ML20126B411

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Insp Rept 50-341/92-17 on 921014-1208.Violation Noted.Major Areas Inspected:Action on Previous Insp Findings & Concern, Operational Safety Verification,Esf Sys,Onsite Event Followup,Reactor Startup,Security & Maint Activities
ML20126B411
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 12/11/1992
From: Phillips M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20126B311 List:
References
50-341-92-17, NUDOCS 9212220080
Download: ML20126B411 (16)


See also: IR 05000341/1992017

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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Report No. 50-341/92017(DRP)

Docket No. 50-341

License No. NPF-43

Licensee:

Detroit Edison Company

2000 Second Avenue

Detroit, MI 48226

Facility Name:

Fermi 2

Inspection At:

Fermi Site, Newport, Michigan

Inspection Conducted: October 14, 1992 through December 8, 1992

Inspectors:

W. J. Kropp

K. Riemer

R. Twigg

S. Stasek

T. Colburn

R. Stransky

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Approved By:

'M.

P. Phillips, Chief

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Reactor Projects Section 2B

Date~

Inspection Summary

inspection from October 14. 1992 mthrough December 8. 1992

(Recort No. 50-341/92017 (DRP))

Areas Insoected: Routine, unannounced safety inspection by the resident

inspectors of action on previous inspection findings and a concern;

operational safety verification; engineered safety feature systems; onsite

event followup; reactor startup; current material condition; housekeeping and

plant cleanliness; radiological control::; security; safety assessment / quality

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verification; maintenance activities; surveillance activities; and performance

evaluation activities.

Results: Of the thirteen areas inspected, no violations were identified in

twelve areas, and one violation was identified in one area pertaining to

overtime (paragraph 3.a).

Two Unresolved Items were identified that pertained

to: the failure of notifying the NRC of an Unusual Event within the specified

time frame (paragraph 3.c), and the process of reviewing Service Information

Letters (Sils) (paragraph 4).

In addition, three Inspection Followup Items

were identified that pertain to the use of computer analysis for simulator

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taodeling (paragraph -3.c); the contrcl of fire doors (paragraph 3.d); and use

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of procedures (paragraph 5.a).

The licensee's performance in operations was

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considered good. The operator's initial response to the loss of feedwater

transient was considered excellent. However, subsequent notification to the

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9212220080 921211

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NRC of the event was-not timely.

Shift briefings were thorough which allowed-

on shift personnel to be cognizant of' plant conditions. Operator's response

to annunciator alarms were good, however,-repeat backs pertaining to equipment

manipulations were not consistently implemented.

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DETAILS

1.

Persons Contacted

Detroit JJ11 son C_ompaDI

C. Cassise, General Supervisor, Mechanical Maintenance

  • W. Colonnello, Supervisor Plant Evaluation, Plant Safety

J. Contoni, Supervisor, Plant Systems

  • R. DeLong, Manager, Radiation Protection

R. Eberhardt, Superintendent, Radiation Protection

P. Fessler, Director, Nuclear Training

  • D. Gipson, Vice President, Nuclear Operations
  • L. Goodman, Director, Quality Assurance
  • E. Hare, Senior Compliance Engineer, Nuclear Licensing

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J. Hughes, General Supervisor, Electrical Maintenance

J. Korte, Director, Nuclear Security

  • A. Kowalczuk, Superintendent, Maintenance and Modifications
  • R. Matthews, Assistant Superintendent, Maintenance
  • R. McKeon, Plant Manager, Nuclear Production
  • W. Miller, Superintendent, Technical Engineering
  • R. Newkirk, General Director, Regulatory Affairs
  • W. Orser, Senior Vice President, Nuclear Operations
  • D

Ockerman, General Superintendent, Training

  • J. Plona, Superintendent, Operations
  • R. Russell, Outage Manager
  • A. Settles, Director, Licensing
  • R. Stafford, General Director, Nuclear Assurance
  • R. Szkotnicki, Director, Plant Safety
  • J. Tibai, Supervisor, Compliance
  • J. Walker, General Director, Nuclear Engineering
  • Denotes those attending the exit interview conducted on

December 8, 1992.

The inspectors also had discussions with other licensee employees,

including members of the technical and engineering staffs; reactor and-

auxiliary operators; shift supervisors; electrical, mechanical,- a.id

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instrument maintenance personnel; and. security personnel.

2.

Action on Previous Insoection Findinos and a Concern'(92701)

a.

(Closed) Open Item (341/89008-15(DRP)): Due to a reactor water

cleanup (RWCU) isolation, the licensee had proposed-to relocate

the RWCU . blowdown flow control valve (FCV) G33 F033 downstream of

the flow control element G33-FE-N0ll. The licensee concluded that

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moving- the- valve-upstream of_ the flow element would decrease the-

probability of water: flashing to steam across the flow element.

The licensee had experienced:a- series of RWCU system isolation

trips due to' spurious signals from the blowdown transmitter. The

licensee had issued EDP.4885 to move the valve.

An evaluation by

the licensee concluded that moving the FCV was not necessary.

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Instead, the licensee added a caution to the RWCU operations

procedure 23.707, controlling the length of time that the two

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valves, downstream of FCV G33 F033, could remain open

The

caution further stated a differential flow isolation could occur

when the instrument _ lines were not full of water. The item is

closed based on the administrative control of the two downstream

valves.

b.

(Closed) Open Item (341/90010-Ol(DRP)): Diversity requirements of

10 CFR 50.62. The licensee's design for the recirculation pump

trip and alternate rod insertion, as endorsed through the NRR SER,

was implemented acceptably with one exception. Regarding

diversity from the existing reactor protection system (RPS),'the

SER concluded that the use of the Rosemount analog

transmitter / master trip units (ATTUs) in both the ATWS'and RPS did

not meet the diversity requirements of 10 CFR 50.62.

The licensee

prepared PDC 12029. Rev 0, to replace 12 Rosemount trip units with

GE units.

In a letter to the NRC dated July 12, 1991, the

licensee committed to an implementation schedule to replace the

units. The inspector verified, via a review of licensee records,

that the work requests to replace the trip units had been

completed. This matter is considered closed,

c.

(Closed) Open item (341/90013-ll(DRP)): The use of uncontrolled

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handwritten labels attached to electrical cabinets. The licensee

recognized that during construction many uncontrolled labels were

installed on electrical cabinets to assist construction personnel

in locating specific components. As part of the corrective

actions to DER 90-0672, the licensee initiated a labeling upgrads

program for labeling plant equipment.

In addition, the licensee

issued procedure, FIP-0Pl-04, " Equipment Labeling," that

prescribed the method for generating, installing, maintaining, and

controlling plant equipment labels and signs. The licensee

recently completed the labeling upgrade system on the high

pressure coolant injection (HPCI) and residual heat removal (RHR)

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systems. The inspectors walked down part of the HPCI system'and

found that the old handwritten labels had been removed from the

HPCI electrical panels and motor control centers (MCCs).

In

addition, the inspectors noted that the new labels were consistent

with the guidance provided in procedure FIP-OPI-04 that required

labeling.be based on operator terminology. This item is closed

based on current corrective actions and the licensee's commitment

to complete the labeling upgrade program by 1994,

d.

(Closed) Open Item (341/90020-04(DRP)): Additional licensee

review for control room modifications;following operator

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inadvertent closure of a main steam isolation-valve. -The

inspectors reviewed records for additional occurrences of

inadvertent operations, the completed deviation event report, _and

the independent review. .The inspectors concluded that the

licensee's independent review appeared to be effective and

comprehensive. Additional identified human factors enhancement

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were tentatively scheduled for completion in refueling outage

RF04.

This matter is considered closed.

e.

(Closed) AMS-RIII4 ?-A-Oll2: A concern was received by Region III

regarding exceeding overtime limits without proper management

review and approval. This matter was referred to the licensee for

review and disposition by Region III letter dated October.20,

1992. The licensee respor.ded by letter dated November 23, 1992.

Even though the specific concern was not substantiated, the

subject of overtime use and approval was inspected by the resident

inspectors. This inspection resulted in a violation which is

addressed Ir iaction 3.a of this report. The followup will be

tracked tnder the violation and, therefore, this concern is

considered closed.

3.

Plant Operations

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On November 4, the licensee commenced a reactor startup following the

plant's third refueling outage. The outage, cheduled for 52 days, was

completed in 57 days. Major work completed during the outage includeo

the following items:

power uprate modifications, rea. tor vessel

inservice inspection (ISI), reactor vessel pressurc test, safety relief

valve (SRV) replacements, high pressure coolant injection (HPCI) turbine

inspections, addition of an eighth condensate filter demineralizer,

erosion / corrosion piping replacement, installation of the torus hardened

vent, and replacement of the 28 main transformer. The reactor was

placed in mode 2 at 3:30 p.m. on November 4 and criticality was achieved

at 11:57 p.m.

After the plant heatup, plant personnel commenced an

extended startup test program following a power uprate license change.

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The resident- inspector staff, augmented by NRR personnel, observed and

monitored the reactor startup and test program activities.

On November 11, 1992, during steady state operation at 98 percent power,.

the licensee experienced a manual reactor trip. The action was taken-

following a loss of feedwater to the reactor vessel when the heater feed

pumps tripped, followed-several seconds later by the tripping of both

reactor food pumps.

Following the investigation and subsequent

corrective action, the reactor was restarted and the generator

synchronized to the grid on November 11, 1992.

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On December 1, the-plant experienced a runback of the recirc pumps due-

to the loss of the Heater Drains System'. Subsequent investigation by

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the licensee determined the-cause of the event to be a leak in the

extraction steam line from the Center Low Pressure Turbine to the number

4 North Feedwater Heater. The licensee commenced a plant shutdown on

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December 4 to perform various repairs to leaking plant equipment.

Critical path during the outage will.be repairs to the extraction steam

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line to the number 4 North Feedwater Heater. Other items scheduled for

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the outage include repairs to the Moisture Separator Reheater drain line

bellows and repairs to the South Reactor Feed Pump Turbine High Pressure

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steam isolation -valve flange leak. A drywell entry was also planned to

perform work on a drywell equipment drains sump pump, investigate a

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possible low oil level on the

"B" reactor recirc pump, and troubleshoot

problems on the Loose Parts Monitor. The-licensee tentatively plans to

restart the plant December 13 and synchronize to the grid December 14.

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a.

Operational Safety Verification (71707)

The inspectors verified that the facility was being operated in

conformance with the license and regulatory requirements, and that the

licensee's management control system was effective in ensuring safe

operation of the plant.

On a sampling basis, the inspectors verified proper control room _

staffing and coordination of plant activities; verified operator

adherence with procedures and technical specifications; monitored

control room indications for abnormalities; verified that electrical

power was available; and observed the frequency of plant and control

room visits by station management. The inspectors reviewed applicable

logs and conducted discussions with control room operators throughout

the inspection period. The inspectors observed a number of control room

shift turnovers.

The turnovers were conducted in a professional manner

and included log reviews, panel walkdowns, discussions of maintenance

and surveillance activities in' progress or planned, and associated LC0

time restraints, as applicable. The inspectors considered the.

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operator's response to annunciator alarms as good. However, repeat

backs pertaining to equipment manipulations were' not consistently

implemented.

During the inspection period, the licensee informed the inspectors of an

overtime issue identified in a QA surveillance performed in. September

1992 (92-0134) and documented in DER 92-0592. The DER identified that'

administrative procedure FIP-AD4-03, " Overtime and Fitness For Duty

Guideline," had not been properly implemented during the recent

refueling outage (RF03). Specifically, on approximately 65 occasions,

noncomformance with the procedure occurred with some identified as

violations of Technical Specification when overtime limits were exceeded

without proper management approval. The September su veillance was

performed to assess the effectiveness of corrective actions taken after

a surveillance in May and April 1991 (No 91-0128) during RF02 on the

same subject and documented in DER 91-0542.

The inspectors issued a

non-cited violation (50-341/91015(DRP)) in August 1991 for the

deficiencies identified by the licensee during Surveillance 91.0128.

One additional _ surveillance (No. 91-0219) was conducted dur.ing a. forced

outage.in December 1991. .Each of the three surveillances consisted of a

sampling of the hours reportad by site personnel.- The inspectors

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identified the following common problems during each of the.

surveillances.

Failed to track seven consecutive days as a rolling seven days-

instead of a standard work week.

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DER 91-0542 noted that many groups on site were interpreting

seven consecutive days to mean the pay week,_rather than any

seven consecutive days which may have occurred over two pay

periods. The DER (No. 92-0008) resulting from the December 1991

surveillance was based on an individual's interpretation of the

seven day rule as a work week.

The inspectors noted that the

October surveillance data showed most of the violations were the

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result of hours extending across two work weeks.

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Confusion over the length of allowable shift turnover time.

DER 91-0542 stated that the amount of time allosed for shift

turnover varied from one-half hour to two hours per day.

The DER

issued during the December 1991 surveillance was closed based on

the Plant Manager's revised interpretation of FIP-AD4-03 from one

hour of allowed turnover per shift to one hour before and one hour

after the shift (Prior to RF03). The procedure was modified to

one 30 minute turnover per shift. A number of possible procedure

violations in the October 1992 surveillance were caused by site

personnel not appropriately reporting turnover time.

Failed to perform monthly reviews of overtime.

DER 91-0542 noted that there was no evidence that the plant

manager was reviewing personnel overtime at least monthly as

required by the procedure. The procedure was revised.to require

all section heads to document overtime in a monthly memo to the

plant manager to ensure excessive hours had not been worked by any

individual. This requirement was not uniformly complied with

during RF03.

Based on the above identified repetitive problems, the failure to

correct deficiencies noted in the overtime process in April 1991 is

considered a violation of 10 CFR 50, Appendix B, Criterion XVI

(341/92017-01(DRP)).

b.

Enaineered Safety Feature (ESF) System Walkdowns (71710)-

During the inspection, the inspectors selected accessible portions

of several ESF systems to verify status.

Consideration was given

to the plant mode, applicable Technical Specifications, Limiting

Conditions for 0peration requirements, and other applicable

requirements.

Through observation, the inspectors verified that the following-

was acceptable:

installation of hangers and supports;

housekeeping; freeze protection, if required, was installed and

operational; valve position and conditions; no potential ignition

sources; and major component labeling, lubrication, cooling, etc.

The inspectors also verified that instrumentation was properly

installed and functioning and that significant process parameter

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values were consistent with expected values; that instrumentation

was calibrated; that necessary support systems wve operational;

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and that locally and remotely indicated breaker and valve

positions agreed.

During the inspection, the accessible portions of the following

ESF systems were walked down:

Standby Liquid Control

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High Pressure Coolant Injection

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c.

Onsite Event Follow-up (93702)

On November 11, 1992, at 8:29 p.m., during steady state operations

at 98 percent power, the licensee experienced a loss of. feedwater

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to the reactor vessel when the Heater Feed Pumps tripped followed

several seconds later by tripping of both Reactor Feed Pumps.

During the transient, both High Pressure Coolant Injection (HPCI)

a7d Reactor Core Isolation Cooling (RCIC) automatically started to

restore reactor vessel water level. Upon identification that a

loss of.feedwater had occurred, operator actions were taken to

manually scram the reactor. This was accomplished just prior to

reactor water level decreasing to the low level scram setpoint and

was done within approximately 12 seconds of the loss of feedwater.

The inspectors considered the operator's response to the transient

as excellent. The operators entered the Emergency Operating

Procedures (EOPs) to recover reactor vessel water level and

declared an Unusual Event due to actuation of an engineered safety

feature (ESF). The lowest level reached was 77 -inches

(1.95 meters), approximately 120 inches (3.05 meters) below the

normal level . With level restored, the operators manually secured

HPCI and RCIC and utilized the Standby feed Water system (SBFW) to

maintain reactor vessel water level. At 9 p.m. all conditions

were stable and the licensee terminated the Unusual Event. 'The

resident-inspector responded to the event end monitored the

licensee's recovery actions.

The inspectors determined that all

- required 15 minute notifications were made within the specified

timeframe with the exception of the required one hour notification

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to the NRC which was made approximately-46 minutes after the one-

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hour limit. This is considered an Unresolved Item pending'further

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NRC review by Region III Emergency Pieparedness inspectors.

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(341/92017-02(ORP))-

All systems functioned as expected with the exception of valve-

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Gil-F019, the drywell equipment drain sump upstream isolation

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valve. The valve failed.to indicate fully closed at the control

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room panel.

Per Technical Specification requirements, the

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licensee deenergized closed another isolation valve in that line.

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Subsequent investigation revealed that the valve was actually

closed,- and the dual indication received was due to a limit switch

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problem. A work request was initiated to correct the position-

indication problem, and the work was completed prior to restarting

the plant.

The licensee subsequently determined the most probable root cause

of the transient was a personnel error by a non-licensed operator

during a backwash evolution of the "H" condensate filter

domineralizer. An inadvertent opening of a 10-inch (25.4 cm)

influent line to the demineralizer diverted flow from the heater

feed pumps causing all three pumps to trip on low suction

pressure.

This, in turn, caused the reactor feedpumps to trip on

low suction pressure, resulting in a loss of feedwater to the

reactor vessel.

The inspectors reviewed the response of the reactor and safety

systems after the scram through direct observation of control room

indications and discussions with licensee personnel.

Plant

parameters, emergency systems status, and plant effltsent levels

were verified to be within required limits during and following

the scram. The inspector reviewed operator and shift supervisors'

logbooks, sequence of events recorder (SOER) alarm printouts,

strip chart recorders, and other information relating to the

event, and verified that all systems responded per design. The

inspectors noted following the scram that the decrease in water

level to an approximately indicated 77 inches (1.95 M) was' as

predicted by the General Electric (GE) analysis and associated

power uprate submittals to the NRC.

However a Detroit Edison

RETRAN computer modeled analysis appeared to be inconsistent with

both the GE analysis and actual plant response.

The RETRAN

modeled analysis indicated that with a loss of feedwater, water

level would decrease to a minimum of 100 inches (2.54 M) versus

the 77 inches (1.95 M) that actually occurred. Although not

affecting the licensee's overall review and power uprate

submittals, there was a concern that simulator modeling could have

utilized the RETRAN analysis. Therefore, the present simulator

response could differ from actual plant response based on the

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recent power uprate.

Pending-further licensee review to ascertain

the use of the specific RETRAN analysis, this matter is considered

an Inspection Followup Item (341/92017-03(DRP)).

The inspector reviewed portions of the licensee *s preparations for

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restart. Overall, activities observed or reviewed were found to

be in conformance with applicable administrative requirements. The

reactor was subsequently restarted on November 23 and synchronized -

to the electrical grid the following day.

d.

Reactor Startuo

The inspectors attended the onsite safety review organizmtion

(0SRO) startup meeting to monitor that preparations for startup

were comp 1ete,-documented, and reviewed by-the= appropriate

management level. The meeting was conducted in a professional

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manner with good command and control exhibited by the OSR0

chairman. All power uprate related issues, modifications,

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signoffs, etc., were completed.

The chairman reserved signoff

authority until all open issues had been resolved.

Activities within the control room were observed by the

inspectors. The decorum within the control room was well

maintained with almost no exceptions.

Shift Supervisors and

Assistant Shift Supervisors were very aware and in control of

noise levels and personnel within the control room environment.

Control of evolutions was good. However, a drop in reactor level

of approximately 5 inches (12.7 cm) resulted-in a low level alarm

d en a feedwater heater feed pump was brought online.

Recovery

actions by the Assistant Shift Supervisor were very good.

Positive action to stabilize the plant on the start up level

controller was exhibited.

The inspectors also monitored the performance of the HPCI flow

test.

The Shift Supervisor displayed excellent command presence

and system knowledge in troubleshooting a high differential

pressure across the oil strainer. The Shift Supervisor did not

accept convenient explanations and recommendations to continue the

test. The cause was properly diagnosed as a malfunctioning

pressure gage. During the evolution, the control room noise level

was low and communications were professional.

The inspectors conducted numerous walkdowns of the reactor and

turbine buildings prior to and during the startup to assess the

licensee's readiness and material condition of_ the plant.

Several

minor material deficiencies were noted. The most significant of

these was the inability of fire door RA2-7 to close by itself.

The inspectors observed an operator pass through the door, and

even though the door did not fully close, the operator continued

on his rounds apparently unaware.of the door's conditicn.

Several

operations by the inspector showed that the door failed to fully

close most of the time. The door was-in the same fire area-as

RA2-6 whose latching mechanism was found taped open, presumably

because of the same door problem. The control of fire doors is an

Inspection Followup item (341/92017-04(DRP)).

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Current Material Condition (71707)

The inspectors performed general plant as well as selected system

and component walkdowns to assess the general-and specific

material condition of the plant, to verify that work requests had

been initiated for identified equipment problems, and to evaluate

housekeeping. Walkdowns-included an assessment of the buildings,

components, and systems for proper identification and tagging,

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accessibility, fire and security door _ integrity, scaffolding,

radiological controls, and any unusual conditions. Unusual

conditions included but were not-limited to water, oil, or other

liquids on the floor or equipment; indications of leakage through

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ceiling, walls or floors; loose insulation; corrosion; excessive

noise; unusual temperatures; and abnorma'i ventilation and

lighting.

The inspectors noted that the licensee continued to

experience some difficulties with respect to the heater drains

system.

Following the startup after the plant's third refuel

outage, maintenance personnel had to perform repairs _to correct

various leaks. Examples included a shaft seal leak on the south

heater drains pump (HDP), a union leak on the center HDP, a

discharge pressure tap on the center HDP, and a sensing element-

leak on the center HDP train. Overall, the inspectors considered

the material condition of the plant as satisfactory,

f.

Housekeepina and Plant Cleanliness (71707)

The inspectors monitored the status of housekeeping and plant

cleanliness for fire protection and protection of safety-related

equipment from intrusion of foreign matter. Housekeeping was

considered satisfactory. During an inspection of the drywell

prior to close out, the inspectors found cbbris that included a

piece of rope and a hard hat. The drywell had been previously

inspected by the licensee in the area where the debris was found,

g.

Radioloaical Controls (71707)

The inspectors verified that personnel were following health

physics procedures for dosimetry, protective clothing, frisking,

posting, etc., and randomly examined raoiation protection

instrumentation for use, operability, and calibration.

During routine inspection tours of the reactot , turbine', and

auxiliary buildings, the inspectors noted, on several occasions,-

candy wrappers, gum wrappers, gum, and cigarette butts within the

radiological controlled area (RCA). The inspectors' observations

were communicated to the appropriate radiation protection

supervisor.

h.

Security .(71707)

Each. week during routine activities or tcurs, the inspectors

monitored the licensee's security-program to ensure that observed

actions were being implemented according to the approved security

plan. The inspectors noted that persons within-the protected area-

displayed proper photo-identification badges,- and those

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individuals requiring escorts were properly escorted.

Additionally, the inspectors also_ observed that personnel and

packages entering the protected area were searched by appropriate

equipment or by hand.

One violation was identified.

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Safety Assessment /0uality Verificati9D (40500 and 92700)

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Through direct observations, discussions with licensee personnel, and

review of records, the following event reports were reviewed to

determine that reportability requirements were fulfilled, that immediate

corrective action was accomplished, and that corrective action to

prevent recurrence had been or would be accomplished in accordance with

Technical Specifications (TS):

LClosed) LEP (341/90-002) Revision 1:

Under this revision, the

licensee performed setpoint evaluations of all the Technical

Specification radiation monitoring alarm setpoints.

The

evaluations were performed under DER 87-398 as part of the

Technical Specification Improvement Program concerns. During the

previous review of this LER, the licensee had completed all but 20

discretionary items.

In September 1991, the licensee completed

all remedial and corrective actions associated with the radiation

monitoring alarm setpoints. This LER is closed.

(Closed) LER (341/90-011): On October 6, 1990, the reactor

scrammed due to low reactor water level.

Prior to the scram, the

instrumentation and controls (I&C) technicians were investigatin9

a 20 inch (50.8cm) discrepancy between the "A" and "B" reference

legs.

The instruments off the "A" reference leg were indicating

193-195 inches (490-495cm) while the instruments off the "B"

reference leg were indicating 20 inches lower. While

troubleshooting efforts were in progress, the low reactor water

level setpoint of 173.4 inches (440.4cm) was reached. The

licensee attributed the cause of the event to air voids in the "A"

reference leg which gave an erroneous high reading. -The licensee.

indicated that air bubbles may have been introduced into the:

reference leg when some of the transmitters were replaced during

the outage.

In September 1988, the licensee had received a General Electric

(GE) Service Information Letter (SIL) 470 from the vendor t.hich

identified concerns with reactor water level mismatches. Two of

the recommendations provided by the SIL for reducing the chances

of unexpected water level mismatches were: backfill the process

instrument piping after surveillance testing; and train-plant

operations personnel in appropriate methods for responding to

mismatches between water level instrument indications. At the

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time of the reactor water level scram, the licensee had -already

evaluated the SIL under DER 88-1833; however, the licensee decided-

not to implement the two recommendations mentioned above. The

licensee determined that the recommendation for backfilling the

reference legs should have been implemented. The licensee issced

DER 90-0625 to reevaluate GE SIL 470.

Pending a review of DER 90-

625, the SIL process is considered an Unresolved Item (341/92017-

05(DRP)).

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As part of the corrective actions to LER 90-011, the licensee

implemented the following corrective actions:

(1)

Lower heatup rate to allow additional time for monitoring

level instrument response.

(2)

Data collection to check the effectivehess cf corrective

action.

(3)

No steam draw until 125 p..ig (862 kPa) to minimize level

transients.

(4)

Conservative level control (use lowest reading instrument).

(5)

Following extended outages (29 or more days) a backfill

and/or flush of the reference leg will be performed.

The inspector verified that the lict :ee implemented all the

corrective actions listed above.

No violations or deviations were identified.

5.

Maintenance /Surveillante (62703 & 61726)

a.

Maintenance Activities (62703)

Routinely, station maintenance activities were observed and/or-

reviewed to ascertain that they were conducted in accordance with

approved procedures, regulatory guides and industry codes or

standards, and in conformance with technical specifications.

The following items were also considered during this review:

limiting conditions for operation were met while components or

systems were removed _from service; approvcis were obtained prior

to initiating the work; functional testing and/or calibrations

were performed prior to returning components or systems to

service; quality control records were maintained; and activities

were accomplished by qualified personnel.

Portions of the following maintenance activities were observed

and/or reviewed:

920902

Scale Changeout for RHR Disd.%e Pressure

.

Indicator

920516

Calibration Charcoal Absorber Temperature

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controller for Standby Gas Treatment

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The inspectors identified concerns witn the above maintenance

activities-in the area of procedures.

In both cases, the

activities appeared not to have been performed in accordance with

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the maintenance procedure.

Procedure 44.030.219 used for-a' scale

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change out required steps 6 through 13 to be performed if the "As

Found" data was found to be out of tolerance.

For work request 920902, steps 6 through.13 were performed even though the "As

Found" data was acceptable. The maintenance aethity for

calibrating the charcoal absorber temperature controller for the

Standby Gas Treatment System utilized work request 920516 and

procedure 46.000.044. While observing the work, the-inspectors

noted that the maintenance personnel lifted leads to defeat the

lockin function when testing the control unit relays. The lockin

feature locks in the actuation relay for 10 minutes.

In order to

obtain the actuation relay's reset value without waiting 10

minutes,.the workers lifted leads to defeat the lockin relay

feature. The work request and procedure 46.000.044 did not

delineate in a step the lifting of these leads.

The workers did

document the lifting and relanding of the leads including an

independent verification. The concerns #,th procedures 44.030.219

and 46.000.044 are considered an Inspection Followup Item pending

further NRC review (341/92017-06(DRP)).

No violations or deviations were identified,

b.

Surveillance Activities (61726)

During the inspection period, the inspectors observed technical

specification required surveillance testing and verified that

testing was performed in accordance with adequate procedures, that

test instrumentation was calibrated, that results conformed with

technical specifications and procedure requirements and were

reviewed, and that any deficiencies identified during the testing

were properly resolved.

The inspectors also witnessed portions of the following

surveillances:

SOE 91-01

FW-C-1, Rev 0, Feedwater System Level

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Setpoint Changes

SOE 92-01

PR-C-1, Rev 0, Pressure F.rgulator Test-

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24.307.17

Emergency Diesel Generator No. 14

.

Start and Load Test, Slow Start

24.307.16

Emergency Diesel Generator No.13

.

Start and Load Test, Slow Start

24.307.32

(EDG-13) 24 Hour Run Followed By Loss

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of Offsite Power Test

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82.000.04

Refuel'.ng and Core Post-Alteration

.

Verification

82.000.14

Control Rod Friction Testing

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c.

Performance Evaluation Activities

The inspectors witnessed portions of tests performed under the

licensee's performance evaluation program.

Even though the tests

were not defined as Technical Specification (TS) surveillances,

the tests determined that support functions for TS components were

operable and not in a degraded condition which could jeopardize

the operability of the TS component. The folicwing performance

evaluations procedures were reviewed or portions witnessed by the

intt'ectors:

27.202.01, Revision 0, "HPCI Overspeed Trip Test"

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27.206.02, Revision 0, "RCIC Overspeed Trip Test"

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On November 5, 1992, the inspectors witnessed a portian of the

overspeed trip test on the High Pressure Coolant injection (HPCI)

turbine using procedure 27.202.01. The inspectors had the

following observations pertaining to procedure 27.202.01:

The criteria for the overspeed trip function was 5000 rpm,

.

plus or minus 100 rpm.

The function was tested three times

during each overspeed test on June 1991 and November 1992.

The criteria was not always met during the three trips due

to oil temperature variances.

In each case when the

criteria was not met, there was justification documented on

the Performance Form.

Since the overspeed criteria has not

been consistently met during overspeed tests, the licensee

should evaluate the acceptability of the trip criteria.

Note (1) after step 5.35 in the current revision of

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procedure 27.202.01 states the next step will start the HPCI

turbina.

However, step 5.37, the opening of the bypass

valve, E4150-F600, will cause the HPCI start, not step 5.36.

Note after step 5.30 states that when valve E4150-F001 is

.

opened, the HPCI turbine may roll if leakage occurs around

the turbine stop and control valves, (E4100-F067 and E4100-

F068) located downstream of E4150-F001. However, to have a

HPCI turoine roll would also require leakage past the E4150-

F003 bypass valve, E4150-F600, and the E4150-F003 valve.

These valves were closed in step 5.29.

The note should be

reviewed to clarify the leakage source that could.cause a

HPCI turbine roil when valve E4150-F001 is opened.

The licensee acknowledged the observations and will evaluate the

recommendations.

No violations or deviations were identified.

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6.

Inspection Followuo items

Inspection Followup items are matters which have been discussed with the

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licensee, which will be reviewed by the inspector, and which involve

some action on the part of the NRC or licensee or both.

Inspection

Followup Items disclosed during the inspection are discussed in

paragraphs 3.c, 3.d, and 5.a.

7.

Unresolved Items

Unresolved items are matters about which more information is required in

order to ascertain whether they are acceptable items, violations, or

deviations.

Unresolved items disclosed during the inspection are

discussed in paragraphs 3.c and 4,

8.

Meetinas and Other Activities

a.

Management Meetinos (30702)

On November 9 and 10, 1992, the Branch Chief for Branch 2 toured

the Fermi plant and met with licensee management to discuss plant

performance and plant material condition.

Also, on November 30 through December 2, the DRP Section Chief

toured the Fermi plant and met with licensee management to discuss

plant performance and plant material condition.

b.

Exit Interview (30703)

The inspectors met with the licensee representatives denoted in

paragraph I during the inspection period and at the conclusion of

the inspection on December 8, 1992. -The inspectors summarized the

scope and results of the inspection and discussed the likely.

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content of this inspection report. The licensee acknowledged the

information and did not indicate that any of the-information

disclosed during the inspection could be considered proprietary in

nature.

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