non safety related aspects of the PASS.

If the alleged work was done

on a " safety related" section of the PASS by workers qualified to the

less stringent licensee criteria for non-safety grade work, this could

have led to a violation of GDC 1 and Appendix B,

10 CFR 50

requirements.

The information provided in the allegation was not

sufficient to support the charge nor was the inspector able to

determine the validity based on records review, examination of

eguipmentanddiscussionwithlicenseerepresentatives.

The writer of the allegation used the terms " install" and " implement"

in apparent reference to the same job or task.

" Install" is usually

taken to mean the physical placement and assembly of a system such as

the PASS, including all activities necessary to get the system ready

for operation.

Such activities included electrical, plumbing,

mechanical and electronic control connections.

" Implement" is usually

taken to mean performing the activities necessary to prepare the

installed system (PASS) for operational use in the plant.

Such

activities included acceptance testing, adjustments, repairs or

modifications of the system necessary to make it operational,

verification of the design functions and capabilities of the system,

preparing operational procedures, the training of operations personnel

in the use of the system and the training of maintenance personnel in

the maintenance of the system.

Discussions with PASS system engineers

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indicated that as many as ten engineers and an estimated 30 to 40 craft

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workers were associated with the installation of the PASS and that as

many as eight engineers and 20 to 25 technicians were associated with

the implementation of the PASS.

Chronologically, the PASS was ordered in September 1980, the first

components were delivered in early 1982, and installation was completed

in June 1983, when hot functional tests initiated the implementation

phase.

Full implementation was completed August 1, 1984, approximately

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one year prior to the period specified in the allegation.

The fourteen months required for full implementation was the result- of: g

series of problems primarily caused by two defective pressure

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reduction valves in the reactor coolant sampling line.

Both of these

valves were nuclear grade, safety related items.

Both failed by

internal leakage, which allowed full reactor coolant pressure to enter

the PASS system instead of performing the design function of reducing

pressure to a maximum of 60 psig.

The resulting overpressure caused

the rupture of several components of the automatic chemical analytical

subsystem.

Substantial delays were entailed in the re-design and

fabrication of the custom-built replacement components.

Minor leaks

also developed in other system valves and components and these were

either repaired or replaced.

The defective nuclear grade valves were

replaced with nuclear grade valves of a different design and

manufacturer.

The replacement values have performed in a satisfactory

manner.

In no instance was any PASS system valve or other component found to

have been improperly installed as the allegation implies.

The writer of the allegation used the term " qualified" without being

specific as to what sense of the term was meant.

There are several

degrees of " qualification" which may be aoplied to the licensee's

evaluation or assessment of an individual with respect to that

individual's training, experience, education and skill or competence in

performing a specific task or craft.

For example, a welder applying

his skills for non nuclear applications would be required to

demonstrate a lesser degree of proficiency or " qualification" in

welding than a welder employed to perform welding on a nuclear grade or

safety-related pipe.

Since the PASS was a new and unique system, there was no " qualified

person" available since no one had previously operated a similar

system; procedures had to be written based on vendor instructions and

test experience; and, no instructor was available to teach system

operation to the implementing personnel.

It was only after the PASS

was installed and available for implementation that training

procedures could be written and formal training provided to qualify

individuals to operate the PASS.

Implementation of the Hatch PASS was

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performed by a number of individuals who had previously demonstrated

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competence in doing similar work.

Each step was performed under a

Quality Assurance Program and was subjected to surveillance.

By

corporate and industry policy and practice the PASS was implemented by

qualified personnel.

In view of the licensee's practices in qualifying

personnel to operate this "first-of-a-kind" system, the alleger's

concern about lack of a " qualified person" cannot be supported.

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As an example of the qualification of personnel to work on ESF systems,

the inspector requested the licensee to provide the qualification

records of the welders who installed replacement PASS liquid sample

line isolation valves in 1984.

On December 16, 1985, the licensee

transmitted copies of the welding qualification records of the six

welders who did the welding which connected the replacement isolation

valves to the PASS liquid sample lines.

The documentation verified

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that the welders had been examined in accordance with the requirements

of Section IX of the ASME (American Society of Mechanical Engineers)

Code.

Finding

The allegation was not substantiated.

More than 70 licensee, vendor

and contractor personnel were involved in the installation and

implementation of the PASS, not two as stated.

No circumstances could

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be identified as having any correlation to the statement that "... it

was done completely wrong."

d.

Allegation

"At present (the allegation was apparently written approximately

October 10, 1985) an outside contractor has been brought in to

straighten out this mess."

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Discussion

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Based on the inspector's discussions with several plant staff engineers

and employees and on review of plant records on the PASS, no "outside

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contractor" had been brought in to work on the system at the

approximate date of the allegation and either prior to or subsequent to

that date.

Licensee representatives stated that during the period of

installation and implementation of the PASS, from early 1982 until

August 1,1984, several representatives of the PASS vendor, two vendor

subcontractors, and the architect engineering firm were at the Hatch

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facility at various times to support the installation of the PASS and

to provide technical assistance during the implementation phase.

It is

possible that some of these persons might be the "outside contractor"

referred to in the allegation; however, the period of time involved,

i.e. ,1982 to 1984, does not coincide with the period specified in the

allegation.

In discussions with licensee representatives and the

various system engineers and from review of the licensee's maintenance

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history files for the PASS, the inspector was not able to identify any

"outside contractor" as having been specifically brought in to resolve

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any problem connected with the PASS other than outlined above.

Finding

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The allegation was not substantiated.

The inspector found no evidence

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of an "outside contractor" having been brought in for any purpose

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having to do with the PASS since the PASS implementation date of

August 1, 1984,

e.

Allegation

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numerous valves

were improperly installed (in the PASS

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...

system).

Because of this, the off gas readings read incorrectly and no

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one could determine how much radioactive gas was discharged into the

environment."

Discussion

The allegation contains a technical discrepancy in that the "off gas

system" is a separate dedicated system which processes air and

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noncondensible gases extracted from the main condenser and is unrelated

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to the PASS.

The "off gas" system has a limited operating capacity and

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is designed for a nominal input of 30 standard cubic feet per minute of

condenser air inleakage.

Any extraneous air inputs to this system

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would defeat the system's design function of minimizing the release of

short-lived fission product noble gases to the environment.

It is

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extremely unlikely that this was the system to which the alleger meant

to refer.

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It is more likely the alleger meant to refer to one of the building

ventilation exhaust systems.

The PASS system is physically located in

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the area designated as the " hot machine shop" within the Unit 2 reactor

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building.

The PASS area ventilation is vented to the reactor building

ventilation system, which is treated through HEPA filters and charcoal

absorbers prior to release to the en, conment.

Each building vent

release point is continuously monitored by a detector sensitive to

radioactive noble gases which may be present in the exhaust air.

Additionally, continuous samples of airborne particulate material and

airborne iodine are collected for periodic analysis,

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The allegation implies that the "off gas readings read incorrectly" as

a result of improper installation of valves in the PASS.

It should be

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recognized that the improper installation of a valve in the PASS would

likely have no physical effect on the operation of radiation detection

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instruments monitoring the releases of radioactive materials in plant

gaseous effluents.

If a valv( were to be installed incorrectly, system

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operation would likely be af fected in such a manner as to be identified

during the system checks and verifications made during system

implementation.

No improper insta'lations were identified.

However, a

defective valve properly installed could and did result in a leak of

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liquid and gas to the PASS area.

In the latter event, however, the level

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of activity in the primary coolant was sufficiently low that the event

was of little consequence from a radiological stand point.

This

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occurred during functional testing beginning in June 1933, and does not

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coincide with the period covered by the allegation.

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During the entire period specified in the allegation, i.e. , " July 1

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through July 21" (presumed to mean July 1-21, 1985), plant logs

indicated that all effluent monitoring instrumentation was functioning

properly.

The inspector noted that the log of gaseous effluent monitor

operation for July 25-26, 1985, showed the Unit 1 post-treatment of f-

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gas noble gas monitor to. be. out-of-service; however, the downstream

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main stack effluent monitor, which serves as a backup, was. operab3etand

show ed 'no increase in effluent activity.

It is possible that'th'ii'may

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have been the monitor referred to in the allegation; however there is

no technical basis for any imputed relation between PASS malfunction

and the outage cf this instrument.

Finding

The allegation was lot substantiated.

The inspector could find no

evidence that an improperly installed valve in the PASS system could in

any manner affect the radiation detection instrumentation of a totally

separate system such as the of f gas system.

Two defective valves had

been part of the original installation but were replaced in 1984, more

than a year prior to the period of time covered by the allegation.

f.

Allegation

"Under the Code of Federal Regulation, the NRC must be notified of any

improper release to the environment . . . no reports (were made) ...

actions violated Federal Codes (and) Regulations."

Discussion

The allegation failed to cite specific instances of either " improper"

or abnormal releases of either liquid or gaseous radioactive effluents.

The inspector reviewed plant records and logs for the specified period

and did not identify any releases exceeding any existing regulations or

Technical Specifications.

In the absence of specific information

concerning such improper releases and in the absence of any information

or records indicating or confirming that such improper releases

actually occurred, the inspector concluded that no regulatory

requirements had been violated.

Finding

The allegation was not substantiated.

Nothing was found in plant

records or in discussions with plant personnel concerning the

allegation to indicate that any regulatory requirements had been

violated or exceeded. The inspector concluded that no reporting

requirement had been violated.

4.

Georgia Power Company Investigation in Response to Allegations

Prior to the inspector's first visit to Plant Hatch (October 28, 1985),

Georgia Power Company had obtained a copy of the allegation from an

unidentified source and had conducted and completed their own investigation

of the allegation.

The inspector reviewed a copy of the Georgia Power

Company investigation report.

The allegation appeared to be a copy of the allegation received at RII and

no differences in appearance, wording, or phrasing were apparent.

The

investigation report of the allegation by Georgia Power Company concluded

that no regulatory requirements were violated.

The licensee's investigation

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report found that an independent consultant had been hired in early 1985,

for the purpose of adapting a computer program to fit the needs of the Hatch

site relative to the Radiological Effluent Technical Specifications (RETS)

and the calculation of offsite radiation doses resulting from plant

radioactive _ releases.

The subject computer program, however, had no bearing

on or connection with the operation or functioning of the PASS.

The

licensee concluded that it was possible that this individual may have been

the "outside contractor" referred to, if it can be assumed that the alleger

mistook the implementation of the Radiological Effluent Technical

Specifications (RETS) for the implementation of the PASS.

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