05000366/LER-1979-078-03, /03L-1 on 790622:hydrogen Gas Concentration Downstream of Recombiners Exceeded Tech Specs.Caused by Improper Operation of Preheater Which Resulted in Insufficient Gas & Droplet Temp.Investigation Underway

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/03L-1 on 790622:hydrogen Gas Concentration Downstream of Recombiners Exceeded Tech Specs.Caused by Improper Operation of Preheater Which Resulted in Insufficient Gas & Droplet Temp.Investigation Underway
ML20132A699
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 08/10/1979
From: Rogers W
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20132A689 List:
References
LER-79-078-03L, LER-79-78-3L, NUDOCS 7908200323
Download: ML20132A699 (2)


LER-1979-078, /03L-1 on 790622:hydrogen Gas Concentration Downstream of Recombiners Exceeded Tech Specs.Caused by Improper Operation of Preheater Which Resulted in Insufficient Gas & Droplet Temp.Investigation Underway
Event date:
Report date:
3661979078R03 - NRC Website

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.a Update to a previous r.1pcrt

  • TEMSEE EVENT REPORT c

sut tttd August 2, 1979 COtJinOL Pl.CC4: l l]

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EVENT D Af ti d4 7b RErOHT DATE 60 60 fe l CGON ET NU'.*SE a 8

EVENT DESCRIPTION aND PRO 3 ACLE CONSEQUENCES h t tion, raeasured down-

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2 If) l Durinc startup operations at 25 K4t, the hydrogen gas concen ra This value is greater than the E Lstrean cf the recombiners, increased to about 13%.

h limit of 40.

The hydrogen level l

3 N i l Technical Spacification Appendix B Section 2.1.3.

There l ues greater than 4% for approxistely two hours before returning to nonnal.

j 3jij o lo 1 I hes besn tio more events of this type, one occurring on 7-15-79 at 320 IMt and one The hydrogen level for the event on 7-7-79 exceeded the 4%

o li) I on 7-7-79 at 256 Kit.

,c_Jsj i limit for about 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> and the event of 7-15-79 exceeded the 4% limit for about 6 su'scE6E sMEs

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M i The orebable cause for the event en.6-22-79 was the inroper operation of'th l

i.i l'l hecter vhich resulted in insufficicnt temperature of the gases and droplets of moist g it The probable

!i t :.j i ure enterinc the recorrbiner, thus reducing its recombining ability.

ii i g I cause for the other two events was excessive moisture entering the recombin g

An investigation is undervey to j

a L transient conditions of plant startup operations.

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6-Georgia Power Company Plant E. I. Hatch Baxley, Georgia Reportable Occurrence Report !! umber 50-366-1979-078 Event Description and Probable Consequences continued hours. There were no effects upon the public health and safety due to these events.

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Cause

Description and Corrective Actions continued 4dentify and correct defic enc es in the operation of this equiptr.ent.

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