ML20126M750
| ML20126M750 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 01/21/1985 |
| From: | Fobes R CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | Morley F MICHIGAN, STATE OF |
| Shared Package | |
| ML20126M704 | List: |
| References | |
| PAL-85-01-AD104, PAL-85-1-AD104, NUDOCS 8506200453 | |
| Download: ML20126M750 (2) | |
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January 21, 1985 Mr Fred Morley District Supervisor Plainwell District Office Bldg 621 North 10th Street PO Box 355 Plainwell, MI 49080 FILE NO: P10.2.1 INCIDENT NO: DAL-85-01-AD104 This is in regard to NPDES Permit No MI 0001457 for the Company's Palisades Plant. In accordance with Part II, A4, the attached " NPDES Notification,"
Incident No PAL-85-01-AD104, is submitted as a report of an apparent differ-ence from the daily maximum effluent limitations for this facility.
If you have any questions regarding the attached report, please contact this office.
R L Fobes Senior Environmental Advisor CC USEPA, Enforcement Division, Region V BCC RBDeWitt, P-26-117B KFBieszke, P-24-329 BDJohnson, P-24-606 BWMarguglio, JSC-220A JFFirlit, Palisades JRSchepers, Palisades SFPierce, Palisades ATUdrys, M-1023 OC0185-0235A-TP13 8506200453 850531 PDR ADOCK 05000255 R
Filo No P10.2.1 Incident No: PAL-85-01-AD104 4
6 NPDES NOTIFICATION Apparent Difference Fre: Daily Average / Maximum Limitation January 21, 1985 Plant: Palisades Permit No: MI 0001457 Outfall
Description:
Turbine Surp 011 Separator Outfall Code No: 800216 Discharge (00G)
Paraneter: Oil and Grease (Freon)
Parameter Code No: 00556 1.
Dates of Incident:
1/10/85 and 1/14/85 2.
Identification of specific effluent limitation or monitoring requirenent affected:
Oil and grease daily maxi =um limitation of 20 zg/L.
3.
Description of Incident:
Routine weekly grab sa:ples for oil and grease collected on 1/10/85 and 1/14/85 measured 72.2 eg/L and 56.1 mg/L. respectively.
4 Apparent Cause:
The new API oil / vater separator was re=oved from service for maintenance purposes. Tank T-41 oil separator re=ained in service during this period.
5.
If not immediately corrected, the anticipated time the condition is expected to continue:
NA 6.
Corrective Action - The folleving corrective action was taken or vill be taken to reduce, eliminate and prevent recurrence:
The API oil / vater separator was placed back in service on 1/16/85.
7.
Additional Comments:
The final discharge to Lake Michigan showed no visible signs of oil.
8.
Signed:
RLFobes7qy(jCI 4
MIO185-0235A-TP13
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