05000316/LER-1985-023-01, :on 850823,discovered That Incorrect Essential Svc Water Sample Point Being Used to Fulfill Table 3.3-12 of Tech Spec 3.3.3.9.Procedure 12 Thp 6020 LAB.037 Revised to List Specific Sample Points

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:on 850823,discovered That Incorrect Essential Svc Water Sample Point Being Used to Fulfill Table 3.3-12 of Tech Spec 3.3.3.9.Procedure 12 Thp 6020 LAB.037 Revised to List Specific Sample Points
ML20132E572
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 09/24/1985
From: Blind A
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
Shared Package
ML20132E534 List:
References
LER-85-023-01, LER-85-23-1, NUDOCS 8510010120
Download: ML20132E572 (1)


LER-1985-023, on 850823,discovered That Incorrect Essential Svc Water Sample Point Being Used to Fulfill Table 3.3-12 of Tech Spec 3.3.3.9.Procedure 12 Thp 6020 LAB.037 Revised to List Specific Sample Points
Event date:
Report date:
3161985023R01 - NRC Website

text

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F ACILITY NAME (19 DOCKET NUMBER 121

' AEI 13' D. C. COOK NUCLEAR PLANT, UNIT 2 o l5 l 0 l0 l 0131116 1lOFl0l1 TITLE 14p USE OF INCORRECT SAMPLE POINT IN OBTAINING TECHNICAL SPECIFICATION REQUIRED SAMPLES EVENT DATE (93 LER NUM6ER (si REPORT DATE (7) e OTHER F ACILITIES INVOLVED 181 f

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ON AUGUST 23,1985, AT 1900 HOURS WITH BOTH UNITS 1 AND 2 IN MODE 5 (COID SIRTIIX)WN) IT k%S DISCOVERED, WHILE INVESTIGATING AN UNREIATED OOCURRINCE, THAT TIE INOORRICT ESSENTIAL SERVICE WATER (ESW) SAMPLE POINT WAS BEING USED TO FULFIIL TIE REQUIRIMNT OF TECHNICAL SPECIFICATION 3.3.3.9, TABLE 3.3-12, ACTION ITEM 25.

ACTION STATDENT COMPLIANCE WAS REQUIRED DUE TO THE INOPERABILITY OF PROCESS RADIATION MONI'IORING INSTRUMENTATION (R-28).

l 71E SUIUKT SAMPLE WAS OBTAINED FROM TIE NORMAL ESW SAMPLE POINT m THE DISCHARGE

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OF TIE COMPCNENT OOOLING kATER HEAT EXCHANGER. TIE SAMPLE SHOULD HAVE BEEN DRAWN j

FROM TIE SAMPLE POINT IOCATED ON THE DISCHARGE OF THE CONTADENT SPRAY HEAT EXCHANGER. 71'E APPLICABLE PROCEDURE (12 71IP 6020 IAB.037) DID ?UT SPECIFY TIE SAMPLE POINT TO BE USED. INVESTIGATION REVEALED THAT THIS SAMPLING IOCATION HAD BEEN ERRONEOUSLY USED NUMEROUS TIMES IN THE PAST TO SATISFY TIE ABOVE REFERENCED TECHNICAL SPECIFICATION.

TO PREVDTT RTURRENCE,12 7" RIP 6020 IAB.037 HAS BEEN REVISED TO PROVIDE A LISTHE OF THE SPECIFIC SAMPLE POINTS TO BE USED TO OBTAIN GRAB SLMPLES UFON 7EE INOPERABILITY OF PROCESS RADIATION FONITORING INSTRUMDTTATION.

PREVIOUS OCCURRENCES OF A SIMIIAR NATURE INCLUDE LER 50-315/85-002.

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