ML20129K191

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Insp Repts 50-250/84-23 & 50-251/84-24 on 840715-0817. Violations Noted:Failure to Originate Operating Records, Perform Adequate Surveillance Test & Complete Unreviewed Safety Questions
ML20129K191
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 09/27/1984
From: Elrod S, Jenison K, Peebles T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20129K167 List:
References
50-250-84-23, 50-251-84-24, NUDOCS 8507230480
Download: ML20129K191 (16)


See also: IR 05000250/1984023

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  1. E{p

_ UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION il

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101 MARIETTA STREET, N.W.

ATLANTA, GEORGI A 30303

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Report Nos.:

50-250/84-23 and 50-251/84-24

Licensee:

Florida Power and Light Company

9250 West Flagler Street

Miami, FL ' 33101

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Docket Nos.:

50-250 and 50-251

License Nos.:

DPR-31 and DPR-41

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Facility Name: Turkey Point 3 and 4

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' Inspection Conducted: July 15, 1984 through August 17, 1984

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Inspectors:IW

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T/A.Peples,SeniorRFsidentInspector

ITate/ Signed

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K'M.Jefison,ProjectInspector

Fate / Sighed

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" : Accompanying Personnel.

D. R. Brewer

Approved by:

kN

S~. A. Elrod, Section Chief

04te Signed

Division of Reactor Projects

SUMMARi

Scope:

This routine, unannounced inspection entailed 168 inspector-hours on

site, including 43 hours4.976852e-4 days <br />0.0119 hours <br />7.109788e-5 weeks <br />1.63615e-5 months <br /> on backshift, in the areas of licensee action on

previous inspection findings, Licensee Event Re~ port (LER) followup, annual and

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monthly surveillance, annual and monthly maintenance, operational safety,

Engineered Safety Features walkdown, Plant Events, design changes, calibration,

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independent inspection and exit interviews.

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Results: Of the 15 areas inspected, no violations or deviations were identified

in four areas: four violations were identified in three areas (failure to origi-

nate operating records

paragraph 6; failure to perform an adequate surveillance

test - pz.ragraph 6; failure to follow procedure

paragraph 9, with additional

examples in paragra4'.., 11 and 13; failure to require complete unreviewed safety

question determinations) and two examples of a previous violation were noted in

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two areas (inadequate safety evaluation

paragraph 3; inadequate -curve book

procedure

paragraph 14).

8507230480 841011

PDR

ADOCK 05000250

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REPORT DETAILS

1.

Licensee Employees Contacted

  • K. N. Harris, Vice President - Turkey Point

C. J. Baker, Plant Manager - Nuclear

  • J. P. Mendietta, Service Manager - Nuclear
  • D. D. Grandage, Operations Superintendent - Nuclear

R. A. Longtemps, Assistant Superintendent Mechanical Maintenance - Nuclear

W. R. Williams, Assistant Superintendent Electrical Maintenance - Nuclear

  • J. W. Kappes, Maintenance Superintendent - Nuclear

E. F. Hayes, Instrumentation and Control Supervisor

T. A. Finn, Operations Supervisor

  • W. C. Miller, Training Supervisor
  • V. A. Kaminskas, Reactor Engineering Supervisor

J. S. Wade, Chemistry Supervisor

P. W. Hughes, Health Physics Supervisor

M. J. Crisler, Quality Control Supervisor

  • J. A. Labarraque, Technical Department Supervisor
  • J. Arias, Regulations & Compliance Lead Engineer
  • K. Jones, Site QA Superintendent
  • D. W. Haase, Chairman Safety Engineering Group

W. Bladow, QA Operations Supervisor

J. E. Moaba, Section Supervisor Licensing

R. E. Garrett, Plant Security Supervisor

G. J. Boissy, PEP Frogram Manager

D. Tomaszewski, Plant Engineering Supervisor

  • M. R. Costa, I&C Prod. Supervisor
  • F. A. Houtz, QC

Other licensee employees contacted included construction craftsmen,

technicians, operators, mechanics, electricians and security force members.

  • Attended exit interview

2.

Exit Interview

The inspection scope and findings were summarized during management inter-

views held throughout the reporting period with the plant manager - nuclear

and selected members of his staff.

An exit meeting was held on August 3,1984, with the persons noted above.

The areas requiring management attention were reviewed, including: failure

to require a complete unreviewed-safety question determination per the

Facility Operating License (250/84-23-01 and 251/84-24-01); failure to

conduct adequate surveillance tests (250/84-23-02 and 251/84-24-02); failure

to originate records as required by the Facility Operating License

(250/84-23-03 and 251/84-24-03); failure of the startup test group to

adequately perform a walk down and turn over a system (250/84-23-04 and

251/84-24-04); an Unresolved Item (URI) concerning how and when the oil vent

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pipe to the bearing on the containment spray pump was replaced URI (250/

84-23-05); and review of construction control of work Inspector Followup

Item (IFI) (250/84-23-06 and 251/84-24-06).

The licensee acknowledged

the findings.

Another exit was held with the plant manager - nuclear on August 17, 1984.

An IFI (250/84-23-07 and 251/84-24-07) concerning the progress of revising

the Inservice Test (IST) program and the submittal of another proposed

Technical Specification (TS) was discussed.

The licensee acknowledged the

commitment. The 10 CFR 21 Report on non-vital power to the safety related

pressure switches on the RWST line is considered to identify another example

of previous Severity Level III violation for inadequate safety evaluation

(250/84-09-10).

3.

Licensee Action on Previous Enforcement Matters

a.

On July 17, 1984, the licensee notified the NRC of a 10 CFR 21 report

which they had received from their architect engineer.

The control

circuitry for safety-related pressure controllers PC-600 and PC-601 is

powered from a single non-vital source.

These controllers are to

protect the Refueling Water Storage Tank (RWST) line from overpressure

during cooled-down operations. Loss of power to this circuit would not

allow the suction and discharge valves to the Residual Heat Removal

pumps to be opened from the control room.

The failure of a single

component (power from the non-vital bus) coincident with a loss of

coolant accident would not allow the recirculation phase of safety

injection to operate. The cause of the deficiency is that these relays

and the control circuitry were not identified as safety related. This

is another example of failure to properly identify equipment as safety

related, and therefore, a failure to adequately review items for

effects on safety as stated in report 250,251/84-09 and is an example

of that violation (250/84-09-10 and 251/84-09-10).

The licensee's immediate corrective actions of changing procedures to

provide guivance to operators to override these relays were reviewed

and were adequate.

The licensee intends to provide proper separate

power sources to these relays.

b.

Monthly Update of Performance Enhancement Program (PEP)

The inspector reviewed the PEP to determine if commitments were being

met. The program to upgrade the facility TS to standard TS is in the

preliminary scoping stage and has yet to be funded or staffed and

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therefore, is progressing slowly.

In addition, a definitive schedule

has yet to be set for this program. Other aspects of the PEP appear to

be progressing according to schedule.

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4.

Unrcsolved Items *

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An unresolved item is identified in paragraph 7.

5.

Licensee Event Report Followup

The following LER's were reviewed and closed. The inspector verified that

reporting requirements had been met, causes had been identified, corrective

actions appeared appropriate, generic applicability had been considered, and

the LER forms were complete. A more detailed review was performed to verify

that the licensee had reviewed the event, corrective action had been taken,

no unreviewed safety questions were involved, and violations of regulations

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or TS conditions had been identified.

(0 pen) LER 251/84-15. On July 16,1984, the 4A high head safety injection

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pump started spuriously.

The licensee's investigation showed that it was

probably started by construction electricians working near the 4160 VAC

switchgear. However, no one would admit to having bumped the switch.

The

licensee - decided that the event was not reportable.

The next day, the

inspector reviewed the decision and contacted the region for an interpreta-

tion. It was determined that the event should have been reported per 10 CFR 50.72(b)(2)(ii) as it was an actuation of an Engineered Safety Feature. The

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licensee was notified of the interpretation and reported the event. Further

followup concerning control of construction activities will be conducted

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under this LER.

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(Closed) LER 251/84-16. On June 24, 1984, manual initiation of the three

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auxiliary feedwater pumps during a transient occurred.

At 8:15 a.m. , a

rapid load reduction was being accomplished on Unit 4 as- turbine oil

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problems had caused control valves to close and the hotwell level was

decreasing due to a divert valve failing to open.

The shift supervisor

ordered the manual start of the auxiliary feedwater pumps to alleviate the low

hotwell level until the divert valve could be reset. The licensee deter-

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mined on July 24, 1984, that the event was not reportable as the pumps were

not required to function as they were only started in a precautionary

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manner.

However, NRC Region II interpreted the event to be reportable as

the pumps were started during a transient condition which was not preplanned

and the pumps were fulfilling their role as an Engineered Safety Feature.

The licensee was informed on August 2,1984, of the region's interpretation

and reported the event.

This event and the LER are considered closed.

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' *An Unresolved Item is a matter about which more information is required to

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determine whether it is acceptable or may involve a violation or deviation.

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(Closed) LER 250/84-21. On July 14, 1984, a reactor trip occurred on Unit 3

while the unit was shutdown with the shutdown control rods withdrawn. The

instrument technician working on Nuclear Source Range Instrument NI-32

caused a loss of control power to relays which resulted in a reactor trip.

The inspector witnessed and later reviewed the event and has no further

questions. This event and the LER are closed.

No violations or deviations were identified.

6.

Monthly and Annual Surveillance Observation (61726/61700)

The inspectors observed TS required surveillance testing and verified that

testing was performed in accordance with adequate procedures; that test

instrumentation was calibrated; that limiting conditions for operation (LCO)

were met; that test results met acceptance criteria and were reviewed by

personnel other than the individual directing the test; that deficiencies

were documented and that any deficiencies identified during the testing were

properly reviewed and resolved by appropriate management personnel; and that

system restoration was adequate.

For completed tests, the inspector

verified that testing frequencies were met and tests were performed by

qualified individuals.

The inspector witnessed / reviewed portions of the

following test activities:

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Engineered Safety Features Logic Periodic Test

Containment Spray Pump Periodic Test (OP 3204.1)

Residual Heat Removal (RHR) System Periodic Test (OP 4004.1)

High Head Safety Injection (HHSI) System Periodic Test (OP 4104.1)

Auxiliary Feedwater System Periodic Test (OP 7304.1)

Intake Cooling Water System Periodic Test (OP 3404.2)

Emergency Diesel Generator Periodic Test (OP 4304.1)

a.

While witnessing the testing of

"A" Emergency Diesel Generator per OP

4304.1 on July 26, 1984, the inspector noticed that out of specifica-

tion readings were being taken on one of the cylinder exhaust

temperatures. The reading for cylinder No. 2 was 120F and the other

cylinder temperatures in service were reading 790 - 880F.

The

acceptance criteria allowed no greater than 1100 and a deviation

between cylinders of less than 200; however, the acceptance criteria

did not give instructions as to action to be taken if a reading was not

within tolerance. Also, the Data and Record Sheets did not have spaces

to identify the performer of the test and the reviewer of the test and

did not have information required as to disposition of deficiencies.

The Facili ty Operating Licenses (DPR-31 and DPR-41)Section III.D

requires that the licensee shall originate and maintain operating

records in accordance with TS.

TS 6.10.1.d requires records of

surveillance activities required by TS be kept for five years.

These

data sheets are also Quality Assurance records as defined by 10 CFR 50,

Appendix B,

Criterion XVII which requires that records affecting

quality shall include the results of tests and that test records shall

identify the data recorders, the acceptabil.ity and the action taken in

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connection with any deficiencies. The FP&L QA topical section 17.2,

Revision 0, and Quality Procedure 17.1, Revision 11 implements these

10 CFR 50, Appendix B requirements. This is a violation (250/84-23-03

and 251/84-24-03) of the operating license as the records were not

originated,

b.

On July 27, 1984, the procedures for RHR and HHSI pump testing (OP

4004.1 and OP 4104.1) were reviewed for adequacy of compliance against

TS 4.5.

The intent of the TS is to verify that the subject systems

will respond promptly and perform their design functions. Both of the

pumps have mechanical seals with seal water pumped to a seal water heat

exchanger which is cooled by component cooling water. The seals have a

manufacturer's design maximum leak rate. TS 4.5.2.a requires that the

pumps be started monthly; that they sthrt and reach their required head

and that the instruments and visual observations indicate proper

functioning; and that the test be run for fifteen minutes. Neither of

the procedures verified that the seals, seal water system or component

cooling water system was meeting design functions during the fifteen

minute run by either visual or instrument observations. Therefore,

this is a violation (250/84-23-02 and 251/84-24-02) as the surveillance

tests were inadequate.

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The licensee was informed of the finding on July 27, 1984.

On

August 1,1984, the RHR pumps were tested and the precedure was not

corrected.

The licensee was again notified of the discrepancy on

August 3,1984, at a formal exit, and agreed to correct the problems

with the surveillance tests as it was apparent that the tests were for

ASME Section XI, IST compliance and not TS operability compliance.

The other pump operability surveillance tests have similar discrep-

ancies and have not been adequate.

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7.

Monthly and Refueling Maintenance Observation (62703)

Station maintenance activities of safety-related systems and components were

observed / reviewed to ascertain that they were conducted in accordance with

approved procedures, regulatory guides, industry codes and standards, and in

conformance with TSs.

The following items were considered during this review: LCO were met while

components or systems were removed for service; approvals were obtained

prior to initiating the work; activities were accomplished using appraved

procedures and were- inspected as applicable; functional testing and/or

calibrations were performed prior to returning components or systems to

service; quality control records were maintained; activities were accom-

plished by qualified personnel; parts and materials used were properly

certified; radiological controls wcre implemented; and fire prevention

controls were implemented.

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The following maintenance activities were observed / reviewed:

Replacement of holddowns for packing gland followers on Unit 4.

Charging pump 38 piston valve replacement.

Replacement of air lines to CV-4-2907, component cooling outlet valve

from 4C Emergency Containment cooler.

3A Containment Spray Pump bearing oil vent replacement.

Safety Injection Pump 3B motor rotor overhaul.

a.

The broken air lines on CV-4-2907, which were found on July 24, 1984,

by an auxiliary building operator, caused the valve to fail in the

" unsafe" closed position. The licensee's investigation indicated that

construction crews in the area were the contributing factor.

Construction Work Permits (CWP) are reviewed and signed by the shift

supervisor with the intent of providing guidance to construction

personnel as to critical equipment in the area of work. Many of the

CWP's are not specific enough to allow the shift supervisor to do an

adequate review,

e.g., " cable pulling to be conducted throughout the

auxiliary building." The licensee is reviewing the CWP program. This

will be followed as IFI (250/84-23-06 and 251/84-24-06).

b.

On August 1,

1984, the 3A containment spray pump was taken out of

service as the constant level oiler fell off during the pump run.

Subsequent investigation conducted by the licensee showed that a one

half inch pipe vent, on top of the bearing housing, did not have a vent

hole and running the pumps built up pressure which caused the cooler to

be forced from its mounting. How and when the vent pipe was replaced

is under investigation and the potential for the pump to have been out

of service for an extended period of time is considered an URI pending

NRC review of investigation results URI (250/84-23-05).

c.

Following the repair of 3A high head safety injection pump motor rotor

reported in report 250/84-22, the licensee shipped the 3B high head

safety injection pump motor rotor to Westinghouse for evaluation as

there was some indication of vibration. Westinghouse did not find any

significant problems. After reconditioning, the rotor was shipped back

and reinstalled.

The other two rotors (4A and 4B) are not to be

shipped out as no abnormal vibrations have been seen. The motors are

on a scheduled five year preventive maintenance program and vibration

readings will continue to be taken and are expected to identify any

significant deterioration in motor performance.

No violations or deviations were identified.

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8.

Operation and Safety Verification (71707)

The inspectors observed control room operations, reviewed applicable logs,

conducted discussions with control room operators, observed shift turnovers,

and confirmed operability of instrumentation.

The inspectors verified the

operability of selected emergency systems, reviewed tagout records, verified

compliance with TS LCO and verified return to service of affected

components.

The inspectors by observation and direct interviews verified that the

physical security plan was being implemented in accordance with the station

security plan.

The ir.;pectors verified that maintenance work orders had been submitted as

required and that followup and prioritization of work was on going.

The inspectors observed plant housekeeping / cleanliness conditions and

verified implementation of radiation protection control.

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Tours of the spent fuel pit pumps rooms, auxiliary, control, diesel, and

turbine buildings were conducted to observe plant equipment conditions,

including potential fire hazards, fluid leaks, and excessive vibrations.

The inspectors walked down accessible portions of the following safety-

related systems on Unit 3 and 4 to verify operability and proper valve

alignment:

Containment Spray System

Auxiliary Feedwater System

Emergency Diesel Generators

a.

The Unit 3 safety injection accumulators have been requiring increasing

attention to keep their levels within specifications as leakage has

increased. The licensee is pursuing corrective action.

b.

The Unit 4 'C' Pressurizer Safety valve is leaking at about the same

rate as it has been since the start-up in April. The STA has been

closely monitoring the leakage for any increase. Parts to rebuild the

valve with are on-site and will be installed if leakage begins to

increase or during a cold shutdown of sufficient duration.

c.

During a tour of the Unit 3 Spent Fuel Pit Pump Room, a boric acid leak

onto the spent fuel pit pump controller box was reported to the

licensee for correction.

d.

On August 14, 1984, Unit 4 power was reduced to 50% to lessen a

possible transient that might occur while a broken lead was replaced on

the B main feedwater pump control switch located on the control room

. panel.

The wire was found broken at the lug while other maintenance

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was being performed. The broken circuit would have partially affected

the B auxiliary feedwater initiation logic. The wire was repositioned

and the unit returned to 100% power.

No violations or deviations were identified.

9.

Design Changes and Modifications (37700)

On July 27, 1984, a review was made of design changes (PC/M) 81-29 and 81-30

(Units 3 and 4) for the installation of bypass switches around the lockout

circuitry for the B backup pressurizer heaters.

The breaker for these

heaters is located in the D 480 Vac load center for each unit. The lockout

circuitry is energized as a load shedding feature during an undervoltage

event and the installation of the keyed bypass switch in the back of the

load center allows these heaters to be re-energized. The inspector found

that the circuits have been operable since the last refueling, which on

Unit 3 was January 1984, and Unit 4 was May 1984.

Neither switch was

labeled as to function and the Unit 4 switch did not have an' indication

plate so that its position could be determined. The drawing for the opera-

tion logic of the circuit 5610-TL-1 Sheet 23 still had the notation that

this was for Unit 3 only, even though, Revision 8 was issued specifically to

incorporate that PC/M for Unit 4.

The start-up test group had respon-

sibility for the walkdown of the system to identify discrepancies and to

have the operating drawing updated.

These requirements are stated in AP

0103.17 - Systems / Equipment Acceptance / Turnover to Plant Staff. This is a

violation (250/84-23-04 and 251/84-24-04) for failure to follow procedures

as required by TS 6.8.1.

10.

Independent Inspection Effort (92706)

a.

Tne inspectors routinely attended meetings with licensee management and

shift turnovers between shift supervisors, shift foremen and licensed

operators during the reporting period. These meetings and discussions

provided a daily status of plant operating and testing activities in

progress as well as discussion of significant problems or incidents.

As a result of discussions with the licensee management, the following

items are to be actively pursued by the licensee: the shift supervisor

is to be responsible for knowing the qualifications of his shift

personnel; the operations supervisor (or superintendent) is to be

responsible to assure operations personnel training is current; and

training briefs will require a separate sign off.

b.

The Inservice Test (IST) Program was reviewed as to the appropriate

scope for pump testing.

Discussions with licensee personnel and with

NRR reviewers led to the agreement that the charging pumps and boric

acid transfer pumps were required for an orderly shutdown and cooldown

of the plant and therefore should be a part of the IST program as

required by 10 CFR 50.55a(g). On July 27, 1984, the Vice-President -

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Turkey Point and the Plant Manager - Nuclear agreed to include the

charging-pumps, boric acid transfer pumps and spent fuel pit pumps into

the IST program and to change the IST TS submittal of April 2, 1984, to

reflect the change. However, on August 22, 1984, no responsibility or

time table'for action had been initiated.~

The IST TS submittal of April 2,1984 has several discrepancies, two

are briefly listed below.

The entire submittal will be further

reviewed:

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(1) The letter states that in the submittal they are adopting the

wording of the Standard Technical Specifications; however, this is

not done.

(2) The margin of safety assured by the current surveillance testing

requirements would be reduced as the requirement to assure the

support systems are operable during the testing is being deleted.

The IST program will be reviewed as IFI (250/84-2-07 and 251/84-24-07).

c.

A review of evaluations for unreviewed safety question determinations

per 10 CFR 50.59 was conducted. The requirement for this evaluation is

in the facility operating licenses (DPR-32 and DPR-41) section III. 10 CFR 50.59(2) discusses that the evaluation for an unreviewed safety

question determination be made against evaluations previously made in

the Final Safety Analysis Report (FSAR).

Discussions with licensee

personnel revealed that they believed that only those items addressed

in the Chapter 14 Accident Analysis chapter of the FSAR were of

significance in evaluations for unreviewed safety question's and that

other chapters discussed back up equipment which did not require the

same level of review. A review showed that the following licensee's

procedures stated management acceptance of this concept as the

procedures only required a review be made against Chapter 14 of the

.FSAR:

Administrative Procedure 0109.1 page 14 - Preparation, Revision and

Approval of Procedures - Procedure Change Safety Evaluation

Administrative Procedure 0103.3 page 15 - Control and Use of Temporary

System Alterations - Safetu F. valuation

Administrative Procedure 0190.2a, page 34 - Plant Projects - Approvals,

implementation

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Regulatory Requirements - Appendix A

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Suggested Format for Safety Evaluations.

Therefore, this is a violation (250/84-23-01 and 251/84-24-01) of the

facility operating license as the evaluations were not required to be made

as stated in the license.

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Calibration (65700)

References:

NUREG CR 1369 Evaluation of Maintenance Test and

Calibration Procedures in Nuclear Power Plants

ANSI N18.8 1971

ANSI N45.2.4 1972

TS, Section 4.1

AP 0190.9 Control of Measuring and Test Equipment

a.

The following maintenance, test and calibration procedures were

evaluated for conformance with the above references.

The review

included calibration frequency, acceptance criteria, maintenance of

procedure revisions, review and approval of procedures, deviated

procedures, return-to-service of out-of-calibration equipment, and

primary standard control:

A-1-I

PWO 8714-TIC 627

PWO 8734

A-2-I

PWO 8715-TIC 625

PWO 8363

A-3-I

PWO 8727

PWO 8230

A-4-I

PWO 8493

MP14007.13

PWO 815B

MP14007.14

PWO 8230

Revision control on some procedures was found to be inadequate in that

pen and ink changes had been made to controlled copies of certain

procedures without management approval.

b.

Records for selected gages, instruments and measuring and test equip-

ment used to determine compliance with TS vere examined to determine if

the equipment was calibrated against certified equipment having a known

valid relationship to nationally recognized standards.

The following

equipment was examined:

Heise gage"

803

General Radio Meg Chm Meter 803

Heise gage

1004

Techtronix 5A21N

Fluke meter

81000A 1000-1

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Fluke meter

81000A 1000-4

Ashcroft Gage 1,500 psig

Fluke meter

81000A 103-3

Ashcroft Gage 10,000 psig 4227

Fluke meter

81000A 103-5

Ashcroft Gage 10,000 psig 4228

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Fluke meter

81000A 103-6

Ametek pump 704-5

Techtronix X-Y module 553

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Several discrepancies were noted during this review of calibration and

test equipment:

Tecktronix

5A2IN

PTP509

Invalid calibration

sticker affixed to the

amplifier.

Ashcroft

0-1500 psig

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No calibration sticker and

no PTP control number

assigned.

No current

calibration data avail-

able.

Ashcroft

0-10,000 psig PTP4227

No calibration sticker

affixed.

No current

calibration data avail-

able.

Ashcroft

0-10,000 psig PTP4228

No calibration sticker

affixed. No current

calibration data avail-

able.

This item was used on

Ametek Pump

704-5

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PWO 8067 on 5/31.

It was

overdue for calibration on

5/23 and not recalibrated

until 6/14.

Tektronix

X-Y output

PTP553

No calibration sticker

module

affixed to the module.

Ametek 93cg

0-15 psig

PTP178

This equipment was out of

Ametek 93cg

0-15 psig

PTP 179

service without the proper

Ametec 93cg

0-15 psig

PTP 180

identification tag

affixed.

The above discrepancies collectively constitute a failure to comply

with AP 0190.0 - Control of Measuring and Test Equipment and will be

considered a further example of violation (250,251/84-24, 23-04).

These

discrepancies will be reviewed as IFI (250,251/84-24, 23-08).

c.

In addition the master calibration schedule, calibration stickers

affixed to equipment and individual completed procedures were compared.

~Several examples were identified in which the data listed on the

different documents did not agree.

This appears to be a clerical

problem in nature, and plant management has committed to review this

area.

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d.

The calibration of gages which are used by tne licensee only for local

indication was reviewed.

It was discovered that local gages are not

calibrated on a routine schedule unless they are a part of a remote

indication calibration loop. In addition these gages are not used for

operability determination or IST by the licensee. This item will be

reviewed as IFI (250,251/84-24, 23-09).

12.

Engineered Safety Features Walkdown (71710)

The inspector verified the operability of the Units 3 and 4 Safety Injection

(SI) system on August 2,

1984, by performing a partial walkdown of the

accessible portions of the system. The following specific attributes were

reviewed / observed as appropriate:

that the licensee's system lineup pro-

cedures match plant drawings and the as-built configuration; that equip-

ment conditions and items that might degrade performance (hangers and

supports are operable, housekeeping, etc.) were identified; with assistance

from licensee personnel that the interior of the breakers and electrical or

instrumentation cabinets were inspected for debris, loose material, jumpers,

evidence of rodents, etc.;,that instrumentation was properly valved in and

functioning and calibration dates were appropriate; and that valves were in

proper position, power was available and valves were locked as appropriate;

and local and remote position indication was compared.

Valves and piping flow paths were verified to be built in accordance with

plant drawings 5610-TE-4510 Revision 29, 5610-TE-4512 Revision 12, and

5610-TE-4501 Revision 34. During the inspect'on of the area, no violations

or deviations were identified, however, various discrepancies were noted:

a.

Numerous valves in the SI system have no valve identification tags,

although the valves have been numbered on applicable drawings. This is

an example of inadequate equipment identification which is being

addressed by the PEP.

b.

In both Units 3 and 4 boric acid injection tank (BIT) areas, boric acid

residue from valve leakage was readily apparent. Several large valves

showed signs of long-term minor leakage with boric acid build up and

valve stud corrosion.

c.

The licensee was informed that the seal water lines, including vent

valves, and safety injection side of the seal water heat exchangers do

not appear on drawings.

13.

Refueling Water Storage Tank (RWST) Level Indication

References

Operating Procedure (0P) 16.122

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Operating Procedure (0P) 0204.2

Drawing 5610-C-18-393

RG-7-3-80

Tank Book drawing figure 5 - RWST

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OP 0204.2 States that an operator should " read pressure, convert to gallons

and record 'the Refueling Water Storage Tank head pressure and check against

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tank level indicators LI *-6583A and LI *-6583B TS (4.1-1(15)) Head Pressure

(PSI) = Test Gauge Pressure (PSI) + Correction Factor (PSI). Level (GALS.)

= Head. Pressure (PSI) X 16620 gallons / PSI. A minimum of 320,000 gallons is

required by.TS 3.4.1.a.1.

The correction factor is given on the engraved

name plate mounted next to the gauge. Check this name plate each time, as

this correction factor may have changed."

When inspected, the local Ashcroft test gauge pressure correction factor was

not mounted next to the gauge plate. It was however, attached to a plastic

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tape attached to a calculator which was used by the reactor operator to

calculate RWST level. Several operators, when questioned on August 1, 1984,

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indicated that the correction factor used was not verified prior to each

calculation in accordance with OP0204.2. This is a violation and will be

considered as a further example of violation (250,251/84-24, 23-04).

This

item will be reviewed as IFI (250,251/84-24, 23-10).

In addition, there appeared to be a 10 inch discrepancy between the data

used to install Magnetrol LS-3-1584A under PCM-80-100, and drawing

5610-C-18-393.

This discrepancy was later attributed to an error in the

data used to calculate figure five - Refueling Water Storage Tank, in the

Unit 3 control room curve book. This level switch is the TS low level alarm

which is used to backup control room level indication LI-3-6583B.

In

addition drawing 5610-C-18-393 (AG 7-3-80) was not updated after the

addition of the Magnetrol level switch. This is a 'tiolation and will be

considered as a further example of violation (250,251/84-24, 23-04). This

item will be reviewed as inspector followup item IFI (250,251/84-24, 23-11).

The local ashcroft meter had several items of concern associated with it.

The meter face vibrated severely and when held still oscillated two tenths

of a pound. It was mounted to a sample line which leaked. When the gage

was held the reading varied three tenths of ' a pound depending on the

pressure used to steady the gage. Because this reading was multiplied by a

factor of 16620 (which could institute significant error) to calculate RWST

level and was the gauge used to calibrate the Magnetrol LS-3-1584A TS alarm

the calculational method was reviewed.

The method seemed to be sound

although water density as a function of temperature or Boron concentration

was not addressed.

The licensee placed a newly calibrated Bailey level

indication in parallel with the Ashroft gage and the indicated level was

4000 gallons above the level calculated using the Ashcroft gage.

The

inspector had no further concerns with respect to the use of the Ashcroft

gage.

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14. Control Room Tank / Curve Book

The control room curve book was reviewed and compared the control room

indications in order to the verity certain TS limits. During the review the

reactor operator on Unit 4 was observed using a table entitled " Allowable

Flux Difference vs. Percent of Reactor Power."

This table was not an

official part of the curve / tank book however, the information included in

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the table appeared to be consistent with a flux vs. power curve in the

curve / tank book.

This table was not controlled and was not listed on the

index nor did it appear in any other control copy.

This is a further

example of violation (250,251/84-24, 23-04), and will be reviewed as

IFI (250,251/84-24, 23-11).

15.

Independent Inspection - Annunciated Control Room Alarms

A review of control room annunciated alarms was conducted with the following

concerns noted:

a.

The Unit 3 reactor coolant pump (RCP) thermal barrier cooling water

high temperature annunciator was alarmed. Maintenance work was being

conducted on the heat exchanger of one train of component cooling water

(CCW) which supplies cooling to the RCP. The licensee stated that one

train of CCW is not sufficient to meet normal cooling requirements

'during the summer months as a result of high canal intake water

temperatures. The review of special allowances for the failure of one

train of CCW is identified as IFI (250,251/84-24, 23-13).

b.

Unit 4 had a high pressure relief tank temperature alarm. This is a

repeat of an item identified in inspection report (250,251/84-06).

Indications of long term corrective actions mentioned in the February,

1984 report are still not evident. In order to comply with OP 1300.1

almost continuous purges of the tank are required. The licensee stated

that an evaluation of this problem was in process. Licensee corrective

action will be reviewed as IFI (250,251/84-24, 23-14).

c.

The Units 3 and 4 containment high Hydrogen monitor alarm was

annunciated in the control room and after review it was determined that

it was permanently alarmed as a result of system lineup. The monitor

is part of the Post Accident Monitoring system and alarms as a result

of one or more of the below situations:

(i)

Low calibration bottle gas pressure

(ii) Low sample gas flow

(iii) Low temperature

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(iv) Heat tracing failure

In this instance, the monitor alarm is the result of low sample gas

flow because the sample gas flow is isolated during normal operations

in order to maintain containment integrity, Diagram 5610-T-E-4534 and

control schematic K-111-01430 were reviewed.

This item is identified

as a possible human factor and/or design concern and the licensee has

agreed to review possible changes to eliminate the continuously alarmed

annunciator.

There were no violations or deviations identified in this section.

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16.

Procedure Upgrade Program (PUP)

The PUP portion Turkey Point Performance Enhancement Program (PEP) was

reviewed.

The following approved procedures were reviewed for content,

detail, and compliance with INP0 or other industry standards:

ADM-101

Writers guide for Administrative and Norma; Operations

Procedures

ADM-100

Procedure Preparation, Review and Approval

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Two preliminary procedures (Residual Heat Removal System OP-050 and Intake

Cooling Water OP-019) were reviewed and compared to the PDG procedure status

report of August 1, 1984. These documents appeared to be clear and well

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written and will be reviewed further.

The schedule / personnel requirements .of the PUP were also reviewed.

The

OP schedule and personnel availability appear to be well matched and should

meet the overall schedule committed to by the licensee. The maintenance

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procedure upgrade portion of the PUP appears to be under staffed with

respect to two issues.

The first issue that appears to be a possible

impediment to the accomplishment of the committed to schedule is the support

of "real time" or intermediate procedure changes. The intermediate changes

have monopolized the available maintenance procedure staff time and no

significant preventive action has been taken by the licensee to effectively

deal with the sharp increase in "real time" procedure change requirements.

This item will be reviewed as IFI (250,251/84-24, 23-15).

This item was

discussed with both the PUP project manager and the resident Vice President

Turkey Point Nuclear Plant, who committed to evaluate the situation.

The

second issue that appears to be a possible impediment to the accomplishment

of both the operations and maintenance procedure upgrading / rewriting efforts

is the implementation training resources available. Presently, there is an

inadequate number of staff available to raview and write updated training

material to support the procedure implementation schedule.

In addition,

there doesn't appear to be any integration of training requirements into the

overall PUP. This item was also discussed with the .UP project manager and

the Vice President, Turkey Point Nuclear Plant who committed to also evaluate

training requirements.

No violations or deviations were identified in this area.

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