ML20126M714
| ML20126M714 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 03/19/1985 |
| From: | Fobes R CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | Morely F MICHIGAN, STATE OF |
| Shared Package | |
| ML20126M704 | List: |
| References | |
| PAL-85-02-AD108, PAL-85-2-AD108, NUDOCS 8506200443 | |
| Download: ML20126M714 (2) | |
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March 19, 1985 Mr Fred Morley District Supervisor Plainwell District Office Building 621 North 10th Street PO Box 355 Plainwell, MI 49080 FILE N0: P10.2.1 INCIDENT NO: PAL-85-02-AD108 This is in regard to NPDES Permit No MI 0001457 for the Company's Palisades Plant. In accordance with Part II, A4, the attached " NPDES Notification,"
Incident No PAL-85-02-AD108, is submitted as a report of an apparent differ-ence from the monthly average effluent limitations for this facility.
If you have any questions regarding the attached report, please contact this I
office.
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R L Fobes Senior Environmental Advisor BCC RBDeWitt, P-26-117P KFBieszke, P-24-329 BDJohnson, P-24-606 BWMarguglio, JSC-220A JFFirlit, Palisades JRSchepers, Palisades SFPierce, Palisades ATUdrys, M-1023 8506200443 850531 1
PDR ADOCK 05000255 R
PDR OC0385-0223B-TP13
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c Filo No P10.2.1 Incident No: PAL-85-02-AD108 NPDES NOTIFICATION Apparent Difference From Daily Average / Maximum Limitation March 19, 1985 Permit No: MI 0001457 Plant: Palisades Outfall
Description:
Turbine Sump Oil Separator Outfall Code No: 800218 Discharge (00G) i Parameter: Oil and Grease (Freon)
Parameter Code No:
00556 1.
Date of Incident:
2/28/85 2.
Identification of specific effluent limitation or monitoring requirement affected:
Oil and grease monthly average limitation of 15 mg/1.
3.
Description of Incident:
The monthly average oil and grease for February 1985 neasured 27.3 eg/1.
4 Apparent Cause:
The monthly average limitation was exceeded as a result of an apparent malfunction of the new oil / water separator during the first half of the month, which caused the daily maximum limit to be exceeded on February 4, 10 and 11, 1985. As previously reported, there was a carry-over of oil from the separator into Tank T-41.
5.
If not immediately corrected, the anticipated time the condition is expected to continue:
We believe that some of the basic problems have been resolved. The last two samples for the month of February were in compliance.
6.
Corrective Action - The following corrective action was taken or will be taken to reduce, eliminate and prevent recurrence:
i As previously reported, performance of the new API oily waste treatment system continues to be evaluated and fine tuned to plant operations. As a result of the high readings, the interior of the separator was cleaned and accumulated oil removed from Tank T-41.
The separator's oil skimming weir was also readjusted to manufacturer's specifications. System performance samples were collected and are being analyzed.
7.
Additional Comments:
At no time was oil visible on the receiving waters of Lake Michigan.
8.
Signed:
gy R L Fobes RP0385-0223B-TP13