ML20127P094
| ML20127P094 | |
| Person / Time | |
|---|---|
| Site: | Summer |
| Issue date: | 04/19/1985 |
| From: | Dixon O SOUTH CAROLINA ELECTRIC & GAS CO. |
| To: | Grace J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| Shared Package | |
| ML20127P006 | List: |
| References | |
| NUDOCS 8505230696 | |
| Download: ML20127P094 (3) | |
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SOUTH CAROLINA ELECTRIC & gas COMPANY pos7 oppics 7ee CotuMelA. south CAnoLINA 29218 O. W. OlXoN. JR.
Vice PassiosNT April 19, 1985 NucuAR OpsRAT1oN=
Dr.
J., Nelson Orace
-Regional Administrator U.S. Nuclear Regulatory Commission Region II, Suite 2900 101.Marietta Street, N.W.
Atlanta, Georgia 30323
SUBJECT:
Virgil C. Summer Nuclear Station Docket No. 50/395 '
Operating License No. NPF-12 Response to Notice of Violation NRC Inspection Report 85-08
Dear Dr. Grace:
Attached is South Carolina Electric-and Gas Company's response for the Violation as addressed in Enclo ur 1 of NRC Inspection Report 85-08.
If there.are any questions, pleas al l us at your convenience.
V krulyyo pv I
. W. Dixon, Jr
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RJB:OWD/ led Attachment
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V.
C.
Summer C. L. Ligon (NSRC)
T. C. Nichols, Jr./0. W. Dixon, Jr.
K. E. Nodland E. H. Crews, Jr.
R. A. Stough E.'C.
Roberts G. Percival W. A. Williams, Jr.
C. W. Hehl D. A. Nauman J. B. Knotts, Jr.
Group' Managers I & E (Washington)
O. S. Bradham NPCF C. A. Price File S. R. Hunt i
g5230696850430 ADOCK 05000395 G
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- Y; ENCLOSURE :1 RESPONSE TO NOTICE OF; VIOLATION-INSPECTION REPORT 85-08 I.
~ ADMISSION OR DENIAL OF;THE ALLEGED VIOLATION
. South Carolina. Electric and Gas Company'is in agreement with
'the alleged violatio'n.
II.j iREASON FOR THE VIOLATION
,The failure to issue the proper torque conversion chart as-required by Mechanical Maintenance Procedure)(MMP) 285.003,
" Calibration of - Torque Wrenches Preventative Maintenance," was
.due to personnel' error.
At the time, predetermined torque-conversion data. sheets were allowed to be issued for field use Land ~the lab attendants issued ~an incorrect. data sheet for the specific wrench /crowsfoot/ angle combination.
A second_ violation, which was caused by personnel error, was
-identified in that a degraded fire barrier was not promptly reported as' required by. Station Administrative Procedure (SAP)
,146, "Nonconformance Control Program."
Specifically, the Shift-Supervisor was not'promptly notified of a plant.
condition which required compensatory actions.
III.
CORRECTIVE STEPS TAKEN AND RESULTS ACHIEVED
.The Licensee performed additional testing and verified that.
the ; torque applied by-the torque wrench and crowsfoot combination was within the acceptable tolerance of the specified conversion chart.
For the second violation, the Hourly Fire. Watch Patrol' Log was reviewed and it was verified that hourly fire watch patrol of the area was in effect.
Thus, the required compensatory measures for the-degraded fire barrier were in effect within one hour of the discovery time satisfying the requirements of the Technical Specifications.
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CORRECTIVE ACTION TAKEN TO AVOID FURTHER VIOLATION It is now required that a torque conversion chart be prepared
.to correlate the torque output to the input indicated on the torque' wrench.for the specific wrench /crowsfoot/ angle combination at the time of issuance.
The use of predetermined developed torque data sheets which reflect the exact combination has been discontinued.
A procedure change deleting the'use of predetermined developed torque data sheets will be implemented by April 30, 1985.
For the second violation, the Director, Nuclear Plant Operations has issued a letter to all station personnel addressing the importance of notifying the Shift Supervisor as soon as possible whenever a potential problem is identified.
V.
DATE OF FULL COMPLIANCE South Carolina-Electric and Gas Company will be in full compliance by April 30, 1985.. -
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