ML20127G993
| ML20127G993 | |
| Person / Time | |
|---|---|
| Site: | Oyster Creek |
| Issue date: | 12/31/1992 |
| From: | Egan D, Krall J GENERAL PUBLIC UTILITIES CORP. |
| To: | |
| Shared Package | |
| ML20127G988 | List: |
| References | |
| NUDOCS 9301220142 | |
| Download: ML20127G993 (6) | |
Text
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HONTHLY OPERATING Mf_0g 0
1 klGENSEE EVENT REPORTS ollowing Licensee Event Report was submitted during the month of December, LER 92 013 On November 30, 1992 local leak rate testing results indicated that Main Steam isolation valve NSO4B exceeded the leak rate limit of 12.08 SCTH at 20 psig as specified in plant Technical Specifications. The leak rate was unquantifiable, therefore it is assumed that-the.60 La combined leakage limit of all type B and C leak rate tests was also exceeded. The.60 La limit is calculated by combining the maximum leakage of each component that makes up a penetration.
The cause, corrective action, and safety significance cannot be determined at this time and will be reported at a later date.
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9301220142 930115' gDR ADOCK0500g9
Oyctor Creek Static.: #1 Docket No. 50-219 REFUELING It1 FORMATIO!1 - I, EMBER, 1992 Name of Facility: Oyster Creek Station #1 Scheduled date for next refueling shutdown:
Currently projected for October, 1994 Scheduled date for restart f ollowing ref ueling Currently projected f or January,1995 Will refueling or resumption of operation thereafter require a Technical Speci fication change or other license amendment?
No Important licensing considerations asoociated with refueling, e.g.,
new or different f uel deuign or supplier, unroviewed design or performance analysis methodo, significant changoo in fuel design, new operating procedures:
1.
General Electric Fuel Assemblies Fuel design and performance analysis methods have been approved by the NRC.
2.
Exxon Fuel Assemblien - No major char.;es h <e baan made nor are there any anticipated.
0 The number of fuel assemblies (a) in the core
=
(b) in the spent fuel storage pool = 2438 8
(c) in dry storage
=
The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:
Present Licensed capacity:
2600 The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
Full core discharge capacity to the spent fuel pool will be available through the 1996 refueling outage.
14RC_RPT.WPD/72
AVERAGE DAILY POWER LEVEL liET Mile DOCKET #.
.50-219 UNIT.
. OYSTER CREEK #1 REPORT DATE.
JANUARY 10, 1993 COMPILED BY
. JIM KRALL TELEPil0NE #
.609-971-4115 MONTH:
DECEMBER, 1992 UAE E
Db.E M
1.
0 16.
0 2.
0 17.
0 3.
0 18.
0 4.
0 19.
0 5.
0 20.
O a
6.
0 21.
0 7.
0 22.
0 8.
0 23.
0 9.
0 24.
0 10.
0 25.
0 11.
0 26.
0 12.
0 27.
0 13.
0 28.
0 14.
0 29.
0 15.
0 30.
0 31.
O NRC_RPT.WPD/73
~ ~.
- -.... ~... - _ -. -
OPERATING DATA REPORT OPERATING STATUS
- t
- 1. DOCKET:
50-219
- 2. REPORTING PERIOD:-
12/92
- 3. UTILITY CONTACT:
JIH KRALL (609)971-4115
- 4. LICENSED THERMAL POWER (HWt):
1930
- 5. NAMEPLATE RATING (GROSS MWe):
687.5 x 0.8 = 550
- 6. DESIGN ELECTRICAL RATING (NET HWe):
650
- 7. MAXIMUM DEPENDABLE CAPACITY (GROSS HWe):
632
- 8. HAXIMUM DEPENDABLE CAPACITY (NET MWe):
610 f
- 9. IF-CHANGES OCCUR ABOVE SINCE LAST REPORT, GIVE REASONS:
NONE
- 10. POWER LEVEL TO WHICH RESTRICTED, IF ANY (HET HWo):
NO!1E
- 11. REASON FOR RESTRICTION, IF ANY:
NONE i
i M01118 YEAR CUHULATIVE I
- 12. REPORT PERIOD HOURS 744.0 8784.0 201840.0
- 13. HOURS RX CRITICAL 0.0 7545.8 131908.4
- 14. RX RESERVE SHUTDOWN HRS 0.0 0.0 918.2 i
- 15. HRS GENERATOR ON-LINE 0.0 7465.0 128547.3 j
- 17. GROSS THERM ENERGV (HWH) 0 14143277 218468635
- 18. GROSS ELEC ENERGY (HWH) 0
,4710508 73396138 19.14ET ELEC ENERGY (HWH)
-3127 4528828 70435516
- 20. UT SERVICE FACTOR 0.0 85.0 63.7
- 21. UT AVAIL FACTOR 0.0 85.0 64.3 l
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'84.5 56.4 I
- 24. UT-TORCED OUTAGE RATE 0.0 3.4 11.0
- 25. FORCED OUTAGE HRS 0.0 266.1 15957.3
- 26. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, DURATIOtl):
NONE
- 27. IF CURRENTLY _ SHUTDOWN, ES"' MATED STARTUP.DATE:
02-02-93 o
L NRC_RPT.WPD/74
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