ML20137L521

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Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-312/85-30
ML20137L521
Person / Time
Site: Rancho Seco
Issue date: 01/22/1986
From: Kirsch D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To: Reinaldo Rodriguez
SACRAMENTO MUNICIPAL UTILITY DISTRICT
References
NUDOCS 8601280009
Download: ML20137L521 (1)


See also: IR 05000312/1985030

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Docket No. 50-312

Sacramento Municipal Utility District

P. O. Box 15830

Sacramento, California 95813

Attention:

Mr. R. J. Rodriguez

Executive Director for Nuclear Operations

Gentlemen:

Thank you for your letter dated December 23, 1985, informing us of the steps

you have taken to correct the items which we brought to your attention in our.

letter dated November 20, 1985. Your corrective actions will be verified

during a future in;pection.

Your cooperation with us is appreciated.

Sincerely,

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Dennis F. Kirsch, Acting Director

Division of Reactor Safety and Projects

bcc w/ copy of letter dated 12/23/85:

J. Martin

B. Faulkenberry

G. Cook

RSB/ Document Control Desk (RIDS)

Resident Inspector

Project Inspector

State of CA

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SACRAMENTO MUNICIPAL UTILITY DISTRICT O 6201 S Street. P.O. Box 15830. Sacramento CA 95852-1830.(916) 452 3211

AN ELECTRIC SYSTEM SERVING THE HEART OF CALIFORNIA

RJR 85-595

December 23,1985

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J B MARTIN REGIONAL ADMINISTRATOR

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REGION V 0FFICE OF INSPECTION AND ENFORCEMENT

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NOTICE OF VIOLATION FOR NRC INSPECTION 85-30

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The Sacramento Municipal Utility District hereby submits in Attachment I to

this letter, a response to the subject Notice of Violation in accordance with

10 CFR 2.201.

If there are any questions concerning this response, please

act Mr. Ron W. Colombo at the Rancho Seco Nuclear Generating Station.

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ASSISTANT GEN AL MANAGER,

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ATTACHMENT I

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DISTRICT RESPONSE TO NRC INSPECTION 85-30

NOTICE OF VIOLATION

As a result of the inspection conducted by Mr. J. Eckhardt and Mr. G. Perez

between September 28 and October 31, 1985, the following two (2) violations

were identified. Each violation is followed by the District's response to~

the violation.

A.

Technical Specification 6.8.1 requires that written procedures be es-

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tablished, implemented, and maintained covering activities including

surveillance and test activities of safety related equipment. Also,

Administrative Procedure 2 " Review, Approval and Maintenance of Pro-

cedures" establishes the licensee's guidelines for revisions or

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temporary changes to procedures.

Contrary to the above requirements, on September 29, 1985, the licensee

used an unapproved procedure in performing the calibration of the A

channel power range instrument.

DISTRICT RESPONSE:

On September 29, 1985, Instrumentation and Control (I&C) Procedure I.103,

" Power Range Calibration," was being performed with the reactor power level

at approximately 2.51

The power level was not sufficient to allow the pro-

cedure to be performed as written. The I&C technician, using outside instruc-

tions in violation of the procedure, changed a multiplier link from 10X tn IX

so that Section 6.3 of I.103 could be completed. The event was observed by a

NRC resident inspector and reported to the shift supervisor.

The I&C technician,

upon realizing his violation of the procedure, prepared an internal Occurrence

Description Report (AP.22) to alert plant management personnel of the concern.

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The immediate action taken to address the procedure violation was to incorporate

a temporary change in Revision 7 of I.103 to include instructions describing

how to change the multiplier link from 10X to IX. This action was completed

on September 29, 1985. A permanent revision to I.103 is being prepared to in-

clude the multiplier link change instructions.

The procedure revision will be

completed and full compliance achieved by February 28, 1986.

B.

Technical Specification 3.1.2.2 states, in part "...Heatup and cooldown

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rates chali G t exceed the rates stated on the associated figure." Figure

3.1.2- ) states a reactor coolant system cooldown rate of 100 F/Hr at

temperatures greater than 270F.

~ On October 2, 1985, with the reactor at approximately 15 percent power, a

loss of main feedwater caused a high reactor coolant system pressure,

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resulting in a reactor trip. Primarily due to the inappropriate opening

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of the fourth point feedwater heater relief valves,.the reactor coolant

-temperature decreased to below the normal post reactor trip temperature

of approximately 550 F to approximately 490 F in 20 minutes.

This cooldown exceeded the Technical Specification limit as specified

above and is a Severity Level IV Violation (Supplement I).

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DISTRICT RESPONSE:

The District has evaluated the October 2, 1985 reactor trip and agrees that ex-

ceeding the Technical Specification 3.1.2-2 reactor coolant system cooldown

rate was primarily caused by the. inappropriate lifting of the 4A/4B heater

steam relief valves. When the unit is tripped, pegging steam..is supplied to

the 4A/48 heaters to provide preheating to the feedwater.

The pegging steam

pressure controller should control the pressure at a point lower than the

relief valve setpoints.

It was found that the controller setpoints were

adjusted so that the controller dead band actually overlapped the relief valve

setpoints.

This led to the lifting of the relief valve and subsequent cool-

down.

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To address this concern, the relief valve setpoints.were raised and the

pegging steam pressure controller setpoints were reduced accordingly. A sub-

sequent reactor trip on December 5, 1985, resulted in lifting the relief valves

and revealed that the concern had been only partially resolved, even though

the cooldewn rate was consistent with normal post-trip response. Although

the setpoints were found to be satisfactory, it was found that the controller

had an overshoot characteristic that had not been taken into consideration.

An engineering evaluation concluded that the pegging steam controller setpoint

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should be further reduced to compensate for this condition. Following this

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final setpoint adjustment, functional test STP.187, "2nd, 3rd, 4th point FWH

Relief Valve Test," was performed. STP.187 tests the relationship between the

pegging steam controllers and the opening of the 4A/4B heater steam relief valves.

The test demonstrated that, with the final setpoints, pegging steam '#ill be

supplied to the 4th point feedwater heaters without lifting the relief valves

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following a plant trip.

Full compliance was achieved with the' successful completion of this test on

December 7, 1985.

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