ML20126J218

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Insp Rept 50-285/92-30 on 921207-11.No Violations or Deviations Noted.Major Areas Inspected:Actions in Response to Previous Insp Findings & LER Issues
ML20126J218
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 12/30/1992
From: Chamberlain D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20126J193 List:
References
50-285-92-30, NUDOCS 9301060081
Download: ML20126J218 (17)


See also: IR 05000285/1992030

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APENQIX

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-285/92-30

Operating License:

DPR-40

Docket:

50-285

Licensee: Omaha Public Power District

444 South 16th Street Hall

Omaha, Nebraska 68102-2247

Facility Name:

Fort Calhoun Station

Inspection At:

Blair, Nebraska

1

Inspection Conducted: December 7-11, 1992

Inspectors:

P. Goldberg, Reactor Inspector, Engineering Section, Division

of Reactor Safety

D. Kelley, Reactor inspector, Maintenance Section, Division of

Reactor Safety

P. Wagner, Team Leader, Division of Reactor Safety-

Accompanying Personnel:

B. Pendlebury, Consultant, AECL, Ltd.

Approved:

nhuu1/ OLLMVL

!1lb 91

/ Dwight D.' Chan.berlain, Deputy Director

'Date'

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hDivisionofReactorSafety

Inspection Summary

Areas Inspected:

A routine inspection of the licensee's actions in response to previous

inspection findings and licensee event report issues.

Results:

The licensee's calculations and evaluations related-to the electrical

distribution system were noteworthy.

The Fire Protection System lateraction Checklist included in Procedure

gel-4 was excellent.

No violations or deviations were identified during the inspection.

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9301060001 921231

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ADOCK 05000205

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innary of Inigettign_[_tadiagi:

Inspection followup Item 285/9230-01 - AdeqJacy of the 161kV Offsite

power Supply - was opened in paragraph 2.2.

Violation 9210-01 is discussed in paragraph 3 but remains open.

The following Inspection followup Items were closed in paragraph 2:

9101-01 - 4160 Volt Short Circuit Analysis

9101-02 - Degraded Voltage Analysis

9101-03 - Circuit Bretker/ fuse Coordination

9101-04 - 125 Volt dc Voltage Drop Analysis

9101-05 - Fuse Control

9101-06 - Device Ratings

The following Inspection followup Items were closed in paragraph 4:

8942-01 - Surveillance Test Requirements

9001-01 - Emergency feedwater Storage Tank Level

9001-03 - Post Accident Monitoring Instruments

9021-01 - Wiring interlocks

The following Licensee Event Reports (LERs) were closed in paragraph 5:

89-014 - Electrical Cable Modifications

90-007 - Main Steam and feedwater System Piping

90-016 - Overpressurization of auxiliary feedwater system piping

90-022 - Fire Barriers91-003 - Hechanical Containment Penetration H3

91-004 - Offsite Power low Signal

91-005 - Violation of Technical Specification Requirement

91-007 - Circuit Breaker Coordination of 480 Volt System

92-008 - Relief Valves92-010 - Circuit Breaker Coordination of de System

92-012 - Steam Generator Differential Pressure Trip Setpoints

92-016 - Containment Spray Pump Suction llead

92-017 - Cam followers in SBN Type Switches

92-022 - licater Crain Pump Hotor Electrical Cables

Attachment:

Persons Contacted and Exit Heeting

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DETAILS

1

INTRODUCTION

The NRC performed an inspection of the electrical distribution system

functional capabilities (EDSFI) in February 1991 as documented in NRC

Inspection Report 50-285/91-01.

There were some issues identified during the

EDSF1 which required additional licensee action and followup inspection by the

NRC.

In addition, some issues were reported to the NRC as a result of the

licensee's continued review of the EDSFI findings.

This inspection was

conducted to review the licensee's completed actions for those issues related

to the EDSFI and to review the status of some additional issues that had been

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identified.

2 ELECTRICAL DISTRIBtJTION SYSTEM FOLLOWUP INSPECTION (2515/111)

The inspectors reviewed the status of the issues identified during the EDSFI

as part of this inspection effort.

The review of additional issues related to

the EDSFI are documented later in this report.

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2.1

(Closed) Inspection Followgo item 285/9101-01:

Short Circuit Analysis

During the EDSFI, some questions were raised about the capability of various

components (switchgear and circuit breakers) in the 4160V distribution to

wit 1 stand or interrupt potential short circuit currents. The licensee was

verifying and revising the inputs and assumption that were utilized-in

computing the maximum short circuits that could be generated as part of the

on-going design basis reconstitution effort.

The licensee committed to

complete the analysis by December 31, 1991.

During this inspection, the licensee's Engineering Analysis FC-90-055,

Revision 1, was reviewed. The licensee calculated that the largest attainable

short circuit currents on the 4160V buses would occur when the buses were

connected to the main generator. -The inspectors also noted that the

calculations were revised to consider the effects of electrical cable

temperatures of-25"C verses the 90*C temperatures utilized in the earlier

calculations.

The licensee had also initiated operating instructions (A0P-31)

to caution the operators to control the main generator output voltage within

the analyzed limits.

The inspectors observed that the calculated maximum short circuit currents

were within the interrupting capabilities of the switchgear. The inspectors

noted, however, that there was no margin in the momentary interrupting

capability of the Bus lA4 Switchgear and the calculated maximum current.

The inspectors also reviewed the licensee's actions to resolve concerns raised

with the sizing of the Heater Drain Pump Motor's feeder Cables (see Licensee

Event Report 92-022).

The inspectors reviewed Engineering Change

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Notice 92-0311 which directed the replacement of the No. 2 AWG cables with

No. 4/0 AWG cables.

The inspector agreed that the replacement cables would

resolve the fire safety concern.

2.2

1 Closed) Inspection followuo item 285/9101-02:

Deoraded Voltang

Analysis

The EDSFI noted problems witn the assumptions that had been used in the

licensee's calculation of the minimum voltage that would be available to

various components while autonatically sequencing emergency loads.

The

concerns included loading onto the emergency generators (EDGs) and under

degraded offsite power conditions.

The licensee committed to include the

EDSFI observations in a revised degraded voltage study that was being

conducted n part of their design reconstitution effort.

During this inspection, the licensee's Engineering Analysis FC-92-072,

Revision 0, was reviewed. The licensee had calculated the values of voltage

and frequency that would result from the automatic loading of the EDGs at

discrete intervals.

The alculations were performed using the computer

program "ETAP" and indicated that the EDGs would perform as designed.

The

inspectors verified that the assumed loading times and values corresponded to

the as-built design.

In addition, the inspectors utilized the computer

program "MATHCAD" to perform independent calculations.

The results of the

inspectors' calculations showed good correlation with the values obtained by

the licensee.

The inspectors also reviewed Engineering Analysis FC-90-057, Revision 1.

This

analysis evaluated the voltage available at the 4160V buses during automatic

sequencing of emergency loads.

The inspectors noted that the licensee had

increased the Offsite Power Low Signal (0PLS) relay setpoints to approximately

97 percent of nominal voltage to ensure that adequate voltage would be

available. The revised OPLS setpoints, however, required an offsite power

supply voltage of approximately 166.3kV at the onsite switchyard.

The

inspectors reviewed the voltage profiles at.the onsite switchyard that were

obtained in 1984 and those obtained in 1992.

The inspectors noted a decrease

in the available voltage levels had occurred.

The inspectors questioned

whether adequate voltage would be available to automatically sequence safety

loads during an accident condition. llowever, the present condition meets

regulatory requirements _ for safe shutdown power supply capability and the

onsite emergency power sources are appropriate for accident' condition load

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sequencing. The inspectors discussed this concern with licensee personnel and

were informed that a number of options were-being reviewed. The licensee was

in the process of providing an additional 161kV transmission line to the

onsite switchyard to improve redundancy and power capability.

Licensee

personnel also stated that additional adjustments to the OPLS relay setpoints

was being considered.

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The licensee's actions to ensure an adequate source of offsite power for

automatic sequencing of accident loads will be. reviewed with the Office of NRR

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and will be evaluatec iuring a future inspection.

(Inspection followup Item

285/9230-01)

2.3

1 Closed) Inspection followfo item 285/9101-03:

Circuit Breaker

(gprdination Study

The licensee was performing circuit breaker and fuse coordination studies for

the 480V and 120V ac systems and the 125V de system at the time of the EDSFI

The licensee committed to complete those studies and implement any necessary

corrective actions in response to that inspection.

During this inspection, the licensee's studies and corrective actions were

reviewed.

The inspectors reviewed Engineering Analysis FC-91-004, Revision 1,

and found it to be acceptable. The inspectors noted that the licensee had

replaced the trip units from various motor control center supply circuit

breakers.

The modifications were implemented in accordance with Modification

Request FC-88-013 in order to provide acceptable coordination of the trip

function.

The 120V circuits were modified in accordance with FC-91-020. This

modification installed 30 ampere fuses downstream of the load distribution

circuit breakers in Distribution Panels AE-40A and -400.

The inspectors

verified that the addition of these fuses provided the necessary coordination.

The inspectors also verified that the battery output fuses were replaced in

accordance with FC-91-084 on A)ril 20, 1992.

The replacement fuses provided

the necessary coordination wit 1 the battery distribution system.

The

inspectors also noted that Engineering Analysis FC-91-084 dispositioned the

additional de system coordination concerns that had been raised during earlier

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reviews.

The inspectors found the analysis to contain sound bases for the

conclusions.

2.4

(Closed) 10Haction Followun Item 285/9101-04:

Voltane DroD Analysis

for the 125 Volt de System

The EDSFI concluded that insufficient information was available to provide

assurance that all safety-related, de powered devices would have an adeouate

terminal voltage throughout the battery duty cycle.

The licensee committed to

perform a bounding voltage drop analysis for selected devices powered by the

125V de system.

During this inspection, licensee Calculation FC05827, "125VDC System Voltage

Drop Study," Revision 2, dated December 3, 1992, was reviewed.

The licensee

selected limiting components and determined the minimum operational voltage

levels.

The voltage drop occurring in the electrical wiring and-control

devices (e.g., circuit breaker and relay contacts) were calculated and

subtracted from the assumed battery terminal voltage of 105V dc.

The voltage

was determined to be adequate to ensure proper operation of the devices except

or three motors related to the emergency diesel generators.

However, the

licensee determined that the potential inoperability of the motors would not

prevent the automatic start of an emergency diesel generator.

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The inspectors also noted that the internal shutdown circuitry of the

inverters had been adjusted to lower the setpoint to 104V de to provide margin

to the calculated minimum terminni voltage of 104.57V dc. The inspectors

found the licensee's calculation and related evaluations to be noteworthy and

considered the quality of the engineering effort and its documentation to be a

program strength.

2.5

IClosed) Inspectign_followuo item 285f9101-05:

Fuse Control proorg

The fitst phase of a three phase fuse control effort was underway at the time

of the EDSFl.

The first phase consisted of sampling 5-10 percent of the

station fuses; the remaining two phases were to verify ap)roximately 25

percent of the facility fuses and obtain design data on tie remaining fuses to

compile a fuse list.

During this inspection the inspectors examined the licensee's progress and

determined that all phases had been co.npleted.

The licensee had also

developed a fuse list (approximately 4000 fuses) that had been published,

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addition, the inspectors noted that the licensee had established provisions to

control fuses in the procedures that controlled maintenance and modification

activities.

2.6

1Clg. sed) Insoection Followuo item 285/9101-06:

Ratino of Control

Circuitry Devices

The EDSF1 questioned the capability of various control devices assembled by

equipment vendors. The team was especially interested in those devices

supplied as part of the emergency diesel generator package.

The licensee was

unable to retrieve the necessary electrical ratings for some of those devices.

Therefore, the itcensee committed to review selected devices to ensure that

the ratings were appropriate for their function.

During this inspection, licensee Engineering Analysis FC-92-049, " Analysts of

the Electrical Ratings of Selected EDG Components," was reviewed.

The

inspectors found the analysis to be complete and comprehensive.

The licensee

utilized manufacturers' data when avellable and performed type testing and

inspections to verify findings. During this inspection, the licensee issued

Revision 1 to the analysis to incorporate the recent 125Vdc system voltage

drop study.

The licensee concluded that the selected coniponents were all

adequately rated to ensure proper operation.

The inspectors determined that the licensee-had used a conservative

methodology in evaluating the operability of the selected components.

3 FOLLOWP ON CORRECTIVE ACTIONS FOR A VIOLATION (92702)

3.1 IQpen) Violation 285/92]O-01:

failure to Maintain Adecuate Procedures

for Containment Sumn level Calibration

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An NRC inspection in April 1992 determined that the narrow range containment

sum) ievel instruments LT-599 and LT-600, had not been calibrated by the

met 1od stated in the Technical Specifications.

In 1990, an NRC inspection had

ideatified the same concern with the calibration of these instruments.

The

calibration procedures were revised in response to that inspection finding to

include the Technical Specification requirement. However, during the 1992

refueling outage, the procedures were revised again and the Technical

Specification requirement that had been added, was deleted.

During the April 1992 inspection, Surveillance Procedures IC-ST-WDL-0001 and

IC-ST-kDL-0002 were revised (Revisions 11 and 8) to once again incorporate

physical measurement of the containment sump level.

The licensee also added a

caution note to the procedures stating that changes should not be made without

Plant Review Committee review of the NRC commitment.

In addition, the

licensee performed the surveillance test to the revised procedures.

The licensee's response to the Notice of Violation, dated June 22, 1992,

contained corrective action steps to insure the violation would not reoccur.

The corrective actions included:

1) performing a root cause analysig 2)

issuing a memorandum to all members of the Plant Review Committee and Nuclear

Safety Review Group emphasizing the need to aerform a thorough review of

procedure revisions to insure compilance wit 1 the Technical Specifications; 3)

revising Procedure N00-QP-3, "10 CFR 50.59 Safety Evaluations," to provide

additional guidance in determining Technical Specification compliance; and 4)-

a review of other float level calibration procedures to determine if revisions

were necessary to clarify the method of calibration required by the Technical

Specifications.

The NRC found these proposed actions to be acceptable by

letter dated July 28, 1992.

During this inspection, the " Root Cause and Generic imp 1tcations Analysis

Report, Containment Sump Level Miscalibration," No. IR-920381 dated June 16,

1992, was reviewed.

The inspectors found the report to be a comprehensive and

detailed analysis of the root cause. Quality Procedure N0D-QP-3, "10 CFR 50.59 Safety Evaluation," Revision 11, was also reviewed.

Section 9.4 of the

procedure was revised to include a statement to ensure that the change

complied with the Technical Specifications.

The inspectors also reviewed

Memorandum FC-0792-92 dated July 17, 1992, that was sent to the Plant Review

Committee and Nuclear Skfety Review Group members. This memorandum discussed

the violation and emphasized the importance of reviewing changes to procedures

for compliance with the Technical Specifications. The inspectors' considered

these corrective action items to be complete.

The last corrective action item included a review other float level

calibration procedures to ensure Technical Specification cyliance.

This

item was being tracked by the licensee as commitment identincation No. 920573

and had a scheduled completion-date of December 31,1992.

This violation

remains open pending verification that this corrective action item has been

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4 FOLLOWUP (92701)

4.1

1[lgtedL[nmetion followuo item 285/8942-011 Waiver of Surveillans.g.,

Etniremitt.1

During an inspection of the licensee's surveillance procedures and records,

some instances were noted where surveillance requirements had been waived.

The technical basis for the waivers were not always adequately documented and

the authority for waiving survelliance requirements had been granted to the

system engineers.

The Itcensee acknowledged this apparent weakness and

initiated corrective actions.

During this inspection, the inspectors reviewed the licensee's corrective

actions.

The Itcensee redefined the waiver process as a procedure change and

revised Standing Orders G-23, " Surveillance Test Program," and G-30,

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'Setpoint/ Procedure Changes and Generation," to implement the actions.

The

inspectors found these changes to be acceptable in resolving the concern.

4.2

IClosed) Inspection followuo item 285/9001-01:

Electrical SepardlDB

for the Emeroency feedwater Storace Tank level Transmitters

The licensee identified a problem with the separation distance between the

electrical cables for the two level transmitters.

The separation was

acceptable for normal service applications, but did not appear to satisfy the

requirements for redundant applications of Post Accident Monitoring

Instruments specified in Regulatory Guide 1.97.

The licensee performed walkdowns of the instrumentation loops during the 1992

refueling outage and determined that problems existed which required rerouting

of some cables.

The licensee initiated Modification Request FC-92 0ll to

accomplish the necessary rework. The inspectors found the proposed

modifications to be acceptable and verified that the modification request was

scheduled to be completed during the 1993 refueling outage.

4.3

(Closedi

Iqioection followuo item 285/9001-03:

Labelino of Reaulatory

Guide 1.97 Instrumentation

During the inspection of the Post Accident Monitoring Instrumentation, the

inspectors noted that the licensee had not provided the required unique-

identification for the instruments,

The licensee included a provision for

identifying the specified instrum:nts in Modification Request FC-88-22,

" Detailed Control Room Design Review Labeling, Demarcations Himics and Color

Padding Project."

During this inspection, the modifications were verified to have been

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completed. The inspectors also toured the control room simulator and verified

thht the unique orange dot designator had been attached to selected instrument

labels,

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4.4

(Closed) Inspection Followuo item 285/9021-01:

Wirina Interlock on

Diesel caenerator Outout Breaker

During the followup inspection of the loss of shutdown cooling event that

occurred on February 76, 1990, a wiring deficiency in the emergency diesel

gener kor auto-close circuit was identified. The wiring deficiency prevented

the dier.cl generator outoui breaker from closing on an automatic start unless

largo loads, including the ;ow pressure safety injection pump, had tripped.

However, the Irw pressure safety injection pu.np does not load shed when

manually startsd,

Therefore, ne diesel generator output breaker would not

automatically close dar N c loss of offsite power ir.cident if the pump had

been manually started.

During this inspection, the licensee 5s corrective actions were reviewed.

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licensee had implemented Modification Request FC 90-024 to jumper the low

pressure safety injection pump permissive contacts in the diesel generator

output breaker closing circuit. The licensee's evaluations verified that

innediate loading of the low pressure safety injection pump on the diesel

generator bes would have minimal effect on plant response to a loss of offsite

power incic M .

5 ONSITE REVIEW OF LICENSEE EVENT REPORTS (92700)

5.1

(Closed) Licensee Event Report 285/89-014:

Auxiliary Feedwater Wirina

Outside Desian Basis

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During the design basis reconstitution effort, the licensee discovered that

wiring for the wide range steam generator pressure instrument on the auxiliary

feedwater control panel had been routed through the control room,

A fire in

the control room could, therefore, have rendered this instrument inoperable.

In addition, the pressurizer pressure and steam generator narrow range level

indicators were powered from the 'C" inverter that was fed from Battery 1.

However, the use of Battery 1 had not been analyzed in the fire safe shutdown.

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In the interim, the licensee performed a Safety Analysis for Operability (SAO)

and revised the abnormal operating procedures to address forced evacuation of

the control room.- Finsi resolution consisted of a plant modification to

supply analyzed power to the above instruments and rerouting the wiring so it

would not be affected by a control room fire.

During this inspection, the

modifications were verified to have been completed.

5.2

(Closed) Licensee Event Report 285/90-007: Main Feedwater and Main

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-Steam Pioina Outside Desian Basis

The licensee reported concerns

'th the main feedwater and main steam piping

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and supports outside of conta..went that could be overloaded during a seismic

event. An evaluation was performed which determined that the main feedwater

piping and supports were outside the design basis specified in-licensing

correspondence and in the Updated Safety Analysis Report (USAR) for high

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energy line break locations,

in addition, tne main steam piping stress and

support allowable values were outside the USAR design basis.

The licensee implemented short-term corrective actions during the 1990

refueling outage.

These corrective actions included the preparation of SA0

90-04, dated April 9, 1990, which established an interim acceptance criteria

for plant operation.

The inspectors reviewed the SA0 and found it to be

comprehensive in scope.

In addition, two modifications were completed on main

steas and main feedwater supports during the outage.

The inspectors reviewed

Modihcation Requests FC-90-19. Revision 0, " Main Steam Supports in Room 81

and Turbine Building," and FC-89-45, Revisien 0, "Feedwater Supports in

Room 81 ana Turbine Building." The inspectors noted that the modifications

were well written and well documented.

The licensee's long-term corrective actions included:

1) the clarification of

the USAR concerning seismic requirements for the main steam and main feedwater

piping outside of containmer.t. 2) the modification of piping supports to

comply with the design basis, and 3) the initiation of a review of seismic

classification of the systems identified ie the NRC safety evaluation

concerning the potential for flooding caused by ruptures of non-seismic

Class I systems.

The inspectors also reviewed Modification Request FC-90-038,

Revision 1, ' Main Steam and Feedwater Supports Room 81 and Turbine Building.'

The purpose of the modification was to restore the main feedwater and main

steam systems between the isolation valves and the turbine builaing to Seismic

Class I requirements. The nonsafety-related piping and supports were

reanalyzed to design basis requirements and supports were corrected as needed.

In addition, Engineering Analysis FC-92-030 was initiated to review the

seismic classification of systems with the potential for flooding.

This

analysis had not been completed but was being tracked in the licensee's

commitment tracking system as C10 900217/09.

5.3

(Closed) Licensee Event Report 285/90-016:

Potential for

QyJroressurization of Auxiliary feedwater Floina

The licensee reported concerns with the potential for the turbine driven

auxiliary feedwater pump (FW-10) to overspeed and cause the discharge piping

to be overpressurized.

The report stated that the pump had a speed limiter

but did not have an overspeed trip; therefore, a single failure of the speed

limiter could cause the pump to overspeed.

The inspectors reviewed SA0 90-012 dated May 13, 1990.

The SAO justified the

continued plant operation based on Engineering Analysis FC-90-28, Revision 1

"Effect of_ Single Failure of FW-10 Speed Limiting Governor.' The inspectors

noted that the engineering analysis determined that the maximum discharge

pressure would not cause a failure in the auxiliary feedwater piping.

The SA0

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concluded that since the overspeed and overpressure postulated event would not

cause a loss of safety function of the auxiliary feedwater system, no

immediate compensatory measures were required.

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The long-term corrective actions included incorporation of lessons learned

from the event into the 10 CFR Part 50.59 safety evaluations training program

and a permanent resolution to the concern for overpressurization of the:

auxiliary feedwater piping from overspeeding of the pump.

The inspectors

reviewed the Student Handbook Lesson Plan: 2327-07, Revision 3. "10 CFR 50.59

Safety Evaluations,"

and noted that the lessons learned were incorporated

into the lesson plan that satisfied the first comitment.

The licensee

determined that the current configuration of the auxiliary feedwater system

was acceptable and no modification was required.

The determination was

documented in OPPD Position Paper, " Overpressure of Auxiliary Feedwater

Components due to FW-10 Overspeed," dated June 24, 1991. This position was

based on a review of codes concerning the overpressure of piping. A 10

percent increase over design pressure was allowed under conditions of safety

relief valve actuation.

The maximum overpressure expected if pump FW-10 were

to overspeed was less than 5 percent for the most limiting components.

5.4

(Closed) Licensee Event Report 285/90-022:

Fire Barriers

The licensee reported that some fire barrier penetrations were declared non-

functional due to either a lack of documentation to verify critical parameters

or inconsistencies between the as-built configuration and the approved

configuration. The licensee committed to:

1) perform the necessary

evaluations, 2) repair or replace barriers as necessary, 3) revise affected.

drawings as part of any modifications, and 4) upgrade the procedures related

to fire barrier configuration control.

The inspectors verified that the engineering evaluations utilized the

guidelines of Generic Letter 86-10. " Implementation of Fire Protection

Requirements," and that the modifications had been completed in accordance

with Modification Request FC-90-072, " Repair / Replacement-of Fire Barrier

Seals and Dampers." The inspectors also reviewed Procedures MEl-20. " Fire

Barrier Evaluations," Revision 0; MEl-21. " Fire Barrier Configuration Control,

Revision 0; and gel-4, " Fire Protection Systems Interaction " Revision 0.

The

inspectors determined that the procedures provided detailed guidance to

accomplish the required tasks.

In particular, the inspectors found the Fire

Protection System Interaction Review Questions Checklist included in gel-4 to

be excellent.

5.5

(Closed) Licensee Event Report 285/91-003:

Mechanical Containment

Penetration M-3_putside Desian Basis

The licensee determined that Containment Penetration M-3 (Chemical Volume

Control System) was outside the basis that allowed exclusion from the Type C

leak testing required by 10 CFR 50, A>pendix J.

The basis for the Ty)e C

testing exemption had been based on tie charging line pressure being ligher

than containment pressure during accident conditions.

The most recent

reanalysis of the post-accident containment pressure response and the .

Emergency Operating Procedure (EOP) charging pump criteria indicated that the

previous basis for an exclusion was not valid.

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The licensee completed SA0 91-01 in February 1991 to provide the basis for

continued operation. The E0Ps were revised to require closing the charging

pump manual discharge valves whenever the charging pumps were secured.

In

addition SA0 91-01 and the USAR were revised to include the updated

containment pressure analysis and the design basis for Containment

Penetration M-3.

The licensee had requested exclusion from the Type C l u k testing required by

Appendix J based upon a new justification.

That request had not been approved

at the time of this inspection.

However, the inspectors determined that the

status of the test exclusion request had no bearing on the continued safe

operation of the facility.

5.6

(Closed) Licensee Event Report 285/91-004: Offsite Power low Sianal

Outside Desion Basis

A licensee engineering analysis revealed that the voltage supplied to some

480V safeguards equipment could fall below 87.5 3ercent without the offsite

power low signal (OLPS) being actuated.

Since t11s voltage reduction was

lower than the 90 percent recommended voltage for some safeguards loads, the

licensee determined the plant was outside its design basis.

The licensee's corrective actions included administrative controls of

equipment configurations and bus loadings, as well as raising the OPLS

setpoints. The long-term corrective action was to alter the existing logic

circuitry such that, upon receipt of a safety injection actuation signal,

large equipment not required for accident mitigation would be automatically

load shed.

During this inspection, Modification Request FC-91-008, which changed the load

shed logic, was verified to have been fully implemented and tested during the-

1992 refueling outage. The completion of the modification negated the need

for continued administrative control of equipment configuration and bus

loading.

5.7

(Closed) Licensee Event Report 235/91-005: Violation of Instrument and

Control Technical Specification 2.15

On February 28, 1991, the Instrument and Control technicians were performing

maintenance on Steam Generator Instrument B/PIC-905.

The instrument was

declared inoperable at 25 minutes past midnight- and the trip units were placed

in bypass. At 11:44 a.m., a mechanical jumper (bypass) was installed on the

instrument. At that time it was realized that the bypass should have-been

installed within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> of the instrument being declared inoperable.. The

cause was determined to be wrong interpretation of the requirement by

operations personnel.

The licensee's corrective actions. included training on this event and the

documentation of a-Technical Specification Interpretation. During

this inspection, all corre.ctive actions were verified to have been completed.

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5.8

10hird) Licentes_ty.ettLRengrL2M131-007: Circuit Breaker cosrdination

2L.iD0V_ Distribution Svitsa

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As discussed in paragraph 3.4.4 of the EDSil Report, the licensee identified

and reported pro)1 ems with the overcurrent trip coordination of various 480V

circuit breakers.

The licensee's report provided a commitment to complete a

coordination study and resolve any problems.

The inspectors reviewed the circuit breaker coordination study and the related

modifications as part of Inspection followup Item 285/9101-03 and found them

to be acceptable.

(See paragraph 2.3.)

5.9 (Closed) Licenne Event Report 205/92-008:

Safety Religf Valve ScLooints

Greater lhan Ogalified System Desian Pressure

The licensee reported concerns with four, safety injection system, relief

valves.

Valves SI-187, S1-309, SI-310, and S1-311 had setpoints that were

greater than the system design pressure as qualified by the original

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hydrostatic tests.

Reviews of relief valve setpoints in the safety injection,

chemical and volume control, raw water, component cooling water, auxiliary

feedwater, and the reactor coolant systems were performed in accordance with

Engineering Assistance Request (EAR)91-097 to determine if any other relief

valves had nonconforming setpoints. No other nonconformances were identified.

During this inspection, the licensee's response to EAR 91-097 for the four

valves identified above was reviewed.

Valves SI-187 and S1-310 had a setpoint

of 600 psig while the piping was qualified to 500 psig by hydrostatic test.

Valve $1-309 had a setpoint of 350 psig while the pipin9 was qualified to

300 psig.

The licensee determined that the piping systems were operable

because the pressure ratings for the most limiting. components exceeded the

setpoints of the relief valves.

Valve SI-311 had a setpoint of 150 psig while

the piping was qualified to 66 psig during the original hydrostatic test.

However, in 1983 a hydrostatic test had been cor, ducted at 190 psig.

The

licensee considered the 1983 test sufficient to qualify the piping for

150 psig.

Modification Request FC-92-009, Revision 0, was prepared to reduce the

setpoints of SI-187 and S1-310 from 600 to 500 psig and SI-309 from 350 to

300 psig.

The inspectors-reviewed the Maintenance Work Orders 910725, 910733,

and 910732, and determined that the setpoints had been changed and that the

valves returned to service during April 1992.-

The licensee's long-term corrective actions included revising plant drawings,

updating design basis documents, and performing the required 10-year

hydrostatic test to verify the acceptability of the piping associated with

Relief Valve S1-311.

The inspectors reviewed the controlled plant drawings of

the relief valves and determined that _the valve setpoints-had been )roperly

revised. The inspectors also reviewed marked-up revisions to the $1utdown

Cooling System and Low Pressure Safety injection System design basis documents

and determined that they had been updated to reflect'the changes in relief

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valve setpoints and component design pressures.

The 10-year hydrostatic test

for the piping associated with 51-311 was completed on September 29, 1992, in

accordance with Surveillance Test Procedure S5-51-51-3002, Revision 4 '(SI)

Class 150 Piping 10 Year Hydrostatic Test." The hydrostatic test pressure was

195 psig which qualified the piping for a design pressure of 150 psig.

5.10 LClgiesD Licenite_ItnaLEspatLZM/22-010:

Circuit _ Breaker and fuse

2pordination of 125Vdc Distribution System

The licensee reported that problems had been identified during the design

basis reconstitution effort with the coordination of 125Vdc circuit breakers

and fuses.

The problems occurred because system coordination had not been

properly considered during the 1980 replacetient of the batteries and their

output fuses or during the 1985 changes to the system.

The licensee replaced the battery output fuses during the 1992 refueling

outage in accordance with Hodification Request FC-91-026.

The replacement

fuses had a slower response time and provided proper system coordination.

The insaectors reviewed the licensee's coordination study and found it to be

accept ule.

(See paragraph 2.3.)

5.11 10101tdLLkensee Event Report 2R5/92-012:

Nonconserative 511am

Etatra. tor Differential Pre 11ure Trin SetDoints

The licensee determined that the setpoints for all four channels of the steam

generator transient protection trip function were greater than that allowed by

the Technical Specifications. The cause was determined to be an inadequate

program for implementing and controlling setpoints.

The licensee's corrective actions included the initiation of a new procedure,

SEl-9, "Setpoint/ Tolerance Change and Review." Additionally, the procedures

for design change, electrical system interaction and configuration control

were revised to stress the areas of calculation input and uncertainty.

During this inspection, all of the corrective actions were verified to have

been implemented.

285191-Qlr _ Insufficient Containment

5.12 LClqirdLLicensee Event Report

a

EDLav Pumo Net positive Suction Head

The licensee reported that the containment spray pumps might not have an

adequate suction head during the recirculation phase of operation. This issue

was also discussed in NRC Inspection Report 50-285/92-09, dated May 15, 1992.

The report documented that the licensee had approved SA0 92-02, " inadequate

Containment Spray Pump Net Positive Suction Head."

The SA0 stated that the

existing licensing basis did not allow consideration of subcooling in net

positive suction head calculations.

However, there would be sufficient net

positive suction head available under all accident conditions if subcooling

were considered in the calculation.

The report also stated that the licensee

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had performed a 10 CFR part 50.59 safety evaluation which determined that no

unreviewed safety question existed.

The licensee's long-term corrective actions consisted of:

1) the mechanical

design engineering group performing a review of the condition and its root

cause analysis to emphasize the importance of confirming USAR assumptions when

performing calculations, and 2) a revision to USAR Section 6.2.1 which would

take credit for liquid subcooling in the net positive suction head

calculation.

The inspectors reviewed Memorandum PED-fC-92-1908, dated June 5,

1992, which stated that mechanical design engineers had reviewed the condition

and the root cause analysis.

In addition, the inspectors reviewed the program

document review signoff sheet with the signatures of the engineers that had

reviewed the package.

The inspectors also reviewed the USAR Section 6.2

revision which took credit for 25 percent of the net positive suction head

available from sump subcooling.

(The previous revision to the USAR did not

take credit for subcooling.) This revision to the USAR was submitted to the

NRC on September 18, 1992.

5.13 IClosed) Lictasee Event Report ZMR2-017: C ackina of Cam followers iD

SMLlype Switches

The licensee discovered an inoperable General Electric Ty>e SBN Switch

associated with a 4160V circuit breaker.

Inspection of tie switch revealed

that the Lexon cam follower was broken rendering the switch inoperable.

Previous industry experience, including NRC Information Notice 80-13, had

addressed cracking of polycarbonate cam followers due to exposure to

hydrocarbons during manufacture. A General Electric service inforr.ation

letter was issued in 1976 reconsnended the replacement of switches that had

been manufactured between 1972 and 1976.

The licensee determined that none of

the installed switches were manufactured during that period.

In response to Information Notice 80-13, the licensee performed an inspection

of one switch and found 50 percent of the cam followers exhibited the cracking

described in the information notice. A detailed inspection program using

fiber optic techniques was initiated, but due to visual clarity problems, the

inspections were abandoned in 1984. During the 1985 refueling outage, 30 of

the 90 of the safety-related switches in the control room were replaced.

Some

cracking was discovered, but it was attributed to stress rather than

hydrocarbon exposure.

No switch failures were discovered and the replacement

of s.vitches was suspended.

The licensee's corrective actions related to this recent switch failure

included the inspection and replacement of switches in the 4160V switchgear,

contcol board and auxiliary panel that were cracked or deteriorated.

Additional inspection and replacement activities were also >cheduled for

implementation during future refueling outages.

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5.14 1 Closed) LiceDsee Event Report 285/92 022:

Heater Drain Pumo Cables

During the electrical system short circuit studies, the licensee discovered

and reported a problem with the sizing of sone electrical cables.

The

licensee determined that a fire could result in a short circuit between the

,

three phases of the cables that supplied power to some components, including

,

the heater drain pumps' motors.

A ' bolted short connection" caused by the

fire could cause the cable jacket temperature to increase above allowable

limits in other areas where the cables were routed.

The high cable jacket

tem)eratures could, in turn, cause problems with other, adjacent, cables.

Alt 1ough the heater drain pump motor cables were not safety-related, they

could impact the operability of adjacent safety-related cables.

Therefore,

the licensee replaced the heater drain pump cables in accordance with

Engineering Change Notice 92-311.

The inspectors reviewed the licensee's analysis and actions as part of

Inspection followup Item 9101-01 (see paragraph 2.1) and found that they

resolved the problem.

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AUAGEUil

1 PERSONS CONTACTED

1.1 Omaha Public Power District Personnel

  • R. Andrews, Division Manager, Nuclear Services
  • G. Cook, Supervisor, Station Licensing
  • S. Gambhir, Division Manager, Production Engineering
  • J. Gasper, Manager, Training
  • C. Guliani, Supervisor, Dperations Training
  • R. Jaworski, Manager, Station Engineering
  • L. Kusek, Manager, Nuclear Safety Review

R. Lewis, Principle Engineer, Design Engineering

  • D. Li3py, Licensing Engineer
  • R. Meiaffey, Principal Engineer, Electrical Engineering
  • S. Miller, System Engineer
  • R. Hueller, Supervisor, Electrical Engir.eering
  • J. O'Connor, Manager, Design Engineering - Electrical

,

  • W. Orr, Manager Quality Assurance and Quality Control
  • T. Patterson, Manager, fort Calhoun Station
  • R. Phelps, Manager, Design Engineering
  • R. Short, Manager, Nuclear Licensing and Industry Affairs
  • C. Simmons Station Licensing Engineer
  • J. Tills, Assistant Manager, fort C41hodn Station

>

1.2 NRC Reaion IV Personnel

  • J. Whittemore, Reactor inspector
  • Denotes personnel that attended the public exit meeting conducted on

December 11, 1992.

2 EXIT MEETING

An exit meeting was conducted on December 11, 1992.

During this meeting, the

lead-inspector reviewed the scope and findings of-the inspection.

The

licensee did not identify as proprietary any of the materials provided to, or

reviewed by, the inspectors during this inspection.

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