ML20133D207

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SALP Rept 50-382/96-99 for 950429-961130
ML20133D207
Person / Time
Site: Waterford Entergy icon.png
Issue date: 01/06/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20133D170 List:
References
50-382-96-99, NUDOCS 9701090055
Download: ML20133D207 (6)


See also: IR 05000382/1996099

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SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE REPORT

WATERFORD STEAM ELECTRIC STATION, UNIT 3

50-382/96-99

1.

BACKGROUND

The SALP Board convened on December 4,1996, to assess the nuclear safety

performance of Waterford 3 for the period April 29,1995, through November 30,1996.

The Board was conducted in accordance with Management Directive 8.6, " Systematic

Assessment of Licensee Performance." The Board members included: K. E. Perkins (Board

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Chairperson), Director, Walnut Creek Field Office, Division of Reactor Projects;

K. E. Brockman, Deputy Director, Division of Reactor Safety; and W. D. Beckner, Director,

Project Directorate IV-1, Office of Nuclear Reactor Regulation. This assessment was

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reviewed and approved by the Regional Administrator.

Functional Areas and Ratinas

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Current

Previous

Plant Operations

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Maintenance

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Engineering

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Plant Support

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II.

PLANT OPERATIONS

Overall safety performance in Operations was good. The training program and the

experience of the operating crews were considered to be <trengths. Weaknesses were

identified with operator tolerance of degraded plant material conditions and poor support

from other organizations, difficulty in recognizing situations that required entry into

Technical Specification Limiting Conditions for Operation (LCO), and f ailure to identify

misaligned valves and switches. Under the new management team, corrective actions are

being implemented to address identified problems and operators have become less tolerant

of workarounds and poor quality support.

Management generally assured good support and oversight for safe operation of the

facility, but did not consistently assure that problems were identified and resolved. Early in

the assessment period, after significant problems were identified by the NRC, several

management changes were made using experienced personnel from other Entergy sites.

During the latter part of the assessment period, the new management team was clarifying

its expectations and implementing initiatives to improve the fundamental operations at the

site; however, insufficient time had passed to determine whether these initiatives would be

effective.

Operations procedures provided apprcpriate guidance for performing day-to-day activities

and for responding to events. The licensee was in the process of upgrading their

emergency operating procedures to more closely comply with the owners group guidelines.

Operating crews were staffed with experienced and skilled personnel who were

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knowledgeable of the plant and procedures. The licensee established an effective training

program with excellent performance during initial and requalification license examinations.

However, in one instance, an emergency diesel generator was improperly used as an

on-the-job training aid by instructors.

Overall, the conduct of operations was mixed. Operators continued to demonstrate

excellent response to offnormal conditions in the control room and simulator as evidenced

by the effective response to plant transients and a complicated switchgear fire that

occurred early in the assessment period. Similarly. the conduct of nonroutine refueling

activities appeared to be sound. However, during routine power operations, operators

demonstrated a weak understanding of situations requiring Technical Specification LCO

entry. Recently, lapses in configuration management were also noted where operators

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failed, across several shifts, to recognize a mispositioned switch on the dry cooling tower

fans and a misaligned safety injection isolation valve. Management initiatives to reduce

operator tolerance for degraded conditions appear to have had some success, as evidenced

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by recent operator insistence on testing a questionable valve rather than relying solely on

an engineering evaluation for an operability determination.

Licensee self-assessments of the operations area performed by line and independent

assessment organizations were not fully effective in identifying and correcting program and

performance problems before NRC intervention. Significant operability issues with the

auxiliary component cooling water (ACCW) system and LCO entry were examples where

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NRC inspectors raised initial concerns for licensee followup. Operators demonstrated an

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appropriate threshold for initiating corrective action documents, but did not always

recognize conditions that met that threshold. Although there were instances where the

resolution of problems was not effective, strong corrective actions were generally

implemented when management became aware of the problem. For example, management

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changed the fire brigade staffing, initiated a modification to eliminate operator

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workarounds, and reprioritized resources to accelerate Improved Standard Technical

Specification implementation in response to identified problems.

The performance rating in the operations area is Category 2.

Ill.

MAINTENANCE

Overall safety performance in the maintenance area during this assessment period was

determined to be good. Throughout the assessment period, inconsistencies were noted

during the performance of maintenance and surveillance activities. These inconsistencies

included problems with attention to detail, configuration control, planning, and procedural

adequacy and adherence. Significant problems were also identified with the inservice

testing program. The overall material condition of the plant was considered to be good.

Ciaf t personnel were well qualified, trained, knowledgeable, and competent. However,

during the conduct of maintenance, there were instances where inadequate

communications and inattention to detail resulted in systems not being properly returned to

operation and equipment being used in improper applications.

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Throughout the assessment period, isolated deficiencies were identified with the adequacy

of and compliance with maintenance and surveillance procedures. Problems with the level

of detailin both task procedures and work authorizations were noted. Occasionallack of

compliance with procedures also contributed to maintenance problems. Taken together,

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these deficiencies resulted in instances where safety-related systems were unnecessarily

challenged, equipment was rendered inoperable, and surveillance tests were not properly

completed.

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Deficiencies were also noted in some maintenance programs, the most significant being in

the area of inservice testing. During this assessment period, significant problems were

identified with both the scope and the depth of the inservice testing program. Safety-

related valves were found to have not been included in the program, as required, and the

original licensing submittals, upon which inservice testing requirement exemptions were

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based, were found to have been inaccurate. Other programmatic deficiencies included

instances of measuring and test equipment not being properly controlled and preventive

maintenance tasks not being properly scheduled.

The overall material condition of the plant was good. The corrective maintenance backlog

was large, but properly controlled and prioritized. However, there were instances where

maintenance-related problems resulted in the plant being placed in an unanticipated

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operational condition.

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Licensee self-assessment and corrective action activities were not fully effective at

identifying and resolving issues with the maintenance and testing programs. There were

instances where corrective actions implemented in response to identified problems were

not effective or were not given the necessary priorities. Most notably, the resolution of the

licensee-identified problems with the omission of several valves from the inservice testing

program went uncorrected for an excessive amount of time.

The performance rating in the maintenance area is Category 2.

IV.

ENGINEERING

Overall, saf ety performance in Engineering was determined to be acceptable during this

assessment period. The significantly lower rating in this functional area, compared to the

previous r.ssessment, reflected performance insights gained through the NRC inspection

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program during this period. The NRC identified several old, existing design problems that

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the licensee either had not previously identified or effectively corrected. At the end of this

assessment period, a new management team was working to direct the engineering

organization toward rigorous application of the design and license bases; however, tne

licensee was still not consistently applying the bases to emerging issues without

involvement by the NRC.

Overall, the engineering staf t was technically competent and knowledgeable of plant

operations. However, the NRC identified deficiencies with the implementation of design

control programs and technical evaluations in support of plant operations. Past engineering

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evaluations too often justified operability of systems rather than fixing the deficient or

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nonconforming condition. The historicallack of rigor when applying design and licensing

basis requirements resulted in potential operability concerns. The technical evaluations and

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calculations to support the design bases were not always available and, in some cases, the

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actual design values were inconsistent with those stated in the Updated Final Safety

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Analysis Report (UFSAR). Use of incorrect assumptions in some technical evaluations

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performed by the engineering staff resulted in weaknesses in both original design and

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recent engineering work.

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Severallongstanding design problems were identified by the NRC. For example, a design

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deficiency that allowed void formation in the ACCW system was known but not corrected

for an extended period, and the configuration of the containment vacuum relief system

differed from that described in the UFSAR, but no written safety evaluation was performed

to determine whether an unreviewed safety question was involved.

Various engineering products lacked sufficient detail and contained inaccurate information

that resulted in incorrect operational decisions. Engineering inputs were extensively used

to provide plant guidance, but were not controlled, independently verified, or reviewed by

supervision for adequacy. The 10 CFR 50.59 evaluations completed for plant

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modifications were generally adequate; however, examples of inadequate 10 CFR 50.59

evaluations supporting calculations, licensing document changes, and condition reports

were identified. The calculation control procedure did not require timely correction of

omissions or errors, updating of licensing documents, or conducting 10 CFR 50.59

evaluations if the assumptions and conclusions in the calculation changed design bases

documents.

Past quality assurance audits of the corrective action processes were programmatic and

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not intrusive. For example, problems identifieri by outside groups were not identified

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earlier by licensee personnel despite prior opper. unities. Similarly, the Entergy corporate

assessments were ineffective in identifying adverse trends that had existed for some time.

Earlier root cause and operational experience engineering evaluations did not always

prevent problem recurrence, in some cases, corrective actions were not timely or thorough

in resolving the deficiencies. However, more recent evaluations appeared to effectively

identify and correct problems, and recent engineering support for field work was good.

The recent self-assessments of the corrective action processes, engineering, and technical

support were good. Many good issues were identified through the safety system self-

assessraents of the ultimate heat sink and emergency feedwater, although the self-

assessments did not identify a number of the issues raised by recent NRC inspections.

The new site management team had implemented several initiativer directed toward

improving program and personnel performance in the engineering ft s tional area, but it

was too early to determine the effectiveness of the initiatives. The kensee recently

implemented a design review committee concept and accelerated the schedule for

submitting the improved Standard Technical Specifications to simplify interpretations for

operability determinations.

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The performance rating in the engineering area is Category 3.

V.

PLANT SUPPORT

Overall safety performance in the plant support area during this assessment period was

determined to be good. While the licensee maintained an appropriate focus on

safety-related issuec, performance declined in the radiological controls and security areas,

and inconsistencies were identified with the implementation of otherwise strong programs

for emergency preparedness and fire protection. A number of corrective actions have been

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initiated to re-establish the performance standards of the past, but their effectiveness had

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yet to be determined.

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Generally, good performance was noted in the radiological controls area. An appropriately

trained and qualified staff was maintained. The radiation protection program remained

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sound, but declined from the previous performance level. Problems were noted with

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material and contamination controls and worker adherence to radiological control

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requirements. The goals for skin and clothing contamination events were not met during

the 1995 refueling outage, and the 3-year average exposure at the site was at the national

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average. The effectiveness of the ALARA program was good but inconsistent and did not

meet management expectations in several cases. Conversely, quality assurance audits

were performance-based, included specialists from outside the site, and were part of the

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licensee's self-improvement efforts.

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The emergency preparedness program continued to be an overall strength. Actual events

were correctly classified and offsite agency notifications were timely. Quality assurance

audits, management controls, and self-critiques were effective. However, there were

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several exceptions to the superior indicators typical of past performance. Although good

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performance was observed in all response facilities during the biennial exercise, an exercise

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weakness associated with communications problems was identified and two poor

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emergency planning practices at the emergency operations f acility were noted. Finally,

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during the annual program review, declaration of a General Emergency was delayed

because two operating crews had difficulty diagnosing fuel integrity status.

Performance in the security area was good but inconsistent. As a result of the

preparations for the Operational Safeguards Response Evaluation, coordination between the

security and operations organizations improved. Significant changes were made within the

management structure of the security organization, partly in response to daily operational

and morale issues, such as those associated with the conduct of fire watches and the

differentiation of duties between armed and unarmed officers. Deficiencies were also

noted in the implementation of the access authorization program, the identification of

degraded lighting conditions, and the establishment of compensatory measures. While,

overall, there was a decline in security during this assessment period, there was evidence

of improvement in the latter part of this assessment period.

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The fire protection program was found to be effective. The transition to the updated fire

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protection system went well; however, examples of inconsistent and questionable conduct

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of fire watch rounds detracted from the overall performance. Housekeeping remained at an

acceptable level. While several problems were noted early in the assessment period and

during outage conditions, performance improved and was considered very good during

normal plant operating conditions.

The performance rating in the plant support area is Category 2.

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