ML20111B013
| ML20111B013 | |
| Person / Time | |
|---|---|
| Site: | Hatch |
| Issue date: | 03/31/1996 |
| From: | Shannon Rogers GEORGIA POWER CO. |
| To: | |
| Shared Package | |
| ML20111A997 | List: |
| References | |
| NUDOCS 9605140134 | |
| Download: ML20111B013 (2) | |
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Plant Hatch Unit 2 J
i Monthly Operating Report i
l March 1996 l
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9605140134 960510 PDR ADOCK 05000321 l
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!!I 5164
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO:
50-366 DATE: APRIL 3, 1996 UNIT NAME:
E. I. HATCH - UNIT TWO COMPLETED BY:
S. B. ROGERS TELEPHONE:
(912) 367-7781 x2878 REPORT MONTH: MARCH 1996 R
M S
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LICENSEE SC Y
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EVENT T0 COMPGNENT CAUSE & CORRECTIVE P
DURATION 0
0 REPORT ED CODE ACTION TO NO.
DATE E
(HOURS)
N D
NUMBER ME (SUBC00E)
PREVENT RECURRENCE 96-003 960312 S
82.7 A
2 N/A CC VALVEX The unit was manually (X) scrammed to replace Main i
(B)
Steam Line SRVs "D" and "H".
Main Steam Line SRVs "D" and "H" were replaced and the unit was returned, to rated thermal power.
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l TYPE:
REASON:
METHOD:
EVENTS REPORTED INVOLVE A GREATER THAN 20%
F-FORCED A EQUIPMENT FAILURE (EXPLAIN) 1-MANUAL REDUCTION IN AVERAGE S-SCHEDULED B-MAINTENANCE OR TEST 2-MANUAL SCRAM DAILY POWER LEVEL FOR C-REFUELING 3-AUTOMATIC SCRAM THE PRECEDING 24 HOURS.
D-REGULATORY RESTRICTION 4-CONTINUATIONS E-0PERATOR TRAINING & LICENSE 5-LOAD REDUCTION F-ADMINISTRATIVE 9-0THER (EXPLAIN)
G-0PERATIONAL ERROR (EXPLAIN)
H-0THER (EXPLAIN) 1 E2-4 l
,