ML20129D103

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Advises That post-fuel Loading Startup Test Program Essentially Complete W/Listed Minor Outstanding Items. Incomplete Startup Tests Have No Adverse Impact on Continued Safe Operation
ML20129D103
Person / Time
Site: Catawba 
Issue date: 07/12/1985
From: Tucker H
DUKE POWER CO.
To: Adensam E, Harold Denton
Office of Nuclear Reactor Regulation
References
NUDOCS 8507160421
Download: ML20129D103 (3)


Text

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DUKE POWER GOMPANY P.O. BOX 33180 CHARLOTrE, N.O. 28242 HALB. TUCKER TELEPHONE vic. e..es.m.T (704) 373-4531 July 12, 1985 Mr. Harold R. Denton, Director Office of Nuclear Reactor Regulation U. S.. Nuclear Regulatory Commission Washington, D. C.

20555 Attention:

Ms. E. G. Adensam, Chief Licensing Branch No. 4 Re: Catawba Nuclear Station, Unit 1 Docket No. 50-413

Dear Mr. Denton:

License Condition 3 of Facility Operating License NPF-35 requires that Duke Power Company : conduct the post-fuel-loading startup test program as described in Chapter 14 of the FSAR, as amended. This is to advise that the test pro-gram is now essentially complete with only minor outstanding items as noted below.

Piping System Vibration Test-Table 14.2.12-1 (Page 37)

Steady state vibration measurements have not been performed on the following:

1.

Spent Fuel Cooling System, Train B - Operability of this train will be verified prior to placing spent fuel into the pool.

2.

Boron Thermal Regeneration System - The status of this system is discussed below.

3.

Boric Acid Transfer Pump 1B and associated piping - This pump was damaged as reported in LER 413/84-01. This portion of the test will be completed after the pump is repaired.

Unit Load Steady State Test-Table 14.2.12-2 (Page 19)

The purpose of this test is to verify that Reactor Coolant System and appropriate secondary system parameters are within specified limits when measured at steady state conditions. At full power, the steam generator steam pressures exceeded the predicted values. This condition was not totally unexpected since the predicted values include some allowance for steam generator fouling. Clean steam generator tubes transfer heat more efficiently.

which results.in the slightly higher steam pressure. The turbine control-valves automatically. control the steam pressure to the high pressure turbine.

The net result is a higher pressure drop across the turbine centrol valves and therefore a slight decrease in efficiency.

8507160421 850712 PDR ADOCK 05000413 P

PDR-4

Mr.11 rold R. Denton, Director July 12, 1985 Page Two Steam line pressure is an input to safety injection and steam line isolation functions. However, a slightly higher steam line pressure would have no effect on these functions since actuation is on low steam line pressure.

The observed pressure of approximately 1035 psia is well with the system design pressure of 1200 psia.

Secondary Systems Functional Tests This test was written to complete outstanding items not completed in the Reactor Coolant System Hot Functional Testing program _(FSAR 14.2.12-1 Page 3).

Specifically, vacuum in the Main Condenser C is less than expected (higher absolute pressure). Efforts are underway to identify / correct the problem. The effect of the condenser vacuum being lower than expected is to reduce the turbine cycle efficiency.

Boron Thermal Regeneration System Functional Test There is not a specific FSAR Chapter 14 commitment to perform this test.

However, this system will be tested prior to use in accordance with the recommendations of Regulatory Guide 1.68, Rev. 2, Appendix A, Section 1.b 2.

Major system design changes have been identified to install a recirculation loop to speed up the temperature stabilization times between boration/ dilution-modes. To minimize personnel exposures for implementation of this change, use of this system will be delayed. Administrative actions have been taken to prohibit the use of this system. This system is non-safety related and is not required for unit operation. When the system changes have been performed, the system will be tested as stated in FSAR Section 3.9.2.1.1 and 9.3.6.6 and Table 14.2.12-1 (Page 37).

Each of the above incomplete startup tests have been reviewed to assess their impact on unit operation.

It was concluded that none of these test deficiencies have an adverse impact on the continued safe operation of Catawba Unit 1 and therefore pose no undue risk to the health and safety of the public.

A summary of the Catawba Unit 1 startup and power escalation testing, along with the resolution of the above items, will be provided in the Startup Report and any supplements in accordance with Technical Specification 6.9.1.

Very truly yours, b $ olfh Hal B. Tucker ROS:slb

2.-

Mr.' Harold R. Denton, Dir:ctor

. July 12, 1985 Page-Three cc:. Robert Guild, Esq.

P. O. Box 12097

Charleston, South Carolina 29412 Mr. Jesse L. Riley.

Carolina Environmental Study Group 854 Henley Place Charlotte, North Carolina 28207 NRC Resident Inspector Catawba Nuclear Station Dr '. J. Nelson Grace, Regional Administrator U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia. 30323 Palmetto Alliance 2135h Devine Street Columbia, South Carolina 29205

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