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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20126F1181975-09-0505 September 1975 AO 50-213/75-3:on 750904,greater than 2 Delta Dissolved Oxygen Alarm Received.Caused by Oxygen Scavanging from Canal Water on Start of Dredging Operation.Backup Sys Started. Monitoring & Grab Sample Results Encl ML20126F1791974-05-0606 May 1974 AO 74-08:emergency Diesel Generator 2B Caught Fire Before Completion of Monthly Load Test.Caused by Overheating of Field Excitation Transformer & Subsequent Burn in Winding. Transformer Removed Pending Receipt of Replacement ML20126F1831974-04-0505 April 1974 AO 74-06:containment Penetration P-60 Failed to Meet Acceptable Leak Rate During Routine Surveillance Test. Cause Under Investigation 1975-09-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K3301999-10-19019 October 1999 Safety Evaluation Supporting Amend 195 to License DPR-61 ML20206C8761999-04-28028 April 1999 Safety Evaluation Supporting Amend 194 to License DPR-61 CY-99-047, Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use1999-03-23023 March 1999 Ro:On 981217,identified Unsuccessful Dewatering of Cnsi HIC, Model PL8-120R,containing Resins.Caused by Apparent Failure of Dewatering Tree.Other HICs Have Been Procured,Recertified & Returned to Plant for Use ML20206F1971998-12-31031 December 1998 Annual Rept for 1998 for Cyap. with CY-99-027, Annual Rept for 10CFR50.59, for Jan-Dec 1998.With1998-12-31031 December 1998 Annual Rept for 10CFR50.59, for Jan-Dec 1998.With ML20198G9101998-12-22022 December 1998 Proposed Rev 2 of Cyap QAP for Haddam Neck Plant. Marked Up Rev 1 Included ML20238F2131998-08-28028 August 1998 SER Accepting Defueled Emergency Plan for Emergency Planning for Connecticut Yankee Atomic Power Co CY-98-136, Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line1998-08-12012 August 1998 Ro:On 980727,flow Blockage Occurred & Caused Pressure in Sys to Increase,Resulting in Relief Valve Lifting & Pipe Vibration,Which Caused Leaks to Develop.Caused by Nearly Closed post-filter Inlet Valve.Repaired 2 Leaks in Line ML20237B7461998-07-22022 July 1998 1998 Defueled Emergency Plan Exercise Scenario Manual, Conducted on 980722 ML20202D1621998-06-30030 June 1998 Safety Evaluation Supporting Amend 193 to License DPR-61 CY-98-068, Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms1998-04-15015 April 1998 Follow-up to Verbal Notification on 980413 of Film on Discharge Canal.Investigation Continuing.Samples Collected for Petroleum Analyses & Biological Characterization at Intake Structure & Discharge Canal.Replaced Sorbent Booms CY-98-045, Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing1998-04-13013 April 1998 Ro:On 980212,0219,0225 & 0312,separate Sheens of Approx One Cup of oil-like Substance Was Observed at Discharge Canal. Cause Has Not Been Clearly Identified.Called in Vendor Spill to Install Sorbent Booms to Absorb Sheen.W/One Drawing ML20217F0611998-03-31031 March 1998 Historical Review Team Rept ML20217A0001998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Haddam Neck Plant ML20217K2101998-03-27027 March 1998 Safety Evaluation Supporting Amend 192 to License DPR-61 CY-98-046, Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal1998-03-12012 March 1998 Follow-up to 980311 Verbal Notification of Film on Discharge Canal.Cause Not Yet Determined.Film Is Contained & Will Be Absorbed by Containment & Sorbent Booms That Were in Place in Discharge Canal ML20216D6531998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Haddam Neck Plant ML20217D7381998-02-28028 February 1998 Revised MOR for Feb 1998 Haddam Neck Plant CY-98-012, Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant1998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Connecticut Yankee Haddam Neck Plant CY-98-010, Annual Rept for 10CFR50.59,Jan-Dec,19971997-12-31031 December 1997 Annual Rept for 10CFR50.59,Jan-Dec,1997 ML20198N6681997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Haddam Neck Plant ML20217P4861997-12-31031 December 1997 1997 Annual Financial Rept, for Cyap ML20199L5891997-12-24024 December 1997 Independent Analysis & Evaluation of AM-241 & Transuranics & Subsequent Dose to Two Male Workers at Connecticut Yankee Atomic Power Plant ML20203K4271997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Haddam Neck Plant ML20199B1141997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Haddam Neck Plant ML20198M8101997-10-14014 October 1997 SER Accepting Proposed Revs to Util Quality Assurance Program at Facility ML20198J8811997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Haddam Neck Plant ML20210P8721997-08-31031 August 1997 Post Decommissioning Activities Rept, for Aug 1997 ML20217Q3171997-08-31031 August 1997 Addl Changes to Proposed Rev 1 to QA Program ML20210U9301997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Haddam Neck Plant CY-97-082, Special Rept:On 970708,routine Surveillance Testing of Seismic Monitoring Sys Instrumentation Revealed,Data Was Not Being Reproduced by Portion of Playback Sys.Station Presently Pursuing Replacement of Seismic Monitoring Sys1997-08-14014 August 1997 Special Rept:On 970708,routine Surveillance Testing of Seismic Monitoring Sys Instrumentation Revealed,Data Was Not Being Reproduced by Portion of Playback Sys.Station Presently Pursuing Replacement of Seismic Monitoring Sys ML20210L0521997-07-31031 July 1997 Monthly Operating Rept for July 1997 for HNP ML20149E4451997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Haddam Neck Plant ML20141A0041997-05-31031 May 1997 Independent Assessment of Radiological Controls Program at Cyap Haddam Neck Plant Final Rept May 1997 ML20140H5241997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Haddam Neck Plant ML20141K4201997-05-22022 May 1997 Safety Evaluation Supporting Amend 191 to License DPR-61 ML20141D4141997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Connecticut Yankee Haddam Neck ML20138G5901997-04-25025 April 1997 Proposed Rev 1 to Cyap QA Program for Haddam Neck Plant ML20137W8051997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Haddam Neck Plant ML20137H3031997-03-31031 March 1997 Rev 2 to Nuclear Training Loit/Lout Audit Reviews ML20137C6281997-03-14014 March 1997 Redacted Version of Rev 1 to Nuclear Training Loit/Lout Audit Reviews ML20137A0801997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Haddam Neck Plant ML20135C5101997-02-26026 February 1997 1996 Refuel Outage ISI Summary Rept for CT Yankee Atomic Power Co B16268, Special Rept:On 970205,declared Main Stack-Wide Range Noble Gas Monitor Inoperable.Caused by Inadequate Calibr Methods. Will Revise Calibr Procedure to Technique to Demonstrate Accuracy & Linearity Over Intended Range of Monitor1997-02-19019 February 1997 Special Rept:On 970205,declared Main Stack-Wide Range Noble Gas Monitor Inoperable.Caused by Inadequate Calibr Methods. Will Revise Calibr Procedure to Technique to Demonstrate Accuracy & Linearity Over Intended Range of Monitor ML20135E3221997-02-13013 February 1997 Independent Review Team Rept 1996 MP -1 Lout NRC Exam Failures ML20134L2751997-02-0303 February 1997 Draft Rev to GPRI-30, Spent Fuel Storage Facility Licensing Basis/Design Basis ML20138K5721997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Haddam Neck Plant.W/ ML20134L2791997-01-10010 January 1997 Rev 0 to QA Program Grpi ML20134L2911997-01-0808 January 1997 Rev 0 to UFSAR Rev Grpi ML20134L2721996-12-31031 December 1996 Commitment Mgt Grpi 1999-04-28
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AbN0'TlLi OCCURRENCE REPORT 60- 2t 3 Report Utr6er: 50-213/75-3 Report Dctu: September 5, 1975 Occurrence Date: September 4,1975 Facility: Haddan Hec k Plant Connecticut Yatikee Atomi; Power Comnany Idnetification of Occurrence: Correspondence CYH-3058; Seetember 5, 1975; Tech. Spec. B, Section 2.3.3.1; Diss. Oxygen Conditions Prior to Occurrcnce: Steady State Power Descrintion of Occurrence:
A greatcr than 2 delta dissolved oxygen alarm was received across the plants cooling uater on 9/d at 0930. Grab samples were taken and analyses rude to veri fy coriditions. It was not ii.rediately apparent what could be causing this condition and sampling %dicated we were back in specifications by 1235 on the san.2 day. Tne grab samples also identified that the continuous monitors were not functioning properly even though they had alarmed. He switched to our back-up system. Attachnent A is a record of our continuous monitoring results and grab samples spanning this period.
Designation of Anonrent Cause of Occurrence _:
Unusual Service Condition Including Environnental Analysis of Occurrence:
There was no traceable clant event that paralled the time span of this occurrence. However, c.. aging in the canal upstream of the monitor had started on the same day. It is conceivable and believed that reducing material icosened on the start of the dredging operation scavanged oxygen from the canal water. The dissolved oxygen parameters have remained within acceptable limits since this occurrence.
Corrective Action:
Tnis event is not considered remediable by corrective plant operation.
Failure Data:
See Attachment.
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[ Attacl- -)t 50 'i13/75-3 Ill-00T IfiTAKE DISCH. , _
PACKAGE GRAB SAMPLE PACKAGE GRAB SAMPLE ;
DATE TIIiE D155. O DISS. 02 DISS. 02 0.1S5. 02- A DISS 02
,9-4-75 0920 4.4- 9.0 > +2.0 Package S-4-75 1030 5.0 8.5 8.8 4.5 - 4.0 Grab 9-4-75 1100 6.4 9.0 > +2.0 Package 9-4-75 1205 6.2 8.7 9.2 l
9-4-75 1220 6.3 9.3 6.5 - 2.2 Grab 9-4-75 1235 7.2 9.2 7.6 - 1.1 Grab {
9-4-75 1245 7.2 9.15 8.1 - 0.6 Grab 9-4-75 1300 7.2 9.1 9.2 4 9-4-75 1315 7.2 9.4 9-4-75 1400 7.6 9.1 8.4 - 0.7 Grab 9-4-75 1600 8.0 8.8 + 1.1 Package j
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P C O N N ECY g C U T VA N SC MM ATO M f C P" O W E R COMPANY
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January 73 1976 CYH - 3160 U. 5. Nucl ea r Regu Ta tory caserri s s ion Directorate of Regu1 story 0;aeratic>ns Hegion I h h #m ,. o 3 631 Perk Avenue t Ki ng o f Pru s sia . Pennsylvanta 19506 Attention: P' r . James P. O'Refily.
Director Ocar Hr. O'Rc411y-In acroccance with the reportino requirements of Connecticut Yanben Technical spec i f ica t ions . Section G.9.2.a. the following prefirinary renort "p(ressure concerninais 7 5 -1 LP )transettters thehereby r.si runction sutei t ted. of two nain stean emcess flow differential During severe sub-rero weather conditions, sensinn itnes to two high steen flua diffurential pressure transr .i tters frnre. The c oi n e-i d en c e n t" the tw s hich steam flow stq%els satisfied the trippinq lofjic and a reactor /
turbine trip occurred from fu17 p o w e r- (s SD3 Pr.(e ) . Tne instru ent sens1ng lines were thawed and the ins trv%n ta tion return ed to n o rs .a l .
i Tne instru w=ntw in quention are housed in en enclosure attached to the ';
outside of the Henctor contein w nt. Sub-zero coupled with scre openingr. Inadvertently lefttaw- in .s erawall the tu re ass and stronn wints a result of a recent (hion eneroy nine break) rodification to the enclosure overcam the encler.ure hen ti n g systm and caused locyl freezing of the sensing lines.
The enclosure but1 ding openings were pT u gg ed ans addi tional free 7e pro-tection was applied to the sensing lines.
Very truly yours, d s/A . t ~
Rfchard H. Graves Plant Superintendent FUlG/ved
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