ML20126L020
| ML20126L020 | |
| Person / Time | |
|---|---|
| Site: | Oyster Creek |
| Issue date: | 05/21/1981 |
| From: | Carroll J JERSEY CENTRAL POWER & LIGHT CO. |
| To: | Grier B NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| References | |
| 50-219-81-22-01, 50-219-81-22-1, NUDOCS 8105270350 | |
| Download: ML20126L020 (2) | |
Text
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Jersey Central Power se Light Ompany Oyster Creek teaclear Generating Statim Dociet m. 50-219 Ftarked Jtiver, New Jersey 08731 SE3mcr2 hmportable Occurrence Rupert No. 50 -219/91-22/OlP 1ha *11~4== is a preliminary mi being submitted in mi(- with the Technical W #4ca+4<-=, parr :p4 6.9.2.a.6.
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citSTE5t CREEK MI2EMt GNERNNNG SUC2Gi Forked River, New Jersey 08731 Licensee Event Report Reportable Ocarrance No. 50 219/81-22/OlP Rasm+ caes May 21, 1981 occurrence Data May 20, 1981 Identification of occurrerce Victlation of 'Dochnical W Wr=+4r-is, W.,44 3.5.B.1 dien meccmdary containment integrity was not maintained at all times.
Both perscrmel access air 1cck doces cm the Marthmest side of the Reactor mMd4=y were found ajar.
This event is considered to be a ei.able occurrence as defined in the Technical i
& 4'4 r=&4 ram, pere,
a 6.9.2.a.6.
Confiticms Prior to Occurrence
%e het was ahnatdcam in the IWmEE. mode with reactor taesperature laes then Analysis of h wrenos C+ ----M containment is designed to minimize any ground relmese of r=dia=etive materials Wticit might result fri:za a serious ar=-4darat.
na Reactor P41A4mg i
pn: wides secondary cxmtainment during reecbor operaticut dun the drywell is sealed and in service and provides primary ocatairusent when the reacter is shutdtman and the drywell is open.
Wan this event occurred, all of the Technical *l;=r 4 Fication requirunents, emcept for the reactor node switch positim, were ramt for ccmditions Wiich do not require secondary c:mtairment integrity. The reactor mode switcts was in
" Refuel", wheroes the Technical Specifica+1 ram recpire "Shutdomm" if secondary i
contaizzaent integrity is not maintainsi.
t G.. dive Action,
' %e outer door was <-le=ad lm==diately by the Group shi.ft Superviser.
i The strike plate en the imer door was repelred by maintenance pers:innel within several mirastas after the problan was discovered.
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.Future -Kim dve action, if any, will be datemined after a sore thorough investigatica is m1-ted.
Failure Data Not M1441=.
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