ML20136G796
| ML20136G796 | |
| Person / Time | |
|---|---|
| Site: | Beaver Valley |
| Issue date: | 10/31/1985 |
| From: | Smith P DUQUESNE LIGHT CO. |
| To: | |
| Shared Package | |
| ML20136G794 | List: |
| References | |
| NUDOCS 8601080562 | |
| Download: ML20136G796 (8) | |
Text
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NARRATIVE
SUMMARY
OF 1
MONTHLY OPERATING EXPERIENCE OCTOBER 1985 l
l October 1 At 2001 hours0.0232 days <br />0.556 hours <br />0.00331 weeks <br />7.613805e-4 months <br /> on October 1, the power level was through reduced to perform maintenance on Condensate Pump October 3
( CN-P-1 A).
Maintenance was completed at 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> t
on October 2 and power level was subsequently increased.
l The repairs made failed to resolve the problem and following a pump performance evaluation, power level was again reduced at 0045 hours5.208333e-4 days <br />0.0125 hours <br />7.440476e-5 weeks <br />1.71225e-5 months <br /> on October 3 and a complete overhaul was begun on the Condensate Pump.
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October 4 A reactor trip due to the loss of Vital Bus III occurred j
at 1402 hours0.0162 days <br />0.389 hours <br />0.00232 weeks <br />5.33461e-4 months <br />. The reactor was taken critical at 1911 hours0.0221 days <br />0.531 hours <br />0.00316 weeks <br />7.271355e-4 months <br /> and the Unit was synched to the grid at 2043 hours0.0236 days <br />0.568 hours <br />0.00338 weeks <br />7.773615e-4 months <br />.
October 5 The Station continued to operate at a reduced power through level of approximately 42% as overhaul work continued October 11 on Cor.densate Pump (CN-P-1A).
October 12 Repair work completed on the Condensate Pump (CN-P-1A) at 1900 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.2295e-4 months <br /> and power level was subsequently increased ~
L to nominal 100 percent at 2340 hours0.0271 days <br />0.65 hours <br />0.00387 weeks <br />8.9037e-4 months <br />.
1 October 13 The Station was in Operational Mode 1 with reactor power through at a nominal 100 percent.
Reactor Coolant System was October 24 at a normal operating pressure and temperature.
October 25 At 1149 hours0.0133 days <br />0.319 hours <br />0.0019 weeks <br />4.371945e-4 months <br /> on October 25, a reactor trip occurred l
through due to a Reactor Coolant System flow transmitter spike.
October 26 The reactor was taken critical at 0155 hours0.00179 days <br />0.0431 hours <br />2.562831e-4 weeks <br />5.89775e-5 months <br /> on the 26th and the Unit was synched to the grid at 0529 hours0.00612 days <br />0.147 hours <br />8.746693e-4 weeks <br />2.012845e-4 months <br />.
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October 27 The Station was operating at a power level of through approximately 95% due to flow induced noise and October 30 vibration in Feedwater Regulating Valve (FCV-FW-498).
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8601080562 851107 PDR ADOCM 0$000334 R
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October 1985 Summary of Monthly Operating Expertence i
October 31 At 1221 hours0.0141 days <br />0.339 hours <br />0.00202 weeks <br />4.645905e-4 months <br /> an Unusual Event was declared when i
contaminated water was found flowing from a pipe at l
Beaver Valley Unit I into a building located at Beaver l
Valley Unit II.
The initial as well as follow-up t
notifications were made to the NRC and others required by I
the Emergency Preraredness Plan. The Unusual Event was
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terminated at 1550 hours0.0179 days <br />0.431 hours <br />0.00256 weeks <br />5.89775e-4 months <br />.
Plant power output remained at approximately 95% throughout the day, i
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0
MAJOR MAINTENANCE 1.
Overhaul of Condensate Pump (CN-P-1A) i 1
a.,
,x_,
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OPERATING DATA REPORT DOCKET NO, _50-334 DATE 11/9/85 COMPLETED BY f A.
smith TELEPHONE. 417-661 1825
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OPERATING STATUS
- 1. Unit Name: Beaver Valley Power Station, Unit 'f1 Notes
- 2. Reporting Period:
October 1985
- 3. Licensed Thermal Power (MWt):
No
- 4. Nast.episte Rating (Grom MWe):
923
- 5. Demon Electrical Rating (Wt MWe):
835
- 6. Maximum Dependable Capacity (Grom MWe):
860
- 7. Maximum Dependable Capacity (Nt MWe):
810
- 8. If Chamens occur in Capacity Ratings (Items Nwnber 3 Through 7) Since Last Report, Give Reasons:
2
- 9. Power Level To Which Restricted,If Any (Net MWe):
None
- 10. Reasons For Restrictions. If Any; N/A This Month Yr..to.Dete
' Cumulative
!!. Hours in Reporting Period 745.0 7;296.0 83,304.0
- 12. Number of Hours Reactor Was Critical 725.8 6,788.0 44,143.7
- 13. Resetor Rewrve Shutdown Hours 0.0 0.0 4,482.8
- 14. Hours Generator on Line 720.7 6,635.7 42,718.6 l$. Unit Rewrve Shutdown Hours 0.0 0.0 0.0
- 16. Grom Therma! Energy Cenersted (MWH) 1,491,565.0
_16,004,565.9 99,403,079.9
- 17. Gross Electrical Energy Generated (MWH) 467.000.0 5.124.000.0 31.618.400.0
- 18. Net Electrical Energy Generated (MWH) 436.920.0 4.803.470.0 29,428,313.0
- 19. Unit Service Factor 96.7 90.9 53.7
- 20. Unit Aisilability Factor 96.7 90.9 53.7
- 21. Unit capacity Factor (Using MDC Nel 72 4 81.3 47.I
- 22. Unit Capacity Factor (Using DER Net) 70.2 78.8 45.7
- 23. Unit Forced Outage Rate 3.3 7.9 24.5
- 24. Shutdown (Scheduled Over Nem 6 Months tType. Date.and Duration of Eacht:
N/A
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Unlis In Test Status (Prior to Commercial Operationi:
Forecast Achieved j
INITIAL CRITICALITY N/A INITIAL ELECTRICITY N/A _
N/A N/A _
COMMERCIAL OPERATION N/A N/L (9/77)
AVERAGE DAILi UNIT power LEVEL 50-334 DOCKET.NO.
UNIT BVPS Und: #1 11/7/85 DATE P. A. Sn W:
COMPLETED BY TELEPHONE (412) 643-1825 OCTOBER 1985 Mom DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net)
(MWeNel 705 j
g7 791 627 830 2
g 218 747 3
178 4
20 829 789 I
23 788 6
22 260 788 I
23 786 8
3 9
303 378 3
261 501 10 24 02 755 gg y
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12 302 746 3
788 13 29 788 14 84 746 30 825 746 g3 3
16 788 INSTRUCTIONS
.I',
"*' P'*" Im!In MWe Nel for each day in the reputting month.C. mpute tu
- r i hole (9/77)
UNITSHUTDOWNS ANDPOWER REDUCTIONS DOCRE T NO.
50-314 UNIT NAME AVI'S Unitt i1 DATE 11/7/85 REPOR T MONIH OCTOBER COMPLE1 Fin gy P.A. Smith TELEPHONE f412) 643-1825 c^
% 60 O o*
0 Ct Licensee c
4 Cause & Corrective No.
Date E
3U Event
!=
5E Action to R
y5 l
f E" Report #
=3 a0 Prevent Recurrence e
o gmg yu g
e 33 851001 F
0 B
5 N/A HH PUMPIX At 2001 hours0.0232 days <br />0.556 hours <br />0.00331 weeks <br />7.613805e-4 months <br />, the power level was reduced to perform maintenance on Condensate Pump [CN-P-1Al.
Maintenance was completed at 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> on the 2nd.
34 851003 F
0 B
5 N/A HH PUMPII Power level was reduced at 0045 hours5.208333e-4 days <br />0.0125 hours <br />7.440476e-5 weeks <br />1.71225e-5 months <br /> and a complete overhaul commenced on Condensate Pump [CN-P-1Al.
35 851004 F
6.7 A
3 85-18 EC ELECOlt A reactor trip due to the loss of Vital Bus III occurred at 1402 hours0.0162 days <br />0.389 hours <br />0.00232 weeks <br />5.33461e-4 months <br />, The Station returned on-line at 2043 hours0.0236 days <br />0.568 hours <br />0.00338 weeks <br />7.773615e-4 months <br /> on the 4th.
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3 F: F w.eJ Reasem:
4 n.thod:
- 1. shebes G - lasteis tiains 5 S< heJa'eil A Fquipmens failure (I uplain) 1-Manu:1 leu feerarJ'* m 8 Da's B Maintenance i.e Tes8 2-Manual scene I nit) Sheets 1.w I a rence C Refueling 3-Autcestic Scrae F*csis Rep.=o si I H II sir iNilMI G D ReFula8'"> Resielcai.*
4-Continued From Previous Month 01613 I (hiesseus Toaining A IAense I sanwaati'*
5-Retuetton I AJnunesseiteve 9-Other 5
t, Operalsemd I sp. il splaeval I sluhet I Sainr %me.c P'/77)
II Osters il splane t e.
1 1
UNIT SHUIDOWNS AND POWER REDUCTIONS DOCKETNO.
50-334 UNIT NAME AVI'S Untit #1 ~
DATE - 11/7/85 REFOR T MONIH OCTOBER COMPLETEI) av P. A. Smith TEl EPilONE
- AU
- J-I D gn w MO d
o=
oot Licensee g
{
Cause, & Corrective No.
Date "e,
"5 E
3 u" Event gj Action to ee R
$5 5
- f..E "
Report #
f*@
g gu Prevent Recurrence H
O m
u 8
36 851004 F
0 B
5 N/A HH PUMPII Af ter returning to the Crid, the Station operated at a reduced power level as work continued on condensate Pump [CN-P-IA).
Work completed on the Condensate Pump at 1900 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.2295e-4 months <br /> on the 12th and the power level was subsequently increased.
37 851025 F
17.7 A
3 85-19 CB INSTRU At 1149 hours0.0133 days <br />0.319 hours <br />0.0019 weeks <br />4.371945e-4 months <br />, a reactor trip occurred due to a Reactor Coolant System flow transmitter spike.
i The Station was back on-line at 0529 hours0.00612 days <br />0.147 hours <br />8.746693e-4 weeks <br />2.012845e-4 months <br /> on the 26th.
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3 4
T: T.w eJ Reas.m :
Method:
E stul+it G - Insions tiims S 5< hedu'cJ A Figuipment raileveII uplaini 1-Mano.i t sin Pierma88 m 8 Ih'a B Maineenance e r Tes8
'2-Manual scra.
Intr > Siwers3.w Ia cmcc
)
0-Refueling 3-Autonette Scras bent Rep.= eI I HiI ele INIIRI G D Repidassw) Resisicti'"
4-Continued From Frevious Month (litel l I (hwsatin Tsaining A I.iscoise I sanenasi'*
5-Reduction i Adnunesseative 9-Other 5
f thwsate.mtal I ss..e ll mplassel I slubet I Sauer %me.c l**l77)
Ilthlicsilsplamit i
L
UNIT SifUTDOWNS AND POWER REDUCTM)MS DOCKET NO.
50-314 UNIT NAME __BVPS Unit i1 DATE 11/7/85 REM T WIN OCTOBER COMPLETEll ey F- ^- N Eh TELEFilONE (412) 643-1825 es 6.
ca be te O 0*
O C, O Licensee e
No.
Date 3 II E Event
!e
{E Action to Cause, & Corrective
$3 E
f.E "
Report #
H A
j"$
- g g
Prevent Recurrence m
o oa 38 851026 F
0 5
5 N/A CR VALVEZ After returning to the Crid, the Station operated at a reduced power level due to flow induced noise and vibration in Feedwater Eegulator Valve [FCV-FW-498I.
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1 2
F-T.= sed Reasen:
3 4
S-Schedn'cJ Methed:
A F; ';_ ; failevelt nyisint INhdwe G. insisus ehes B"'^_
_:;e e r Tess 1-seneu=1 l'w Petrasses.m a'l lia'a d
C Refueling 2-etennat Scree I ases Shcres 8.w l* rsesec D Reyselseos) Restricth"'
3-Autonetic Scram Isene Repest 1 i NII el< t NilRI G I O erraine Tsaineseg A liense l'zansnach" 4-Cosettassed From Frevious Month Ultill t
I Adnenestrati" 5-Bee.ction Pt/77) t thereatnestal I ssese il agilasest 9-Other 5
Il Ostics ii ig4amel I sisehes ! - Ssesm,Smesc t
e-
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