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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17335A5201999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp Unit 1.With 990208 Ltr ML17335A5191999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp,Unit 2.With 990208 Ltr ML17335A4831998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 2.With 990108 Ltr ML17335A4841998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 1.With 990108 Ltr ML17335A3951998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 2.With 981207 Ltr ML17335A3941998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 1.With 981207 Ltr ML17335A3331998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Plant,Unit 1.With 981105 Ltr ML17335A3381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Power,Unit 2.With 981105 Ltr ML17335A2931998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 2.With 981005 Ltr ML17335A2941998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 1.With 981005 Ltr ML17335A2131998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 2.W/980903 Ltr ML17335A2151998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 1.W/980903 Ltr ML17335A1741998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 2.W/980806 Ltr ML17335A1731998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 1.W/980806 Ltr ML17334B8171998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Plant Unit 2.W/980706 Ltr ML17334B8131998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Station,Unit 1.W/980706 Ltr ML17334A7511998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 2.W/980609 ML17334A7521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 1.W/980609 Ltr ML17334B7921998-04-30030 April 1998 Addendum to Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Station,Unit 2 ML17334B7721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Plant,Unit 1.W/980506 Ltr ML17334B7911998-03-31031 March 1998 Addendum to Monthly Operating Rept for Mar 1998 for DC Cook Nuclear Plant,Unit 2 ML17334B7171998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980407 Ltr ML17334B7181998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980407 Ltr ML17334A6831998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980309 Ltr ML17334A6811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980309 Ltr ML17334B7901998-02-28028 February 1998 Addendum to Monthly Operating Rept for Feb 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6481998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2.W/980209 Ltr ML17334B7891998-01-31031 January 1998 Addendum to Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6051997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 2 ML17334A6021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 1.W/980108 Ltr ML17334B6711997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 2.W/971208 Ltr ML17334A6061997-11-30030 November 1997 Revised Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Station,Unit 2 ML17334B6651997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 1.W/971208 Ltr ML17333B1421997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Donald C Cook Nuclear Plant,Unit 1.W/971110 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
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. DCCTI NO.90-316
~
. . - DATI 10/2/84
, C O.V _- . _- . .v..
climnr t _? ::u.n.s
. 616-465-5901 C???aT*NG 5 A I*E .
- 1. Uni: N =.. Donald C. Cook 7 Nor:s . ,
,-. .Re-or" . ,.* #.cc Septanber 1984 -
- 3. t '---* d. Th-- ' ?:wer p. W::: 3411 ,
- 4. N =:rizi:?.:: .;(Cro::5:W:): 1133 .
- 5. Desi;= II:=:i=! R..:ia;(Nec 51We): 1100
- 6. 3" " :== De::=>:hte Cay::i:f (Cress 31We): 1100
- ~. Sfaxi==
- 2 C:-- d-h!: C===:7 (Nec 31We): 1060 .
S. If C.=;;s C:=:in Capui:7 R::i=;: (1::== Ne=h:: 3 I..:: -h -) SI::: I.=: R: er:. Cive R:==ns: .
- 9. Power !. ve! To W5d 5- R==i=:e'. !! Any (N:: 5:We): *
- 10. R : sons .ror R...=-;::i:::.1f A v. : .
~ '
Pis 5 ton:h Yr.-te-C :: . Cu==!::ive
- 11. Hour: != '.:;o:.!:; P::i=d ??n 6.579 99.199 12 Nu=h:r Cf Hec = R==::rw:: C i:i=t .
700.8 3,582.4 41,367.6
- 13. Re:c::r R=sene Sw:d=vm H:= 0 0 0
- 14. Ec== Ce: _-t:: Ca.I.i. = -
691.1 3,496.8 40,296.9
- 15. Uni: R- erve Sh :down Ec:== 0 0 0
- 16. Cr:ss Th==:1 I::::;r Cen==: d (5 WH) ? '4?9.729 11.489.712 ,129,962,680
- 17. Ccore. II :=:=12:. .;y Ces=::d t..'.!WE) 745.310_, 3,733,550 41,960,160
- 13. Net II:=:i=1I ::;y Cce==:::: g,;WH) 719.171 3.603,327 40,456,698
- 19. U. i
- Serri= .:=::r 96.0 53.2 70.9
- 20. Uni: Astil:hi!!:7 .:=:or 96.0 53.2 70.9
!. Uni: C::::d:/ 7==r(Usin; .ittC Net) -
, 94.2_ 51.7 67.7
- 22. Unit C.:ceci:y F::::.-(Usin; O Ey, -)<:) 90.8 49.8 66.4 O.3. Uni: . Tor::d Cc:::: R :: 4.0 3.1 13.0]
- 04. Sh : dawns Sched !:d Cver Ney.: 3.\to..::s (Ty;e. 0:::.:r.d 0 =::en afI::J. I: ,
c:nvvnil l nnco & Maintnnnnce Outace scheduled to st-net 12/22/84. Estinn'ted dur-ation-two weeks.
- 25. If Sh : Down A: E::d Cf R:;::: ?:-icd. I:::==:ed '::: ei 5::r .:::
25.' Units la Tc:: S::: s Pnorio C:==:=i:10:en:ic..r: Fore _:t Ae .ieved 1.N.I ..- .,. .. e.. .. .. w.s . t .! .f .
IN. ..~. !A a.. . .. . . . . .. .. .. . . .
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. . -c.. . ,. .. . - . .3 ;..... .. ..
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4
- ,: p AVERAGE DAILY UNIT POWER LEVEL 00CXET NO. 50-316 UNIT 2 DATE 10/2/84 COMPLETED BY D. Climer TELEPHONE (616) 465-5901 i -
! MONTH nnnenmsor 1984 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL .
(MWE-Net) (MWe-Net) 4 1 1038 17 1030 2 1037 18 1050 .
3 1047 19 1065 .
4 1049 20 1061 5 1049 21 1060 6 1050 1054 22 7 1051 23 los2 8 1053 24 1059 l 9 1055 25 1061 10 1052 25 1064 l 11 609 27 1065 l
l 12 ,a 28 1060 t
13 gr;7 29 1057 14 1o56 30 1065 15 1058 31 l
16 1036 i INSTRUCTIONS On this fonnat list the average daily unit pcwer level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
.o -
DOCKET NO. 50-316 UNITSilUTDOWNS AND POWER REDUCTIONS UNIT NAME D.C. Cook - Unit 2 '
DATE October 4 1984 September, 1984 COntPLETED HY B.A. Svensson HEPORT Af0NTil TELEFilONE 616/465-5901
't -
-, jg 3 E* 1 icensee ,E,*,, "1. Cause & Can secsive No. D.ite Q 5@ % .2 s $ livent p pO Acti.m to H y5 $ j g5 g Repos ** un U g Prevens itecturence 6
149 840911 F 16.1 A 3 84-024-00 EF INSTRU A reactor / turbine trip occurred from 100% power due to a failure of vital A.C. instrument bus, CRID III, invert-er. The inverter failure was due to a failed capacitor, C-2. The inverter was repaired and the Unit returned to service at 0722 hours0.00836 days <br />0.201 hours <br />0.00119 weeks <br />2.74721e-4 months <br /> on 840912.
150 840912 F 12.8 G&H 3 84-025-00 ZZ ZZZZZZ At 0733 hours0.00848 days <br />0.204 hours <br />0.00121 weeks <br />2.789065e-4 months <br />, 11 minutes after the Unit was paralleled, a turbine /re-actor trip occurred due to High-High water level in No. 2 steam generator.
The high steam generator water level ~
occurred due to overfeeding the steam generator. This was caused by a com-bination of operator error and level control problems while with feedwater control in manual. The Unit was re-turned to service the same day and 100%_ reactor power was reached on
~
840913.
l 2 3 .I 12: 170sced Reason: Me:In>J: Exinbit G -Instsuctions S: Stheiluted A Fipupmer.: I;adme(Explam) 1 Manual for Picparation ut Data li-Maintenance or' Test 2 Manual Scram. linisy Slicens fm I.icensee C Refueling 3 Automatic Steam. livent Iteposi (11RI l'ile iNilRIL D Regulasuiy Resiliclion -l-Othes ( E xplain) 0161) 110perato l'saining & l.icense I:xamination 12 Administeative G Opesalion.il Essos (Explaint Inhibit I - Same Somce r8/77) 11 Othes (Esplain)
y - -
m UNIT SHt TDOWNS AND POWER REDUCTIONS
(
INSTRUCTIONS This report should describe all plant shutdowns dunng the in accordance with the tab:a appearing on t'te report form.
report penod. In addition.it should be the source of explan- If category 4 must be used. supply brief comrnents.
i atton of significant dips m average power levels. Each signi. '
ficant reduction in power level (grnter than 20% reduction LICENSEE EVENT REPORT :. Reference the applicable in 'averase daily power lesel for the preceding 24 hnurs) reportacle occurrence pertammg to the outage or power should be noted, even though the umt may not have been reduct:en. Enter the first four parts (event year sequent:a!
shut down completelyl . For such reductions in power level, report number. occurrence code and report type) of the five the dursuon should be listed as zero, the method of reducuan part designation as descnbed in item 17 of Instruct:ons for should be listed as 4 (Other), and the Cause and Correcuve Preparanon of Data Entry Sheets for Licensee Event Report Action to Prevent Recurrence column should explain. The (LER) File (NUREG-016th This information may not be Cause and Correcuve Action to Prevent Recunence column immediately evident for all such shutdowns, of course, smee 1 should be used to provide any needed explanation to fully further investigation may be required to ascertam whether or describe the circumstances of the outage or power reduction. not a reportable occurrence was involved.) If the outage or
- power reduction will not result in a reportable occurrence.
NUMBER. This column should indicate the sequential num, the pas tive indication of this lack of correlation should be
, bet assigned to each shutdown or signancant reductionin power noted as not applicable (N/A).
for that calendar year. When a shutdown or sigmncant power SYSTEM CODE. The. system in which the outage - - . or power greduction begms m one report period and ends m another.
an entry should be made for both report periods to be sure reduction ortgmated should be noted .oy the two dig 2t code or.
all shutdowns or sigm6 cant power reducuons are reported. Extubit G -Instrucuans for Preparanon of Data Entry Sheets Until a unit has achieved its first power generatien, no num, for Licensee Event Report (LER) File (NUREC.0161).
ber should be assigned to each entry. Systems that do not 6t any existmg code snould be designs.
g ted XX. The code ZZ should be used for those events where DATE. This column sould indicate the date of the start a system is not applicable.
of each shutdown or sigmncant power reduction. Report
- as year. menth, and day. August 14.1977 would be reported COMPONENT CODE. Select the most appropriate componen
as 770814 When a shutdown or sigmficant power reducuan from Exhibit ! Instructions for Preparation of Data Entr3
! begins m ene report penod and ends m another, an entry should Sheets for L' ensee Event Report (LER) File (SUREG.0161).
be made for both report periods to be sure all shutdowns usmg the following critiena:
or ngmncant power reductions are reported. ,
I '
TYPE. Use "F" or "S" to indicate either " Forced" or " Sche.
duled." respecuvely, for each shutdown or signifbant power B. If not a component fadure, use the related component.
- reducuon. Forced shutdowns include those required to be e.g.. wrong valve operated through error; hst valve as initiated by no later than the weekend following discovery component.
of an off. normal condition. It is recognized that some judg.
- ment is required in categonzmg shutdowns in this way. In C. If a chain of fatlures occurs, the first component to mai.
general. a forced shutdown is one that would not have been function should be listed. The sequence of events. inc!ud.
g completed in the absence of the condition for which corrective ing the other components which fail, should be desenbed action was taken. under the Cause and Correcuve Action to Prevent Recur.
rence column.
DURATION. Self. explanatory. When a shutdown extends Components that do not fit any existing code should be de.
beyond the end or a report penod. count only the time to the signated XXXXXX. The code 777777 should be used for end of the report penod and pick up the ensumg down time events where a component designation is not applicaole.
1 in the following report penods Report duration of outages
- ruunded to the nearest tenth of an hour to facilitate summation.
' CAUSE & CORRECTIVE ACTION TO PREVENT RECUR.
The sum of the total outage hours plus the hcurs the genera.
RENCE. Use the column in a narranve fashion to ampitfy or tor was on line should equal the gross hours in the reportmg explam the circumstances of the shutdown or power reduction penod. The column should include the spectile cause for each shut.
wn r ugnu ant pwn reducon ad h unmdate and REASON. Categonze by letter designation in accordance contemoisted long term corteenve action taken, if appropn.
with the table appearmg on the r. port form. If category H ste. This column should also be used for a desenption of the .
i must be used.suppiy brief eumments.
ma or safety.re!sted corrective mamtenance performed dunna the outage or power reduction mcluding an identificanon of METHOD OF SHUTTING DOWN THE REACTOR OR the cntical Path JeuvitY 2nd 2 report of any smale release et REDUCING POWER. Categonze by number designatten radioaetmty or smgle radiation exposure specificaily associ.
1% e that this differs from the Edison Electne Institute ated with the outage wiuch accounts for more than 10 per ent IEEll derimtions of " Forced Parnal Outage" and " Sche. of the allowsoie annual values.
duled Partial Outage." For these terms. eel uses 4 hange or' For long textual recorts contmue narrative on separate pacer
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i Dockat No.: 50-316 Unit Namn D.C. Cook Unit 2 Completed By: G. J. Peak
> Telephone: (616) 465-5901 Date: 10/04/84 Page: 1 of 1 MONTHLY OPERATING ACTIVITIES - SEBTEMBER, 1984 HIGHLIGHTS:
The unit entered the reporting period in Mode 1 with the reactor at 100% of rated thermal power. The unit tripped on 9-17-84 due to the failure of the Crid III inverter. The inverter was repaired and the unit was returned to service.
The unit tripped again during the power accension following the previous trip. The cause of this second trip was Hi-Hi steam generator level. The unit was returned to service again and subsequently loaded to 100% power where it was operating as the reporting period came to an end. No other major power reductions occurred during the reporting period.
Total electrical generation for the month was 745,310 MWH.
SUMMARY
9-04-84 The East Containment Spray Pump was inoperable for a 10 hour1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> period due to the pump Delta P being in the the high action range of the ISI pump review program.
9-11-84 The unit tripped at 1517 hours0.0176 days <br />0.421 hours <br />0.00251 weeks <br />5.772185e-4 months <br /> due to the failure of the Crid III inverter.
9-12-84 The reactor was made critical at 0350 hours0.00405 days <br />0.0972 hours <br />5.787037e-4 weeks <br />1.33175e-4 months <br /> and Mode 1 was entered at 0508 hours0.00588 days <br />0.141 hours <br />8.399471e-4 weeks <br />1.93294e-4 months <br />. The main turbine was rolled at 0612 hours0.00708 days <br />0.17 hours <br />0.00101 weeks <br />2.32866e-4 months <br /> and the main generator was paralleled at 0722 hours0.00836 days <br />0.201 hours <br />0.00119 weeks <br />2.74721e-4 months <br />. The unit tripped at 0733 hours0.00848 days <br />0.204 hours <br />0.00121 weeks <br />2.789065e-4 months <br /> due to Hi-Hi steam generator level. The reactor was taken critical again at 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br /> and Mode 1 was entered at 1628 hours0.0188 days <br />0.452 hours <br />0.00269 weeks <br />6.19454e-4 months <br />. The main turbine was rolled at 1841 hours0.0213 days <br />0.511 hours <br />0.00304 weeks <br />7.005005e-4 months <br /> and the main generator was paralleled at 2029 hours0.0235 days <br />0.564 hours <br />0.00335 weeks <br />7.720345e-4 months <br />.
9-13-84 Power reached 100% at 1230 hours0.0142 days <br />0.342 hours <br />0.00203 weeks <br />4.68015e-4 months <br />.
9-15-84 Power was reduced to 97% at 1012 hours0.0117 days <br />0.281 hours <br />0.00167 weeks <br />3.85066e-4 months <br /> for turbine valve testing.
9-18-84 Power was returned to 100% at 1138 hours0.0132 days <br />0.316 hours <br />0.00188 weeks <br />4.33009e-4 months <br />.
The Control Room Cable Vault Halon System remains inoperable as of 1707 hours0.0198 days <br />0.474 hours <br />0.00282 weeks <br />6.495135e-4 months <br /> on 4-14-83. The backup CO 2 system remains operable.
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DOCKET No. 50 - 316 UNIT NAME D. C. Cook - Unit No. 2 DATE 10-5-84 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 PAGE 1 of 1 MAJOR SAFETY-RELATED MAINTE"ANCE SEFFEMBER, 1984 M-1 Replaced three (3) studs and two (2) standoffs on Unit 2 AB Diesel Generator Exciter diode ring. Torqued all nuts and tack welded. Cleaned exciter and generator windings. Re-connected all wiring and returned unit to service.
C&I-1 2CD-2 Battery Charger lost output voltage while the charger was in service. The C-1 capacitor on the gate filter was replaced on boards 2, 3, 4 and 6. A defective firing board
- F4 was also replaced. The float and equalizing voltage were adjusted to 260.5 vde and 277 vde respectively. The current limit was adjusted to 110 amps. Declared 2CD-2 Battery Charger operable at 1057, August 29, 1984.
C&I-2 Containment Atmosphere Radiation Monitor, ERS-2400, failed to shift from AC power to battery backup when the normal AC supply, CRID III, failed. The battery backup circuit had failed and was replaced.
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'L moam aDonald arcwaa rucrac cman C. Cook Nuclear Plant P.O. Suu 458, Bridgman, Mchgan 49106 October.j,1984 Director, Office Of Management Information and Program Control U. S. Nuclear Regulatory Commission Washington, D. C. 20555 Gentlemen:
Pursuant to the requirements of Donald C. Cook Nuclear Plant Unit 2 Technical Specification 6.9.1.6, the attached Monthly Operating Report for the Month of September, 1984 is submitted.,
Sincerely,
- g. -
W. G. Smith, J .
Plant Manager i WGS:ab Attachments
, cc: J. E. Dolan M..P.'Alexich R. W. Jurgensen NRC Region III E. R. Swanson R. O.'Bruggee (NSAC)
R. C. Callen' S. J. Micrzwa R. F. Kroeger B. H. Bennett.
J. D. Huebner.
(
J. H.' Hennigan Z. Cordero R. F. Hering J. F. Stietzel PNSRC File INPO Records Center ANI Nuclear Engineering Department 9 ss
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